ML20202G307

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Insp Repts 50-254/97-22 & 50-265/97-22 on 971027-1121. Violations Noted.Major Areas Inspected:Hpci Sys Operational Performance for Operations,Maintenance & Engineering
ML20202G307
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 02/13/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20202G241 List:
References
50-254-97-22, 50-265-97-22, NUDOCS 9802200105
Download: ML20202G307 (41)


See also: IR 05000254/1997022

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U. S. NUCLEAR REGULATORY COMMISSION

REGIONlli

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' Docket Nos: 50-254; 50-265

Lloonse Nos: DPR 29; DPR 30

Report Nos: 50 254/97022(DRS); 50 265/97022(DRS)-

. Lloonsee: . Commonwealth Edison Company

Facility: Quad 9ities Nuclear Power Station -

Location: 22710 206th Avenue North '

Cordova,IL. 61242

Dates: October 27 through November 21,1997

Inspectors: ' D. St..',or, Team Leader, Rill

. J.- Noisier, Reactor Engineer, Rlli

J. Guzman, Reactor Engineer, Rlll'

- D. Muller, Reactor Engineer, Rill'-

R. Pulsifer, Licensing Project Manager, NRR

J. Mallanda, NRC Contractor

S. Khabir, NRC Contractor :

Approved by: J. Jacobson, Chief, Lead Engineers Branch

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O k o M 54 '

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EXECUTIVE SUMMARY

Quad Cities Nuclear Power Station

NRC Inspection Report 50 254/g7022(DRS); 50 265/g7022(DRS)

This inspection assessed the HPCI system operational performance. In addition, the inspection

assessed the effectiveness of licensee controls in identifying and resolving problems. The

inspectors concluded that the HPCI system was capable of performing its safety function and

that, with exceptions, licensee controls were adequately identifying and resolving problems.

Qoerations

l .

During walkdowns on the Unit 1 ar . 2 High Pressure Coolant injection (HPCI) systems,

minor problems with material condition were identified. These minor problems did not

affect the operability of either units' HPCI systems. Minor procedure errors were also

l Identified with both the Unit 1 and 2 HPCI system checklists used to locally verify valve

positions. (Section 02.1)

1

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.

Some problems with HPCI system procedures were identified. One procedure,

concerned with local operation of the HPCI system, was inadequate. This was

considered a violation of NRC requirements. (Section 03.1)

.

The level of knowledge of two operators intervi9wed concerning the HPCI system was

Good. (Secilon 04.1)

e

Overall quality of the HPCI lesson plan used for training licensed operators was good.

Two minor nontechnical problems with the lesson plan were identified. HPCI system

training observed during this inspection was technically accurate and adequate overall.

(Section 05.1 and 05.2)

Mal 0lenaDCQ

.

Licenst., maintenance procedures were technically adequate, sufficient to perform the

required maintenance and inspection tasks and had the necessary provisions to identify

and evaluate deficiencies. (Section M3.1)

.

The performance by an instrument technician during an observed surveillance was

good. The technician precisely followed the procedure and demonstrated a good level

of skillin the use of the test equipment involved. (Section M4.1)

.

The mainteriance training program was adaquate to assure qualified maintenance

technicians. The training facilities were very good and were considered a strength.

(Section MS.1) l

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Maintenance activities were well controlled. The assignment of work week managers to I

coordinate activities was considered a strength. (Section MB.V '

Engineering

.

The inspectors noted that important calculations that form part of the Quad Cities HPCI

design basis were not easily retrievable, or did not exist. For example, at the inspecdon

onset, the licensee lacked a calculation to ensure that the HPCI design basis flow of

5000 gpm could be delivered against reactor pressure to support the acceptance criteria

in the Technical Specification surveillance procedure. The inspectors also noted that

the design basis for varicus safety related systems was not clearly established.

However, the licensee had initiated actions such as the Design Basis initiative UFSAR

review and was plannirig generation of approximately 15 missing analyses. (Section

E1.1)

+ While overall, the HPCI system mechanical calculations reviewed were found to be

acceptable, weaknesses were noted with nonconservative assumptions in an Initial

" white paper" analysis and with not consistently accounting for instrument inaccuracles.

(Section E1.1)

  • The HPCI system electrical calculations reviewed were generally acceptable, but

numerous examples of inattention to detall and weaknesses in the design verification

review process affected the quality of the analyses. Also, for some of the calculations

reviewed, the tracking of assumptions and of results which may impact other

calculations or procedures was weak. (Section E1.2)

.

The sample of HPCI system modifications reviewed was acceptable; however, a

violation of design control was identified. Other minor issues raised by the inspectors

were satisfactorily addressed by the licensee.

.

Overall, the inservice testing and Technical Specification (TS) surveillance testing

specifically related to the HPCI system were satisfactory. Based on a recent trend of TS

surveillance noncompliance and potential programmatic testing inadequacies, the

licensee had undertaken a root cause investigation to evaluate the trend and

recommend corrective actions to prevent recurrence. The effectiveness of these actions

could not yet be determined. (Section E2.2)

.

The inspectors concluded that the HPCI toom cooler was being adequately cicaned and

inspected pursuant to GL 89-13 commitments. Flow md differential pressure were

trended and monitored for degradation and cleaning v. 1 scheduled on a regular basis.

(Section E2.3)

+ Contrary to procedural requirements, the 50.59 screenings for two temporary alterations

failed to evaluate the physicalinsta!!ation of allinstrumentation installed by the

alteration. (Section E2.4)

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  • While the 50.59 safety evaluations reviewed were adequate with supportable

conclusions, weaknesses were identified with the overall 50.59 program. These

weaknesses included poorly written safety evaluations, incomplete summary report

submittals to the NRC, difficult to retrieve screenings, and incomplete corrective actions

to identified deficiencies. The incomplete summary report submittals were considered a

violation of procedural requirements. The Off Site review group, however, was

providing good assessments and comments. (Section E3.1)

+ Inaccurate figures and text in the UFSAR were Identified but the Inspectors also noted

ongoing licensee efforts to improve UFSAR accuracy such as line by line reviews of the

UFSAR design information and an initiative to ensure all facility changes had been

incorporated into the UFSAR. (Section 3.2)

+ Ouad Cities design basis information weaknesses were also exhibited with numerous

errors identified with the HPCI system design basis document (DBD). However, the

licensee was aware of the DBD shortcomings and had designated the DBDs as

"information only" pending completion of a validation process. (Section E3.3)

+ The inspectors reviewed commitments from Comed's March 28,1997, response to the

NRC's request for information pursuant to 10 CFR 50.54(f). The inspectors concluded

that eighteen 10 CFR 50.54(f) commitments were closed. (Section E7.1)

+

The inspectors reviewed the actions taken by Quad Cities staff for eight Systematic

Evaluation Program (SEP) topics and concluded that the actions taken were sufficient

for niosure of these items. NRC review of nine remaining SEP ltems was ongoing.

(Section E8.2)

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Report Detalla

1. Ooerations l

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02 Operational Status of Facilities and Equipment

02.1 High Pressure Coolant inlaction (HPCI) Sys'.em Walkdown

a. insoection Semne ,

The inspectors conducted walkdowns of the Unit 1 and 2 HPCI systems, which included '

- observations concerning the status of major HPCI components, piping, valves, and ,

associated electrical switchgear. During the walkdowns, the following procedures were  !

checked for adequacy:

. QOM 123001, " Unit 1 HPCI Checkoff List," Revision 4

+- QOM 2 23001, * Unit 2 HPCI Checkoff List," Revision 7

. QOM 12300-02,"HPCI System Fuse and Breaker Checklist," Revision 2

in addition, the above listed checkoff sheets and the as found statue of both units' HPCI

systems were compared to mechanical drawings M 46 for Unit i HPCI and M 87 for

Unit 2 HPCl.

b. Observatic,ns and Findings

Checkoff lists were used, in part, by the licensee to ensure that the HPCI system was

operable. Numerous mirar deficiencies were identified with checklist QOM 123001.

Checklist QOM 12300-1 incorrectly referred to valves 1239916 and 17 as HPCI

Booster pum' dMcharge vent valves, As determined by drawing M 46 and the label

tags attached so the valves, valves 1239916 and 17 were, in fact, HPCI Main pump

discharge vent valves. Checklist QOM 12300-1 incorrectly checked the HPCI steam

line drain line steam trap inlet valve 1230154. As determined by drawing M-46 and the

system walkdown, valve 12301 54 does not exist. It was later confirmed that this valve

had been removed by a system modification in 1994. Checklist QOM 12300-1 did not

indicate that the HPCI steam line drain line steam trap outlet valve 1230155, was to be

locked in position. As determined by drawing M-46 and the system walkdown, valve 1-

. 230155 was locked in position. Checklist QOM 12300-1 did not indicate that the HPCI

cooling water pump discharge valve 1230181, was to be locked in position. As

determined by drawing M 46 and the system walkdown, valve 1230181 was locked in

position.

With the exception of the 12399-16 and 17 valves nomenclature discrepancies, all of

the other discrr :ncies had been previously identified by the licensee and had been

incorporated into a procedure revision. At the time of this inspection, this procedure

revision to QOM 1-2300-1 was awaiting final reviews prior to implementation. Licensee

staff initiated action to conect the NRC identified nomenclature dlscrepancies

associated with the 1239916 and 17 valves.

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An additional discrepancy was also noted common to both units' checklists (OOM

123001 and 2 2300-1). Neither of these checklists required a check on keep fillline

test valves 1(2)-2399 78 and 79. If these valves were inadvertently in the wrong

position, there would have been the potential that keep fill would not have been

established, as required, if the operators manually selected the torus as the HPCI

suction source. These valves, however, were checked in the proper position quarterly

as part of surveillance procedure CCOS 2300 22," Quarterly HPCI Keep Fill Supply

Check Valve Closure Test," Revision 1. Control of these valves' positions was thus

never in doubt; however, the licensee agreed that these valves should be added to the

checklists,

During the system walkdowns, minor problems with material conditions were also noted.

The Unit i HPCI system had a small amount of oil on the floor in the vicinity of the oil

reservoir. Two valves for the Unit 1 HPCI system had no valve label tags, and one

valve for the Unit 2 HPCI system had no label tag. Two gages in the Unit i HPCI oil

system were not properly labeled. The licensee initiated action to correct these issues,

c. Conclusions

There were no issues identified during the walkdowns that affected either units' HPCI

system operability. Minor errors with the system checklists were identified (some of

these errors were previously identified by the licensee). Minor problems with material

condition were identified.

03 Operations Procedures and Documentation

03.1 HPCl System Procedures Reviews

a. Insoection Scogg

The inspectors reviewed the HPCI systems' (Unit i and 2) normal, abnormal,

surveillance, and annunciator response procedures for edequacy. In addition, several of

the above procedures were evaluated using real-time control room simulator exercises.

