ML21132A095

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Integrated Inspection Report 05000440/2021001
ML21132A095
Person / Time
Site: Perry FirstEnergy icon.png
Issue date: 05/12/2021
From: Billy Dickson
NRC/RGN-III/DRP/B2
To: Penfield R
Energy Harbor Nuclear Corp
References
IR 2021001
Download: ML21132A095 (25)


See also: IR 05000440/2021001

Text

May 12, 2021

Mr. Rod L. Penfield

Site Vice President

Energy Harbor Nuclear Corp.

Perry Nuclear Power Plant

10 Center Road

Perry, OH 44081

SUBJECT:

PERRY NUCLEAR POWER PLANT - INTEGRATED INSPECTION REPORT

05000440/2021001

Dear Mr. Penfield:

On March 31, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at Perry Nuclear Power Plant. On April 28, 2021, the NRC inspectors discussed the results of

this inspection with you and other members of your staff. The results of this inspection are

documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding

involved a violation of NRC requirements. We are treating this violation as a non-cited violation

(NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this

inspection report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector

at Perry Nuclear Power Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the

NRC Resident Inspector at Perry Nuclear Power Plant.

R. Penfield

2

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public

Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Billy C. Dickson, Jr., Chief

Branch 2

Division of Reactor Projects

Docket No. 05000440

License No. NPF-58

Enclosure:

As stated

cc w/ encl: Distribution via LISTSERV

ML21132A095

SUNSI Review

Non-Sensitive

Sensitive

Publicly Available

Non-Publicly Available

OFFICE RIII

RIII

NAME

RRiuz:ve via email

BDickson via email

DATE

5/11/2021

5/12/2021

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Number:

05000440

License Number:

NPF-58

Report Number:

05000440/2021001

Enterprise Identifier: I-2021-001-0045

Licensee:

Energy Harbor Nuclear Corp.

Facility:

Perry Nuclear Power Plant

Location:

Perry, Ohio

Inspection Dates:

January 01, 2021 to March 31, 2021

Inspectors:

S. Bell, Health Physicist

V. Myers, Senior Health Physicist

J. Neurauter, Senior Reactor Inspector

T. Ospino, Resident Inspector

J. Steffes, Senior Resident Inspector

T. Taylor, Fermi Resident Inspector

Approved By:

Billy C. Dickson, Jr., Chief

Branch 2

Division of Reactor Projects

2

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Perry Nuclear Power Plant, in

accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs

program for overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Human Performance Error Resulted in Unplanned RCIC Unavailability

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000440/2021001-01

Open/Closed

[H.12] - Avoid

Complacency

71111.22

A finding of very low safety significance (Green) and associated non-cited violation of

TS 5.4.1, "Procedures," was self-revealed on January 19, 2021, when an unexpected isolation

of the RCIC steam supply occurred. Specifically, during performance of SVI-E31-T5395A,

"RCIC Steam Line Flow High Channel Functional for E31-N684A," Revision 8, the licensee

failed to lift the lead from terminal B4 for relay 1E51-K24, resulting in the closure of the RCIC

steam supply outboard valve and an unplanned limiting condition for operation (LCO) entry

and unavailability of the RCIC system.

Additional Tracking Items

None.

3

PLANT STATUS

Perry Nuclear Power Plant began the inspection period at 97 percent of rated thermal power in

coastdown operations before a refueling outage. On January 10, 2021, the 1B feedwater heater

isolated. The isolation resulted in a power perturbation. In response to the power perturbation

and feedwater heater isolation, the operators lowered reactor power to 79 percent to maintain

margin to thermal limits per abnormal operating procedures. High water level conditions caused

the heater isolation. The high-water level condition resulted from a failed circuit card in the level

transmitter for the alternate level controller. Operators restored level using the normal level

controller. The operators returned the unit to maximum attainable power and continued

coastdown operations on January 11, 2021. On March 6, 2021, operators shutdown the

reactor to commence refueling outage 1R18. The reactor remained shut down in the refueling

outage for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors reviewed selected procedures and records,

observed activities, and interviewed personnel to assess licensee performance and compliance

with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President

of the United States on the public health risks of the Coronavirus Disease 2019

(COVID-19), resident inspectors were directed to begin telework and to remotely access

licensee information using available technology. During this time, the resident inspectors

performed periodic site visits each week; conducted plant status activities as described in

IMC 2515, Appendix D, Plant Status; observed risk-significant activities; and completed on-site

portions of IPs. In addition, resident and regional baseline inspections were evaluated to

determine if all or portions of the objectives and requirements stated in the IP could be

performed remotely. If the inspections could be performed remotely, they were conducted per

the applicable IP. In some cases, portions of an IP were completed remotely and on-site. The

inspections documented below met the objectives and requirements for completion of the IP.

4

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1)

High pressure core spray (HPCS) system on February 9, 2021

(2)

Division 2 diesel generator while division 1 vital bus was removed from service for

modification on March 13, 2021

(3)

Residual heat removal (RHR) B partial alignment due to outage configuration on

March 14, 2021

(4)

Electrical bus and load alignment due to outage configuration on March 15, 2021

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1)

Quarterly fire protection alarm test on January 14, 2021

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1)

Fire protection drill on January 27, 2021

71111.08G - Inservice Inspection Activities (BWR)

BWR Inservice Inspection Activities Sample - Nondestructive Examination and Welding

Activities (IP Section 03.01) (1 Sample)

(1)

The inspectors verified that the reactor coolant system boundary, reactor vessel

internals, risk-significant piping system boundaries, and containment boundary were

appropriately monitored for degradation and that repairs and replacements were

appropriately fabricated, examined and accepted by reviewing the documentation of

the following activities from March 8, 2021 to March 18, 2021:

03.01.a - Nondestructive Examination and Welding Activities.

