06-08-2009 | On April 10, 2009, at 0538 hours0.00623 days <br />0.149 hours <br />8.895503e-4 weeks <br />2.04709e-4 months <br />, with Nine Mile Point Unit 1 ( NMP1) operating at 28 percent Rated Thermal Power ( RTP), operators manually tripped the turbine in response to rising turbine bearing vibrations.
Following the turbine trip, the High Pressure Coolant Injection (HPCI) System automatically initiated as designed. The HPCI System initiation signal was immediately reset. Reactor water level was maintained in the normal operating range throughout the transient. There was no reactor scram since the turbine was tripped at a power level that is below the generator load rejection scram setpoint. After determining and addressing the cause of the vibration, the turbine was restarted and the generator was synchronized to the grid at 11:39 on the same day without any complications.
The HPCI System is a mode of operation that uses selected equipment of the Condensate and Feedwater System to perform its function. The HPCI System is not an Emergency Core Cooling System (ECCS).
The apparent cause of the turbine trip was failure to follow an operating procedure for placing the second stage reheaters in service.
To prevent recurrence, the applicable procedure has been revised to include better guidance on placing second stage reheaters in service. In addition, pre-outage Just-In-Time training material will be revised to include the proper method for placing second stage reheaters in service and to review this event as an internal operating experience event. |
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I. DESCRIPTION OF EVENT
A. PRE-EVENT PLANT CONDITIONS:
On April 10, 2009, at 0538 hours0.00623 days <br />0.149 hours <br />8.895503e-4 weeks <br />2.04709e-4 months <br />, Nine Mile Point Unit 1 (NMP1) was operating at 28 percent Rated Thermal Power (RTP).
B. EVENT:
On April 10, 2009, at 0220 hours0.00255 days <br />0.0611 hours <br />3.637566e-4 weeks <br />8.371e-5 months <br />, with NMP1 operating at 44 percent RTP with power ascension in progress from refueling outage number 20, operators commenced placing the second stage reheaters in service. While placing the second stage reheaters in service, procedural requirements to maintain a heat up rate of not more than 3 degrees/min with less than 50 degrees difference between the reheaters were exceeded. At 0523 hours0.00605 days <br />0.145 hours <br />8.647487e-4 weeks <br />1.990015e-4 months <br />, the unit received a high vibration alarm on one of the turbine bearings. In response, operators entered the Alarm Response Procedure (ARP) for high turbine vibrations. In preparation for a potential manual turbine trip, operators reduced the reactor power, in accordance with a Special Operating Procedure, to provide margin for reactor pressure control on the turbine bypass valves.
As power was being reduced, bearing vibration levels and the rate of rise continued to increase. At 05:38 with reactor power at 28 percent, the operators manually tripped the turbine prior to reaching the procedural limit of the turbine vibration. Coincident with the turbine trip, the High Pressure Coolant Injection (HPCI) System automatically initiated as designed due to the turbine trip with the reactor mode switch in Run.
The HPCI System is a mode of operation that uses selected equipment of the Condensate and Feedwater Systems to perform its function. The HPCI System is provided to ensure adequate core cooling in the unlikely event of a small reactor coolant line break. The HPCI System is not an Emergency Core Cooling System (ECCS). Since the reactor water level was maintained within the normal level control band during the transient, and there was no small reactor coolant line break, the HPCI System initiation signal was immediately reset.
There was no reactor scram since the turbine was tripped at a power level that is below the generator load rejection scram setpoint.
After determining and addressing the cause of the vibration, the turbine was restarted and the generator was synchronized to the grid at 11:39 on the same day without any complications.
C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO
THE EVENT:
None.
D. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
April 10, 2009, 0220:T Operators commenced placing second stage reheaters in service.
April 10, 2009, 0312:T Turbine vibration started to rise.
April 10, 2009, 0523:T Turbine Bearing Number 4 High Vibration Alarm received and Alarm Response Procedure entered.
April 10, 2009, 0532:T Emergency power reduction commenced in accordance with a Special Operating Procedure.
April 10, 2009, 0538:T Turbine manually tripped. The HPCI System initiated automatically.
April 10, 2009, 1108:
T After completion of immediate corrective actions, turbine roll commenced.
April 10, 2009, 1139:T Generator synchronized to the grid.
E.OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None.
F.METHOD OF DISCOVERY:
This event was immediately apparent by control room indications.
G. MAJOR OPERATOR ACTION:
Operators failed to maintain a heat up rate of not more than 3 degrees/min with less than 50 degrees difference between the reheaters. To prepare for a potential manual turbine trip, operators reduced the reactor power to provide margin for reactor pressure control on the turbine bypass valves. The turbine was manually tripped. The HPCI initiation signal was reset. After determining and addressing the cause of the vibration, the turbine was restarted and the generator was synchronized to the grid without any complications.