The inspectors also reviewed the sections of the Technical Specifications (TS)

corresponding to the HPCI system.

b. ObseIyfitions and Findings

Various procedures were exercised and system responses were observed using the

control room simulator. The exercises conducted included: auto initiation of the HPCI

system, HPCI turbine trip, auto isolation of the HPCI system, testing various HPCI valvo

interlocks, performing the quarterly HPCI full-flow surveillance, and a HPCI system oil

leak with the HPCI system injecting into the reactor vessel. There was no difficulty

encountered with any of the procedures used, and the HPCI system responded as

indicated in the procedures.

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During the procedure reviews, QCOP 2300-08, THPCI Local Manual Opera:lon,"

Revision 10, was identified by the inspectors as inadequate. Step F.2.b.(5)(b) of OCOP

2300-08, used to rapidly open HPCI steam isolation valve MO 1(2) 2301-4, instructed

operators b place jumpers between terminals FF 9 and FF 29 at incorrect panels. The

panel designations per this step were 90139 3E for Unit 1 and 902 39 iW for Unit 2. If

an operator had to rapidly open valve MO 1(2) 2301-4 per step F.2.b.(5)(b), he would

have:

(a) for Unit 1, realized that panel 90139 3E does not exist, or,

(b) for Unit 2 proceeded to panel 902 39-1W and realized that the jumper could not

be installed, since terminals FF 9 and FF 29 do not exist at panel 902 391W.

l In either case, the jumper would not have been installed. The correct panels would

have to be determined and authorization would have to be granted to proceed contrary

to the procedure as written. The licensee determined by conducting panel walkdowns

and reviews of the electrical prints that the correct panels for step F.2.b.(5)(b) were

90133 3E for Unit i and 902-331W for Unit 2.

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In addition QCOP 2300-08 Attachment A. "HPCI Local Manual Operation Restoration

Verification Sheet," has the operators verify a jumper removed for vacuum breaker

i isolation valve 2 2399-40, at panel 902 39 2W. The correct panel for this jumper was

902 391E. Additionally, Attachment A has the operators verify a jumper removed for

steam isolation valve MO 2 2301-5, at panel 902 39-2W. The correct panel for this

jumper was 902 39-1E. The licerisee initiated action via a PlF to correct these panel

deficiencies with a revision to procedure QCOP 2300-08.

10 CFR 50, Appendix B Critorion V," Instructions, Procedures, and Drawings," requires,

l In part, that act;vities affecting quality be prescribed by cocumented procedures and

shall be accomplished in accordance with these procedures. The inaccurate procedure

steps in QCOP 2300 08 which would not allow for rapidly opening the HPCI steam

isolation valve were considered a violation of 10 CFR, Appendix B. Criterion V (VIO

50 254/265/97022 01(DRS)).

During the review of HPCI system TS,it was discovered that all of the reactor water

level instrument setpoints (not just for the HPCI system) have different values than

those found in the normal, abnormal, surveillance, and annunciator response

procedures. This was due to a different choice of reference points for reactor water

level between TS and procedures, TS setpoints were referenced to the level in inches

above the top of active fuel (TAF). Setpcints in the procedures were referenced to TAF

being equivalent to 143 inches, which corresponds to the set up of the control room

water level indicators. For example, TS lists the HPCI low reactor water level auto

initiation setpoint as 84 inches above TAF, whereas the procedures list this setpoint as

59 inches. These setpoints are equivalent since TAF was equal to -143 inches

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Indicated water level. While this setpoint value difference was not considered a

significant issue and operators interviewed were aware of the distinction, the inspectors

coricluded it unnecessarily added confusion concoming the level setpoints,

c. Conclusions

While there was no difficulty encountered with any of the procedures exercised nor with

HPCI system response using the control room simulator, some problems with HPCI

system procedures were identl'ied. inspectors identified a violation of procedural

requirements in that the HPCI local manual operation procedure had three sections

where the procedure would have directed operators to incorrect panels, and therefore

this procedure could not have been performed as written.

04 Operator Knowledge sad Performance

04.1 ljPCI System Knowledge '

a. . Inspection Scone

The inspectors interviewed a licensed senior reactor operator and a licensed reactor

operator conceming the HPCI system.

b. Observations and Findings

The licensed operators interviewed were normally assigned positions on an operating

shift crew The licensed senior reactor operator typically was assigned the position of

shift supervisor and the licensed reactor operator typically was assigned a position at

the controls of one of the units. Without the use of reference material (except for

mechanical prints to explain system response), the licensed operators were asked the

following questions conceming the HPCI system:

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What is the purpose of the HPCI system?

+ When is the HPCI system required to be operable?

+ What measures are taken to ensure that HPCI la operable?

+ Describe HPCI OGA support proceoures.

+ Describe the HPCI auto initiation sequence. What setpoints cause an auto

initiation?

+ Describe the HPCI auto isolation sequence. What setpoints cause an auto

isolation?

Some additional questions were also asked conceming valve interlocks and recovery

from an auto isolation. Both operators interviewed provided accurate and detailed

answers to the above questions.

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c, . Conclusions

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The level cf knowledge of the two operators interviewed concerning the HPCI system

was good Both operators had no difficulty in answering the above questions

concerning the HPCI system.

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05 Operator Training and Qualification

05.1 HPCl System Lesson Plan

a. InspaciloDJacope

The inspectors reviewed the lesson plan used to train licensed operators on the HPCI

system. The inspectors also reviewed a sampling of modifications that have been

performed on the HPCI system, to check on their inclusion in operator training.

b. Observations and Findinas

Based on a comparison between the lesson plan and various other references

(procedures, TS, Updated Final Safety Analysis Report (UFSAR), mechanical and

electrical prints), no technical errors in the lesson plan were discovered, in addition, the j

lesson plan appeared to correctly incorporate modifications that have occurred to the ,

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HPCI syt, tem.

Hewover, two minor nontechnical problems were discovered with the lesson plan. The

first problem was that setpoints were not consistently presented in the lesson plan. For

example, in one location of the lesson plan, the actual setpoint for the reactor low

pressure isolation signal was listed (125 psig). In another location the TS required

setpoint for this function was listed (100 psig). The lesson plan by itself was unclear

about this setpoint, and the inspectors had to obtain clarification from the licensee. The

second minor problem discovered was that the section on HPCI auto initiation was

incomplete, in this section of the lesson plan, there was no mention of the repositioning

of three air-operated valves. However, the lesson plan previously mentioned these

effects when each valve was individually discussed. The auto initiation section,

therefore, would have been more complete if these three air-operated valves had been

included in the discussion within this section.

c. Conclusions

Overall quality of the HPCIlesson plan was good. The lesson plan was fairly extensive,

detailed, and accurato. Two minor nontechnical problems were discovered: the

treatment of setpoints and the completeness of the auto initiation section. One

additional measure of the effectiveness of the lesson plan was the previously discussed

(Section 04.1) good level of knowledge displayed by the operators conceming the HPCI

system.

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05.2 Trainina Effectiveness and Periodicity

a. Insoection Sggt

The inspectors observed the conduct of a HPCI system training presentatiori given to a

group of non-licensed operators. Additionally, the inspectors reviewed training

documents which Indicated the periodicity and scope of training which had been given--

l on the HPCI system.

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i b. Observations and Findinos

A training department instructor presented a lecture on the HPCI system to a group of

approximately 15 non licensed operators. The training session lasted approximately two

hours. The instructor followed the non-licensed operator lesson plan, which was similar

to the lesson plan previously discussed in section 05.1. The instructor presented

essentially factualinformation during the murse of the lecture. In some cases, the level

'of detail of the presentation was low. Hr. .sver, this appeared consistent with the fact

that this was a part of the licensee's continuing re-tralning program.

The HPCI system was trained on as part of the licensee's continuing re. -

training /requalification program. Additional training on the HPCI system had also

occurred (on a non-scheduled basis) when procedure changes and/or modifications to

} the HPCI system have occurred and during portions of control room simulator exercises,

c. Conclusions

The observed HPCI system training, presented by a training department instructor to a

group of non licensed operators, was technically accurate and adequate overall. The

periodicity of training on the HPCI system also appeared to be adequate. One measure

of the effectiveness of training on the HPCI system was the previously discussed

- (Section 04,1) good level of knowledge displayed by the operators conceming the HPCI

system.

II. Maintenance

M3 - Maintenance Procedures and Documentation

M3.1 Bay [gw of Maintenance Procedutta

a. - Insoection Scone

The inspectors reviewed selected maintenance and surveillance procedures for the

systems selected for inspection. The reviews were for technical adequacy and

satisfaction of vendor requirements and recommendations.

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b. Observations and Findinas ~

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The licensee procedures reviewed during this inspection appeared to be technically

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adequate to perform the specific maintenance task and provide for the identification and i

' evaluation of equipment and work deficiencies. Procedures included in the review were

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current. Modifications to equipment or systems had been included in the procedures  !

reviewed. .

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Maintenance and surveillance procedure content was compared against vendor's

' recommendations for the HPCI components. The procedures appeared to satisfy the

vendor's maintenance and inspection requirements.

- The licensee recently initiated the practice of conducting user reviews of maintenance ,

procedures. The inspector reviewed two of the procedures that had been reviewed and -

rearranged by the technicians who would be using the procedures and found the i

procedures were much Pnproved when compared to the original procedures.

c. Conclusions -

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The inspectors concluded that the licensee's procedures were technically adequate,

sufficient to perform the required maintenance and Inspection tasks and had the

- necessary provisions to identify and evaluate deficiencies.

M4.1 Performance of a HPCI System Surveillance

a. IDaggetion Scope

- The inspectors observed the performance of a non-licensed instrument technician

during the conduct of HPCI system surveillance, QCIS 2300-02, "HPCI Reactor Low

Pressure Analog Trip System Calibration and Functional Test," Revision 4. .

b. Observations and Findinas

QCIS 2300 02 was conducted on the Unit 2 HPCI system. The Unit 2 HPCI system was l

not required to be operable during the conduct of this survolliance, due e Unit 2 being in

cold shutdown. This surveillance consisted of the instrument technician hiserting

various test currents into the analog trip unit associated with each channel of the HPCI

reactor low pressure isolation function. The status of the trip unit and associated relays

were then observed to datermine if the trip and reset setpoints of each channel were -

within tolerance. Phone communications were utilized between the technician and

those personnel who observed the associated relays. During the performance of this

surveillance, the inspectors observed the following: ,

. The test equipment used appeared to be within calibration.

  • The procedure was precisely followed.

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The technician demonstrated a strong familiarity with the procadure and use of

the test equipment.

The technician understood the effects that procedure steps had on the system.

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The as found conditions of all of the trip units'setpoints were within tolerance. ,

No further calibrations were required. I

c. Conclusions

The overall performance of this surveillance was good. The technician had no difficulty

in following the procedure. The technician demonstrated a good understanding of what

each step in the procedule accomplished, in addition, the technician possessed a good

level of skillin the use of the test equipment.

