Similar Documents at Perry |
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Category:CORRESPONDENCE-LETTERS
MONTHYEARPY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20217F3901999-10-14014 October 1999 Discusses Request That Proprietary Document NEDE-32907P,DRF A22-0084-53, Safety Analysis Rept for Perry NPP 5% Power Uprate, Class III Dtd Sept 1999 Be Withheld.Determined Document Proprietary & Will Be Withheld ML20217G9201999-10-14014 October 1999 Discusses Utils Request for Approval of Quality Assurance Program Changes PY-CEI-NRR-2435, Responds to NRC Re Violations Noted in Insp Rept 50-440/99-13.Corrective Actions:Ts SRs with Incorrect Descriptions Were Annotated to Ensure That CR Operators Are Aware That ACs Are Effect1999-10-13013 October 1999 Responds to NRC Re Violations Noted in Insp Rept 50-440/99-13.Corrective Actions:Ts SRs with Incorrect Descriptions Were Annotated to Ensure That CR Operators Are Aware That ACs Are Effect ML20212K9271999-09-30030 September 1999 Refers to 990927 Meeting Conducted at Perry Nuclear Power Plant to Discuss Initiatives in Risk Area & to Establish Dialog Between SRAs & PSA Staff ML20212J1451999-09-30030 September 1999 Forwards Order,In Response to 990505 Application PY-CEI/NRR- 2394L.Order Approves Conforming License Amend Which Will Be Issued & Made Effective When Transfer Completed ML20217E7111999-09-30030 September 1999 Documents Telcon Conducted on 990929 Between M Underwood of Oh EPA & D Tizzan of Pnpp,Re Request to Operate Pnpp Sws,As Is,Until Resolution Can Be Obtained ML20212G4161999-09-24024 September 1999 Informs of Completion of Licensing Action for Generic Ltr 98-01, Y2K Readiness of Computer Systems at Nuclear Power Plants, for Perry Nuclear Power Plant ML20212G5811999-09-23023 September 1999 Informs That Licenses for Ta Lentz,License SOP-31449,PJ Arthur,License SOP-30921-1 & Dp Mott,License SOP-31500 Are Considered to Have Expired,Iaw 10CFR50.74(a),10CFR55.5 & 10CFR55.55 PY-CEI-NRR-2432, Forwards NRC Form 536, Operator Licensing Exam Data, in Response to Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams1999-09-21021 September 1999 Forwards NRC Form 536, Operator Licensing Exam Data, in Response to Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams PY-CEI-NRR-2428, Submits Resolution to Seventh Question Proposed within NRC 980615 RAI Relating to Cooling Water Sys That Serve Containment Air Coolers & Assessment,Post Accident,Of Potential Water Hammer & two-phase Flow Conditions1999-09-16016 September 1999 Submits Resolution to Seventh Question Proposed within NRC 980615 RAI Relating to Cooling Water Sys That Serve Containment Air Coolers & Assessment,Post Accident,Of Potential Water Hammer & two-phase Flow Conditions ML20212D0151999-09-14014 September 1999 Requests Cancellation of NPDES Permit 3II00036.Permit Has Been Incorporated in Permit 3IB00016*ED.Discharge Point Sources & Associated Fees Currently Covered Under Permit 3IB00016*ED ML20212A8371999-09-13013 September 1999 Forwards Insp Rept 50-440/99-13 on 990712-30 & Notice of Violation.Insp Included Evaluation of Engineering Support, Design Change & Modification Activities,Internal Assessment Activities & Corrective Actions ML20217A8971999-09-0909 September 1999 Forwards Insp Rept 50-440/99-09 on 990709-0825.One Violation of NRC Requirements Occurred & Being Treated as NCV, Consistent with App C of Enforcement Policy PY-CEI-NRR-2431, Forwards Revised Emergency Plan for Perry NPP, IAW 10CFR50.54(q).Changes Constitute Revs,Temporary Changes or Reissued Pages1999-09-0909 September 1999 Forwards Revised Emergency Plan for Perry NPP, IAW 10CFR50.54(q).Changes Constitute Revs,Temporary Changes or Reissued Pages ML20211Q6911999-09-0606 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Perry Operator License Applicants During Wks of 010108 & 15.Validation of Exam Will Occur at Station During Wk of 001218 IR 05000440/19990011999-08-31031 August 1999 Requests That Page Number 4, P2 Status of EP Facilities, Equipment & Resources, of Insp Rept 50-440/99-01 Be Replaced with Encl Rev PY-CEI-NRR-2425, Forwards Copy of Oh EPA Approval for Use of Nalco 7348 & Nalco 7468 at Pnpp,Iaw License NPF-58,App B,Epp,Section 3.21999-08-26026 August 1999 Forwards Copy of Oh EPA Approval for Use of Nalco 7348 & Nalco 7468 at Pnpp,Iaw License NPF-58,App B,Epp,Section 3.2 PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20210Q8421999-08-13013 August 1999 First Final Response to FOIA Request for Documents.Records Listed in App a Being Released in Entirety & Records Listed in App B Being Withheld in Part (Ref FOIA Exempt 5) ML20210R7861999-08-12012 August 1999 Forwards Insp Rept 50-440/99-12 on 990712-16.No Violations Noted.New Emergency Preparedness Program Staff & Mgt Personnel Were Professional & Proactive ML20210S3961999-08-11011 August 1999 Requests That Ten Listed Individuals Be Registered to Take 991006 