H.SAFETY SYSTEM RESPONSES:
The HPCI System initiated upon turbine trip as designed. The HPCI System is a mode of operation that uses selected equipment of the Condensate and Feedwater System to perform its function. The HPCI system is not an ECCS.
II. CAUSE OF EVENT:
The cause of this event is failure to follow the operating procedure for placing the second stage reheaters in service. The procedure guidance required raising the second stage reheater tube temperatures at a maximum rate of 3 degrees F per minute while placing the second stage reheaters in service. The procedure guidance also required limiting the temperature differential between the left and the right sides of the turbine to 50 degrees F. The operators utilized an average heat rate of 3 degrees F per minute for the second stage reheater's tube temperatures while placing the second stage reheaters in service. This resulted in reheater outlet temperature varying more than 50 degrees F between the left and the right sides of the turbine causing a turbine rub.
NMP Condition Report (CR) 2009-002238 applies to this LER.
III. ANALYSIS OF THE EVENT:
This event is reportable in accordance with 10 CFR 50.73(a)(2)(iv)(A) which states that any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph 10 CFR 50.73(a)(2)(iv)(B) is reportable. The NMP1 HPCI System is a feedwater coolant injection system, which is one of the systems listed 10 CFR 50.73(a)(2)(iv)(B).
There were no equipment failures associated with this event, and all safety related structures, systems, or components performed per design. Therefore, there was no adverse impact on the operability/functionality of any safety related structures, systems, or components associated with this event. It is therefore concluded that had a design bases accident occurred coincident with this event, plant systems would have responded per design to mitigate the accident.
As plant systems performed per design and plant parameters (other than turbine vibrations) remained within normal bounds throughout this event, this event did not pose a significant threat to the health and safety of the public or plant personnel.
IV.CORRECTIVE ACTIONS:
A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
The HPCI System initiation signal was immediately reset following the turbine trip.
B. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
NOTE: There are no NRC regulatory commitments in this LER.
To prevent recurrence, the applicable operating procedure has been revised to include better guidance on placing second stage reheaters in service. In addition, pre-outage Just-In-Time training material will be revised to include proper placement of second stage reheaters in service and to review this event as an internal operating experience event.
V. ADDITIONAL INFORMATION:
A. FAILED COMPONENTS:
None.
B. PREVIOUS LERs ON SIMILAR EVENTS:
None.
C. THE ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) COMPONENT FUNCTION IDENTIFIER
AND SYSTEM NAME OF EACH COMPONENT OR SYSTEM REFERRED TO IN THIS LER:
COMPONENT IEEE 803 FUNCTION IEEE 805 SYSTEM
IDENTIFIER IDENTIFICATION
Generator GEN TB High Pressure Coolant Injection System NA BJ Reheater RHTR SN Turbine
TRB TA
D.SPECIAL COMMENTS:
None.
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05000410/LER-2009-001 | Momentary Loss of Control Power to High Pressure Core Spray, Pump Due to Degraded Fuse Block Connection | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000266/LER-2009-001 | Component Coolina Water PumD Inoperable In Excess of Technical Specification Allowed Completion Time | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2009-001 | Containment Overpressure Not Ensured in the Appendix R Analysis | 10 CFR 50.73(a)(2)(ii) | 05000250/LER-2009-001 | Procedure Inadequacy Causes Control Room Ventilation Isolation Technical Specification Noncompliance | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000237/LER-2009-001 | Common Mode Failure of Reactor Building Isolation Dampers | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000530/LER-2009-001 | Manual Reactor Trip Due to a Loss of Instrument Air to the Containment Building | | 05000457/LER-2009-001 | Reactor Trip on Over Temperature Delta Temperature due to a Signal Spike on One Channel With Another Channel Placed in the Tripped Condition for Surveillance Testing | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000413/LER-2009-001 | Both Trains of Chemical and Volume Control, Auxiliary Feedwater and Containment Spray Systems were Inoperable due to a Component Failure | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000412/LER-2009-001 | Equipment Operability for Steam Generator Tube Rupture Safety Analysis Not Met | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(vi) | 05000461/LER-2009-001 | Safety Function Lost Due to Capacitor Failure on Circuit Card | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000382/LER-2009-001 | Waterford 3 Steam Electric Station 05000382 1 OF 3 | | 05000370/LER-2009-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000346/LER-2009-001 | Containment Air Cooler Fans Inoperable Due to Misapplication of Potter and Brumfield Rotary Relays | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2009-001 | Reactor Trip Due to High Pressurizer Pressure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000305/LER-2009-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000281/LER-2009-001 | Manual Reactor Trip Initiated to Replace a Rod Control Data Logging Card | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000261/LER-2009-001 | Emergency Diesel Generator Inoperable in Excess of Technical Specifications Allowed Completion Time | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000220/LER-2009-001 | Failure to Implement Required Technical Specification Actions Associated with Failed Surveillance Test | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000389/LER-2009-001 | Unit 2 Main Feedwater Isolation Valves Stroke Time Potentially Affected by Temperature | 10 CFR 50.73(a)(2)(I)(B) | 05000321/LER-2009-001 | Pump Suction Swap for HPCI and RCIC Non-Conservative With Respect To Technical Specification Requirements | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2009-001 | Surveillance Test Inadvertently Violates Technical Specification 3.6.1 for Containment Operability | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2009-001 | III Duke Energy® BRUCE H HAMILTON Vice President McGuire Nuclear Station Duke Energy Corporation MGO1VP / 12700 Hagers Ferry Road Huntersville, NC 28078 704-875-5333 704-875-4809 fax bhhamilton@duke-energy.com June 24, 2009
U.S. Nuclear Regulatory Commission
ATTENTION: Document Control Desk
Washington, D.C. 20555
Subject: Duke Energy Carolinas, LLC
McGuire Nuclear Station, Units 1 and 2
Docket Nos. 50-369, 50-370
Licensee Event Report 369/2009-01, Revision 0
Problem Investigation Process (PIP) M-09-02216
Pursuant to 10 CFR 50.73 Sections (a) (1) and (d), attached
is Licensee Event Report 369/2009-01, Revision 0, regarding
the past inoperability of the Nuclear Service Water System
"A" Trains due to potential for strainer fouling.