1. Ultrasonic Examination (UT) of Main Steam System 26 Inch Elbow to Pipe

Weld, American Society of Mechanical Engineers (ASME) Category R-A,

Component 1B21-0006

2. UT of Reactor Vessel Top Head Meridional Weld, ASME Category B-A,

Component 1B13-DM

3. UT of Reactor Vessel Feedwater Nozzle Weld, ASME Category R-A,

Component 1B13-N4E-KB

5

4. Liquid Penetrant Examination (PT) of Control Rod Drive System Piping

Support Welded Attachment, ASME Category C-C, Component

1C11-H0040-WA

5. Magnetic Particle Examination (MT) of Reactor Vessel Top Head to Top Head

Flange Meridional Weld, ASME Category B-A, Component 1B13-AG

6. MT of Main Steam System Flued Head Fitting to Process Pipe Attachment

Weld, ASME Category B-K, Component 1B21-P124-WA

7. Visual Examination (VT-3) of High-Pressure Core Spray System Pipe

Restraint, ASME Category F-A, Component 1E22-H0034

8. Visual Examinations of Chilled Water System: VT-3 of Pipe Anchor, ASME

Category F-A, Component 1P47-H0219 and VT-1 of Pipe Anchor Integral

Attachment Weld, ASME Category D-A, Component 1P47-H0219-WA

9. AVR-R17-01, ASME Section XI Flaw Evaluation, Weld ID 1B13-AE

10. Pipe Replacement of Essential Service Water System B Piping between

Valve 1P45F0541B and Heat Exchanger 1P42B0001B and between

Valve 1P45F0541B and Second Downstream Elbow; Weld Numbers

200726587-01, -02, -03, -04, -05, -06 and -07 (WO 200726587)

11. Pipe Replacement of Reactor Water Clean Up System; Spool Piece between

Heat Exchangers 1G33B0001C and 1G33B0002A; Weld Numbers

200724734-01, -02, -03, -04, -05, -06, and -07 (WO 200724734)

The above volumetric (UT) and surface (PT and MT) examination records were

selected from the previous outage in 2019 (1R17), since there were no ISI exams or

aging management related exams performed during this outage (1R18).

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

(1 Sample)

(1)

The inspectors observed and evaluated licensed operator performance in the

Control Room during plant shutdown and cooldown activities for the 1R18 refueling

outage on March 6 to 7, 2021.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (4 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following

structures, systems, and components (SSCs) remain capable of performing their intended

function:

(1)

Combustible gas mixing system A failure on December 22, 2020

(2)

Containment radiation monitor outboard isolation loss of indication on

January 15, 2021

(3)

Inclined fuel transfer system failure on March 16, 2021

(4)

Division 1 emergency core cooling systems (ECCS) integrated test failures and

resolution on March 22 to 24, 2021

6

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1)

Plant risk assessment related to D1A electrical bus emergent work started on

November 30, 2020

(2)

Emergent work for annunciator system ground alarms on January 7, 2021

(3)

Emergent work related to electro-hydraulic pump A leak and spill on

January 25, 2021

(4)

Reactor feed pump turbine "B" emergent work on February 22 to 24, 2021

(5)

Plant risk assessment during the Division 1 ECCS integrated test between

March 22 to 24, 2021

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1)

Combustible gas mixing system A (CR 2020-09635) failure and common cause

review on December 22, 2020

(2)

Operability review based on CR 2020-09501 related to the Technical Support Center

radiation monitor on January 4, 2021

(3)

Reactor core isolation cooling (RCIC) system operability verification based on

CR 2021-00338 on January 19, 2021

(4)

Operability review for SCRAM insertion times after shutdown on March 6, 2021

(5)

Operability review for safety relief valves (SRV) after set pressure testing on

March 29, 2021

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)

(3 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1)

Dedicated open phase control room annunciator modification on December 17, 2020

(2)

Installation of temporary jumpers to bypass the rod block as part of outage emergent

activities on March 17, 2021

(3)

Breaker EH1114 relay modification associated with Engineering Change 11-0559-002

on March 16, 2021

7

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (8 Samples)

The inspectors evaluated the following post-maintenance test activities to verify system

operability and functionality:

(1)

Technical support center testing following radiation monitor repair work on

December 16, 2020, to January 4, 2021

(2)

Division 3 emergency service water testing following packing adjustment on

January 5, 2021

(3)

Testing of the containment radiation monitor outboard isolation valve following blown

fuse replacement on January 15, 2021

(4)

Testing following average power range monitor A and B power supply replacement

on January 19, 2021

(5)

"B" reactor protection system trip channel Potter-Brumfield relay replacement for

1C71A-K012B, work order 200391663

(6)

Testing following replacement of control rod drive mechanisms on March 17, 2021

(7)

Testing following replacement of "A" RHR relays on March 22 to 24, 2021

(8)

SRV test following replacement on March 29, 2021

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Partial)

(1)

(Partial)

The inspectors evaluated refueling outage 1R18 activities from March 6 to

March 31, 2021. Activities evaluated by the inspectors included, but were not limited

to, shutdown and cooldown operations, reduced inventory control, containment

walkdown, reactor vessel disassembly for heavy load controls, refueling operations,

reactor coolant system instrumentation, outage plan and shutdown risk.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01) (6 Samples)

(1)

SRV pressure actuation channel A test on January 20, 2021

(2)

HPCS pump test on February 1, 2021

(3)

Fuel pool cooling and cleanup system surveillance on February 3, 2021

(4)

Control rod maximum scram-based insertion time on March 6, 2021

(5)

Division 1 standby diesel generator load rejection test on March 8, 2021

(6)

Division 1 ECCS integrated test between March 22 to 24, 2021

Inservice Testing (IP Section 03.01) (1 Sample)

(1)

"C" RHR system pump and valve operability test, work order 200792521.

