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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20084N6461977-03-31031 March 1977 Followup AO 50-249/75-44A:on 751125,offgas Activity Increased.Ge Insp Revealed Major Defect in Fuel Assembly DD-418.Assembly Removed from Reactor ML20084E3631976-06-29029 June 1976 Supplemental AO 50-237/75-11A:on 750127,core Spray Injection Line through-wall Cracks Discovered.Stainless Steel Portion of Core Spray Piping from Vessel Nozzle to Second Isolation Valve Replaced w/SA-333 Grade 6 Carbon Steel ML20084N6831976-06-29029 June 1976 Supplemental AO 50-249/1975-42A:motor Operated Valve 3-1501-5D Failed to Open During Testing Due to Thermal Overload Trip.Caused by Undersized Overload Heaters.Overload Heater Will Be Replaced W/Larger Capacity Unit ML20084D1191976-04-13013 April 1976 AO 50-237/75-39A:on 750612,diesel Generator Experienced Starting Failures.Possibly Caused by Two Gouged & Burred Areas on Ring Gear.Ring Gear Repaired ML20084D1541976-01-14014 January 1976 AO 50-237/75-38A Supplementing AO-50-237/75-38 Re Failure of MO-2-1301-2 Valve to Operate.Apparently Caused by Excessive Cycling of Valve.Valve Stem Probably Experienced Metal Fatigue Due to Multiple Actuations ML20090E4581975-12-17017 December 1975 Supplemental AO 50-237/75-44:diesel Generator Failed to Start.Caused by Air Relay Valve Failure Due to Sticking O-rings.O-rings Replaced ML20084N6541975-12-11011 December 1975 AO 50-249/75-44:on 751125,offgas Increase Exhibited Which May Have Represented Abnormal Degradation of Fuel Cladding.Cause Unknown.Investigation Underway ML20090E4321975-11-20020 November 1975 AO 50-237/75-52:on 751116,MSIV AO 2-203-1C Closing Time Found Below Tech Spec Section 3.7.D.1.Caused by Out of Adjustment Hydraulic Bleedoff Valve.Bleedoff Valve Readjusted ML20090E4751975-11-0606 November 1975 AO 50-237/75-51:on 751031,torus Water Level Exceeded Tech Spec Limit During HPCI Sys Surveillance.Caused by Operator Failure to Verify Proper Valve Lineup.Water Pumped from Torus Until Level Dropped Below Tech Spec Limits ML20084N6881975-10-20020 October 1975 AO 50-249/75-42:on 750920,motor Operated LPCI Suction Valve 3-1501-5D Failed to Open Twice During Testing. Apparently Caused by Defective Valve Motor.Valve Motor Will Be Replaced ML20090E4781975-10-17017 October 1975 AO 50-237/75-49:on 751009,LPCI Loop Selection Logic Circuitry Failed to Select Preferred B Loop.Caused by Out of Calibr Differential Switch 261-34 & Electrically Shorted Switch 261-34D.Mod to Provide Signal Dampening Initiated ML20090E4471975-10-17017 October 1975 AO 50-237/75-48:on 751007,through-wall Crack Discovered in Drywell/Torus Nitrogen Purge Line 1604-18.Caused by Rapid & Uneven Contraction of Line Tee Connection Due to Liquid Nitrogen Impingement Resulting from Boiler Failure ML20084N8331975-10-15015 October 1975 Supplemental AO 50-249/75-22:plant Mod Being Initiated to Eliminate Valve Seat Failures Due to Cryogenic Stress ML20090E4811975-10-0909 October 1975 AO 50-237/75-45:on 750929,HPCI Turbine Failed to Trip at Designated Reactor Coolant Level.Caused by Open Circuit in Turbine Trip Solenoid Valve Coil Due to Failure of Cold Solder Joint within Coil.Hpci Trip Solenoid Valve Replaced ML20090E4821975-10-0909 October 1975 AO 50-237/75-46:on 750929,reactor Scrammed on High Drywell Pressure During Drywell Inerting Process.Caused by Operator Valving Error,Allowing Nitrogen Flow to Bypass Inerting Pressure Control Valve Into Drywell.Operators Cautioned ML20084N6711975-10-0707 October 1975 AO 50-249/75-43:on 750927,leak Discovered in Drain Line from Feedwater Heater 3D3 to Heater 3C3.Caused by Poor Weld Installation of Drain Line Pipe Support.Crack Ground Out & Pipe Rewelded ML20090E4641975-10-0202 October 1975 AO 50-237/75-44:on 750923,diesel Generator Failed to Start.Caused by Operator Failure to Follow Monthly Insp Procedure & QC Procedure for safety-related Component