This report is being submitted in accordance. with 10 CFR
50.73 (a) (2) (i)- (B), an Operation Prohibited by Technical
Specifications, and 10 CFR 50.73 (a) (2) (v) (B), any Event.
or Condition That Could Have Prevented Fulfillment of the
Safety Function.
This event is considered to be of no significance with
respect to the health and safety of the public. There are
no regulatory commitments contained in this LER.
If questions arise regarding this LER, contact Rick Abbott
at 980-875-4685.
Very truly yours,
Bruce H. Hamilton
Attachment
www.duke-energy.corn m U.S. Nuclear Regulatory Commission
Date
Page 2
CC: L. A. Reyes, Regional Administrator •U.S. Nuclear Regulatory Commission, Region.II
Sam Nunn Atlanta Federal Center
•61 Forsyth Street, SW, Suite 23T85
Atlanta, GA 30303
J. H. Thompson, Jr. (Addressee Only)
Senior Project Manager (McGuire)
U.S. Nuclear Regulatory Commission
Mail Stop 0-8G9A
Washington, DC 20555
J. B. Brady
Senior Resident Inspector
U.S. Nucle'ar Regulatory Commission-
McGuire Nuclear Station
B. 0. Hall, Section Chief
Radiation Protection Section
1645 Mall Service Center.
Raleigh, NC 27699
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104t EXPIRES: 08/31/2010
(9-2007) Estimated burden per response to comply with this mandatory collection request: 50 hours. Repoded
lessons learned are incorporated into the licensing process and fed back to industry. Send comments
regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information (See reverse for required number of collection does not display a currently valid OMB control number, the NRC may not conduct or digits/characters for each block) sponsor, and a person is not required to respond to, the information collection. LICENSEE EVENT REPORT (LER) 1. FACILITY NAME 2. DOCKET NUMBER I 3. PAGE _McGuire Nuclear Station, . 0369 8 Unit 1 05000- OF 4. TITLE Nuclear Service Water System (NSWS)d
"A" Trains Past Inoperable when aligned
to the Standby Nuclear Service Water Pond due to'corrosion.
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Mitigate the Consequences of an Accident | 05000305/LER-2009-002 | Steam Exclusion Door Blocked Open During Maintenance Activities | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000250/LER-2009-002 | Turkey Point Unit 3 05000250 1 of 10 | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000220/LER-2009-002 | High Pressure Coolant Injection System Initiation Following a Manual Turbine Trip Due to High Turbine Bearing Vibrations | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000298/LER-2009-002 | Manual Scram On Low Water Level Caused By Turbine Trip From Hydraulic Fluid Leak | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000305/LER-2009-003 | Containment Spray Pump A Inoperable At Degraded Voltage Protection Setpoint | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000395/LER-2009-003 | ..Potential Loss of Residual Heat Removal System Safety Function In Mode 4 Due To An Unanalyzed Condition0 | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000389/LER-2009-003 | RCP 2B2 Lower Seal Cavity Line Leak | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000323/LER-2009-003 | Containment Sump Recirculation Valve Position Interlock Failure Due to Inadequate Testing | | 05000263/LER-2009-003 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000261/LER-2009-003 | Manual Reactor Trip Due to Failure of 'A' Steam Generator Level Module | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000440/LER-2009-003 | Reactor Recirculation Pump Failure Results in Manual Reactor Protection System Actuation | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000361/LER-2009-003 | Pressurizer Auxiliary Spray Failed Inservice Test | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | 05000457/LER-2009-003 | Drain Procedure for ECCS Suction Line Creates an Unanalyzed Condition Due to Inadequate Configuration Requirements | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000237/LER-2009-003 | Emergency Diesel Generator Oil Leak | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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