BWR Gfes of Written Operating Licensing Exam.Two Listed Personnel Will Have Access to Exams Before Exams Are Administered PY-CEI-NRR-2423, Provides Final Response to NRC GL 98-01, Y2K Readiness of Computer Sys at Npps. Remediation of Meteorological Monitoring Sys Has Been Completed & Ppnp Facility Is Now Y2K Ready1999-08-10010 August 1999 Provides Final Response to NRC GL 98-01, Y2K Readiness of Computer Sys at Npps. Remediation of Meteorological Monitoring Sys Has Been Completed & Ppnp Facility Is Now Y2K Ready PY-CEI-NRR-2421, Forwards Semiannual fitness-for-duty Rept,Iaw 10CFR26.71(d) for Pnpp Covering Period of 990101-9906301999-08-10010 August 1999 Forwards Semiannual fitness-for-duty Rept,Iaw 10CFR26.71(d) for Pnpp Covering Period of 990101-990630 ML20210Q7981999-08-10010 August 1999 Informs That Intention to Utilize Sulfuric Acid in Pnpp Circulating Water Sys to Lower Ph Is Anticipated to Be Completed in Nov ML20210Q5831999-08-10010 August 1999 Requests Permission to Chemically Treat CWS for Algae Due to Cooling Water Basin Becoming Infected with Algae of Various Types PY-CEI-NRR-2422, Forwards Addl Info Re ASME Section IX Relief Request (IR-023) for Inservice Examination Program at Pnpp,Submitted on 9808261999-08-10010 August 1999 Forwards Addl Info Re ASME Section IX Relief Request (IR-023) for Inservice Examination Program at Pnpp,Submitted on 980826 ML20210K6331999-08-0404 August 1999 Submits Response to Requests for Addl Info to GL 92-01,Rev 1, Reactor Vessel Structural Integrity, for Perry Nuclear Plant,Unit 1 PY-CEI-NRR-2417, Forwards NP0059-007, Pnpp - Unit 1 ISI Summary Rept Results for Outage 7 (1999) First Period,Second Interval, IAW ASME Boiler & Pressure Vessel Code,Section XI,1989 Edition,Article IWA-60001999-08-0202 August 1999 Forwards NP0059-007, Pnpp - Unit 1 ISI Summary Rept Results for Outage 7 (1999) First Period,Second Interval, IAW ASME Boiler & Pressure Vessel Code,Section XI,1989 Edition,Article IWA-6000 ML20210G8411999-07-28028 July 1999 Informs That Based on Determination That Rev 14 Changes to Various Portions of Perry Nuclear Power Plant Emergency Plan Does Not Decrease Effectiveness of Licensee Emergency Plan & Meets Standard of 10CFR50.47(b),no NRC Approval Required ML20210E0661999-07-22022 July 1999 Forwards Insp Rept 50-440/99-08 on 990518-0708.No Violations Noted.Overall Conduct of Activities at Perry Facility, Conservative & Professional with Continuing Focus on Safety PY-CEI-NRR-2419, Forwards Four Copies of Rev 27 to Pnpp Security Plan,Per 10CFR50.54(p)(2).Changes Have Been Determined Not to Decrease Effectiveness of Security Plan.Rev Withheld1999-07-21021 July 1999 Forwards Four Copies of Rev 27 to Pnpp Security Plan,Per 10CFR50.54(p)(2).Changes Have Been Determined Not to Decrease Effectiveness of Security Plan.Rev Withheld PY-CEI-NRR-2415, Submits Estimate of Number of Licensing Submittal for FY00 & 01,for Pnpp,Per Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates1999-07-19019 July 1999 Submits Estimate of Number of Licensing Submittal for FY00 & 01,for Pnpp,Per Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates ML20210A6441999-07-15015 July 1999 Advises That Listed Operator Licenses for Company Personnel Have Expired,As of 990715,per 10CFR50.74(a) & 10CFR55.5. Individuals Listed Have Assumed Responsibilities at Pnpp That Do Not Require Operator Licenses ML20209E5951999-07-0909 July 1999 Ltr Contract:Task Order 46, Perry Engineering & Technical Support (E&Ts) Insp, Under Contract NRC-03-98-021 ML20209D5931999-07-0101 July 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Investigation Rept 3-98-005 Issued on 990510.Corrective Actions Will Be Examined During Future Inspections ML20211A3881999-06-30030 June 1999 Supplements Re NRC Incomprehensible Enforcement Inactions.Understands That NRC Claiming Hands Tied in Matter Re Discrimination Violation at Perry Npp.Requests That NRC Take Listed Two Actions PY-CEI-NRR-2410, Submits Response to NRC Request for Info Re GL 98-01, Y2K Readiness of Computer Sys at Npps. Attachment 1 Provides Y2K Readiness Disclosure for Plant1999-06-29029 June 1999 Submits Response to NRC Request for Info Re GL 98-01, Y2K Readiness of Computer Sys at Npps. Attachment 1 Provides Y2K Readiness Disclosure for Plant PY-CEI-NRR-2413, Advises That Jk Wood Will Replace Lw Myers as Pnpp,Vice President - Nuclear,Effective 9907061999-06-29029 June 1999 Advises That Jk Wood Will Replace Lw Myers as Pnpp,Vice President - Nuclear,Effective 990706 PY-CEI-NRR-2403, Submits Response to RAI Re GL 96-05 Program at Plant1999-06-29029 June 1999 Submits Response to RAI Re GL 96-05 Program at Plant ML20196H9641999-06-29029 June 1999 Confirms 990615 Telcon Request with J Lieberman for Addl Time to Respond to Enforcement Action 99-012.FirstEnergy Has 60 Days to Respond to EA PY-CEI-NRR-2412, Forwards Perry Nuclear Plant Simulator Four Yr Test Rept & NRC Form 474, Simulation Facility Certification, Which Describes Tests Conducted from June 1995-19991999-06-28028 June 1999 Forwards Perry Nuclear Plant Simulator Four Yr Test Rept & NRC Form 474, Simulation Facility Certification, Which Describes Tests Conducted from June 1995-1999 ML20211A3991999-06-28028 June 1999 Submits Concerns Re Proposed Changes to Enforcement Policy. Believes That NRC Existing Regulations & Policies Provide Adequate Controls & That NRC Not Administering Consistent Enforcement Policies in Response to Discriminatory Actions ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 PY-CEI-NRR-2405, Informs NRC That Pnpp Staff Has Implemented Formal Industry Position on Severe Accident Mgt1999-06-14014 June 1999 Informs NRC That Pnpp Staff Has Implemented Formal Industry Position on Severe Accident Mgt ML20195H9051999-06-10010 June 1999 Forwards Two License Renewal Applications Consisting of NRC Form 398 & NRC Form 396 for Bk Carrier,License OP-30997 & Jt Steward,License OP-30564-1 ML20212H5841999-06-10010 June 1999 Responds to NRC Notice of Level III Violation Received by K Wierman.Corrective Actions:K Wierman Has Been Dismissed from Position at Perry NPP PY-CEI-NRR-2408, Forwards Rev 4 to Pump & Valve Inservice Testing Program Plan, Incorporating Changes to Program to Implement Second Ten Yr Insp Interval1999-06-10010 June 1999 Forwards Rev 4 to Pump & Valve Inservice Testing Program Plan, Incorporating Changes to Program to Implement Second Ten Yr Insp Interval ML20195G6741999-06-10010 June 1999 Forwards Insp Rept 50-440/99-03 on 990407-0517.Two Violations of NRC Requirements Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy PY-CEI-NRR-2407, Responds to NRC Re Violations Noted in Investigations Rept 3-98-005.Corrective Actions:Initiated Internal Investigation Into Matter to Discover Party Responsible for Falsification of Training Records1999-06-0909 June 1999 Responds to NRC Re Violations Noted in Investigations Rept 3-98-005.Corrective Actions:Initiated Internal Investigation Into Matter to Discover Party Responsible for Falsification of Training Records 1999-09-09
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217F3901999-10-14014 October 1999 Discusses Request That Proprietary Document NEDE-32907P,DRF A22-0084-53, Safety Analysis Rept for Perry NPP 5% Power Uprate, Class III Dtd Sept 1999 Be Withheld.Determined Document Proprietary & Will Be Withheld ML20217G9201999-10-14014 October 1999 Discusses Utils Request for Approval of Quality Assurance Program Changes ML20212K9271999-09-30030 September 1999 Refers to 990927 Meeting Conducted at Perry Nuclear Power Plant to Discuss Initiatives in Risk Area & to Establish Dialog Between SRAs & PSA Staff ML20212J1451999-09-30030 September 1999 Forwards Order,In Response to 990505 Application PY-CEI/NRR- 2394L.Order Approves Conforming License Amend Which Will Be Issued & Made Effective When Transfer Completed ML20212G4161999-09-24024 September 1999 Informs of Completion of Licensing Action for Generic Ltr 98-01, Y2K Readiness of Computer Systems at Nuclear Power Plants, for Perry Nuclear Power Plant ML20212A8371999-09-13013 September 1999 Forwards Insp Rept 50-440/99-13 on 990712-30 & Notice of Violation.Insp Included Evaluation of Engineering Support, Design Change & Modification Activities,Internal Assessment Activities & Corrective Actions ML20217A8971999-09-0909 September 1999 Forwards Insp Rept 50-440/99-09 on 990709-0825.One Violation of NRC Requirements Occurred & Being Treated as NCV, Consistent with App C of Enforcement Policy ML20211Q6911999-09-0606 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Perry Operator License Applicants During Wks of 010108 & 15.Validation of Exam Will Occur at Station During Wk of 001218 IR 05000440/19990011999-08-31031 August 1999 Requests That Page Number 4, P2 Status of EP Facilities, Equipment & Resources, of Insp Rept 50-440/99-01 Be Replaced with Encl Rev ML20210Q8421999-08-13013 August 1999 First Final Response to FOIA Request for Documents.Records Listed in App a Being Released in Entirety & Records Listed in App B Being Withheld in Part (Ref FOIA Exempt 5) ML20210R7861999-08-12012 August 1999 Forwards Insp Rept 50-440/99-12 on 990712-16.No Violations Noted.New Emergency Preparedness Program Staff & Mgt Personnel Were Professional & Proactive ML20210K6331999-08-0404 August 1999 Submits Response to Requests for Addl Info to GL 92-01,Rev 1, Reactor Vessel Structural Integrity, for Perry Nuclear Plant,Unit 1 ML20210G8411999-07-28028 July 1999 Informs That Based on Determination That Rev 14 Changes to Various Portions of Perry Nuclear Power Plant Emergency Plan Does Not Decrease Effectiveness of Licensee Emergency Plan & Meets Standard of 10CFR50.47(b),no NRC Approval Required ML20210E0661999-07-22022 July 1999 Forwards Insp Rept 50-440/99-08 on 990518-0708.No Violations Noted.Overall