Replacement.Air Start Sys Inspected & Seal Ring Replaced ML20090E4701975-09-19019 September 1975 AO 50-237/75-43:on 750911,diesel Generator Cooling Water Pump Main Breaker Tripped.Caused by Excessive Heat Buildup within Breaker Housing.Breakers on Buses Replaced & Cover Plates Removed for Ventilation ML20084N6911975-09-16016 September 1975 AO 50-249/75-41:on 750908,intermediate Range Monitors 11, 12,14,16 & 18 Failed to Respond During Plant Startup. Apparently Caused by Personnel Accidentally Loosening Cables.Cables Replaced ML20090E4911975-09-0808 September 1975 AO 50-237/75-42:on 750829,diesel Generator Cooling Water Pump Tripped,Followed by Diesel Generator Trip on High Temp. Cause Not Established.Investigation of Cooling Water Pump & Associated Breakers Continuing ML20084N7771975-09-0404 September 1975 AO 50-249/75-38:on 750826,pressure Switches 3-263-52A1 & 52A2 Found W/Setpoints Above Tech Spec Limit.Apparently Caused by Setpoint Drift Due to Long Periods of Inactivity. Switches Reset ML20084N8411975-09-0404 September 1975 AO 50-249/75-37:on 750826,pressure Switches PS3-263-53A,53B & 53C Had Setpoints Above Tech Spec Limit.Apparently Caused by Setpoint Drift Due to Long Periods at Zero Pressure. Setpoints Reset ML20084N7281975-09-0404 September 1975 AO 50-249/75-40:on 750827,during Routine Instrument Surveillance,Pressure Switches PS3-263-51A & 51B Had Setpoints Above Tech Spec Limit.Caused by Drifting Due to Long Periods at Zero Pressure.Switches Reset ML20084N7481975-09-0303 September 1975 AO 50-249/75-39:on 750826,overload Relay Tripped Twice on Motor Operated Isolation Valve 3-220-1.Caused by Defective Overload Relay.Relay Replaced ML20084N7941975-09-0202 September 1975 AO 50-249/75-36:on 750823,reactor High Pressure Sensors 263-55A,55B & 55C Found W/Setpoints Above Tech Spec Limit. Apparently Caused by Extended Periods at Zero Pressure. Switches Reset ML20084N8661975-08-29029 August 1975 AO 50-249/75-35:on 750821,circuit Breaker 152-3403 Failed to Trip During Breaker Trip Test.Caused by Failure of Trip Coil.Breaker Replaced ML20084N8821975-08-15015 August 1975 AO 50-249/75-34:on 750807,isolation Condenser High Flow Switches 1349A & B Exhibited Instrument Setpoint Drift.Cause Unknown.Switches Reset ML20084N9051975-07-31031 July 1975 AO 50-249/75-32:on 750721,clamp Bolt Keeper Tack Welds on Jet Pumps 6 & 17 Failed.Caused by Poor Tack Welding.Clamp Bolt Keepers Rewelded & Successfully Retested ML20084E0461975-07-0303 July 1975 AO 50-237/75-22:on 750507,vol Bounded by Valves 2-301-98 & 2-301-99 Exceeded Max Allowable Limits During Local Leak Rate Testing.Caused by Dirty Mating Surfaces of Disc & Seat. Seating Surfaces Cleaned & Valve Returned to Svc ML20084D2111975-07-0303 July 1975 AO 50-237/75-36:on 750606,MSIV-1C 10% Closure Limit Switch Failed.Caused by de-energized 10% Closure Relay.Switch Reassembled W/Less Torque Applied to Switch Contact Assembly Screws.Switch Operated Successfully ML20084N9141975-07-0303 July 1975 AO 50-249/1975-31:on 750626,cracks Discovered on Collet Housings of Control Rod Drives 984,883,1032 & 1099. Apparently Caused by Temp Cycles Drive Experiences During Reactor Scram.Analyses Initiated ML20084D1771975-06-25025 June 1975 AO 50-237/75-58:on 750615,isolation Condensor Outboard Steam Supply Valve MO-2-1301-2 Found W/Bent Stem.Possibly Caused by Combination of Excessive Cycling of Valve 1301-2 & Maladjustment of Limit Switches for Valve Travel ML20084D0381975-06-23023 June 1975 AO 50-237/75-41:on 750613,electromatic Relief Valve 2-203-3C Failed to Operate During Test at Rated Pressure.Apparently Caused by Leaking Seal Rings in Valve.Valves Replaced by Rebuilt Valves & Successfully Tested ML20084N7741975-06-20020 June 1975 Followup to AO Rept Re Correlation of Fuel Failures, Identified by Wet Sipping Tests to Calcualted Violations of GE Pciomr ML20084D0531975-06-20020 June 1975 AO 50-237/75-40:on 750611,five Arrays Exhibited 