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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217L7971999-10-20020 October 1999 Submits Results of Review of 990521 & 0709 Ltrs Which Provided Core Shroud Insp Results & Tie Rod Stabilizer Assemblies ML20217G1291999-10-15015 October 1999 Forwards Errata to Safety Evaluation for Amend 168 Issued to FOL DPR-63 on 990921.Description of Flow Control Trip Ref Cards to Be Consistent with Application for Amend ML20217K2831999-10-14014 October 1999 Submits Response to NRC Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates, for Fiscal Yrs 2000 & 2001 ML20217H3211999-10-0808 October 1999 Forwards Changed Pages for Issue 5,rev 1 of Nine Mile Point Station Physical Security & Safeguards Contingency Plan,Iaw 10CFR50.54(p).Without Encls ML20212K8601999-10-0606 October 1999 Responds to Concern in 990405 Petition Re Residual Heat Removal Alternate Shutdown Cooling Modes of Operation at Nine Mile Point Nuclear Station,Unit 2 ML20216J9311999-09-30030 September 1999 Forwards Response to NRC 981119 Suppl RAI Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions ML20212J4651999-09-30030 September 1999 Informs of Completion of mid-cyle PPR of Nine Mile Point Nuclear Station on 990916.Determined That Problems in Areas of Human Performance & Work Control Required Continued Mgt Attention.Historical Listing of Plant Issues Encl ML18040A3701999-09-30030 September 1999 Provides Changes to Application for Amend Re Volumes 1-11 of 981016 Submittal & Discard & Insertion Instructions Re Integration of Proposed Changes,In Response to NRC RAIs ML20212K8641999-09-30030 September 1999 Informs That During 990927 Telcon Between J Williams & J Bobka,Arrangements Were Made for Administration of Exams at Plant During Wk of Feb 14,2000.Preliminary RO & SRO License Applications Should Be Submitted 30 Days Prior Exam ML20212J8831999-09-30030 September 1999 Informs That Util 980810 & 990630 Responses to GL 98-01 & Suppl 1, Y2K Readiness of Computer Sys at NPPs Acceptable. NRC Considers Subj GL to Be Closed for Plant ML20212E9801999-09-23023 September 1999 Submits Info in Response to Request for Estimated Initial Operator Licensing Exam Needs,Per Administrative Ltr 99-03 ML20216F7101999-09-17017 September 1999 Forwards Response to NRC 990806 RAI Re USI A-46,verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors.Nrc Is Informed That Actions Required for Resolution of USI A-46 Have Been Completed ML20212B2821999-09-14014 September 1999 Responds to 990712 Correspondence Which Responded to NRC Ltr Re High Failure Rate for Generic Fundamentals Exam of 990407 for Nine Mile Point.Considers Corrective Actions Taken to Be Acceptable ML20212D8981999-09-14014 September 1999 Forwards ISI Summary Rept for Refueling Outage 15 & Flaw Indication Repts.Supporting Info Repts & Calculations, Encl ML20212B2581999-09-10010 September 1999 Requests That Name of Bm Bordenick Be Removed from Nine Mile Point,Units 1 & 2 Service List ML20211P5771999-09-10010 September 1999 Forwards Application for Amends to Licenses DPR-63 & NPF-69, to Transfer Licenses to Amergen Energy Co,Llc.Ts Pages & Proprietary Addendum,Included.Proprietary Encl Withheld ML20212A1341999-09-0707 September 1999 Forwards Summary Rept Secondary Containment Leakage Testing, Dtd June 1999 for Nine Mile Point,Unit 1,IAW TS 6.9.3.f ML20211K8141999-09-0101 September 1999 Forwards Reactor Containment Bldg Ilrt,Iaw Plant TS 6.9.3.e.Testing Confirmed That TS 3.3.3/4.3.3 & 6.16 Primary Containment Leakage Requirements Were Satisfactorily Met ML20211L9221999-09-0101 September 1999 Confirms That Licensee Will Retain Weld 32-WD-050 as IGSCC Category F Until Completion of Reinspection Program,In Response to NRC ML20211J6461999-08-30030 August 1999 Forwards Response to NRC 990625 RAI Re NMPC Responses to GL 92-01,rev 1,supplement 1, Reactor Vessel Structural Integrity ML20211K3001999-08-30030 August 1999 Forwards Semi-Annual Radioactive Effluent Release Rept for 990101-990630 & Revised ODCM, for Nine Mile Point,Unit 1. Format Used for Effluent Data Is Outlined in App B of Regulatory Guide 1.21,rev 1 ML20211K5031999-08-30030 