Conduct of Activities at Perry Facility, Conservative & Professional with Continuing Focus on Safety ML20209E5951999-07-0909 July 1999 Ltr Contract:Task Order 46, Perry Engineering & Technical Support (E&Ts) Insp, Under Contract NRC-03-98-021 ML20209D5931999-07-0101 July 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Investigation Rept 3-98-005 Issued on 990510.Corrective Actions Will Be Examined During Future Inspections ML20196H9641999-06-29029 June 1999 Confirms 990615 Telcon Request with J Lieberman for Addl Time to Respond to Enforcement Action 99-012.FirstEnergy Has 60 Days to Respond to EA ML20195G6741999-06-10010 June 1999 Forwards Insp Rept 50-440/99-03 on 990407-0517.Two Violations of NRC Requirements Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy ML20207G3921999-06-0808 June 1999 Forwards Notice of Consideration of Approval of Transfer of License DPR-58 & Issuance of Conforming Amend & Opportunity for Hearing Re 990505 Application ML20207B7341999-05-26026 May 1999 Forwards Correction of Typo in TS Table 3.3.6.1-1 for Plant, Unit 1 DD-99-08, Informs That to Extent That Union of Concerned Scientists Requests Commission Undertake Formal Review of DD-99-08 & Hold Meeting to Directly Receive View on Decision,Request Denied.With Certificate of Svc.Served on 9905211999-05-20020 May 1999 Informs That to Extent That Union of Concerned Scientists Requests Commission Undertake Formal Review of DD-99-08 & Hold Meeting to Directly Receive View on Decision,Request Denied.With Certificate of Svc.Served on 990521 ML20207B1251999-05-20020 May 1999 Discusses Investigation Rept 3-98-007 on 981210 & Forwards Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $110,000 IR 05000440/19980181999-05-14014 May 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-440/98-18 on 981110 ML20206Q5181999-05-14014 May 1999 Responds to to SL Hiatt Re Fee Exemption Granted to Firstenergy Nuclear Operating Co,Operator of Perry Nuclear Plant.Action Consistent with Longstanding Policy & Practice,As Well as Legal Requirements ML20196F8081999-05-12012 May 1999 Partially Deleted Ltr Referring to Investigation Case 3-1998-007 Re Determination Whether Recipient Discriminated Against Radiation Protection Supervisor at Perry for Providing Testimony as Witness in DOL Hearing ML20206Q0171999-05-12012 May 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization, Division of Licensing Project Management Created ML20206S5381999-05-12012 May 1999 Forwards Insp Rept 50-440/99-07 on 990412-16.No Violations Noted.Insp Consisted of Selective Exam of Procedures & Representative Records,Interviews with Personnel & Observation of Activities in Progress ML20206Q2111999-05-10010 May 1999 Discusses Investigation Rept 3-98-005,completed on 990129 & Forwards NOV & OI Rept Synopsis.Circumstances Surrounding Apparent Falsification of Training Records for Individuals Assigned Position in Er Organization Were Investigated ML20196A2961999-05-10010 May 1999 Discusses Investigation Rept 3-98-005 Conducted on 990129 Re Circumstances Surrounding Apparent Falsification of Training Records for Individuals Assigned Positions in Emergency Response Organization & Forwards NOV & Synopsis ML20206H3981999-05-0606 May 1999 Forwards Insp Rept 50-440/99-06 on 990303-04 & 0412-16.No Violations Noted.Inservice Insp Activities Effectively Implemented with Several Aspects Demonstrating Good Safety Focus ML20206N3161999-05-0606 May 1999 Responds to Ltr to NRC on Continued Events Re Transfer of Generation Assets Between Dl & Firstenergy.Info Will Be Considered as NRC Monitor Pending License Transfer Application of Bvps,Units 1 & 2 & Pnpp ML20206H6731999-05-0505 May 1999 Confirms Discussion Between Members of NRC & Recipient Re Meeting Scheduled for 990520 in Lisle,Il to Discuss Operational Issues & Related Topics of Interest to Licensed Operators at Nuclear Power Plants Located in Region III ML20206G6901999-05-0303 May 1999 Forwards Insp Rept 50-440/99-02 on 990225-0406.Two Violations of NRC Requirements Occurred & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20206G6401999-05-0303 May 1999 Forwards Safety Evaluation Authorizing Relief Requests IR-032 to IR-035 & IR-037 to IR-040 Re Implementation of Subsections IWE & Iwl of ASME Section XI for Containment Insp.Relief Requests IR-36 & IR-41 Withdrawn ML20206D4701999-04-30030 April 1999 Informs That on 990428,FirstEnergy Submitted Post Exam Results of Weld Overlay Repair for Feedwater Nozzle to safe-end Weld at Perry Nuclear Power Plant,Unit 1 (Pnpp) ML20206E2111999-04-29029 April 1999 Discusses Alternative Proposed by Licensee on 990325 & 990401 to ASME BPV Code,Section XI Repair Requirements Along with Separate Alternative to Ultrasonic Exam Acceptance Criteria.Forwards SE Approving Proposed Alternatives ML20205P4041999-04-15015 April 1999 Discusses GL 95-07 Issued by NRC on 950817 & Licensee Responses Submitted on 