M5 Malntenance Training and Qualification

M5.1 Maintenance Trainina and Qualification

a, laspection Scope

The team interviewed supervisors, workers and training staff. The team also reviewed

training records and toured the Quad Cities maintenance training facilities.

b. Observations and Findings

The team reviewed training records and interviewed training department personnel

,

relative to mtsintenance training for department personnel. The licensee had a

comprehensive training program for the Quad Cities maintenance staff both for Initial

training and qualification and for continuing training to malt"
In profielency.

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Th sam toured the Quad Cities maintenance training facility. The facility had

adt,quate space for separate facilities for conducting simultaneous training of

mechanical, electrical and instrument and control technicians. Each facility was well

equipped with training aids that either simulated or were identical to plant systems or

components.

The maintenance shope and supervisors were provided with a matrix t! ot detailed the

training and task qualification of each technician. These matrices were used to assure

that the Individual assigned to perform a task was trained in the performance of that

task,

c. Conclusions

The inspectors concluded that the licensee's maintenance training program was

adequate to assure qualified maintenance technicians. The training facilities were very

good and considered a strength.

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M8 Miscellaneous Maintenance issues

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M8.1 Maintenance Work Control

a, lasgention Ecoce i

The team reviewed work planning orocedures, work requests, planning processes and

interviewed work planners.

b. Observations and Findinga

Quad Cities had a well coordinated and organized control system for maintenance

activities. A work analyst was assigned to each maintenance team.

The NRC team observed a work week planning meeting for work scheduled two weeks

in advance. Work week managers were essigned for each week. Five of these

managers rotate through a three month maintenance cycle. Each is responsible for

coordinating and expediting work activities during their assigned weeks.

Review of work packages and discussion with preparers indicated that sufficient detail

was included in the packages to enable the technician to perform the required tasks.

c. Conclusions

The team concluded that maintenance activities were well controlled. The assignment

of work week managers to coordinate activities was considered a strength.

Ill. Engineerina

E1 Conduct of Engineering

Ei,1 Mechanical Design Calculations

a. insoection Scoon

The inspectors reviewed mechanical calculations to determine if the purpose, scope,

assumptions, analysis methodology, acceptance criteria, and conclusions were

acceptable, in addition, numerous supporting documents were reviewed as reference '

in the calculations. This included design basis calculations for HPCI system thermal-

hydraulic, piping stress, and equipmont sizing,

b. ' Observations and Findings

The inspectors noted that important design basis parameter calculations for the HPCI

systems were not readily retrievable or simply not available. For example, a calculation

to ensure that the HPCI design basis flow of 5000 gpm could be delivered at varying

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reactor pressures was not available. Subsequent interviews with the licensee revealed

that Quad Cities staff had identified this design basis and configuration control concern

and were in the process of scheduling and generating approximately 15 new analyses

and calculations in various systems as part of a corporate wide effort.

During the inspection, minor concerns identified by the inspectors were addressed via '

PIFs, more significant technical or design basis concerns are listed below:

.

Calculation ODC 2300 M-0486,' Verification of HPCI Pump Discharge Flow to

Reactor,' Revision O.

This calculation was not available prior to the inspection and was generated end

completed during the inspection. The inspectors were concerned that the

{

information from this anclysis, which is needed to appropriately determine test '

acceptance criteria, was unavailable in the Quad Olties design basis. However, .

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the calculation successfully confirmed that after accounting for line losses, the l

TS Surveillance test capacity and discharge pressure acceptance criteria, for the

HPCI pump, assured operability by delivering greater than 5000 gpm against '

reactor pressure as high as 1120 psig. The calculation determined that rated

flow of 5,036 gpm can be delivered at the HPCI pump discharge pressure of

i 1189.4 psig and corresponding reactor pressure of 1120 psig, exceeding the

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design basis assumptions. The calculation provided adequate assurance of

HPCI system operability and its capability to deliver rated flow.

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Calculation ODC 2300-M-0489, " Air Entraining Vortices for the HPCI Pumps,"

Revision O.

As part of NRC's initial Inspection information requests and subsequent

l questions on the contaminated condensate storage tanks (CCST) usable

1 volume, the licensee generated this calculation to ensure that air would not be

introduced into the HPCI pump. The engineering staff initially stated in a white

paper analysis that air entraining vortices would D01 be predicted because the

mlnlmum submergence of one pipe diameter (11.7 In.) existed at Quad Cities

CCST. However, in response to inspector and licensee identified concerns with

the white paper's nonconservatism, engineering prepared a formal calculation,

QDC 2300-M-0489 Rev. O, to comprehensively address vortexing and minimum

usable water issues. The calculation addressed: (1) the usable volume

available to the HPCI system and the Reactor Core Isolation Cooling (RCIC)

system from the CCST, (2) adequacy of water supply to preclude vortexing in the

CCST and determine the ability of HPCI and RCIC suctions to switch over to the

torus. The maximum acceptable time for the switchover to prevent entrained air

from reaching the pumps was 115.4 sec. While the inspectors determined the

calculation to be acceptable, the inspectors noted that the elevation of the low-

level switch activation setpoint was determined to be 40 inches above the bottom

of the tank and did not include any inaccuracy. Additionally, the CCST low level

switches 1.S 1(2)-2350A/B/C/D have 3 9/16 inch (switch actuation rising level)

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and 4 7/16 inch (switch actuation falling level) setpoints with +/ 1/4 inch

accuracles which were also not accounted for in the calculation.  ;

Calculation QDC 2300 M-0189, *NPSH Available For the HPCI Pumps," Rev. O

and Rev.1 (PIFs Q1997-03985 & 04087).

The inspectors noted that under LOCA conditions, revision 0 of this calculation

did not include friction losses due to Installation of new torus strainers, The

licensee revlsed the calculation and the inspectors determined that sufficient

NPSH Available margin existed.

c. Conclusions

The insp)ctors noted that important calculations that form part of the Quad Cities HPCI

design basis were not enslly retrievable, or did not exist. In response to NRC questions,

and to clarlfy HPCI operability requirements, the licensee generated various calculations

while the team was onsite. While overall, the HPCI system mechanical calculations

reviewed were found to be acceptable. Weaknesses were noted with non conservative

assumptions In an Initial * white paper" analysis and in not consistently accounting for

Instrument inaccuracles.

l

E1.2 E[ect:.:al Deslan Calculatiqat

a. Insoection Scone

The inspectors reviewed the following electrical calculations to determine if the purpose,

scope, assumptions, analysis methodology, acceptance criteria, and conclusions were

, acceptable, in addition, numerous supporting documents were reviewed as referenced

in the calculations,

b. Observations and Findings

.

Calculation PMED 891377 01," Development Of a Duty Cycle Based On a More

Conservative Application Of Colncident Starting Currents For The 250Vdc

Battery Sizing," Rev 11.

The purpose of this calculation was to assess the impact on battery sizing of a

more conservative assumption ccncerning coincidence of starting currents for

loads actuated by separate relays or devices. In general, electrical Calculation

PMED 891377-01, Rev.11, was adequate but attention to detail affected the

quality of the calculation and weaknesses in the design verification review

process were noted. Specifically:

  • The control power for valves 1/ 2 2399 41 was not modeled in the

calculation. This load was estimated to be less than an ampere and did

not significantly affect the results. PIF 4329 was generated to address

this issue.

15

_ _ _ _ _ _-_ ______-_- - -

,

t

.

Revision 11 of the calculation was performed to evaluate the abnormal

lineup condition when the 250Vdc buses from Unit 2 were connected to

Unit i because the battery was being tested on Unit 2. The conclusions

stated that a review of the previous test results should be performed by

the station to ensure that the battery capacity was close to 100% prior to

configuring the plant in the abnormal configuration. The licensee

generated PlFs 4143 and 4354 to correct plant procedures that do not

contain any prerequisites to require a review of the previous capacity

tests,

i

.

The Inspectors determined that the cable lengths utilized in Attachment 6

of Calculation 004 E-043 were nonconservative for the application due to

the 1.2 multiplier of each estimated cable length. Attachment 7,

Calculation 004 E-044, for Unit 1 was also impacted. The licensee

preliminarily determined and the inspectors concurref " at using the

correct cable lengths will have a minor impact on the battery loading.

(PlF 4302)

l

+

Calculation 8250 50101, "250 Vdc System Short Circuit Current," Revision 1

and Revision 2.

The purpose of these calculations was to determine the Quad Cities Station

250Vdc system available short circuit current at each system bus for use in

studying system coordination and for con.parison with overcurrent device

interrupting ratings.

  • Revision 2 incorporated the overload heater resistance in the circuits with

[ combination starters and reduced the short circuit currents below the

breaker ratings that had been identified. This reduction was

accomplished F 'ertain minimum resistance overload heaters were

installeo. Nine Dreakers had not been identified during walkdowns and

the calculation recommended obtaining the ratings of these breakers.

The inspector questioned the followup of the nine unidentified breakers in

the calculation and the licensee stated that the followup had been-

performed in accordance with Letter 209332,250Vdc Circuit Breaker

identification and Interrupting Capacity, but the calculation had not been

- revised. PlF 4453 was generated to address this issue. The licensee

indicated that the breakers or their use in combination starters had

sufficient interrupting capacity to interrupt the maximum short circuit

currents without damage.

  • The calculation did not include a short circuit analysis for the abnormal

alignment identified in Calculation PMED 891377-01. PlF 4399 was

written to address this issue.

.

The inspectors identified discrepancies lo horsepower ratings for the

HPCI Turbine Gland Steam Condenter Exhauster and the Drain Pump

16

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4

.

i

between the calculation and applicable drawings. The discrepancies did

not appear to have a significant effect on the calculation results. PlF

4366 was written to address this issue.

.- Study SL-4501, 'Overcurrent Protective Device Coordination Study,' Volume 4.

The purpose of this study was to respond to Generic Letter 8815. Technical

issue 5, which discussed the necessity to ensure that circuit breakers and

protective devices within the onsite electrical distribution system were properly

coordinated. The licensee identified that the UFSAR has no specific statement

for 250Vdc overcurrent protection devios coordination. The Quad Cities

Appendix R Fire Protection Program was based primarily on the procedural

- tripping of a particular list of associated circuits for a fire in a particuler fire zone

and, therefore, did not take orodit for protective devios coordination. The study

also noted that the current IEEE Standard 9461985 requires protective device

coordination. The study concluded that certain breakers without starters should

be replaced and somo upstream breakers required replacement with breakers

that have long-time and short time (no Instantaneous) trip units or time delay

fuses or bus rearrangement if system coordination was to be achieved. The

licensee statea tha' r * allure modes and offects analysis dated September 14,

1990, and an evaluation of operability determination checklist, ENC-QE 40.1,

Rev 0, had been completed to document justification for continued operation.