8

Containment Isolation Valve Testing (IP Section 03.01) (1 Sample)

(1)

Leak rate test for the shutdown cooling A to the feedwater shutdown isolation valve

1E12-F050A on March 22, 2021

FLEX Testing (IP Section 03.02) (1 Sample)

(1)

Calibration check of FLEX fuel pool level transmitter on January 27, 2021

RADIATION SAFETY

71124.01 - Radiological Hazard Assessment and Exposure Controls

Radiological Hazard Assessment (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated how the licensee identifies the magnitude and extent of

radiation levels and the concentrations and quantities of radioactive materials and

how the licensee assesses radiological hazards.

Instructions to Workers (IP Section 03.02) (1 Sample)

The inspectors evaluated instructions to workers including radiation work permits used to

access high radiation areas.

(1)

The inspectors evaluated radiological protection related instructions to plant workers

for emergent diving activities on the inclined fuel transfer system.

Contamination and Radioactive Material Control (IP Section 03.03) (2 Samples)

The inspectors evaluated licensee processes for monitoring and controlling contamination

and radioactive material.

(1)

The inspectors observed workers exiting the radiologically controlled area (RCA).

(2)

The inspectors observed licensee surveys of potentially contaminated material

leaving the radiologically controlled area.

Radiological Hazards Control and Work Coverage (IP Section 03.04) (3 Samples)

The inspectors evaluated in-plant radiological conditions during facility walkdowns and

observation of the following radiological work activities.

(1)

Inclined fuel transfer system diving activities under RWP 210910

(2)

Flow accelerated corrosion exams in the reactor water cleanup heat exchanger and

pump room under RWP 210602

(3)

Control rod drive mechanism exchange under RWP 210518

9

High Radiation Area and Very High Radiation Area Controls (IP Section 03.05) (3 Samples)

The inspectors evaluated licensee controls of the following High Radiation Areas and Very

High Radiation Areas:

(1)

Locked high radiation area for reactor water clean-up pump repair in the auxiliary

building 599'

(2)

Locked high radiation area for the fuel pool cooling pump room in the intermediate

building 574'

(3)

Locked high radiation area established for fuel moves in containment 620'

Radiation Worker Performance and Radiation Protection Technician Proficiency

(IP Section 03.06) (1 Sample)

(1)

The inspectors evaluated radiation worker and radiation protection technician

performance as it pertains to radiation protection requirements.

71124.02 - Occupational ALARA Planning and Controls

Implementation of ALARA and Radiological Work Controls (IP Section 03.03) (3 Samples)

The inspectors reviewed as low as reasonably achievable practices and radiological work

controls for the following work activities.

(1)

Inclined fuel transfer system diving activities under RWP 210910

(2)

Flow accelerated corrosion exams in the reactor water cleanup heat exchanger and

pump room under RWP 210602

(3)

Control rod drive mechanism exchange under RWP 210518

Radiation Worker Performance (IP Section 03.04) (1 Sample)

The inspectors evaluated radiation worker and radiation protection technician performance

during:

(1)

Inclined fuel transfer system diving activities under RWP 210910

71124.05 - Radiation Monitoring Instrumentation

Walkdowns and Observations (IP Section 03.01) (5 Samples)

The inspectors evaluated the following radiation detection instrumentation during plant

walkdowns:

(1)

Radiation monitors (portal monitor, personnel contamination monitor and small article

monitor) located at the RCA exit.

(2)

Portable radiation survey instrumentation located at the RCA exit and the

Instrumentation Calibration Facility (Geiger Mueller contamination monitoring

instruments and dose rate survey instruments including ion chambers, pressurized

ion chambers and Telepoles).

(3)

Gamma spectroscopy systems and liquid scintillation instrumentation located within

the Chemistry Counting Room.

10

(4)

JL Shepherd Model 89 instrumentation calibrator.

(5)

Area Radiation Monitors and Continuous Air Monitors in the Fuel Handling Building

Calibration and Testing Program (IP Section 03.02) (1 Sample)

The inspectors evaluated the calibration and testing of the following radiation detection

instruments:

(1)

Canberra Argos Personal Contamination Monitor, SN L70L004V

71124.08 - Radioactive Solid Waste Processing & Radioactive Material Handling, Storage,

& Transportation

Radioactive Material Storage (IP Section 03.01) (2 Samples)

The inspectors evaluated the licensee's performance in controlling, labelling and securing

radioactive materials in the following locations.

(1)

Outside radioactive material storage locations

(2)

Radiation protection radioactive source storage locations (calibration facility and RCA

exit)

Radioactive Waste System Walkdown (IP Section 03.02 (1 Sample)

(1)

Inspectors walked down accessible portions of the solid radioactive waste systems

located in the radioactive waste handling building and evaluated system configuration

and functionality.