951016,960213 & 960624 for Perry NPP, Unit 1.Forwards Safety Evaluation Concluding That Licensee Adequately Addressed Actions Requested in GL 95-07 ML20205P0281999-04-12012 April 1999 Provides Individual Exam Results for Applicants Who Took Mar 1999 Initial License Exam.Information Considered Proprietary in Accordance with 10CFR2.790.Without Encls ML20205J5331999-04-0606 April 1999 Ack Receipt of Denying Request from NRC That Addl Info Be Provided Prior to Informal Public Hearing Held on 990222 Re River Bend Station & Perry Nuclear Power Plant 10CFR2.206 Petitions ML20205K5211999-04-0505 April 1999 Forwards Notice of Withdrawal of 970409 LAR on Refueling Interlocks,In Response to Util .Amend Request Will Be Replaced in Future by Similar Request,Based on Approved STS Change Traveler,Number TSTF-225 ML20196K8461999-04-0202 April 1999 Forwards Insp Rept 50-440/99-05 on 990301-05.No Violations Noted.Informs That Licensee Use of 10-Minute Rule & 4-Hour Rule Remains Under NRC Review.Expresses Re Practice Revising Unavailability Criteria on Recurrent Basis ML20205G3891999-03-31031 March 1999 Forwards Safety Evaluation Re Second ten-year Inservice Testing Program Relief Requests.Proposed Alternatives in Relief Requests VR-6,PR-3 & PR-6 May Be Authorized.Relief Request VR-8 Denied ML20205G0441999-03-26026 March 1999 Advises of Planned Insp Effort Resulting from Perry PPR Review,Which Was Completed on 990202.Overall,performance at Perry Was Acceptable ML20205F0011999-03-25025 March 1999 Responds to Re Safety of Perry Nuclear Power Plant & That Plant Operating with Limited Leaks in Three Fuel Rods for Several Months.Informal Public Hearing Re Leaks at Perry Facility Held in Rockville,Md on 990222 ML20205C1611999-03-25025 March 1999 Discusses GL 96-05 Issued on 960918 & Firstenergy 961118, 970317 & 980930 Responses to GL 96-05 Indicating Intent to Implement Provisions of JOG Program on MOV Periodic Verification at Perry Npp.Forwards RAI Re GL 96-05 Program ML20204D8891999-03-17017 March 1999 Forwards Insp Rept 50-440/99-04 on 990222-26.No Violations Noted.Insp Focused on Radiological Planning for Spring 1999 Refueling Outage,On Assessments of Radiation Protection Program & on Radiological Training for General Employees ML20204E7791999-03-17017 March 1999 Forwards Insp Rept 50-440/99-01 on 990113-0224.Non-cited Violation Was Identified ML20207H9921999-03-11011 March 1999 Informs That Requirements to Pay Fee Under 10CFR170 for Review of Pilot Plant Application for Use of Revised Accident Source Term Methodology for Perry Nuclear Power Plant Unit 1,waived for Reasons Stated ML20207K1991999-03-0404 March 1999 Forwards List of Names of Those Individuals & Their Organizational Affiliation as Appropriate,Who Spoke at Informal Public Hearing Re Petitions Filed Pursuant to 10CFR2.206 for River Bend & Perry Plants on 990222 ML20203F8501999-02-11011 February 1999 Forwards Fr Notice to Be Published on 990219 Re Informal 10CFR2.206 Public Hearing Including Video Teleconferencing 1999-09-09
[Table view] |
See also: IR 05000440/1996008
Text
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January 23, 1997
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EA 96-367 l
Mr. Lew W. Myers
Vice President - Nuclear
Centerior Service Ccmpany
P. O. Box 97, A200
Perry, OH 44081 l
I
SUBJECT: NOTICE OF VIOLATION (NRC INSPECTION REPORT NO. 50-440/96008(DRS)) I
Dear Mr. Myers:
1
This will acknowledge receipt of your letter dated December 6,1996, in response
to our lotter dated November 6,1996, transmitting a Notice of Violation associated with
the circumstances surrounding the loss of both trains of the Emergency Closed Cooling
(ECC) system in 1993, and the loss of both trains of Control Room Emergency
1
Recirculation due to low ECC temperature in 1994 at your Perry facility. We have ;
I
reviewed your corrective actions and have no further questions at this time. These
l
corrective actions will be examined during future inspections. I
Sincerely,
/s/ M. Icach (for)
Geoffrey E. Grant. Director ,
Division of Reactor Safety l
l
Docket No. 50-440
Enclosure: Ltr 12/06/96 L. W. Myers,
Centerior Energy, to US NRC w/ encl i
Distribution:
See attached list 9701290004 970123
PDR ADOCK 05000440
0 PDR
DOCUMENT NAME: G:\DRS\ PERO 1227.DRS
To nelive a copy of this document. Indict.te in the box: "C" = Copy w/o attachment / enclosure "E" = Copy with attachment / enclosure "N" = No copy
0FFICE Bill:DRS l et Rill:DRS l6 RIII:DRP m lm - RIII:EICS l c) RIII:DRS l#
NAME d iDuncan/kjc RingftV/ Jacobsorf\WW Clayton f4- Grant e t h
DATE 01/23/97 01/q3 /97 OlM /47/ \ U 01/1;' /97 ' 01/1:b /97
0FFICIAL RECORD COPY
l
. _ . - - _
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.. - - . - . _ ~ - - . . _ . . . - - . - . - - . . - - --
<
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[-
L. Myers 2 January 23, 1997
a l
j cc w/o encl: J. P. Stetz, Senior Vice i
.