5% Scram Times Exceeding Tech Specs Limits During 2x2 Array Test. Caused by High Regulated Pressure in Scram Valve Air Header. Regulator Reset to Correct Pressure ML20084D1411975-06-18018 June 1975 AO 50-237/75-39:on 750612,diesel Generator Failed to Start During Surveillance Run.Cause Not Known.Suitable Action to Be Taken When Cause Determined ML20084N9751975-06-13013 June 1975 AO 50-249/1975-30:on 750605,standby Liquid Control Pump Discharge Relief Valves Found at Setpoints Lower than Tech Spec Limits.Caused by Setpoint Drift.Valves Cleaned & Reset ML20084D1911975-06-13013 June 1975 AO 50-237/75-37:on 750604,diesel Generator Failed to Start on First Attempt.Cause Undetermined.Suitable Action Will Be Taken When Cause Determined ML20084D2161975-06-0505 June 1975 AO 50-237/75-35:on 750526,explosion Occurred in B Offgas Sys.Cause Not Determined.Load Drop to Minimize Releases Into Bldg Started ML20084D2211975-06-0505 June 1975 AO 50-237/75-33:on 750526,torus Level Found to Be Low.Caused by Personnel Error.Water Pumped from Condensate Storage Into Torus Via HPCI Min Flow Line.Importance of Card Tagging Procedures Emphasized ML20084D2251975-06-0303 June 1975 AO 50-237/75-32:on 750526,electromagnetic Relief Valve 203-3B Failed to Open During post-maint Testing of Valves. Cause Unknown.Corrective Actions to Be Determined When Cause Discovered ML20084D4121975-05-30030 May 1975 AO 50-237/75-31:on 750522,containment Cooling Svc Water Valve MO-1501-3A Failed to Control Flow During Scheduled Surverillance.Cause Not Determined.Design Mods for Valves Being Evaluated ML20084D4271975-05-30030 May 1975 Ao:On 750520,electromagnetic Relief Valve 2-203-3C Failed to Open During Scheduled Surveillance.Caused by Adjustment Problem in Pilot Valve Linkage.Capscrew Out of Adjustment. All Electromagnetic Relief Valves Adjusted ML20084D4321975-05-29029 May 1975 AO 50-237/75-29:on 750519,limit Switch Indicating 10% Closure on 1C MSIV Failed During Startup.Caused by Failure to Reinstall 1C Limit Switch & to Perform Tests.Switch Reinstalled ML20084D8811975-05-27027 May 1975 AO 50-237/75-27:on 750421,control Rod Withdrawn for Friction Testing While Both GE & Util Employees within Direct Line of Sight of Core.Caused by Disregard of Master Procedure & Failure of Testing Procedure to Include Precaution ML20084D3781975-05-23023 May 1975 AO 50-237/75-25:on 750116,Noshua Silver Duct Tape Dropped Into Reactor Vessel Annulus from Feedwater Sparger Work Platform.On 750516,decision Made to Start Reactor W/O Recovering Tape Rendering Tape Drop Reportable ML20084D4411975-05-23023 May 1975 AO 50-237/75-28:on 750506,containment Cooling Svc Water Valves MO-1501-3A & 3B Failed to Control Flow During Lpci/ Containment Cooling Logic Test.Caused by Bent Valve Stems. Increased Size Stem Valves on Order ML20084D8831975-05-23023 May 1975 AO 50-237/75-26:on 750415,diesel Generator Starting Air Motors Failed to Start Diesel Engine.Caused by Motor Pinion Gears Jamming Against Teeth of Ring Gear Preventing Proper Engagement.Vendor Suggested Mod to Regulate Pressure ML20084D8881975-05-21021 May 1975 AO 50-237/75-34:on 750513,drywell Equipment Drain Sump Pump Discharge Valve AO-2001-5 Failed to Close.Possibly Caused by Dirt on Solenoid Diaphragms.Valve Disassembled & Cleaned & Electric Conduit Insulation Repaired ML20084E0431975-05-21021 May 1975 AO 50-237/75-23:on 750511,diesel Generator Overheated After Inadvertent Fast Start & ECCS Inadvertently Initiated. Overheating Caused by Loss of Cooling Water Pump Suction. ECCS Initiation Caused by Valving Out Flow Check Valve 1977-03-31