Waste Characterization and Classification (IP Section 03.03) (2 Samples)

(1)

The inspectors evaluated the licensees characterization and classification of

shipment 19-1030 consisting of reactor water cleanup resin radioactive waste

(2)

The inspectors evaluated the licensees characterization and classification of

shipment 20-1026 consisting of spent resin radioactive waste

Shipment Preparation (IP Section 03.04) (1 Sample)

(1)

The inspectors observed shipment number 21-008, containing radioactive

contaminated laundry.

Shipping Records (IP Section 03.05) (5 Samples)

The inspectors evaluated the following non-excepted radioactive material shipments through

a record review:

(1)

Radioactive waste shipment 19-1030 consisting of reactor water cleanup resin

transported in a Type B package

(2)

Radioactive waste shipment 20-1026 consisting of dewatered resin transported in

a general design package

(3)

Radioactive waste shipment 19-1025 consisting of reactor water cleanup resin

transported in a Type B package

11

(4)

Radioactive material shipment 19-3033 consisting of control rod drive mechanisms

transported in a Type A package

OTHER ACTIVITIES - BASELINE

71153 - Follow-up of Events and Notices of Enforcement Discretion

Event Report (IP Section 03.02) (1 Sample)

The inspectors evaluated the following licensee event reports (LERs):

(1)

LER 2020-002-00, Standby Liquid Control System Rendered Inoperable due to Valve

Misposition (ADAMS Accession No. ML20293A204). The inspection conclusions

associated with this LER are documented in this report under Inspection Results

Section 71153.

INSPECTION RESULTS

Human Performance Error Resulted in Unplanned RCIC Unavailability

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000440/2021001-01

Open/Closed

[H.12] - Avoid

Complacency

71111.22

A finding of very low safety significance (Green) and associated non-cited violation of

TS 5.4.1, "Procedures," was self-revealed on January 19, 2021, when an unexpected

isolation of the RCIC steam supply occurred. Specifically, during performance of

SVI-E31-T5395A, "RCIC Steam Line Flow High Channel Functional for E31-N684A,"

Revision 8, the licensee failed to lift the lead from terminal B4 for relay 1E51-K24, resulting in

the closure of the RCIC steam supply outboard valve and an unplanned limiting condition for

operation (LCO) entry and unavailability of the RCIC system.

Description:

On January 19, 2021, during the performance of SVI-E31-T5395A, RCIC Steam Line Flow

High Channel Functional for E31-N684A, Revision 8, the licensee received several control

room alarms and identified that the RCIC steam supply outboard valve was closed. The

licensee determined that an inadvertent isolation of the RCIC system and an unplanned

inoperability had occurred. The inspectors determined that procedural steps were not

implemented during the surveillance test, as written. Specifically, the licensee failed to

perform Section 5.1 appropriately, steps 72a and 72b, and complete the independent

verification to ensure the correct lead was lifted from terminal B4 associated with relay

1E51-K24. This failure resulted in the closure of the RCIC steam supply outboard valve and

the RCIC system unavailability.

Corrective Actions: Immediate corrective actions included securing from the surveillance,

restoration of the RCIC steam supply flow path and RCIC system operability.

Corrective Action References: CR 2021-00338, Wrong Lead lifted during Surveillance

Performance 1/19/2021.

12

Performance Assessment:

Performance Deficiency: The resident inspectors determined that the licensees failure to

implement Section 5.1, Steps 72a and 72b of SVI-E31-T5395A, RCIC steam line flow high

channel functional for E31-N684A, Revision 8, was a performance deficiency. Specifically,

the failure to ensure the correct lead was lifted from terminal B4 of the relay 1E51-K24 in

accordance with the procedure directly led to the inoperability and unavailability of the RCIC

system.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Human Performance attribute of the Mitigating Systems

cornerstone and adversely affected the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent undesirable

consequences. The resident inspectors determined the performance deficiency was more

than minor because it was associated with the Human Performance attribute of the Mitigating

Systems cornerstone and adversely affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Specifically, the licensee failed to lift the correct lead from

terminal B4 of relay 1E51-K24, which directly led to the closure of the RCIC steam supply

outboard valve and steam flow path isolation, thus negatively impacting the availability of the

RCIC system.

Significance: The inspectors assessed the significance of the finding using Appendix A, The

Significance Determination Process (SDP) for Findings At-Power. The inspectors screened

the finding against the Mitigating Systems screening questions in Exhibit 2 and answered

"NO" to all screening questions. Therefore, the finding screened to very low safety

significance (Green).

Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the

possibility of mistakes, latent issues, and inherent risk, even while expecting successful

outcomes. Individuals implement appropriate error reduction tools. Specifically, the licensee

failed to implement error reduction tools from Section 4.2.5.3 of NOBP-LP-2601, "Human

Performance Program," Revision 13, independent verification which resulted in the failure to

implement the procedure as written.

Enforcement:

Violation: Technical Specification 5.4.1, "Procedures," requires, in part, that written

procedures/instructions be established, implemented, and maintained covering the following

activities: the applicable procedures recommended in Regulatory Guide (RG) 1.33,

Revision 2, Appendix A, dated February 1978. RG 1.33, Revision 2, Appendix A,

Section 8b(2)(r), states, in part, that for the reactor core isolation system "Specific procedures

for surveillance tests, inspections, and calibrations should be written (implementing

procedures are required for each surveillance test, inspection, or calibration listed in the

technical specifications."