President, Nuclear
L. W.- Worley, Director, Nuclear 1
,
~
Services Department l
J. D. Kloosterman, Manager, '
'
Regulatory Affairs
1 W. R. Kanda, Director, Perry Nuclear
Assurance Department
,
N. L. Bonner, Director, Perry l
2 Nuclear Engineering Department 1
H. Ray Caldwell, General Superintendent , l
l Nuclear Operations. l
i R. D. Brandt, General Manager Operations 1
- ,
a 1
1 cc w/ encl: Terry J. Lodge, Esq. '
State Liaison Officer, State of Ohio
- Robert E. Owen, Ohio Department of Health
l C. A. Glazer, State of Ohio, -
'
Public Utilities Commission
Distribution:
, Docket File w/enci SRI, Perry w/ encl J. Goldberg, OGC w/enci j
i MdC]E-0Tw/eticli LPM, NRR w/ encl R. Zimmerman, NRR w/enci '
DU/LFDCB w/enci A. B. Beach, Rlll w/ encl
DRP w/enct W. L. Axelson, Rlll w/enci
) DRS w/ encl Enf. Coordinator, Riti w/ encl
i Rlll PRR w/enci J. Lieberman, OE w/ encl
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CENTERDOR
ENERGY
PERRY NUCLEAR POWER PLANT Mail Address: !
P.O. BOX 97 l
10 CENTER ROAD '
PERRY, OHIO 44081 PERRY, OHIO 44081
(216) 259-3737
l
December 6,1996
'
PY-CEI/NRR-2118L
United States Nuclear Regulatory Commission l
Document Control Desk
Washington, D.C. 20555
1
Perry Nucl:ar Power Plant
Docket No. 50-440
Reply to a Notice of Violation
Ladies and Gentlemen:
1
Enclosed is the reply to the Notice of Violation contained in NRC Inspection Report 50-
440/96-08, which was transmitted by letter dated November 6,1996. The Notice of Violation l
describes three violations involving: a failure to comply with the actions of Emergency
s' Closed Cooling (ECC) system Technical Specification Limiting Conditions for Operation; the
failure to take adequate corrective actions to prevent ECC system temperature from l
decreasing below 55' F; and, the failure to appropriately classify an ECC system valve as an
American Society of Mechanical Engineers Code,Section XI, Category "A" valve in a timely
manner.
If you have questions or require additional information, please contact
Mr. James D. Kloosterman, Manager - Regulatory Affairs, at (216) 280-5833.
Very truly yours,
W W
Lew W. Myers
Vice President - Nuclear
CRE:sc
Attachment
Enclosure
cc: NRC Region III Administrator
, NRC Resident Inspector
NRC Project Manager
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PY-CEI/NRR-2118L
Attachment i
I, Lew W. Myers, being duly sworn state that (1)I am Vice President, Nuclear of the
Centerior Service Company, (2)I am duly authorized to execute and file this certification on
behalf of the Cleveland Electric Illuminating Company and Toledo Edison Company, and as
the duly authorized agent for Duquesne Light Company, Ohio Edison Company, and
Pennsylvania Power Company, and (3) the statements set forth herein are true and correct to
the best of my knowledge, information and belief.
I. Lew
. nW. Myers
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Sworn to and subscribed before me, the [p day of h,, ./996 .
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PY-CEI/NRR-2118L
Enclosure '
Page 1 of 6
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REPLY TO A NOTICE OF VIOLATION
Violation 96008-I
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Restatement of Violation
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I Technical specification 3.7.1.2 requires, for Operational Conditions 1,2,3,4, and 5, the emergency closed
cooling (ECC) loop (s) shall be operable which are associated with systems or components which are ;
required to be operable. With an ECC loop (s) inoperable which is associated with system (s) or
component (s) required to be operable, declare the associated system (s) or component (s) inoperable and
take the action required by the applicable specification (s).
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A. Contrary to the above, from March 19 to July 2,1993, while the plant was in Operational
Conditions 1,2,3,4, or 5, ECC Train A was inoperable and its associated systems or components
were not declared inoperable, and action was not taken for its associated systems or components
as required by the applicable specifications. (01013)
B. Contrary to the above, from 3:13 a.m. on June 14,1993, until 11:05 p.m. on June 15,1993,a
period of about 45 hours5.208333e-4 days <br />0.0125 hours <br />7.440476e-5 weeks <br />1.71225e-5 months <br />, while the plant was in Operational Conditions 1,2, or 3, both trains of
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ECC were inoperable and their associated systems or components were not declared inoperable,
and action was not taken for their associated systems or components as required by the applicable
specificctions. (01023)
This is a Severity Level III problem (Supplement 1).
Reason for the Violation
The ECC train / system inoperability discussed in the Notice of Violation resulted from excessive leakage
through valve OP42-F295A. This leakage was caused by a combination of personnel error and inadequate
procedural direction for setting motor-operated valve (MOV) limit switches and mechanical stops. The
valve was improperly set during maintenance performed on March 19,1993, resulting in the excessive
leakage. A post-maintenance leakage test was not programmatically required nor performed at that time
since the valve was classified as an American Society of Mechanical Engineers (ASME) Code,Section XI,
Category "B" valve, and as such, did not have specific leakage criteria assigned. The valve leakage was
not identified until July 1,1993, when a routine operational evolution identified concerns with the isolation
capability of the ECC system.
Corrective Steos Taken and Results Achieved
The limit switches and mechanical stops for valve OP42-F295A were readjusted on July 2,1993. An
allowable leakage criteria was determined for the valve and a post-maintenance leak test was performed on
the same day. The valve successfully met its leakage acceptance criteria and passed the post-maintenance
test.