August 1999 Responds to Ltr Addressed to Chairman Dicus, Expressing Concerns Involving 990624 Automatic Reactor Shutdown.Insp Findings & Conclusions Will Be Documented in Insp Repts 50-220/99-06 & 50-410/99-06 by mid-Sept 1999 ML20211H1921999-08-26026 August 1999 Forwards Application for Amend to License DPR-63,supporting Implementation of Noble Metal Chemical Addition by Raising Reactor Water Conductivity Limits in TSs 3.2.3.a,3.2.3.c.1 & 3.2.3.b ML20211P5161999-08-26026 August 1999 Discusses Submitted on Behalf of Niagara Mohawk Power Corp Written Comments Addressing 10CFR2.206 Petition & Request That Ltr & Attached Response Be Withheld from Public Disclosure.Request Denied ML20211G4921999-08-26026 August 1999 Advises That Info Re Comments Addressing 10CFR2.206,dtd 990405 Will Be Withheld from Public Disclosure,In Response to ML20211D7731999-08-20020 August 1999 Forwards Semiannual FFD Program Performance Data Rept Covering Period 990101 Through 990630 ML20211B9371999-08-18018 August 1999 Provides Addl Info Re Application of Method a at Nmp,Unit 1 as Described in Generic Implementation Procedure,Rev 2 (GIP-2),NRC Supplemental SER 2 & Documents Ref in GIP-2 Upon Which GIP-2 Is Based ML18040A3691999-08-16016 August 1999 Forwards Response to NRC 990510 RAI Pertaining to NMP Application for Amend Re Conversion of NMPNS Unit 2 Current TS to Its.Nrc Requested Info Re Several Sections,Including Section 3.6, Containment Sys. ML20210Q0031999-08-11011 August 1999 Informs That Due to Printing Malfunction,Some Copies of Author Ltr Dtd 990726,may Not Have Included Second Page of Encl 2 of Ltr ML20210R6661999-08-10010 August 1999 Confirms Conversation on 990721 Re Concerns of Syracuse Anti-Nuclear Effort on Status of 2.206 Petition (Filed 990524) & Upcoming NRC Performance Review Meeting on Nine Mile Point Units 1 & 2 ML20210R8101999-08-10010 August 1999 Forwards 1998 Annual Repts for NMP & co-tenants,including Rg&E,Energy East Corp/Nyse&G,Chg&E & Long Island Power Authority,Per 10CFR50.71(b) ML20210L5321999-08-0606 August 1999 Forwards List of Subjects Discussed During 990714 Telcon with Representatives of Niagara Mohawk Power Corp on Unit 1 Re USI A-46 Issue ML18041A0711999-07-30030 July 1999 Forwards Rev 1 to NMP2-ISI-006, Second Ten Year Interval ISI Program Plan for Nine Mile Point Nuclear Power Station Unit 2. Significant Changes from Rev 0 Listed ML20210J9351999-07-29029 July 1999 Informs That NMP Is Changing Completion Date for Replacement of Valves Having O Rings with Installed Life Greater than Eight Years.Replacement to Be Completed by 991031, During Hydrogen Monitoring Sys Maintenance Outage ML20216E1491999-07-26026 July 1999 Forwards Two Ltrs Received from NMPC Re Nine Mile Point Unit 1 Core Shroud Related to 10CFR2.206 ML20210E9151999-07-23023 July 1999 Discusses Evaluation of Recirculation Line Weld 32-WD-050 Indication Found During 1997 Refueling Outage (RFO14) at NMPNS Unit 1.Requests Notification of Decision to Retain Category F Classification Until Listed Conditions Satisfied ML20209G7911999-07-12012 July 1999 Provides Info Requested in NRC Re 990407 Generic Fundamentals Exam Failure Causes & Corrective Actions ML20209G3711999-07-12012 July 1999 Provides Final Root Cause Evaluation Re GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 1 ML20209G2001999-07-0909 July 1999 Forwards RFO-15 Core Shroud Insp Summary Rept, as Required by GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in BWRs & BWRVIP Rept BWR Core Shroud Insp & Flaw Evaluation Guideline (BWRVIP-01) ML20209F8561999-07-0606 July 1999 Forwards Rev 1 to Nmp,Unit 1 COLR for Cycle 14. Rept Is Being Submitted to Commission in Compliance with TS 6.9.1.f.4 ML20211K5071999-07-0606 July 1999 Submits Concerns Re 990624 Event Involving Automatic Reactor Shutdown.More than 5 Failures Were Identified in Event Number 35857 ML20196J6421999-06-30030 June 1999 Discusses Completion of Licensing Action for GL 96-01, Testing of Safety-Related Logic Circuits, Issued on 960110 ML20209B7071999-06-30030 June 1999 Responds to NRC Request for Info Re Y2K Readiness at Nuclear Facilities,As Contained in GL 98-01,Supp 