ML20236R056

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Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-346/98-07
ML20236R056
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 07/15/1998
From: Grobe J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Jeffery Wood
CENTERIOR ENERGY
References
50-346-98-07, 50-346-98-7, NUDOCS 9807210216
Download: ML20236R056 (2)


See also: IR 05000346/1998007

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July 15, 1998

Mr. John K. Wood

Vice President- Nuclear

Davis-Besse Nuclear Power Station

Centerior Service Company

5501 North State Route 2

Oak Harbor, OH 43449

SUBJECT:

NOTICE OF VIOLATION (NRC INSPECTION REPORT 50-346/98007(DRS))

Dear Mr. Wood:

This will acknowledge receipt of your letter dated June 23,1998, in response to our

letter dated May 26,1998, transmitting a Notice of Violation associated with two examples of a

failure to evaluate the potential radiological hazards and institute appropriate controls prior to

performing work at the Davis-Besse Nuclear Power Station. We have reviewed your corrective

actions and have no further questions at this time. These corrective actions will be examined

during future inspections.

Sincerely,

Original /s/ J. A. Grobe

John A. Grobe, Director

Division of Reactor Safety

Docket No.: 50-346

License No.: NPF-3

Enclosure:

Lir did 6/23/98 from

First Energy to USNRC

See Attached Distribution

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J. Stetz, Senior Vice

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State Liaison Officer, State

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C. Glazer, State of Ohio

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Docket Number 50-346

License Number NPF-3

Serial Number 1-1163

June 23, 1998

United States Nuclear Regulatory Commission

Document Control Desk

Washington, D.C. 20555-0001

Subject: Response to Inspection Report Number 50-346/97008 (DRS)

Ladies and Gentlemen:

Toledo Edison has received Inspection Report Number IR 50-346TS8007froledo Edison Log

Number 1-3964) and the enclosed Notice of Violation issued on May 26,1998. The violation

involves two examples of a failure to evaluate the potential radiological hazards and institute

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appropriate controls prior to performing work. Toledo Edison provides the attached response to

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the subject violation.

Should you have any questions or require additional information, please contact

Mr. James L. Freels, Manager - Regulatory Affairs, at (419) 321-8466.

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Very truly yours,

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A. B. Beach, Regional Administrator, NRC Region III

cc:

A. G. Hansen, DB-1 NRC/NRR Project Manager

S. J. Campbell, DB-1 Senior NRC Resident Inspector

Utility Radiological Safety Board

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Docket Number 50-346

License Number NPF-3

Serial Number 1-1163

Attachment

Page1

Reply to a Notice of Violation (50-346/98007-01)

Alleced Violation

During an NRC inspection conducted from April 27 through April 30,1998, a violation of NRC

requirements was identified. In accordance with the General Statement of Policy and Procedure

for NRC Enforcement Actions," NUREG-1600, the violations are listed below:

10 CFR 20.1501 requires that each licensee make or cause to be made surveys that may be

necessary for the licensee to comply with the regulations in Part 20 and that are reasonable under

the circumstances to evaluate the extent of radiation levels, concentrations or quantities of

radioactive materials, and the potential radiological hazards that could be present.

Pursuant to 10 CFR 20.1003, survey means the evaluation of the radiological conditions and

potential hazards incident to the production, use, transfer, release, disposal, or presence of

radioactive material or other sources of radiation.

10 CFR 20.1201(a)(1)(i) requires, with exceptions not applicable here, that the licensee control

the occupational dose to individual adults to an annual dose limit of 5 rems total effective dose

equivalent.

Contrary to the above, on April 21 and 23,1998, the licensee did not make surveys to assure

compliance with the regulations in 10 CFR 20.1201(a)(1)(i). Specifically:

a.

On April 21,1998, the licensee did not perform surveys to identify the potential for

transient, high dose rates in the annulus area during incore detector movement, prior to

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allowing workers to enter the area. This area had dose rates between 10-20 rem per hour

(contact) on portions of the containment wall during movement of the incore detectors

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(50-346/98007-01a).

b.

On April 23,1998, the licensee failed to evaluate the ALARA controls implemented

during removal of steam generator mirror insulation. Specifically, the radiation

protection technician covering the job, had relaxed the requirements for wearing

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faceshields and for " wetting" the contaminated surface, as discussed in the prejob briefing

or as specified in the Radiation Work Permit, without performing an evaluation of the

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potential radiological consequences. The high contamination levels (50-500 millirad per

hour (smearable)) which existed in the area required that stringent controls be maintained

to prevent the spread of airbome contamination (50-346/98007-01b).

This is a Severity Level IV violation (Supplement IV).

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Docket Number 50-346

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License Number NPF-3

Serial Number 1-1163

Attachment

Page 2

Response to Alleced Violation 50-346/98007-Ola

Reason for Violation

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The annulus between the containment vessel ard the wall of the shield building was not

recognized as an area requiring control as a Locked High Radiation Area during mevement of

activated incore probes. Incore probes are pullen from the shielded incore instrumentation tunnel

into the water-filled incore tank every refueling outage to be cut up for disposa purposes.