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Corrective Steos that Will Be Taken to Avoid Further Violation
The procedure on adjusting Limitorque limit / torque switches, General Electrical Instruction (GEI)-0014,
"Limitorque Limit / Torque Switch Adjustment," was revised to provide the requisite level of direction for
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PY-CEI/NRR-2118L
Enclosure
Page 2 of 6
setting limit and torque switches, and adjusting mechanical stops. The procedure revision also added a
post-maintenance test requirement for butterfly valves that have an established seat leakage limit. Training
was conducted for appropriate Maintenance and Engineering personnel on this issue and on the necessity
of verifying proper butterfly valve closure.
An engineering evaluation was perfonned to determine if other motor operated butterfly valves were
affected by the causes that resulted in the inoperability of 0P42-F295A; other than the other valves in the
ECC system which perform a similar isolation function (0P42-F295B, OP42-F325A, and OP42-F325B,
which were not leaking but had no leakage criteria established), no other concerns were identified. These
valves were re-categorized as an ASME Code ,Section XI, Category "A" valves on October 8,1996. As
such, they will be periodically leak tested as part of the In-service Testing program (ISTP) against specific
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leakage acceptance criteria. Additionally, the Engineering Department conducted a review of other ASME
Code,Section XI, Category "B" valves in the ISTP to determine if their respective categorization needed to
be changed: no additional valves requiring re-categorization were identified.
Date When Full Compliance Will Be Achieved
Full compliance has been achieved.
Additional Information
Both examples in this violation state that the actions required by Technical Specification (TS) 3.7.1.2. were
not taken as required. With respect to example B, although the actions required by TS 3.7.1.2. were not l
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taken, this specification would not have been the most limiting TS. TS 3.8.1.1.e. required that with a - !
Diesel Generator (DG) (e.g., Division 2 DG) inoperable, a " cross-train check" be performed. Given that
ECC train "A" was inoperable, the associated TS 3.8.1.1.e. shutdown statement would have been entered
had the inoperability of ECC train "A" been recognized.
Violation 96008-II
Restatement of Violation
10 CFR Past 50, Appendix B Criterion XVI, " Corrective Action," requires, in part, that measures be
established to assure that conditions adverse to quality are promptly identified and corrected. In the case of
significant conditions adverse to quality, the measures shall assure that the cause of the condition is
determined and corrective action taken to preclude repetition.
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PY-CEI/NRR-2118L I
Enclosure
Page 3 of 6
Contrary to the above, as of September 11,1996, the licensee had failed to promptly correct a significant
) condition adverse to quality as demonstrated by the following:
1.
In February 1986, a control complex chiller tripped on low refrigerant temperature due to
low lake water temperatures (Emergency Closed Cooling water to the chiller must be
greater than 55* F to meet chiller design requirements). As corrective action for this
condition the licensee initiated Design Change Package (DCP) 86-0224 to alleviate the
problem; however, the design change only considered ECC accident heat loads and did
not consider minimum loads when Emergency Service Water was less than 55" F.
2. In February 1994, with ESW "A" and ECC "A" running and supplying a minimal heat
load, ECC "A" temperature was observed to be below 55* F.
3. DCP 94-0027 was implemented in Spring 1996 to maintain ECC temperature above 55
F with low lake water temperature and low heat load conditions and the post.
modification test did not confirm the adequacy of the design. Subsequently, on March 7,
1996, ESW "A" and ECC "A" were in operation with no heat load, and ECC "A"
temperature decreased from 64* F to 56* F before ESW "A" was secured to prevent ECC
"A" from decreasing below 55* F. (02014)
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This is a Severity Level IV violation (Supplement I).
B. Contrary to the above, as of August 26,1996, the licensee had not corrected a significant
condition adverse to quality. Specifically, the licensee had previously identified on January 20,
1994, that valves OP42-F295A/B and OP42-F325A/B were not classified as Category "A" in
accordance with American Society ofMechanical Engineers (ASME),Section XI,1983, Article
IWV-2000, and no corrective action was taken until this condition was identified by the NRC
during a 1996 inspection. (02024)
This is a Severity Level IV violation (Supplement I).
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Violations A. and B. are addressed individually below.
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Background (Violation A3
As stated in the Inspection Report, Control Complex chiller unit operability has been challenged in the past
due to low refrigerant temperatures resulting from ECC supply temperatures being less than 55* F,
particularly with little or no heat loading on the ECC system. This scenario occurs as a result oflow ESW
system temperatures; the ESW system is supplied from Lake Erie and provides the source ofcooling for
the ECC system via the ECC system heat exchangers. The issue was initially identified in February 1986,
when the Control Complex chiller units tripped while operating with ECC supply (i.e., ESW system) water
temperatures at 34* F. The corrective actions resulting from this event primarily involved restricting ESW
flow to the ECC heat exchanger via installation of a bypass line at the ESW discharge of the heat
exchanger, effectively reducing the discharge line from a 14 inch diameter to a 3 inch diameter, thus
' minimizing heat exchanger heat transfer. Throttling instructions were provided to Operations personnel
regarding control of ECC system temperatures to assure adequate heat removal capability during accident
j conditions. These actions were believed to have resolved ECC system temperature control concerns.
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Enclosure
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In Febreary 1994, the ECC system was observed to be drifting below 55' F during RHR heat exchanger ,
performance testing, again challenging the operability of the Control Complex chillers. The event was !
evaluated via the corrective action process, with notification provided to the NRC under LER 94-005. The
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results of the investigation indicated that the 3 inch diameter ESW by-pass line was sized without
considering minimum heat loads potentially generated during testing operations. Plant operators were
locally stationed to continuously monitor and control ECC system temperatures when the Lake Erie water i
temperatures fell below 55 F. An additional modification was pursued to relieve the operator burden by l
installation of automatic temperature control.