However, outstanding coordination issues were pending resolution. Resolution -

of these protective device coordination issues was considered an unresolved

item pending further review of licensee actions (URI 50 254/265/97022-02),

e

Calculation 8913 7719-1, *250Vdc Battery Interconnecting Jumper Ampacity,"

Revision 0,

The existing Unit 1250Vdc battery was being increased from 116 oells to 120

l

- cells. The purpose of this calculation we9 to determine the jumper installation -

ampacity for the connection to the additional four cells and a comparison of the -

calculated ampacity to the battery duty cycle loadin0. Whlie overah the

calculation was adequate, the inspectors noted that at the time that the

calculation was performed the maximum discharge current in the load profile was

'1001 amperes for the first one minute load. <The continuous duty rating of the

jumper cab's was calculated to be 980 amperes. Calculation PMED 891377 01, i

Rev 11, shows 1276.4 amperes for the ce minute load for the abnormal

alignment case. Even though this overload condition of the jumper cables was of

short duration, calculation 8913 7719-1 had not been updated to address this

higher current. PlF 4397 was generated to address this issue.

.-

Calculation QDC-8350-E-0074, ' Input and Output Cable and Circuit Breaker

Sizing for the #2 250Vdc Battery Charger,' Revision 1.

The purpose of this calculation was to size the AC supply and de output cables

for the Unit 2 250Vdc battery charger. The settings of the input and output

,

_ . _ _ _ . _ m _ __ - - - - - - - - - - - - -

.

__

.

I

breakers were also determined. Overall, the calculation was considered

acceptable, but the inspectors noted that the recommendation that the charger

output be limited to 300 amperes DC (120% of rated output) had not been

incorporated into plad procedures,

c. Conclu11ons

The HPCI system electrical calculations reviewed were generally found adequate but

numerous examples of inattention to detMI and weaknesses in the design verification

review process affected the quality of the analyses. Also, for some of the calculations

'

reviewed, the tracking of assumptions and of calculation results which may impact other

calculations or procedures was weak.

E2 Engineering Support of Facilities and Equipment

E2.1 Modifications

a, laspection Scopa

The team reviewed mechanical modification packages to ensure the licensee's

effectiveness in proper implementation of design basis documentation. The review

included the modificaL9 recommendations,10 CFR 50.59, UFSAR, and Technical

Specification changes. r 0st modification test requirements were reviewed to determine

8

if testing was sufficient to ensure that the equipment would perform its intended function,

and determine if plant procedures were properly updated to reflect the modification,

b. Qhservation and Findings

The sample of HPCI modifications reviewed was found to be acceptable with the

exception of the following issues:

  • In response to the SOPl, the licensee identified that the HPCI steamline high

flow 310-9 second time delay to initiate closure of the HPCI AC-inboard-

isolation valve did not factor in the additional 10 second EDG loading time for a

loss of offsite power event concurrent with a HPCI steamline break. PlF 4344

was initiated on November 12,1997, to track this concern. The overall HPCI -

DC-outboard steamline isolation valve closure time was unaffected. The AC and

DC valve close logics were changed by modification M04-1(2)-91-013, * Modify

Break Detection Logic to Prevent Spurious isolation of HPCl"in response to

NUREG-0737, item II.K.3.15. The licensee initiated an issue Screening Form,

dated November 14,1997, to determine if an operability concern existed. The

longest overs AC inboard isolation time was determined to be 69 seconds. The

licensee concluded that the increased AC isolation time was within the time

assumed in the Updated Final Safety Analysis Report (72 seconds including

valve closure time). However, failure of the modification package to address the

additional AC Inboard isolation valve closure time during a loss of offsite power

event was considered a violation of 10 CFR 50, Apoendix B, Criteria Ill, * Design

18

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1

.

!

Control." The inspectors reviewed the lasue Screaning Form and concluded that

the increased AC inboard Isolation valve closure time was within the design

basis. (VIO 50-254/97022-03; 50 265/97022 03)

+

HPCI Booster Pump 4 Vane Impeller Replacement.

The inspectors reviewed the HPCI booster pump 4 vane impeller replacement

with 5-vano impeller modification. The impeller was replaced to address

vibration problems. The pump curves for the new 5 vane Impeller were based

on the known hydraulle performance of the 4-vane Impeller originally supplied.

The added vane reduced the outlet area of the Impeller by a small amount and

l

resulted in a 2% decrease in the impeller tip velocity. Thus, the pump head was

reduced by 2% near the design point. To compensate for the loss in head, the

Impeller diameter was increased from 22.375 to 23 inches. The inspectors noted

that any adverse effects of a potentially higher pump shutoff head resulting from

the larger Impeller had not been addressed, in response, the licensee

demonstrated that the changed shutoff head lik,-ly would be minimal and

generated PlF#Q1997-04459 to address this issue.

.

Modification M04 2-01034, Addition of four Cells to Unit 2 250 Vdc Battery.

Overall this modification was acceptable but the inspectors noted that licensee

had waived the operability testing of the battery since the four cells had

successfully passed an acceptance test by the manufacturer prior to shipping

and the unmodified 250Vdc system had successfully passed a service test eight

months earlier. However, the factory acceptance test was a capacity test and

', did not verify the ability of the new cells to meet their required load profile. The

licensee wrote PlF 4193 to address this issue.

.

Modification M04-0-82-025, " Replace the Unit 0 250Vdc Battery Charger."

On Site Review Checklist QAP 1270-S?.7 indicates that no setpoint changes

were required for this modification. However, the Release for Testing Checklist

QAP 1270-S28 indicated that setpoint changes were required. The inspectors ~

concluded that the setpoints were computer point additions. Further review

indicated that the setpoints had been tested. PlF 4359 was generated to confirm

that the computer points were properly tested during the modification test,

c. Conclusion

Overall, the sample of HPCI system modifications reviewed were acceptable, however a

violation of design control was identified. Other minor issues raised by the inspectors

were satisfactorily addressed by the licensee.

)

19

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. - _ _ _ _ _ _ _ _ _ - _ _ - _

,

.

E2.2 BPCI System IST and TS Surveillance Testlna Review

a. Insoection Scoce

The inspectors reviewed HPCI surveillance and inservice testing (IST) documentation

including test procedures UFSAR, Technical Specifications, calculations and other

design basis documents.

b. Qbservations and Findinas

The team's reviews of the licensee's HPCI system surveillance and IST testing program

Indicated that ths HPCI system test related procedures generally contained clear and

sufficient preparation and alignment steps, acceptance criteria, and verification steps.

The inspectors noted that the TS surveillance test procedures' acceptance criteria

adequately demonstrated continued operability.

IST records reviewed showed that the licensee monitored and trended test results for

each component to detect degradation; reconfirmed or established reference values for

pump vibration, differential pressure, and flow following maintenance or replacement; .

and verified that the new reference values represented acceptable operation. When

testing results indicated component performance was outside the acceptance range, the

licensee took appropriate corrective action as directed by ASME Section XI and the

, licensee corrective action process.

I

Based on reviews of the completed test procedures and followup documentation, the

inspectors noted that engineering staff adequately supported and contributed to

surveillance test evolutions and were involved in review of test results and test

anomalies.

However, as noted elsewhere in this report, an area of concern was raised in the weak

, design basis availability or retrievability. While ultimately the HPCI system test

l acceptance criterla were considered consistent with the design basis, this had not been

I

fully confirmed until completion of all analyses and calculations. For example, the HPCI

pump's differentiel pressure acceptance criteria included an additional discharge

pressure of 100 psl to address frictional line losses between the pump and the reactor.

The licensee identified that no readily recoverable Quad Cities calculation existed to

confirm that the 100 psl was appropriate and had a technical basis. To address this,

during the inspection, the licensee wmpleted an analysis (Calcu.ation QDC-2300 M-

0486) detalling the piping system resistances. As noted in Section E1.1 of this report,

1% talculation satisfactorily documented that the test acceptance criteria for IST and TS

surveillance testing were adequate. The calculation concluded that the HPCI pump

must produce a minimum of 75 psi above reactor pressure when delivering design ,

flowrates therefore the 100 psi pressure drop value used in the test procedures had (

been acceptable.

Based or, a recent trend of licensee and NRC identified TS surveillance non-

compliances, the licensee had also initiated a root cause investigation to evaluate the

_ __

20

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,

,

trend of testing deficiencies indicating a potential programmatic concern. Numerous

licensee and NRC findings of deficiencies in this area including NOVs, LERs, PIFs, and

other corrective action records were assessed under Root Cause Investigation Report

(NTS 254 200 97 SCA000088). The investigation identified root causes to be

programmatic weaknesses in the testing predefine process, inadequacy of proceowes,

inadequacy of work-in-progress testing, and human errors. Corrective actions that were

in progress of being implemented to prevent recurrence included reviewing all

implementing procedures to verify TS requirements were satisfied, validation of the

EWCS data for all TS related predefinC, F':engthening of interfcces related to TS

changes, procedure revision and modifics.,on processes with the surveillance program.

While the inspectors did not identify further testing concerns, the team concluded that

insufficient time had passed to gauge the effectiveness of these corrective actions,

c. Condus10DR

i

l

Overall, the IST and TS surveillance testing specifically related to the HPCI system were

satisfactory. Based on a recent trend of TS surveillance noncompliance and potential

programmatic testing inadequacles, the licensee had undertaken a roct cause

investigation to evaluate the trend and recommend corrective actions to pmvLt

recurrence. The effectiveness of these actions could not yet be determlu ..

E2.3 HPCI Room Coolers / GL 89-13

l a. Insoection Scopa

!

l

'

The team reviewed the inspection and cleaning program for the HPCI toom coolers

developed in response to Generic Letter 8913. Procedures reviewed included QCOS

5750-09, ECCS Room Cooler Monthly Surveillance and OCTP 111012, 'ECCS Room

Cooler Trending Program," Rev. 2 OCOS 5750-05," Quarterly Testing of SW supply

HPCI Room Cooler Check Valves," Rev. 3, QCCP 1005-05, * Equipment inspection

Program,' Rev.1. Additionally, the inspectors reviewed calculations on the heat

removal capacity of the HPCI room coolers versus design basis heat loads as well as

calculation NED-H MSD 26 which determined the minimum flows to the room coolers at

design river temperatures and, for future operability determinations, at varying river

temperatures and flow rates.

b. Observations and Findings

Quad Citics has implemented an inspection program for the HPCI room coolers, with

,

cleaning as necessary, in response to Generic Letter 8913. Tne inspection and i

cleaning on a regular interval was implemented in lieu of thermal performance

monitoring as these coolers were not conducive to thermal performance monitoring.

Additionally, inlet, outlet, differential pressure and flow were monitored monthly to trend

cooler fouling and plugging. Inspections were being performed every refueling outage

or more often depending on the trend information.