Contrary to the above, on January 19, 2020, while performing an activity affecting quality, the

licensee did not accomplish a surveillance test in accordance with the procedure and

incorrectly performed a step in surveillance procedure SVI-E31-T5395A, and failed to lift the

proper lead. Specifically, the licensee failed to lift the lead from terminal B4 from relay

1E51A-K24 resulting in an unplanned entry into Technical Specification 3.5.3, Condition A,

and adversely affected the availability of the RCIC system.

13

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

Minor Violation

71153

Minor Violation: Licensee Event Report (LER) 05000440/2020-002 documented a condition

where the standby liquid control (SLC) system was rendered inoperable due to a valve

alignment issue. The event occurred on August 21, 2020, from 0953 to 1307 hours0.0151 days <br />0.363 hours <br />0.00216 weeks <br />4.973135e-4 months <br />

(approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />). The licensee submitted the LER to the NRC according to

10 CFR 50.73 (a)(2)(v)(A) and 50.73 (a)(2)(v)(D) for a condition that could have prevented

the fulfillment of the safety function of a system needed to shut down the reactor and mitigate

the consequences of an accident.

The LER stated that on August 20, 2020, Periodic Test Instruction, PTI-C41-P0001, Standby

Liquid Control Transfer System Pump, and Valve Operability Test, was being performed on

the SLC system. During the test on August 20, 2020, at 1248 hours0.0144 days <br />0.347 hours <br />0.00206 weeks <br />4.74864e-4 months <br />, a valve misposition

resulted in the inadvertent addition of 226 gallons of water to the SLC storage tank, causing

an unintended dilution of the boron solution. On August 21, 2020, at 0953 hours0.011 days <br />0.265 hours <br />0.00158 weeks <br />3.626165e-4 months <br />, the SLC

system was declared inoperable when the sample results for the SLC storage tank confirmed

the boron solution concentration did not meet Technical Specification (TS) 3.1.7 criteria. The

licensee restored operability on August 21, 2020, at 1307 hours0.0151 days <br />0.363 hours <br />0.00216 weeks <br />4.973135e-4 months <br />.

While reviewing LER 05000440/2020-002, the inspectors identified that the diluted boron

solution concentration existed for a time longer than permitted by TS 3.1.7. Following the

guidance in NUREG-1022 Revision 3 "Event Report Guidelines 10 CFR 50.72 and 50.73, the

inspectors determined that the licensee should have reported the diluted boron solution

concentration to the NRC as a condition which was prohibited by the plant's Technical

Specifications, pursuant to 10 CFR 50.73 (a)(2)(i)(B). Specifically, the diluted boron solution

concentration existed for longer (approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />) than the total 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> allowed for

restoration and shutdown outage time per Technical Specifications. The licensee plans on

submitting a revised LER in response to the minor violation.

Screening: The inspectors determined the performance deficiency was minor. Specifically,

the failure to identify 10 CFR 50.73 (a)(2)(i)(B) on a Licensee Event Report did not impact the

completeness or accuracy of performance indicator data or other information provided to the

agency, as is provided in Enforcement Policy Example 6.9(d)(10).

Enforcement: This failure to comply with 10 CFR 50.73 (a)(2)(i)(B) constitutes a minor

violation that is not subject to enforcement action in accordance with the NRCs Enforcement

Policy.

14

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On April 28, 2021, the inspectors presented the integrated inspection results to

Mr. R. Penfield, Site Vice President, and other members of the licensee staff.

On February 5, 2021, the inspectors presented the radiation protection baseline

inspection results to Mr. R. Penfield, Site Vice President, and other members of the

licensee staff.

On March 18, 2021, the inspectors presented the Inservice Inspection results to

Mr. C. Elliott, Plant General Manager, and other members of the licensee staff.

On March 25, 2021, the inspectors presented the radiation protection baseline

inspection results to Mr. R. Penfield, Site Vice President, and other members of the

licensee staff.

On April 28, 2021, the inspectors presented the integrated inspection results inspection

results to Mr. R. Penfield, Site Vice President, and other members of the licensee staff.

15

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04

Drawings

302-0351-00000

Standby Diesel Generator Starting Air

GG

302-0352-00000

Standby Diesel Generator Fuel Oil System

LL

302-0353-00000

Standby Diesel Generator Lube Oil

T

Procedures

ELI-R22

15KV and 5KV Metal Clad Switchgear

3/15/2021

VLI-E12

Residual Heat Removal System

3/14/2021

VLI-E22A

High Pressure Core Spray

10

VLI-R44

Division 1 and 2 Diesel Generator Starting Air System

6

VLI-R45

Division 1 and 2 Diesel Generator Fuel Oil System (Unit 1)

5

VLI-R47

Division 1 and 2 Diesel Generator Lube Oil

7

71111.05

Procedures

FPI-A-B02

Fire Brigade Drills

01/27/2021

Work Orders

200750956

Quarterly Fire Alarm

01/14/2021

71111.08G Corrective Action

Documents

CR-2019-02185

Foreign Material Head Tensioner Lock Washer Dropped in

Cavity

03/19/2019

CR-2019-02328

Relevant Indication Identified During Containment Surface

Exams

03/14/2019

CR-2019-02523

1C22D0012B Found with Internal Parts Missing - Potential

Foreign Material

03/19/2019

CR-2019-02677

During IVVI Piece of Foreign Material Identified Between Jet

Pumps 16 and 17

03/22/2019

CR-2019-02704

During IVVI Piece of Foreign Material Identified at Jet Pump

17

03/23/2019

CR-2019-02893

Foreign Material Found Inside Reactor Vessel During Core

Verification

03/28/2019

CR-2019-02956

Legacy Foreign Material Discovered in Inner Bellows

03/29/2019

CR-2019-02990

Foreign Material - Piece of Rope Found in Inner Bellows

After Draindown

03/30/2019

CR-2019-03147

Leakage Identified During Reactor Pressure Vessel Test

04/03/2019

CR-2019-03157

Documentation of Identified Mechanical Joint Leakage

Identified During Reactor Pressure Vessel Leak Test (1R17)