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After extensive evaluation of options and conceptual designs for resolution of the effects oflow lake water l
temperatures, DCP 94-027 was developed to install a three-way, electro-hydraulic, temperature control
valve capable of divening and bypassing 100% of ECC system flows around the ECC heat exchanger,
effectively eliminating heat transfer capability between the ESW and ECC systems. Following installation
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of the modification during the fifth refueling outage, temperatures were again recognized as decaying l
toward 55 F. The failure of the modification to control temperature without heat loading on the ECC l
system was investigated in accordance with the corrective action process.
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Reason for the Violation (Violation A3 '
This violation was caused by the failure to adequately recognize the full range of ECC system design and
operating requirements, including those present during testing configurations until 1994. In developing
DCP 94-027, system design and operating requirements were fully recognized and established in the
respective design report. However, a heat transfer mechanism associated with the resultant modified
configuration was not fully recognized during modification development and implementation; therefore,
this heat transfer mechanism was not accounted for in the design nor the post-modification test.
Corrective Steos Taken and Results Achieved (Violation A3
Procedural controls were implemented via precautions in the system operating instructions and guidance in
the alarm response instructions, to avoid challenging the temperature limitations of the ECC system and
Control Complex chillers given the gradual rate of decay of ECC while bypassing 100 percent of ECC heat
exchanger flow.
Corrective Steos that Will Be Taken to Avoid Further Violation (Violation A3
To address the issue associated with not fully recognizing system design and operating requirements,
fuither occurrence should be precluded through changes that have been implemented in the design change
processes. These changes include: development of formalized design reports which contain system
functional and operational requirements, as well as, a complete modification design bases; a multi-
disciplinary modification development and review team; and, integrated Operations involvement
throughout the modification process, including testing.
Revised procedural controls (e.g., revision to Plant Administrative Procedure (PAP) - 0309, " Processing
Plant Modifications," and Nuclear Engineering Instruction (NEI) - 0373, " Initiating, Developing, and
Processing Design Modifications") are being developed to enhance post-modification testing guidelines,
particularly with respect to demonstrating the functionality ofinstalled modifications.
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Enclosure
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In addition, the bases for lowering the alarm setpoint for ECC water supply temperature to resolve system
response to low lake water temperatures and to eliminate the need for administrative measures for
operating the system over the complete range oflake temperatures, are being evaluated. The program
involves establishing the design bases for chiller refrigerant temperature and developing test parameters
and executing testing to demonstrate system operability at ECC supply temperature lower than the current
55* F limitation.
Date When Full Comnliance Will Be Achieved (Violation A3
Full compliance will be achieved with the implementation of the additional post-modification testing
guidelines. This action will be completed by March 31,1997.
Reason for the Violation (Violation B3
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As discussed in the reply to the first violation, valve OP42-295A was initially classified as an ASME Code,
Section XI, Category "B" valve, which does not require leakage testing to a specific acceptance criteria. t
When this issue was being evaluated in late 1993, it was identified that due to limitations that valve
leakage had on ECC system operability, the valve's Code categorization needed to be re-evaluated and
revised. This was documented in Condition Report 93-0508 as Condition Report Corrective Action
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(CRCA) 93-0508-01. However, when this corrective action was evaluated and subsequently closed, the !
corrective action focused on determining a specific leakage acceptance criteria; the issue of Code
categorization was inappropriately not addressed. The reason that this action was not addressed was due to
an oversight on the part of the individual that was responsible for evaluating and closing the respective i
CRCA. Since the valve was already categorized as a Category "B" valve as part of e e approved ISTP,
coupled with the failure to re-categorize the valve when it was identified during issue resolution, the valve ;
remained improperly categorized until questioned by the NRC during their inspection.
Corrective Steos Taken and Results Achieved (Violation B3
Valves OP42-F295A, OP42-F295B, OP42-F325A, and OP42-F325B were re-categorized as ASME Code,
Section XI, Category"A" valves on October 8,1996. As such, they will be periodically leak tested as part
of the ISTP progren against specific leakage acceptance criteria.
Corrective Stens that Will Be Taken to Avoid Further Violation (Violation B3
As discussed in the response to Violation 96008-1, the Engineering Department conducted a review of
other ASME Code,Section XI, Category "B" valves in the ISTP to detennine if their respective
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categorization needed to be changed; no additional valves requiring re-categorization were identified.
Date When Full Comnliance Will Be Achieved (Violation B3
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Full compliance has been achieved. To facilitate additional confidene that valves have been appropriately !
categorized / tested, an additional evaluation is in progress for non-safety to safety related system interfaces
within the Primary Coolant Leakage Reduction for Systems Outside Containment program.
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Enclosure
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The following table identifies those actions which are considered to be regulatory commitments. Any
j other actions discussed in this document represent intended or planned actions, are described for the NRC's
information, and are not regulatory commitments. Please notify the Manager - Regulatory Affairs at the
i Perry Nuclear Power Plant of any questions regarding this doeurnent or any associated regulatory
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commitments.
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Commitments
Date When Full Comoliance Will Be Achieved (Violation A3
Full compliance will be achieved with the implementation of the additional post-modification testing
guidelines. This action will be completed by March 31,1997.
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