21

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_ _ _ _ - _ _ _ _ _ _ - _ _ - -

.

.

OCOS 5750-09, Rev.10, 'ECCS Room Cooler Monthly Surveillance," adequately

provided instructions for performing the differential pressure and flow test for the HPCI

.

room coolers. Features were provided in inspection procedures ud process for timely j

detection of flow degradation. Cooler cleaning and inspecting was conducted as a

regular Mechanical Maintenance PM every outage. OCCP 1000-05, Rev.1

  • Equipment inspection Program," provided sailsfactory instructions for inspecting heat

exchangers, condensers and other equipment for corrosion, foullng and biological

growth.

System engineering used QCTP 111012, *ECCS Room Cooler Trending Program," to

analyze and trend the differential pressure and flow information taken monthly using

QCOS 5760 09. The procedure adequately directed the engineers to set up low and

high dP criteria and gave appropriate criteria on when to write a PlF for adverse trends,

c. ConcluslQD1

The inspectors concluded that the HPCI room cooler was being adequately cleaned and

inspected pursuant te GL 8913 commitments. Flow and differential pressure were

trended and monitored for degradation and cleaning was scheduled on a regular basis.

E2.4 Temocrarv Alterations (TALT)

a. Insoection Scone

The Inspectors reviewed several temporary alterations to ensure the process followed

,

applicable procedures. The documents reviev.ed included the following:

l

QAP 0300-12, Revision 31, ' System Temporary Alterations"

NSWP A-04, Revision 0,"10 CFR Safety Evaluation Process'

TALT No. 96-1005, ' Fine Tune HPCI Flow Controller at Direction of System Engineer"

TALT No. 961063, " Connect Chart Recorder to HPCI Oil Pressure Switches to

Monitor Pressure during Q1R14"

!

TALT No. 961 116, ' Connect Recorder / Monitor HPCI Parameters during 7tartup"

TALT No. 97-2-043, " Block Signals to Prevent Control Room HVAC isolation"

b. Observations and Findings

b1. Temporary Alteration No. 961005 installed test equipment on the Unit 1 HPCI system

to obtain performance data. The 50.59 screening approved on January 26,1996,

described the preposed change as the connection of a strip chart recorder to various

banana Jacks to monitor six (6) parameters in order to fine tune the control system. The

screening stated that the recorder would be the only interface with the affected

instrument loops. Recorder failure modes (open/ shorts) were addressed in the

screening. The inspectors noted that Work Request Task 950119950-01 also installed a

movement transducer on the turbine linear variable differential transformer (LVDT) lever,

a movement transducer on the secondary operating lever, and three (3) pressure

gauges. However, the original screening did not evaluate the physicalinstallation and

22

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4

.

failure modes of the additionalinstrumentation per Procedure NSWP A 04. Section

' 2.5 of this procedure stated, in part, that previously performed screenings can fulfill the

.

scre.,ning requirement provided they meet the validation criteria of Exhibit H. *Valiaation

>f Previously Performed Safety Evaluations and Screenings," to determine if an existing

poening remains valid. The work control process did not identify that the installation of

additional instrumentation to the HPCI system altered the previous screening evaluation.

This example was considered an example of a violation of 10 CFR 50, Appendix B,

Criteria V, for not following NSWP A-04. The licensee initiated PlF 4500 to track this

item. The safety consequences were minimal since the unit was shut down and HPCI

was not required to be operable (VIO 50 254/97022 048).

b.2 TALT No. 961063 installed test equipment on the Unit i HPCI system to record

various parameters during surveillance testing. The screening approved on

r ebruary 28,1996, described the change as the connection of a strip chart recorder.

The screening stated that the recorder would be the only interface with the affected

instrument loops. Recorder failure modes (open/ shorts) were addressed in the

screening. The inspectors noted that Work Regeest Task 950084936 01 also installed

three (3) Valldyne pressure sensors. However, the original screening did not evaluate

the physicalinstallation and failure modes of the additionalinstrumentation per

l Procedure NSWP A-04. Section 6.2.5 of this procedure stated,in part, that previously

performed screenings can fulfill the screening requirement provided they meet the

validation criteria of Exhibit H, Validation of Previously Performed Safety Evaluations

and Screenings," to determine if an existing screening remains valid. The work control

process did not identify that the instal;ation of additional instrumentation to the HPCI

system altered the previous screening evaluation. This example was conslaered an

example of a violation of 10 CFR 50, Appendix b, Criteria V, for not following piocedure

NSWP A 04. The licensee initiated PIF No. Q1997-03981 to track this item. The safety

consequences were minimal since the unit was shut down and HPCI was not required to

be operable (VIO 50 254/97022-04b).

b.3 TALT No. 97 2-43 (Design Change Package 9700126) Installed relay blocks on relays

2 595102A/B/C/D to maintain the relays in a simulated energized state to prevent the

control room ventilat;on system from isolating. These relays Initiate main steam line

Isolation and control room ventilation system isolation for a main steam line high flow

condition. The relays were blocked for instrument mechanic Out-of Service No. 21122

walkdowns. The main steam flow channels were required to be operable during

operational Modes 1,2 and 3, Since Unit 2 was shutdown, the 50.59 screening

preparer determined that only UFSAR chapters for the current operating Mode were

applicable. As a result, NSWP A-04, Exhibit E,"10 CFR Screening For Facility

Change," Question 2, may not have listed all applicable UFSAR sections. While t;ie

Inspectors determined thct the safety consequences were minimal since the unit was

shutdown, this was of concern since the requirement that a full safety evaluation be

completed may have been circumvented. The licenroe initiated PIF 4394 to track this

itern. Pending NRC review of the affect of application of all modes of operations, the

inspectors considered this an unresolved item. (URI 254/265/97022-05)

23

e - -,y

y '

<

\c. Conclualana

s,

.,

" Contrary to procedure NSWP-A-04 requirements,50.59 screenings for two (2) -

~ Temporary Alterations reviewed by the inspectors did.not evaluate the physical ~

Installation of allinstrumentation installed by the alteration.-

'

,

E3 ' Engineering Procedures and Documentation

f E3.1 ~ 10 CFR 50.59 2 * 'W Evah a+' -7 Prae === ,

-

-

. a.1 inapaction Scone

~

The inspector reviewed a sarhpie of HPCI 50.59 safety evaluation reports with

4

- associated PlFs and NTS reports and the following procedures and documents.;

'

.

, ." Changes, Teste, arid Experiments Completed," LWP 96-048, dated July 08 .

.- 1996.

,

'

  • -

" Summary Report of Changes, Tests and Experiments Completed,' SVP-97-251,

" dated October 31,1997

  • -

NSWP-A iO4, Rev. O, "10 CFR Safety Evaluation Report"'

'

Y "50.54(f) Task Assignment, Configuration Control Process"

a

.

s '" Conduct of Off-Site Reviews," N.O.-16, Revision 9, dated October 8,1997

4 ,s )

  • -

" '

. Updated Final Safety Analysis Report (UFSAR) Update," ESK-96-113, dated

f LJune 7,' 1996 -

E .

.

_

a

[ + l " Updated Final Safety Analysis Report (UFSAR) Update," SVP-97-242, dated

. 1 October 22,1997a ' '

b .

-

b.1 Findinga and Observations

. .

N -:b;11 General Weakna==== in 50 59 Proaram --

" -

,

lThe 10 CFR 50.59 safety evaluations (SE) reviewed were adequate and conclusions

were supported; however, several general weaknesses were identified.

i Safety Evaluation (SE)96-061 was approved in July 1996 to correct the i

L op;ating pressure range for HPCI in the UFSAR from 1150 psig to 150 psig to

7".

the value 1120 psig to 150 psig. A mathenutical error was introduced during a

previous UFSAR update when the values were converted from absolute

pressure to gage pressure. On September 24,1996, SE 96-061 was checked to

confirm its accuracy and conclusions against UFSAR, Rev. 3 olus approved l

UFSAR change packages because the subject SE may have been initially  ;

l

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evaluated using UFSAR information which did not contain Rev. 3. ;On June 28,

1996, the NRC approved the new Technical Specmcations (TS) which were -

' implemented on Sopiomber 23,1996. These new TS included the same error in

its Bases of TS Section 3/4.5.A and B; however, it '.vas not recognized by the

- reviewer. This change was made in UFSAR, Rev. 4 issued by letter dated

October 22,1997, and PIF 4147 vias initiated on October 30,1997, to address

the TS Bases error. The development of SE 96-061 and the subsequent review

- should have included a review o' Be new TS Bases in the evaluation.

- i

NSWP-A-04, Rev. O, Attachment G, Step 13, requests the preparer to check one -

of four appropriate conditions to determine the effect on Margin of Safety. One

of the conditions reads: "The change does not affect any parameters upon

which Technical Specifications are based; therefore, there was no reductm in
the margin of safety r proceed to Step 15." The SE does not require an -
explanation as to the rationale for that choice as it does fcr the other three ~ ,
conditions.- This condition was chosen for the majority of the 50.59 summaries

provided in the 50.59 report issued October 31,1997, and the 50.59 SEs

reviewed. Several of these SEs involved changes to' safety related equipment

and, without a rationale for the conclusion of "no effect on any parameter upon

<

' which the TS are based," It was not intuitive to conclude that there was no -

reduction in the margin of safety.

  • -

The 50.59 report," Summary Report of Changes,' Tests and Experiments

Completed," SVP-97-251, dated October 31,1997, included a summary of SE

1

96 043 which evaluated changing the UFSAR to address a new TS concoming -

'

heater power for the am filtration unit heater. The summary states in step 3 that,

_ "The margin of safety as defined for any Technical Specification, is reduced

because the actual Tech Spec requirement for heater-power is not given in the .

UFSAR and would be reviewed by the NRC in the Tech Spec change SER." If

there was a reduction in safety,10 CFR 50.59 requires that this change be an-

-

Unreviewed Safety Question (USQ). There was no discussion of a USQ in the

0 summary. Upon review of SE 96-043 it was determined that the conclusion of

>

the SE was that there was not a reduction in the margin of safety.L This was -

considered an example where an insufficient review of information that was

- provided to the NRC. The staff relies on information provided by the licensees to

be accurate.

N 10 CFR 50.59 screenings which should be documents that are controlled under

! the quality control program, were not easily retrievable when a screening's

_ _

. conclusion was that a full safety evaluation was not required.

- :These above concems noted by the inspectors, along with numerous licensee-identified

PlFs conceming 50.59 problems with screenings, with documentation deficiweies, with

inadequate reviaws, with qualifications of reviewers and preparers l and with lack of off-

site reviews, substantiated a programmatic weakness in the Quad Cities 50.59 program.

Corrective actions initiated by Quad Cities staff included establishment of a third level

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k

review of n,afety evaluations by the Engineering Assurance Group and further training.