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20249C8491999-09-30030 September 1999 1999 Third Quarter Rept of Completed Changes,Tests & Experiments Evaluated,Per 10CFR50.59(b)(2), for Dresden Nuclear Power Station. with ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20210R6081999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Dresden Nuclear Power,Units 1,2 & 3.With ML20209E1291999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20209J3481999-06-30030 June 1999 1999 Second Quarter Rept of Completed Changes,Tests & Experiments, Per 10CFR50.59.With ML20210D3071999-06-30030 June 1999 Corrected Page 8 to MOR for June 1999 for DNPS Unit 3 ML20195G6381999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206N2821999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20206B1901999-03-31031 March 1999 First Quarter Rept of Completed Changes,Tests & Experiments Per 10CFR50.59 for Dresden Nuclear Power Station. with ML20205N7491999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20207M6921999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML20199D3261998-12-31031 December 1998 10CFR50.59 SER for 1998-04 Quarter, of Changes,Tests & Experiments.With ML20199C8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Dnps,Units 1,2 & 3 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20197G8591998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Dresden Nuclear Power Station.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20196J0061998-11-19019 November 1998 Rev 66 to Topical Rept CE-1-A, QA Program ML20195D2861998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Dresden Nuclear Power Station.With ML20154L3681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20154N4131998-09-30030 September 1998 1998 Third Quarter 10CFR50.59 Rept, for Dresden Nuclear Power Station of Completed Changes,Tests & Experiments ML20153C5061998-09-21021 September 1998 SER Accepting Qualified Unit 1 Supervisor Initial & Continuing Training Program for Dresden Nuclear Power Station,Unit 1 ML20151Y2711998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237A7161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20236Q5851998-06-30030 June 1998 1998 Second Quarter 10CFR50.59 Rept, for Dresden Nuclear Power Station of Completed Changes,Tests & Experiments ML20236F8131998-06-30030 June 1998 Rev 0 to Defueled SAR Dresden Nuclear Power Station Unit 1 Commonwealth Edison Co ML20236T8331998-06-30030 June 1998 COLR for Dresden Station Unit 3,Cycle 15 ML20236T8391998-06-30030 June 1998 Rev 1 to EMF-96-141, Dresden Unit 3 Cycle 15 Reload Analysis Rept ML20236M6041998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20248M3021998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F3391998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20216D4411998-03-31031 March 1998 First Quarter Rept of Completed Changes,Tests & Experiments for 10CFR5059 ML20216C9651998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20216E2531998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Dresden Nuclear Power Station ML20202F7831998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Dresden Nuclear Power Station ML20199K1651998-01-23023 January 1998 Rev 65h to Topical Rept CE-1-A, Comm Ed QA Tr ML20198P5321997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Dresden Nuclear Power Station ML20198P7021997-12-31031 December 1997 Fourth Quarter Rept of Completed Changes,Tests & Experiments Per 10CFR50.59 ML20216D3611997-12-31031 December 1997 Unicom Corp 1997 Summary Annual Rept ML20203F8781997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Dresden Nuclear Power Station ML20199B0701997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Dresden Nuclear Power Station ML20217H7201997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20210V2401997-09-19019 September 1997 Rev 65g to Topical Rept CE-1-A, Comm Ed QA Manual ML20216J3781997-08-31031 August 1997 Monthly Operating Repts for Aug 1997 for DNPS ML20210H5511997-07-31031 July 1997 Monthly Operating Repts for July 1997 for DNPS IAW RG 1.16 & GL 97-02 1999-09-30
[Table view] |
Text
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One First P(Aal Plata. Chicago, ihmois Q'
l
,e' Addrsss Heply to: Post Office Box 767 Chicago. Illinois 60690 is p '..