04/04/2019

CR-2019-03358

Roll-Up Condition Report Following 1R17 Refuel - Foreign

Material Focused Observations

04/09/2019

CR-2019-04170

Additional Pitting Discovered in Piping Downstream of

05/07/2019

16

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Emergency Service Water

CR-2020-02539

Mechanical Leakage Identified During ISI-P2-T2200-3

03/23/2020

CR-2020-06809

1R16 Snubber As-Built Discrepancy

08/31/2020

Corrective Action

Documents

Resulting from

Inspection

ATA-2021-4926

Remove "Snubbers" from Definition of VT-3 in NQI-1042,

Paragraph 3.15 to Align with Language Contained in ASME

Section XI (2013 Edition), IWA-2213

03/12/2021

Drawings

304-672-105

Piping Isometric, Reactor Water Clean-Up System, Reactor

Building

D

305-002-113

ISI Piping Isometric, System P47 Chilled Water System Loop

B

A

305-006-103

Reactor Vessel Closure Head, Circumferential and

Meridional Weld Arrangement

A

305-006-108

ISI, System 1B13, Reactor Vessel Feedwater Nozzle Weld

Arrangement

D

305-605-103

ISI Piping Isometric, System B21, Main Steam Loop C

C

305-605-107

ISI Piping Isometric, System B21, Main Steam Loop A,

Steam Tunnel Elevation 620-6

D

305-701-102

ISI Piping Isometric, High Pressure Core Spray

D

305-871-104

System C11, Control Rod Drive, Loop B, Reactor Building

Elevation 620-6

C

92-701-0034

Pipe Support Mark Number 1E22-H0034

A

92-871-0040

Pipe Support Mark 1C11-H0040

2

B-312-641

Containment Penetration Detail, Type K

F

Miscellaneous

RRP 200724734

Repair Replacement Plan: Remove and Replace Reactor

Water Clean Up Heat Exchanger 4 Spool Piece Between

Heat Exchangers 1G33B0001C and 1G33B0002A

0

RRP 200726587

Repair Replacement Plan: Remove 3" Bypass

Piping/Components and Replace 14" Spool Piece Between

Valve 1 P45F0541 B and Heat Exchanger 1 P4280001 B.

Also Replace Portion of Spool Piece Between Valve

1 P45F0541 B and Second Elbow Downstream of the Valve.

Reference ECP 18-0162-002

0

WPS 1.1.2-001

Welding Procedure Specification: P1 Gr. 1 & 2 to P1 Gr,

13

17

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

1 & 2

NDE Reports

0941-19A-003

Liquid Penetrant Examination (PT): Piping Support Welded

Attachment: Component 1C11-H0040-WA

03/13/2019

0942-19A-008

Magnetic Particle Examination (MT): Top Head to Top Head

Flange: Component 1B13-AG

03/21/2019

0942-19A-010

Magnetic Particle Examination (MT): P124 Flued Head

Fitting to Process Pipe Attachment Weld: Component

1B21-P124-WA

03/25/2019

0942-19B-009

Magnetic Particle Examination (MT): 14 Pipe to 14 Elbow

03/13/2019

0942-19B-014

Magnetic Particle Examination (MT): Flange to Pipe

03/13/2019

0942-19B-015

Magnetic Particle Examination (MT): Pipe to Elbow Butt

Welds

03/13/2019

0942-19B-016

Magnetic Particle Examination (MT): (2) Half Coupling to

Pipe and Flange to Pipe Welds

03/13/2019

0942-19B-017

Magnetic Particle Examination (MT): 14 Flange to 14 Elbow

Butt Weld (Repair)

03/13/2019

0942-19B-025

Magnetic Particle Examination (MT): 14 Pipe to 14 Elbow

FW-07

03/25/2019

0942-19B-031

Magnetic Particle Examination (MT): 4 Spool Piping

03/07/2019

1042-19B-018

Visual Examination System Leakage (VT-2): Order

200726587 Piping Replacement

03/27/2019

1042-21-023

Visual Examination of Pipe Hanger, Support, or Restraint

(VT-3): Chilled Water System, Pipe Anchor, Component

1P47-H0219 Located on ISI Drawing 305-002-113

03/04/2021

1042-21-024

Visual Examination of Welds (VT-1): Chilled Water System

Pipe Anchor Integral Attachment, Component

1P47-H0219-WA Located on ISI Drawing 305-002-113

03/08/2021

1042-21-029

Visual Examination of Pipe Hanger, Support, or Restraint

(VT-3): Mechanical Snubber, Drawing 305-701-102,

Component 1E22-H0034

03/04/2021

APR-R17-02

Ultrasonic Examination Summary Sheet, System 1B13, Weld

Number 1B13-N4E-KB, Safe-End to Nozzle

03/282019

MVR-004

UT Report with Calibration Records C-007 and C-008:

Component 1B13-DM

03/23/2019

18

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

UT-19-E006

UT Calibration/Examination Report: Component 1B21-006

03/15/2019

Procedures

GEH-UT-247

Procedure for Phased Array Ultrasonic Examination of

Dissimilar Metal Welds

4

GEH-UT-300

Procedure for Manual Examination of Reactor Vessel

Assembly Welds in Accordance with PDI

12

NOP-CC-5762

Appendix VIII Procedure for Ultrasonic Examination of

Ferritic Welds

3

NQI-0941

Liquid Penetrant Examination

22

NQI-0942

Magnetic Particle Examination

22

NQI-1042

Visual Examination

20

Work Orders

200718215

Reactor Vessel Top Head Meridional Weld Examination

03/21/2019

200718218

Piping Weld Exams on Main Steam Lines

04/17/2019

200724734

Replace 4 Piping - RWCU Piping Between Heat

Exchangers 1G33B0001C and 1G33B0002A

04/11/2019

200726587

Replace 14 Piping - ESW B Piping Between 1P45F0541B

and Heat Exchanger 1P42B0001B and Between Valve

1P45F0541B and Second Elbow Downstream of Valve

04/09/2019

200728323

1B13 Reactor and Internals Non-Destructive Examination

04/18/2019

200794288

System P47 Exams: Pre-1R18

03/12/2021

200794289

ISI of Piping, Supports, and Components of P42, P47, and

E22 Systems

03/12/2021

71111.11Q Miscellaneous

Evolution Specific

Reactivity Plan

Perry Nuclear Power Plant End of Cycle 18 Shutdown

0

Procedures

IOI-3

Power Changes

81

IOI-4

Shutdown

26

71111.12

Corrective Action

Documents

2021-00266

Loss of Indication for Containment Radiation Monitor

Outboard Isolation

01/15/2021

2021-01834

IFT Cable Damaged During Transfer

03/14/2021

Miscellaneous

NOP-ER-3004-03

Maintenance Rule Failure Review Form

04

NOP-SS-3001-02

Procedure Approval Form

12

71111.13

Corrective Action

Documents

2021-00128

Multiple Alarms Received Coincident with Annunciator

System Ground

01/7/2021

2021-00455

EHC Pump A Leak

01/25/2021

19

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2021-01200

Planned Work Not Able to be Released as Scheduled Due to

Leakby Aux Condenser B Air Removal Suction Valve

02/23/2021

2021-02121

Unplanned Division 1 DG Start During Integrated

LOOP/LOCA Test

03/23/2021

Work Orders

200840213

Determine and Correct the Cause Ground on Electrical Bus

D1A CR 2020-09061

11/30/2020

71111.15

Corrective Action

Documents

2020-09501

Ventilation Radiation Monitor Gas Channel Reading Erratic

12/16/2020

2021-00338

Wrong Lead Lifted During Surveillance Performance

01/20/2021

2021-01707

Rod SCRAM Time Recorder Did Not Perform as Expected

03/10/2021

2021-09635

Combustible Gas Mixing Compressor Suction Valve Would

Not Re-Open Following Compressor Start

12/22/2020

Work Orders

200798943

Safety Relief Valve Removes, Replaces and Offsite Testing

03/23/2021

71111.18

Engineering

Changes

11-0559-002

Spring Charging Motor Margin Improvement - EH 1114

0

ECP 15-0057

Installation of U1/U2 Startup Transformer

02/26/2018

Engineering

Evaluations

ECP 19-0203-002 Dedicated Open Phase Control Room Annunciators - Unit 2

07/10/2020

Work Orders

200846449

Jumper Request to Remove Rod Block

03/17/2021

71111.19

Corrective Action

Documents

2021-00266

Loss of Indication for Containment Radiation Monitor

Outboard Isolation

01/15/2021

Procedures

SVI-B21-T2100

Safety Relief Valve (SRV) Set Pressure Testing

7

SVI-D17-T2001

Plant Radiation Monitoring Isolation Valves Operability Test

8

Work Orders

100841399

Technical Support Center Ventilation Radiation Monitor Gas

Channel Reading Erratic Replacement

01/4/2021

200391663

Replace Relay 1C17A-K0112B Reactor Protection System

Trip Channel B

0

200536387

Replace Relays 1E12-K18A/19A

03/22/2021

200594427

Replace Power Supply PS22

01/12/2021

200727023

Install ECP-11-0559-002 74 Power Monitoring Relay in

Breaker EH1114

03/14/2021

200762809

Inspect/Tighten Packing-ESW PMP Div III

01/5/2021

200795982

Control Unit Hydraulic

03/17/2021

71111.20

Corrective Action

Documents

2021-01545

Condensate Booster Pump C Tripped Following Reactor

Recirculation Pump Downshift

03/6/2021

20

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2021-01557

Feedwater Heater 3A Isolated on High Level Following

Recirculating Pump Downshift to Slow Speed

03/6/2021

2021-01564

Control Rod 02-27 Did Not Settle at 00

03/7/2021

2021-01604

Scaffold Level Inadvertently Dropped in the Suppression

Pool During Scaffold Erection

03/8/2021

2021-01829

Leak in High Pressure Core Spray Room

03/14/2021

2021-01857

As Found Blockage of 3-Inch Fire Protection System to

Emergency Service Water Pipe Connection

03/15/2021

2021-01939

Fuel Assembly 18P568 Identified as Cycle 18 Fuel Defect