The effectiveness of these recent actions could not yet be assessed.

- b.2 incomolate 10 CFR 50.59 Summarv Reo_ ort

The inspector reviewed 10 CFR 50.59 summary reports LWP 90-048, dated July 08,

1096, and SVP-97-251, dated October 31,1997, to verify completeness of the reports.

The summaries were being provided pursuant to 10 CFR 50.59(b)(2) and 10 CFR

" 50.71(e). The inspectors noted that each of thew summary reports contained only the

descriptions of 50.59 evaluations tnat actually changed the Updated Final Safety

Analysis Report (UFSAR). It did not Include a description of each changa, test, or ,

, experiment to the fecility as described in the SAR completed since the last report.

Approximately 60 safsty evaluations performsd in accordance with the 50.59 program

were not included in these reports. Listed below are examples of 50.59s SEs reviewed

during the SOPl inspection that were not included in their 50.59 Summary report:

.

SE 96-22; Temporary alteration to discble thermal overload alarm on HPCI '

auxiliary oil pump.

.

SE 97 019; Interim procedure will render the HPCI subsystem unavailable while

the steam isolation valves are closeo. Perform interim procedure to test the

HPCI interlock which runs the motor speed changer to the high speed stop upon ,

a high drywell pressure initiation signal.

.

SE 96-085; Reclassify the HPCI keep-fill lines between valves 1(2)-2381 and

>

1(2)-2399 as Safety Related.

!

.

SE 96 095; install an expandable plug in floor drain to restrict air flow. The floor

drain allows an opening in secondary containment when the reactor building

i'

(Inner) door is opened. The plug will restrict air flow to ensure that the required

negative pressure is maintained in the Reactor Building.

The failure to report a description of each 50.59 safety evaluation was contrary to

procedure NSWP-A-04, Rev. O, "10 CFR 50.59 Safety Evaluation Process, Section

5.4.1.3, which states, in part, that the report shall contain a brief description of each

- change, test, or experiment and a summary of the safety evaluation performed." This

was considered a violation of 10 CFR 50, Apper dix B, Criterion V (VIO

50-254/265/97022-06).

b.3 Off-Site Review

Procedure N.O.-16, Revision 8, " Conduct of Off-Site Review," was reviewed in

conjunction with several Quad Cities Off-Site Monthly Review Reports, and Off-Site

Review Reports on HPCI 50.59 safety evaluations. Procedure N.O.-16 describes the

organization, responsibilities, and duties of the off-site review group including personnel

qualifications and review process. This procedure provided a comprehensive program

for SE review along with reporting requirements on questions and comments on

26

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. '

,

\

individual SEs and the reporting of off-site review activities on a monthly basis.

Questions raised by the off site review group were reported in an Off Site Review l

'

Report where tracking was provideo by the site Nuclear Tracking System (NTS) with

response requested usually within 75 days. Based on the comments provided by the

off site review grouo in the individual HPCI Off-Site Review Reports and the June / July

and August Off-Site Review Monthly Reports the inspectors concluded that the off site

review group was providing good safety focussed feedback when assessing the 50.59

SEs.

b.4 Status of m Mm Task Assignment - Configuration Control Process

.

- In November 1996, the licensee completed a "50.54(f) Task Assignment - Configuration

Control Process," as input into their response to a staff letter * Request For information

Pursuant To 10 CFR 50.54(f) Regarding Adequacy And Availability Of Design Bases

information* dated October 9,1996. This input to the response letter addressed five

corrective acuons after reviewing various inspection and assessment reports. The

inspectors reviewed the status of these corrective actions:

Corrective Action #1 was to perform increased reviews of current 50.59 safety

evaluations and screenings to target trends which show a likely noncompliance,

as stated in the task assignment. It further stated that this was an appropriate

response to the frequency ofinadequate evaluations. PlF 96-03374 was

initiated to address this issue and NTS 254 20196-337401 was assigned to

track this effort. The inspectors noted that this NTS item was still open and had

been passed between various personnel with a due date in January 1998.

Corrective Action #2 was to address inadequacies in offsite reviews. PlF

96-03375 was generated and NTS 254-201-96-337501 was assigned to this

task. This action addressed issues such as 50.59 documentation requirements,

l off-site review location, and adequacy of off-site review requirements. Based on

l reviews of actions taken, the inspectors concluded that this issue was

adequately closed in March 1997.

Corrective Action #3 addressed the adequacy of the current 50.59 safety

evaluation procedure. PIF-03376 was initiated and appropriately closed upon

issuance of a new corporate 50.59 safety evaluation procedure NStNP-A-04,

Rev. O, which was issued January 1997. Although the procedure was under

review by the licensee for further changes to improve written justifications when

addressing a facility change, the procedure was considered a distinct

improvement over the existing site procedures.

Corrective Action #4 was to address the establishment of a site 50.59

coordinator to help maintain consistency in safety evaluations. PIF-03377 under

NTS 254-251-96-08507 was initiated and came to a reasonable conclusion that

a specific 50.59 coordinator was not necessary because of the establishment of

an Engineering Assessment Group that will review and verify the adequacy of

50.59 screenings and safety evaluations.

27

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.< '

.

i

Corrective Action #5 under PIF 03378 and NTS 254 20196-337801 was to

address various PIFs and external processes outside of the 50.59 process to

determine whether 50.59 requirements were being bypassed. The inspectors

noted that this activity was still open, had been passed between various

personnel and was projected to be completed in March 1998. J

c. Conclusions

While the SEs reviewed were adequate with supportable conclusions, weaknesses were i

identified with the overall 50.59 pregram. These included poorly written safety

evaluations, incomplete summary report submittals to the NRC, difficult to retrieve

screenings, and incomplete corrective actions to identified deficiencies. Additional 50.59 i

related concems were discussed in Section E2.4 of this report.- The Off Site review

group, however, was providing good assessments and comments.

E3.2 UFSAR Sections on the HPCI System

a. insoection Scoos

,

The inspectors reviewed UFSAR sections on the HPCI system, and compared the

UFSAR to system prir'ts, TS, and HPCI procedures to check the accuracy of the

UFSAR.

bc Observations and Fir dinos

The inspectors identlW that UFSAR Figures 6.3-14 and 6.3-15 did not

accurately represent me HPCI system. Figure 6.3-14 was a simplified overall

- diagram of major HPCI system components, piping and valves. The valve

positions indicated on the Figure 6.3-14 did not represent any operational state

of the system; not the standby lineup, test lineup, injection lineup, or pressure

control lineup of the system. Additionally, the figure indicated that the HPCI

Contaminated Condensate Storage Tank (CCST) suction valve MO 1(2)-2301-6

was open simultaneously with tM torus suction valves MO 1(2)-2301-35 and 36.

This lineup was generally avr )y the licensee as it creates a potential drain

path between the torus and C,,.,. . Additionally, an interlock exists that if the

torus suction valves were both opea, then the CCST suction valve will auto

close. Figure 6.3-15 also did not accurately represent the HPCI system. Figure

6.3-15 was a simplified functional block diagram for key valves in the HPCI

system. This figure incorrectly indicated that steam isolation valves MO 1(2)-

2301-4 and 5 receive some kind of open signal from a HPCI auto initiation. The

licensee generated a PIF to address this issue and correct these identified errors

with figures in the UFSAR

The inspectors identified that UFSAR Section 6.3.2.1.4, " Core Spray Discharge

Line Fill Provisions," stated that pressure switches were provided to indicate and

alarm high or low pressure in the ECCS pump discharge headers to ensure

proper functioning of the fill system. However, there was no pressure switch

28

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,4 *

,

Installed on the HPCl pump discharae header to indicate loss of fill. The

licensee generated PlF 4050 to address this discrepancy.

.

The licensee reviewed the UFSAR in June 1996, to determine whether the

document reflected all necessary changes in response to a finding at another

facility. The inspectors considered this a good initiative by the licensee to assure

that the most recent update met the intent of 10 CFR 50.71(e). All changes inat ,

were found not to have been incorporated into the UFSAR, some completed as 1

early as 1991, were included in the most recent update, Revision 4, on

October 22,1997. Corrective actions to programmatically ensure that all future

changes will be reflected in the UFSAR in accordance with 10 CFR 50.71(e)

were in progress. NRC review of these plans and of their effectiveness was

considered an inspection follow up item (IFl 50-254/265/97022-07).

.

The inspectors also noted that the Quad Cities Design Basis initiative (DBI)

project was in the process of initiating a line-by-line validation of UFSAR design

basis information.

c. Conclusirms

inaccurate figures and text in the UFSAR were identified but the inspectors also noted

ongoing licensee efforts to improve UFSAR accuracy such as line by line reviews of the .

UFSAR design information ano an initiative to ensure facility changes had been

incorporated into the UFSAR.

E3.3 HPCi System Design Basis Document (DBD)

a. insoection Scone

The inspectors reviewed the HPCI system design basis document DBD, and compared

the HPCI DBD to the UFSAR, TS, end HPCI procedures to check the accuracy of the

DBD.

b. Observations and Findings

At the time of this inspection, the HPCI DBD was in its third revision and was undergoing

further review prior to validation. Numerous discrepancies in the HPCI DBD were

discovered. These included:

.

Inconsistencies within the DBD concerning the response of steam isolation

valves MO 1(2)-2301-4 and 5 to a HPCIinitiation signal, in response to an

initiation signal, page 4-10 of the DBD said that these valves will auto open; page

4-18 of the DBD said that these valves will not auto open. In fact, valves MO

1(2)-2301-4 and 5 will not auto open if an initiation signal was received.

.

The DBD incorrectly omitted HPCI high area temperature as a signal which

would close the steam isolation valves MO 1(2)-2301-4 and 5,

29

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_ _ - _ _ - _ _ _ _ - - - _ _ _ - _ _ _ _ _ -

g , I

,

.

The DBD incorrectly stated that the minimum flow bypass valve MO

1(2)-2301 14, cannot be opened if the HPCI turbine steam suoply valve MO

1(2)-2301-3, was closed.

.. The DBD incorrt,ctly omitted high suppression pool level as a signal which would

'

open torus suction valve MO 1(2) 230136.

c. Conclus10Ds

Quad Cities design basis and configuration controlinformation weaknesses were also

exhibited with numerous errors identified with the HPCI system DBD. However, the

-licensee was aware of the DBD shortcomings and had designated the DBDs as

"information only" pending completion of a validation process.

E7 ' Quality Assurance in Engl9 eering Activities

y

E7.1 10 CFR 50.54(f) Letter Commitment Review

a. Insoection Scoce

The team reviewed the status of commitments pertaining to the licer'see's March 28,

1997, response to the NRC's request for information purruant to 10 CFR 50.54(f). The

following commitments related to engineering and the corrective action program at Quad

Cities were reviewed by the team. The commitment numbers correspond to those used

l by the licensee in their March 28,1997, submittal,

i

b. Observations and Findinas  ;

b.1 Commitment 16: "These actions included, in part, establishment of an engineering

'

assurance function at each site and the NOD central offices to further ensure the quality

of design and technical work, commencement of safety system functional inspections, .