W BBS Ler.#339-74 N' ' < .Dresden Nuclear Power Station
<' k. R. #1 f;k}.-Uf)
C (,j D, Morris,, Illinois 60450 f
M y 13, 1974
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% E$l, Mr. J. F. O' Leary, Directo 4 g Directorate of Licensing U. S. Atomic Energy Comission u g.{g Washington, D. C. 20545
SUBJECT:
LICENSE DPR-25. DRESDEN NUCLEAR POWER STATION. UNIT #3. REPORT '
OF ABNORMAL OCCURRENCE PER SECTION 6.6.B.2 OF THE TECHNICAL SPECIFICATIONS.
_FEEDWATER PRIMARY CONTAINMENT ISOLATION VALVE LEAKACE.
References:
- 1) Notification of Region III of AEC Regulatory Operations Telephone: Mr. F. Maura,1330 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.06065e-4 months <br /> on May 6,1974 Telegram: Mr. J. G. Keppler,1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> on May 6,1974
- 2) Dwgs: P&ID M-347
- 3) Letter to Mr. A. Giambusso from Mr. W. P. Worden (WPW Ltr.
d468-73) dated June 20, 1973.
- 4) Letter to Mr. J. F. O' Leary from Mr. B. B. Stephenson (BBS Ltr.#212-74) dated March 22, 1974.
Dear Mr. O' Leary:
This letter is to report a condition relating to Local Leak Rate Testing while the unit was shutdown for refueling. The test was conducted on the day shift on May 6, 1974. The test of the feedwater check valves, 3-220-58B and 3-220-62B, determined that the leakage through each valve was in excess of the Technical Specification limit. This malfunction is contrary to Section 4.7.A.2.f, which specifMd " at the total leakage rate through any one isolation valve will not eww 4 L o(48) t .
In addition, this letter reports the conclusions of the on site review regarding the fix to the Unit 3 feedwater check valves. This will satisfy the comitment for reporting review conclusions as made in a prior letter, reference 4, reporting test failure of valves 3-220-58A & 62A.
PROBLEM At the time of the deviation, the unit was shutdown for refueling and LLRT was being conducted.- '/ (
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1 -
, Mr. J. F. O'Le -
May 13, 1974 During te' sting of the Unit 3 "B" line check valves on May 6,1974, l excessive leakage was discovered from both tested volumes. One of the tested l volumes is bounded by valves 220-57B & 220-58B and the other is bounded by
- valves 220-575 & 220-62B. The leakage through 220-58B was 1,207.9 sefh.
- The leakage through 220-62B was 7.135.1 scfh. Both rates are in excess of l 5% Leo (48), or 29.381 sfch, the maximum leakage allowed.
I
- INVESTIGATION The 18" diameter swing type check valves (220-58B & 220-62B) were i
disassembled and inspected to determine the cause of the leakage. It was i determined that the "0" ring which seals the valve seat to the valve body was no longer in its groove on either valve.
This is the same condition, as found, on the "A" line check valves
- in March,1974 and reported in a letter dated March 22, 1974 (Reference 4).
