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Category:Accident Sequence Precursor (ASP) Analysis
MONTHYEARML20294A5522020-12-0909 December 2020 Final Accident Sequence Precursor Analysis - Brunswick Steam Electric Plant (Unit 1), Loss of Offsite Power During Hurricane Isaias (LER 325-2020-003) - Precursor ML20168A4402020-06-16016 June 2020 Final ASP Analysis - Brunswick 2 (LER 324-75-005) ML20168A4442020-06-16016 June 2020 Final ASP Analysis - Brunswick 2 (LER 325-79-089) ML20168A4432020-06-16016 June 2020 Final ASP Analysis - Brunswick 2 (LER 324-79-050) ML20168A4422020-06-16016 June 2020 Final ASP Analysis - Brunswick 2 (LER 324-77-054) ML20168A4412020-06-16016 June 2020 Final ASP Analysis - Brunswick 2 (LER 324-75-013) ML20168A4392020-06-16016 June 2020 Final ASP Analysis - Brunswick 1 (LER 325-77-001) ML20147A4762020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-87-004) ML20147A3602020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-82-025) ML20147A3612020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-82-041) ML20147A3622020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-82-054) ML20147A3652020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-84-006) ML20147A3662020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-84-014) ML20147A4692020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-85-059) ML20147A4712020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-82-005) ML20147A4722020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-82-029) ML20147A4732020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-82-123) ML20147A4742020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-84-014) ML20147A4752020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-87-001) ML20147A4772020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-89-009) ML20147A3642020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-82-069) ML20147A4702020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-81-039) ML20147A3592020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-81-032) ML20135G7292020-05-14014 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-91-018) ML20050R5682020-02-20020 February 2020 Final Accident Sequence Precursor Analysis-Brunswick Unit 1, Degraded Principal Barrier, Technical Specification Shutdown, and Automatic System Actuation (LER 325-2019-002)-Training/Reject ML17109A2692017-03-17017 March 2017 Final ASP Analysis-Brunswick 1 (LER 325-2016-001) 2020-06-16
[Table view] Category:Final
MONTHYEARML20294A5522020-12-0909 December 2020 Final Accident Sequence Precursor Analysis - Brunswick Steam Electric Plant (Unit 1), Loss of Offsite Power During Hurricane Isaias (LER 325-2020-003) - Precursor ML20168A4402020-06-16016 June 2020 Final ASP Analysis - Brunswick 2 (LER 324-75-005) ML20168A4442020-06-16016 June 2020 Final ASP Analysis - Brunswick 2 (LER 325-79-089) ML20168A4432020-06-16016 June 2020 Final ASP Analysis - Brunswick 2 (LER 324-79-050) ML20168A4422020-06-16016 June 2020 Final ASP Analysis - Brunswick 2 (LER 324-77-054) ML20168A4412020-06-16016 June 2020 Final ASP Analysis - Brunswick 2 (LER 324-75-013) ML20168A4392020-06-16016 June 2020 Final ASP Analysis - Brunswick 1 (LER 325-77-001) ML20147A4762020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-87-004) ML20147A3602020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-82-025) ML20147A3612020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-82-041) ML20147A3622020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-82-054) ML20147A3652020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-84-006) ML20147A3662020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-84-014) ML20147A4692020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-85-059) ML20147A4712020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-82-005) ML20147A4722020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-82-029) ML20147A4732020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-82-123) ML20147A4742020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-84-014) ML20147A4752020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-87-001) ML20147A4772020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-89-009) ML20147A3642020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-82-069) ML20147A4702020-05-26026 May 2020 Final ASP Analysis - Brunswick 2 (LER 324-81-039) ML20147A3592020-05-26026 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-81-032) ML20135G7292020-05-14014 May 2020 Final ASP Analysis - Brunswick 1 (LER 325-91-018) ML20050R5682020-02-20020 February 2020 Final Accident Sequence Precursor Analysis-Brunswick Unit 1, Degraded Principal Barrier, Technical Specification Shutdown, and Automatic System Actuation (LER 325-2019-002)-Training/Reject ML17109A2692017-03-17017 March 2017 Final ASP Analysis-Brunswick 1 (LER 325-2016-001) 2020-06-16
[Table view] |
Text
h RIIR Service Water Pumps Inoperable at Brunswick 2 sequence was:
ctor was operating at 88% power.
rator gave a mechanic clearance to uncouple 2B RHR pump for alignment c uncoupled pump 2A by mistake.
act ion:
hours later the error was discovered and pump 2A was recoupled and nsure operability.
ose of failed system or component:
R provides reactor core cooling and water level control during normal d shutdown periods. The RHR can also be operated in the LPCI mode.
ity of system per WASH 1400:
- 1.1 x 10-4 /D ty of component per WASH 1400:
- 3 x 10-3 /D operator error 1
ilabilities are in units of per demand D- . Failure rates are in r hour HR'*.
No - normal operation &
HPCI in service.
No SIC 150271 - Actual Occurrence of Both RHR Service Water Pumps Inoperable at Brunswick 2
Severe No.
Core Damage No1 Yes 2 No 3 Yes 4 Yes 5 Yes 6 Yes 7 NSIC 150271 - Sequence of Interest of Both RHR Service Water Pumps Inoperable at Brunswick 2 iFor success the operator must rack the pumps backin within 2-24 hours.
CATEGORIZATION OF ACCIDENT SEQUENCE PRECURSORS CESSION NUMBER: 150271 LER: July 12, 1979 EVENT: June 19, 1979 INVOLVED: RHR NT INVOLVED: service water pumps human error E OF INTEREST: loss of feedwater OCCURRENCE: Both RHR service water pumps inoperable at Brunswick 2 NAME: Brunswick 2 NUMBER: 50-324 TYPE: BWR ELECTRICAL RATING: 821 MWe AGE: 4.25 yr GE CT-ENGINEERS: United Engineers and Constructors RS: Carolina Power and Light N: Three miles N of South Port, NC N: 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> PERATING CONDITION: 88% power FEATURE TYPE OF FAILURE: (a) inadequate performance; (b) failed to start; Onade inoperable; (d) ___________
RY METHOD: operator surveillance
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