(

' review of Technical Specification interpretations, and a review of the top ten risk

significant systems for items that may impact system readiness."

The team determined that the Engineering Assurance Group (EAG) had been

established at Quad Cities. One SSFI-related review and the top ten risk significant

systems reviews have been completed. Technical Specification interpretations were no

longer used at Quad Cities.

_ b.2 Commitment 20: "A nuclear engineering procedure for this effort is being prepared and

will address the review and reconstitution of selected key design basis '

parameters / calculations."

The team verified that procedure NEP-17-08, Revision O, " Design Basis Initiative," May

23,1997, had been implemented at Quad Cities. Design Basis initiative engineering

personnel had been trained on the procedure.

30

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_ _- _ _ _ _ _ _ _ - - - _ _ _ _ _ - - --- - -

.

,.

.

b.3 Commitment 55: "In order to ensure that corrective actions and responses to lessons

learned are consistently and vigorously implemented throughout NOD, a new corrective

action program has been developed by representatives from all six nuclear sites and the

NOD central office."

The team verified that the new corrective action process had been implemented at Quad

Cities on May 12,1997. A common set of performance indicators had been developed

and summarized on a monthly basis,

'

b.4 Commitment 58: "The new process includes several improvements over the current

program. It clearly delineates and standardizes the threshold for problem identification

through Problem Identification Form (PlF) initiation, and establishes common PlF

screening criteria that provide greater ability to analyze PlF data."

The team verified that NSWP A-15, Revision 1, " Problem Identification Form," May 5,

1997, had been implemented at Quad Cities on May 12,1C37. The procedure included

standerdized requirements on when a PlF should be issued and established common

PlF screening criteria,

b.5 Commitment 59: " Groups of these trained individuals will be stationed at each of the

nuclear plant sites and in the NOD central office."

The team verified that the Quad Cities root cause analysis team was trained by an

outside contractor on February 11-14,1997,

b.6 Commitment 61: "The remaining sites have devebped plans to implement this process

during 1997."

The team verified that NSWP-A-15, Revision 1, " Problem Identification Form,"

implementation and initiation of monthly Quality and Safety Assessment Performance

indicator reports satisfy this commitment.

b7 Commitment 63: "The information will be taken monthly and used to evaluate the

effectiveness of corrective action process improvements as well as participation by each

site in the process."

The team concluded that the monthly Quad Cities Quality and Safety Assessment

(Q&SA) reports were adequate to satisfy the commitment,

b.8 Commitment 64: " Performance indicators have also been developed to monitor the

timeliness of implementation, quality of corrective actions, and the number of significant

events which are repeated. These indicators are being tasted at Byron. Site and NOD

central management will take appropriate actions based on performance and results."

Based upon the review of Quad Cities performance indicators in the Q&SA monthly

reports, and the results of corrective action, the team concluded that this commitment

was satisfied.

31

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4

b.9 Commitment 71: "In February 1997, a procedure was issued for evaluating and

initiating NOD-wide action in response to operating experience at any of the Comed

nuclear stations. The procedure also covers response to operating experience

materials both from Comed and non-Comed stations. The procedure provides for

review and screening of operating experience items, development of responsive action,

and review and evaluation of the effectiveness of responsive action."

The inspector's review of procedure NSWP-A-06, Revision O," Operating Experience '

Program," February 27,1997, resulted in the determination that this commitment was

satisfied.

- b.10 Commitment 88: "Esch site also has a group that evaluates the severity of events, and

oetermines whether a root cause analysis is warranted. Processes are being

implemented for evaluation of the effectiveness of corrective action." a

The inspector verified that the Event-Screening Committee was in place and performing

those functic~s delineated in the commitmant.

b.11 Commitment 89: " Monitoring of performance against the indicators, Corrective Action

Requests (CAR), and industry experience; and review of site self-assessments will also

be conducted within SQV."

Quad Cities bd implemented Nuclear Overs:ght procedure NO-19, Revision 1,

" Integrated Analysis Process and Routine Reporting," that contains instructions for

l monitoring performance indicators, CARS and Self-assessments,

b.12 Commitment 91: "The SRBs evaluate station safety performance, corrective actions,

and improvement plans. The SRB chairman will also provide input to the NOC of the

board. The site gains outside perspective aM critical review of performance from this

body."

The inspectors verified that Quad Cities received recommendations from the Safety

Review Board (SRB) independent reviews and entered the recommendations into the

site tracking system. The recommendations were then assigned to on-site managers for

analysis and necessary actions.

b.13 Commitment 284: " Design records were transferred from contract design engineering

organizations to Comed."

Design records had been transferred to Quad Cities and stored in the station central

filing system,

b.14 Commitment 287: "A standardized corporate corrective action program, based on a

review of industry programs, is being implemented throughout NOD. The program

incit' des specific performance measures to gauge program effectiveness. A corporate

corrective actions group is being established to ensure the appropriate response to site

and industry events."

32 1

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.

..

,

The inspectors verified that a corporate corrective actions group had been established

within the Q&SA organization at Quad Cities.

b.15 Commitment 301: "A NOD-wide formal program for evaluating, sharing, and assessing

the effectiveness of responses to lessons leamed at both Comed and other nuclear

stations is being implemented to assure lessons leamed are being shared and

responded to throughout NOD."

The inspectors verified that the Lessons Leamed Program, a corrective Actions

Program and an Operating Experience Program had been implemented at Quad Cities,

b.16 Commitment 304: " Standardized performance measures are being implemented to

gauge processes and effectiveness of Corrective Actions."

The inspectors verified that standardized performance measures have been

implemented at Quad Cities and were evaluated in Q&SA monthly reports,

b.17 Commitment 323: " Design authority and design records were transferred from contract

design engineering organizations to Comed, on-site design engineering capabilities

were increased, and we are developing a series of common engineering processes and

procedures for the division."

Design records had been transferred and on-site capabilities increased. The common

engineering procedures and processes had been developed,

b.18 Commitment 3_24 "We initiated a broad set of initiatives to ensure that each of our sites

has a high quality engineering support to maintain the facility design bases. Engineering

Assurance groups [EAG) were formed at each site to improve the quality of design and

technical work, with a specific focus on maintaining the design basis."

The EAG at Quad Cities produced monthly reports of results of their monitoring of site

engineering activities. EAG staffing was three full time nnd one full time equivalent and

appeared adequate.

c. Conclusions

Based on procedure and other documentation reviews, and interviews with cognizant

licensee personnel, the inspectors concluded that the preceding 10 CFR 50.54(f)

commitments were closed. The remaining 10 CFR 50.54(f) commitments that remained

open will be reviewed in future NRC inspections.

E8 Miscellaneous Engineering issues

E8.1 Ooen items

(Closed) VIO 50-254/265/97013-01: TS Surveillance Requirements for the RHRSW

pumps were not relocated to the IST program as required by TSUP t.ommitments. The

33

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_ _ _ _ _ _ _

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.

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- lST test procedure (OCOS-1000-4 " Quarterly RHRSW Pump Operability Test," Rev,13)

was updated to include the test criteria. The inspectors verified that the required TS

surveillance requirements were appropriately relocated to the IST program. Further, all

TSUP transfers that involved IST relocations were reviewed to ensure that similar

transfers of test requirements were not missed. No other problems were found, this

violation is closed.

E8.2 Systematic Evaluation Procram (SEP)

a, insoection Scone

Subsequent to the Systematic Evaluation Program (SEP) that was completed for

Dresden 2 in 1930 the licensee contracted Sargent & Lundy (S&L) to review the

_

i

Dresden SEP actions for applicability to Quad Cities. S&L recommended action on 17

SEP topics and in Septe.nber 22,1993, QC engineering issued a report acknow! edging

the S&L recommendations. The NRC's November 1993 Quad Cities Diagnostic .

Evaluation Team (DET) inspection report exp.assed concern that action to address the

Dresden 2 SEP issues at Quad Cities had not been initiated and action plans had not .

. been completed (DET Issue #9). . in subsequent correspondence, the licensee informed l

the NRC that the action plans vere completed and subsequently that all actions were

also completed or had been reassessed as not required. The inspectors reviewed these

. actions.

b. Observations and Findinos

I

b.1 SEP ltem 1. SEP Toolc ll-3.B. Floodina Potential and Protection Reauirements

The team reviewed the licensee's assessment of the probable maximum flood (PMF)

effect on Quad Cities to evaluate the plant's ability to cope with extemal flood'.ng

conditions. Quad Cities initial design was based on a PMF with a 200 year racurrence

interval, and . plant design was shown to have sufficient margin to withstt4nd floods

- with 1000 year recurrence interval. Subsequent to plant co,struction, the NRC adopted

the PMF as defined by the US Army Corps of Engineers as criteria for plant design

purposes. The e'fect of the updated PMF was noted and addressed in the UFSAR.

The updated PMF results in flood levels about eight feet above plant grade. Such a

flood would take place with sufficient warning to allow effective maasures to ensure that

the plant to be placed in a safe shutdown condition.

The inspectors reviewed We licensee's flood emergency procedure and determined that

the procedure was adequate to place the plant in a safe shutdown condition and to

maintain structuralintegrity up to a flood elevation of 603 feet elevation. Based on

reviews of the licensee's PMF calculations, flooding assessments, emergency

procedures and discussions with cognizant licensee personnel, the inspectors

concluded that the licensee had adequately addressed this issue. NRC review of SEP

ltem 1, Topic ll-3.B is considered closed.

34

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6

b.2 SEE ltem 2. SEP Tooic !!-3.B.1. Caoability of Ooerating Plant to Cooe with Desin-

Elosding Conditions

The team reviewed the Quad Cities flood emergency procedures and event

classification and notification and comparison to design basis as stated in the UFSAR.

The inspectors reviewed the Quad Cities flood emergency procedures, appropriate

sections of the UFSAR, Technical Specifications and the probable maximum flood

(PMF) esessment for the site. The procedures controlling site activities necessary to

protect the plant and equipment during a PMF appeared sufficiently comprehensive to

maintain plant component and structuralintegrity up to a flood level of 603 feet mean

sea level elevation. Based on the i spectors' review of procedures, UFSAR and

Technical Specifications, the inspectors concluoed that the licensee had adequately

addressed this issue. NRC review of SEP ltem 2, Topic ill-3.B.1 is considered closed.

b.3 SEP Item 3. SEP Toolc lil_;LC. Inservice insoection of Water Control Structures

This topic assessej the at%quacy of the inservice inspection program of water control

structures for operating plants to assure conformance with the intent of Regulatory

Guide 1,127. The recommended actions were to identify or create procedures to ensure

review and approval of the ISI program by qualified engineering personnel and initiate

inspection after extreme events as required by RG 1.127. The *,ensee identified that

procedures were in existence to address the topic and these procedures were reviewed

by the inspectors. The inspectors reviewed Procedure NEP 17-03, " Structures

Monitoring," Revision 0, Procedure QCMPM 4400-11, "RHRSW Intake Bay inspection,"

Revision 3, and Procedure OCMPM 4400-12, " Circulating Water intake Bay inspection,"

l Revision 2. The inspectors noted that the procedures adequately describe a formal

annual inspection of the intake structure by qualified engineering personnel who would

document the results of the inspection. In addition, the inspection program included

provisions for special inspections immediately after occurrence of extreme events.