03/17/2021

2021-02011

Design Discrepancies Contained Within the Engineering

Change Package for the 1B33-F060B Side Drain Appendage

03/19/2021

2021-02117

Ground Detected on DC Bus

03/22/2021

2021-02159

Loose Bushing Terminal Lead Connectors Found in Unit 1

Start-Up Transformer

03/24/2021

2021-02237

Issues Noted on Post Maintenance Tests for Scram

Discharge Volume Vent and Drain Valves

03/25/2021

2021-02312

Control Rod Drive Mechanism Temperature for Rod 34-43

Indicates Failed

03/27/2021

2021-02428

Hard Ground Indicated on DC Bus D-1-B

03/31/2021

Miscellaneous

1R18 Shutdown Defense-In-Depth Report

1

Procedures

SVI-B21-T1176

Reactor Coolant System Heat Up and Cooldown

Surveillance

03/7/2021

71111.22

Procedures

GMI-0067

Under-Vessel Maintenance Activities

19

IMI-E2-47

Installation of Reactor Refuel Level Instrumentation for

IOI-9

03/9/2021

SVI-B21-T2100

Safety Relief Valve (SRV) Set Pressure Testing

7

SVI-E12-T2210

Leak Rate Test for RHR to FWD Injection Valves

1E12-F050A and 1E12-F053A

03/24/2021

SVI-G41-T2002

Fuel Pool Cooling and Cleanup System Operability Test

02/3/2021

SVI-R43-T7000-A Division 1 ECCS Integrated Test

12

TXI-0460

Division 1 Standby Diesel Generator Load Rejection Test

03/8/2021

Work Orders

200751888

SRV Pressure Actuation Channel a Functional for

1B21-N668A

01/20/2021

200778903

Spent Fuel Pool Level Instrument 1X13N0003 Calibration

01/27/2021

21

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Check

200778904

Level Sensor Calibration

02/3/2021

200778926

Standby Oil Pump Testing 1N27C0006A

12/30/2020

200783921

Control Rod Maximum SCRAM Insertion Time

03/6/2021

200792417

High Pressure Core Spray Pump and Valve Operability Test

02/1/2021

71124.01

Corrective Action

Documents

CR-2021-01739

Two Unbriefed Dose Rate Alarms Received in Containment

Annulus 690' Elevation

03/11/2021

Corrective Action

Documents

Resulting from

Inspection

CR-2021-01952

NRC Comment During Radiological Hazards/ALARA

Inspection for Loss of Telemetry

03/16/2021

Radiation

Surveys

N/A

Radiological Surveys for Lower Inclined Fuel Transfer

System

03/15/2021

PY-M-20210310-

7

Reactor Water Cleanup Heat Exchanger Room Post Pump

Failure Verification Survey for Flow Accelerated Corrosion

Exam Work

03/09/2021

PY-M-20210312-

37

Scaffold Extension for Flow Accelerated Corrosion Exam

03/12/2021

Radiation Work

Permits (RWPs)

210518

Undervessel Activities

0

210602

Flow Accelerated Corrosion Exams in the Reactor Water

Clean-Up Heat Exchanger and Pump Room

0

210910

Inclined Fuel Transfer System Diving Activities and Support

Work

0

71124.02

ALARA Plans

ALARA Plan

210518

Undervessel Activities

0

ALARA Plan

210602

Flow Accelerated Corrosion Exams in the Reactor Water

Clean-Up Heat Exchanger Room

0

ALARA Plan

210910

ALARA Plan for Inclined Fuel Transfer System Diving and

Support Activities

0

71124.05

Calibration

Records

Canberra Argos Personal Contamination Monitor;

SN L70L004V

02/17/2021

71124.08

Corrective Action

Documents

2019-03353

Radwaste Processing Inventory Issues

04/09/2019

2019-06245

Radwaste Tanks Require Multiple Iterations of Processing in

Order to Become Transfer Quality

07/24/2019

22

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2020-07918

Pre NRC-Assessment ATA 2020-10589 Identified

Deficiencies in Closure Packages for SVI-E31-T5190

10/13/2020

Miscellaneous

20118

Radioactive Material Transportation Training Record

07/09/2020

451802001

10 CFR 61 Laboratory Analysis of Reactor Water Clean-Up

Resin

05/25/2018

510237001

10 CFR 61 Laboratory Analysis of Spent Resin

02/25/2020

Procedures

NOP-OP-4502

Control of Radioactive Material

7

NOP-OP-5201

Shipment of Radioactive Material-Waste

10

PCP-0000

Process Control Program

15

RPI-1301

Movement of Radioactive Material/Waste Outside of

Radiologically Controlled Areas and Onsite Interim Storage

13

Self-Assessments ATA-2020-10589

Pre NRC-Inspection - Radioactive Solid Waste Processing

and Radioactive Material Handling, Storage, and

Transportation

11/13/2020

Shipping Records 19-1025

Radioactive Waste Shipment of Reactor Water Cleanup

Resin

06/05/2019

19-1030

Radioactive Waste Shipment of Reactor Water Cleanup

Resin

07/23/2019

19-3033

Radioactive Material Shipment of Control Rod Drive

Mechanisms

07/18/2019

20-1026

Radioactive Waste Shipment of Dewatered Resin

11/30/2020

21-2008

Radioactive Material Shipment Containing Radiologically

Contaminated Laundry

03/18/2021

Work Orders

200752735

Radioactive Source Inventory/Leak Test Record

09/03/2020