5 Both the "A" and "B" line check valves were modified in June of
) 1973 (M12-3-73-112) . This modification replaced the original stainless i steel trim seal ring with a silicone "0" ring.
The silicone "0" ring is 3/16" diameter by 16" I.D. and confoms to MILR-5847 Class 2 Grade 70: Military Specification Rubber, Silicone, l Low and High Temperature and Tear Resistance. Class 2 has resistance to 0
extrema high temperature ( 425 F). ?
The absence of this "0" ring is the cause of the excessive leakage.
l CORRECTIVE ACTION An on site review (74-66) to determine a fix to the Unit 3 feed-water check valves was completed on May 2,1974. -
i Af ter reviewing the recommendations made by CECO's Engineering Department the review approved the use of a Viton "0" ring in place of the j Silicone "0" ring. The longevity of the Silicone "0" ring was not acceptable i
for its enviromnent. The Viton ring has good sealing characteristics, it will withstand radiation and should be better able to withstand environ-l mental conditions of the 3500 F water. The Viton "0" rings were installed in the "A" and "B" line valves and were leak rate tested successfully.
Satisfactory longevity can only be assumed based on manufacturer's data l until the next local leak rate test is conducted.
The success of the "0" ring modification and the anticipated' success of Viton "0" ring are such that during the next refueling outage of Unit 2 the same modification will be made.
[
t
, ..- Mr. J. F. O' Lea .
May 13, 1974 The retested data is listed below: i
. 1 Valve 220-58A 0.835 scfh l
- 220-62A 9.90 scfh 220-58B 0.00 scfh 220-62B 1.108 scfh l
1 EVALUATIONS An on site review (74-65) was completed on April 4,1974 regard-ing the missing "0" rings. A sample of the same material as the missing a "0" ring was analyzed. The results of the analysis indicate that they contained no substances to cause stress corrosion cracking. The material will break down under heat and radiation to form water, carbon dioxide and silica. The review concluded that the loss of the rings could have no significant affect on either present or future reactor operations.
i Considering the possibility of loss of the newly installed Viton "0" rings, the results of such loss were evaluated. The disadvantage of Viton, is that it contains flourides. According to DuPont, supplier of Viton, the ring contains 43 weight percent flourides. The flourides are tightly held within the molecules by covalent bonding with carbon. Thus it is unlikely that any significant amount cf flourides will be released.
Assumina a catastrochic failure releasina all flourides. the flouride content of the reactor pressure vessel water inventory will increase by 0.084 parts per million. Any flourides would soon be removed by the clean-up system. -
The modification (M12-3-74-87) which effects the change to Viton addresses the fact that no probability of an occurrence or consequence of
- an accident important to safety as evaluated in the FSAR is increased.
Concerning the leaking check valves, the occurrence did not endanger the safety of the public or of plant personnel.
The particular valves in question serve to prevent excessive release of reactor water (vapor) into the reactor or turbine building should the feedwater line break in either of these areas. Should the
- highly improbable break have occurred, the release would have been minor since the Icakage was through a circuitous path by the seal ring. If the leakage was into the secondary containment,.the Standby Gas Treatment System offers a sufficient barrier to keep offsite doses within 10CFR100 and station procedures protect plant personnel. If the leakage was into the turbine building, motor operated valves are available to effectively
, isolate the leak, with the exception of two lengths of approximately 12 feet each between the MO valves in the turbine building and secondary
, containment. The probability of a failure of this piping is so remote as to be considered non credible. Should it have failed station emergency procedures would have been the only protection.
- . , . . - - - - ,- -. a = - , , - - - , , - - - ,e . -,
o Mr. J. F. O' Leary o May 13, 1974 Cumulative experience on these valves has been poor regarding leak rate tests. As mentioned above, the Unit 3 valves were modified to produce a better seal at the low test pressure of 48 peig and retain equally effective sealing at high differential pressutes.
Now they have been modified to change the "0" ring material to one more suitable to the environment of the system.
Sincerely,
- s, /
j
/hhtfura B. B. Stephenson Superintendent BBS:JR:do 9
I l
.