These actions satisfied the SEP topic concerns. NRC review of SEP ltem 3. Topic 111-

3.C is considered closed.

b.4 SEP ltem 4. SEP Tooic lil-8.C. Iriadiation Damage. use of Sensitized Stainless Steel

SEP ltem 6. SEP Toolc V-4. Pioing and Safe-End Integrity

These topics assessed the safety aspects of intergranular stress corrosion cracking of

sensitized stainless steel used within the reactor vessel systems. For both topics, th

recommended action plan was to confirm that all sensitized safe-ends had been

removed from service. The inspectors reviewed the licensee's actions taken that

included, historical reviews of the ISI program, of code data material reports, and

reviews of historical modifications and licensing basis documents that have replaced

sensitized components. The inspectors concluded that the licensee's determination that

the Quad Cities reactor vessels do not contain any sensitized safe ends was

acceptable. NRC reviews of SEP ltems 4 & 6 Topic lil-8.C and V-4, respectively, are

considered closed.

35

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b.5 Mp item 5
SEP foole ill 10.C. Surveillance Ranuirs nents on BWR RrWlation'

Discharge Valves

~ This topic essessed the necessity to modify the control circuit configuration of the .

' recirculation line suction valves to ensure that these valves remain open on a 1

recirculatbn line break LOCA so that LPCI can be successfully initiated. (GE had

- identified the potential for spurious closure of these valves with a LOCA occurring

between the pump suction and discharge valves.)-The S&L action plan recommended

that the station confirm that the breakers to the recirculation line suction valves were-

racked out.' Subsequent to issuance of the S&L action plan, the licensee identified that

racking out the breakers was not required because these valves had been modified in

1978 to reconfigure the closing logic. The inspectors reviewed these actions and-'  ;

-

'

confirmed that the modifications had been implemented and concurred that the need for

racking out the valves was no longer applicable. NRC SEP ltem 5, Topic lil 10.C is

considered closed.

b.6 SEP ltem 7. SEP Toole V-5. Reactot. Coolant Pressure Boundarv I ask Detardhn -

This topic assessed the adeqtacy of the reactor primary coolant leakage detection

system. The S&L action plan had recommended revising Technical Specifications

_ Section 3.6 / 4.6 to include additional monitoring requirements and tighter limits on

"

unidentified leakage. The licensee identified that these recommendations had been - ,

t

!

Incorporated into the upgraded Technical Speclilcations.- The inspectors reviewed the -

, latest version of the Technical Specifications (the NRR reviewed and approved TSUP) :

and concluded that sections 3.6 G/4.6.G. Leakage Detection Systems, and 3.6.H/4.6.H.

L  : Operational Leakage satisfactorily addressed the SEP issue with the type and sensitivity

ofleak detection systems. NRC review of SEP ltem 7, Topic V-5 is considered closed,

b.7 ' SEP ltem 17. SEP Toolc XV-16. Radioloalcal Consecuences of FalNre of Small Lines

Carrvina Primarv Coolant Outside Containment

' This topic assessed the radiological consequences of failure of small lines carrying

' primary coolant outside containment and reviewed Technical Specifications associated

with primary coolant radioactivity concentrations. 'Similar to Dresden SEP action, the _

~

action plan recommended changes to the Technical Specification to_ limit reactor coolant

specif:c activity during power operation within the BWR Standard Technical Specification -

limits. The licensee identified that these recommendations had been incorporated into

the upgraded Technical Specifications.; The inspectors reviewed the Technical

Specifications and verified that TS Section 3.6.J/4_.6.J, Specific Activity had been revised

- and reviewed under the TSUP program. The specific activity of the reactor coolant was

now limited to less than 0.2 microcurie / gram dose equivalent 1-131 during modes 1,2

and three. NRC rieuw of SEP ltem 17, Topic XV-16 is considered closed.

.

c. Concinalon

The inspectors reviewed the action taken by the Quad Cities staff for eight SEP topics -

and concluded that the actions taken were sufficient for closure of these items. NRC

review of nine remaining SEP ltems was ongoing.

36

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,w e:

3-

V. Management Meetings

-X1 Exit Meeting Summary -

The inspectors presented the liispection results to members of licensee management at

- the conclusion of the inspection on November 21,1997. The licensee acknowledged .

the findings presented and did not identify any documents provided to the inspectors as

' proprietary,

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PARTIAL LIST OF PERSONS CONTACTED j

ucense.

S. Boline, Quad Cities Mechanical Design

D. Brown, S&L

A. Chemick, Comed RA Supervisor.

D. Cook,-Station Manager

< D. Cook, Comed Maintenance 1

D.' Egan, Comed dbl-:

S. Eldridge, Comed, EAG Supervisor- ,

R. Faltbanks, Engineering Manager

' H.; Gavankar, Comed, Chief Engineer, Mechanical

.

W. - Heinmiller, Comed Site Design Supervisor -

R.- Hoyn, Quad Cities Mechanical Design

J. Hosmer, Vice President, Engineering

G. Klone, Quad Cities Operations--

P. Lawless, Quad Cities SOPI Team Lesder

- H. Palas, Comed Pump Specialist

L. Pearce, Site Vice Presidsnt

- K. Salehl, Comed, Engineering Assurance Group-

.

- R.. Svaleson, Operations Manager

'J. Swales, SystemEngineer

T.-. Thorsell, Comed Chief Engineer, Ell &C -

F. Tsakeres, Training Manager .

.- M. Wayland, Maintenance Manager.

JJ.1 Williams l Comed Project Manager

NRC

. L. Collins, Quad Cities Resident inspector .

R. Ganser, Illinois Department of Nuclear Safety .

.

R. Gardner, Chief, Engineering Branch No. 2

C, Miller, Quad Cities Senior Resident inspector

i M. Ring, Chief, Projects Branch No.1

K. Walton, Quad Cities Resident inspector

INSPECTION PROCEDURt:$ USED

lP 40500: . Effectiveness cf Licensee Controls in Ident!fying, Resolving, and Preventing

Problems

IP 93801: Safety System Functional Inspection

IP 37550
Engineering -

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ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

ii . l 50-254/265/97022-01 t VIO - Criterion V, failure to prescribe in procedures

- activities affecting quality (Procedure would not

work)~

-50-254/265/97022-02 . URI. Breaker coordination action plan

'50-254/265/97022-03 VIO Criterion 111, failure to factor additional AC inboard

isolation valve closure time for LOOP concurrent w/

HPCI steamline break .<

50-254/97022-04a VIO Criterion V, failure to fotbw 50.59 procedure

- 50-254/97022-04b - Vio Criterion V, failure to follow 50.59 procedure

50-265/97022 05 URI 50.59 screening did not evaluate al' modes of

operation

5b-254/265/97022 06 VIO Criterion V, fa!!ure to follow 50.59 procedure on

report submittals

i

50-254/265/97022 07 IFl Follow up on corrective action on 10 CFR 50,71(e) i

UFSAR update requirements  !

ggw ^

L  : 50 ,, 5/97013-01 VIO - Tech Spec Surv Requirement not relocated to IST

Program

s

!

4

1

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LIST OF ACRONYMS USED

AOP Abnormal Operating Procedure :

ASME - American Society'of Mechanical Engineers

BWR Bolling Water Reactor

CAR Corrective Action Record

CCST Contaminated Condensate Storage Tank

CFR Code of Federal Regulations

Comed Commonwealth Edison Company-

DBD Design Basis Document

DET Diagnostic Evaluation Team

DCP Design Change Package

DCR Design Change Request

DC/dc Direct Current

EAG Engineerirg Assurance Group _

ECCS Emergency Core Cooling System

EOP Emergency Operating Procedeire

ESW Essential Service Water

EWCS Electronic Work Control System 1

GE General Electric

GL Generic Letter

HVAC Heating Ventliation Air Conditioning

HX Heat Exchanger

. HPCI- High Pressure Coolant injection

l IEEE Institute of Electrical and Electronic Engineering

l

IFl Inspection Follow up Item

ISI- Inservice inspection

_,

,

-lST Inservice Testing

L HPCI- High Pressure Coolant injection System

KV Kilovolt

LCO Limiting Condition for Operation

LER Licensee Event Report

LOCA Loss of Coolant Accident

LPCI Low Pressure Coolant injection System

LVDT. Linear Variable Differential Transformer

MOV Motor-Operated Valve -

NSO Nuclear Station Operator

NSWP Nuclear Station Work Procedure

NPSH Net Positive Suction Head

NRC Nuclear Regulatory Commission

NRR Office of Nuclear Reactor Regulation

'NTS Nuclear Tracking System

PlF Problem identification Form-

PM: Preventive Maintenance

PMF- Probable Maximum Flood

PMT Post-Maintenance Testing

PSIA Pounds Per Square Inch Absolute

40

,.;'*

LIST OF ACRONYMS USED (CONT)

PSIG Pounds Per Square Inch Gauge

QA -Quality Assurance

QC- Quality Control

QCAP Quad Cities Administrative Procedure

QCIS Quad Cit;es instrumen' Rurveillance

QCOP Quad Cities Operating Procedure

QCOS Quad Cities Operating Surveillance Procedure

  • QSA- . Quality and Safety Assessment

-Q&SA Quality and Safety Assessment

-QTP Quad Cities Technical Procedure

RCIC _ Reactor Core Isolatio : Cooling

RG Regulatory Guide

-RHR Residual Heat Removal System

RHRSW Residual Heat Removal Service Water

RR Reactor Recirculation

S&L Sargent and Lundy

SAR' Safety Analysis Report

SE Safety Evaluation

SEP. Systematic Evaluation Program

- SIL Service informatior Letter

SOPl System Operational Performance inspection

SRB Safety Review Board

SROL Senior Reactor Operator

l SRV Safety Relief Valve

L SSFl Safety System Functional inspection

TAF -Top of Active Fuel

TALT Temporary Alteration

TS '- Technical Specification

TSUP Technical Specification Upgrade Project

UFSAR - Updated Final Safety Analysis Report

URI Unresolved item

US - Unit Supervisor

VIO Violation -

WR Work Request

,

41

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