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During the most recent refueling outage, there was an incicese in the amount of work performed

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in the annulus due to replacement of radiant energy shields and repainting cf the lour portion of

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the containment vessel in addition to the normally scheduled outage activities. During previous

refueling outages, either personnel were not in the annulus area during cutting of the incore

probes, or incore cutting occurred during transfer ofirradiated fuel from the reactor to the spent

fuel pool. During fuel transfer, the annulus is controlled as a Locked High Radiation Area

because the fuel transfer tubes traverse the annulus. Due to a failure to survey the annulus area

during the separate evolution ofincore cutting, the annulus was not recognized as a potential area

for high radiation levels during the brief period of time the incore probe is not fully shielded.

The high dose rates in the small affected area of the annulus existed for approximately 30

seconds as the incore probe tip traversed the air gap between the shielded incore instrument

tunnel and the water-filled incore tank.

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Corrective Steps Taken and Results Achieved

When the workers' electronic dosimeters alarmed, the workers immediately evacuated the

annulus area between the containment vessel and the wall of the shield building and contacted

Radiation Protection personnel. Radiation Protection personnel responded by performing a

survey of the work location. The initial survey failed to identify the cause of the alarm, so the

workers were allowed to return to the work location with continuous Radiation Protection

coverage. When a second dose rate alarm occuned the workers were promptly evacuated from

the work location. The transient high dose rate was confirmed by the Radiation Protection

technician, and the entire annulus area was controlled as a Locked High Radiation Area for all

incore probe cutting activities. Administrative controls were imposed to prevent use of the

incore cutter without the annulus space being posted as a Locked High Radiation Area. The

maximum dose recorded by any worker's electronic dosimeter was 7 millirem.

Corrective Steps Taken to Avoid Further Violations

The forms associated with procedure DB-HP-04003, Locked High Radiation Area Boundary

Verification, have been revised in accordance with procedure DB-HP-00000, Radiation

Protection Program Administration, to ensure the annulus area between the containment vessel

and the wall of the shield building is controlled as a Locked High Radiation Area during

handling of activated incore probes. No other areas are affected dur'mg handling of activated

incore probes that are not already controlled as a Locked High Radiation Area. In addition,

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Docket Number 50-346

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License Number NPF-3

Serial Number 1-1163

Attachment

Page 3

training will be provided to Radiation Protection personnel on lessons leamed from this incident;

including proper dosimetry alarm response, proper follow-up and investigation of unexpected

dosimetry alarms, and new controls for incore probe handling. This training will be completed

by September 11,1998.

Date When Full Compliance will be Achieved

Full compliance was achieved on April 22,1998, when the annulus area between the

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containment vessel and the wall of the shield building was surveyed during handling of activated

incore probes and posted as a Locked High Radiation Area.

Eesponse to Alleced Violation 50-346/98007-Olb

Reson for Violation

As a result of personnel error by the contract Radiation Protection technician covering the job,

int.dequate contamination control methods were used for insulation removal in an area known to

be highly contaminated beneath the insulation. Controls to minimize the spread of airborne

contamination were discussed during the pre-job briefing, which was attended by the technician.

However, during the actual insulation removal, the technician did not implement the controls

discussed, and did not consult with Toledo Edison Radiation Protection management personnel

prior to relaxing the controls. A contributing factor to this event was that the associated

Radiation Work Permit covered all insulation removal in containment, and the pre-job brief for

this Radiation Work Permit occurred approximately two weeks prior to this specific task. The

insulation workers and thejob supervisor, who also attended the pre-job briefing, followed the

direction of technician instead of following the guidance received from Radiation Protection

management during the briefing.

Corrective Stens Taken and Results Achieved

The contract Radiation Protection technician who erroneously relaxed the contamination control

controls was counseled regarding the event and was reassigned to a different area of the plant for

the remainder of the refueling outage. The workers were decontaminated, and whole body

counts performed to confinn that any intake of radioactive material was significantly below

regulatory limits. A discussion was conducted between Toledo Edison Radiation Protection

management personnel, the insulation workers, and the job supervisor regarding the event to

reaffirm the expectations regarding compliance with pre-job instructions. A detailed

decontamination effort was planned and executed to correct the high contamination levels that

resulted from the insulation removal from the east steam generator in order to recover the

immediate work area affected. Increased supervisory oversight of further insulation jobs was

provided to ensure proper contamination control methods were taken. No further contamination

control incidents related to insulation removal occurred during the remainder of the outage.

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Docket Number 50-346

License Number NPF-3

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Serial Number 1-1163

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Attachment

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Corrective Steos Taken to Avoid Further Violations

Additional controls will be established for removal ofinsulation from the affected area of the

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east steam generator. A special Radiation Work Permit with a specific brief to keep personnel

dose "As Low As Reasonably Achievable"(ALARA) for this particular area plus an additional

control to contact the duty Radiation Protection Manager prior to insulation removal will be

utilized to ensure proper controls. These actions will be captured in the Radiation Protection

Outage Critique for incorporation into the Radiation Protection plans for the next refueling

outage. Additionally, training will be provided to Radiation Protection personnel involving the

timeliness of pre-job briefs, management expectations regarding compliance with pre-job

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instructions, and the process for documenting changes to Radiation Work Permit requirements.

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This training will be completed by September 11,1998.

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Date When Full Compliance will be Achieved

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Full compliance was achieved on April 25,1998, when controls were implemented to prevent

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further spread of radioactive contamination associated with the east steam generator insulation.

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