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure,Encl ML20211P5271999-06-29029 June 1999 Submits Written Comments Addressing Petition Dtd 990405, Submitted by R Norway as It Relates to Expressed Concerns That Involve NMPC Activities.None of Relief Requested in Petition Warranted ML20196K6461999-06-29029 June 1999 Discusses Ofc of Investigations Rept 1-98-33 Re Unqualified Senior Reactor Operator Assuming Position of Assistant Station Shift Supervisor at Unit 1 on 980616.One Violation Being Cited as Described in Encl NOV ML20209B3501999-06-25025 June 1999 Submits Torus Shell & Coupon Corrosion Rate Determination for Nmpns,Unit 1.Torus Meets ASME Code Requirements,Iaw NRC 920825 & 940811 SERs ML20212J4431999-06-25025 June 1999 Discusses Responses to RAI Re GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20209B3531999-06-25025 June 1999 Informs NRC That All Actions Associated with NRC Bulletin 96-003, Potential Plugging of ECC Suction Strainers by Debris in Bwrs, Has Been Completed.Summary of Actions Completed & Other Pertinent Info Is Provided in Attachment ML20196F5721999-06-23023 June 1999 Forwards Rev 3 to NMP1-IST-003, Third Ten Year Inservice Testing Program Plan, Which Will Begin on 991226.Program Plan Conforms to Requirements of 1989 Edition of ASME Boiler & Pressure Vessel Code.Three Relief Requests,Encl ML20196G1461999-06-23023 June 1999 Informs That Actions Requested in GL 96-01, Testing of Safety-Related Logic Circuits Completed 1999-09-07
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217L7971999-10-20020 October 1999 Submits Results of Review of 990521 & 0709 Ltrs Which Provided Core Shroud Insp Results & Tie Rod Stabilizer Assemblies ML20217G1291999-10-15015 October 1999 Forwards Errata to Safety Evaluation for Amend 168 Issued to FOL DPR-63 on 990921.Description of Flow Control Trip Ref Cards to Be Consistent with Application for Amend ML20212K8601999-10-0606 October 1999 Responds to Concern in 990405 Petition Re Residual Heat Removal Alternate Shutdown Cooling Modes of Operation at Nine Mile Point Nuclear Station,Unit 2 ML20212J4651999-09-30030 September 1999 Informs of Completion of mid-cyle PPR of Nine Mile Point Nuclear Station on 990916.Determined That Problems in Areas of Human Performance & Work Control Required Continued Mgt Attention.Historical Listing of Plant Issues Encl ML20212K8641999-09-30030 September 1999 Informs That During 990927 Telcon Between J Williams & J Bobka,Arrangements Were Made for Administration of Exams at Plant During Wk of Feb 14,2000.Preliminary RO & SRO License Applications Should Be Submitted 30 Days Prior Exam ML20212J8831999-09-30030 September 1999 Informs That Util 980810 & 990630 Responses to GL 98-01 & Suppl 1, Y2K Readiness of Computer Sys at NPPs Acceptable. NRC Considers Subj GL to Be Closed for Plant ML20212B2821999-09-14014 September 1999 Responds to 990712 Correspondence Which Responded to NRC Ltr Re High Failure Rate for Generic Fundamentals Exam of 990407 for Nine Mile Point.Considers Corrective Actions Taken to Be Acceptable ML20211K5031999-08-30030 August 1999 Responds to Ltr Addressed to Chairman Dicus, Expressing Concerns Involving 990624 Automatic Reactor Shutdown.Insp Findings & Conclusions Will Be Documented in Insp Repts 50-220/99-06 & 50-410/99-06 by mid-Sept 1999 ML20211G4921999-08-26026 August 1999 Advises That Info Re Comments Addressing 10CFR2.206,dtd 990405 Will Be Withheld from Public Disclosure,In Response to ML20211P5161999-08-26026 August 1999 Discusses Submitted on Behalf of Niagara Mohawk Power Corp Written Comments Addressing 10CFR2.206 Petition & Request That Ltr & Attached Response Be Withheld from Public Disclosure.Request Denied ML20210Q0031999-08-11011 August 1999 Informs That Due to Printing Malfunction,Some Copies of Author Ltr Dtd 990726,may Not Have Included Second Page of Encl 2 of Ltr ML20210L5321999-08-0606 August 1999 Forwards List of Subjects Discussed During 990714 Telcon with Representatives of Niagara Mohawk Power Corp on Unit 1 Re USI A-46 Issue ML20216E1491999-07-26026 July 1999 Forwards Two Ltrs Received from NMPC Re Nine Mile Point Unit 1 Core Shroud Related to 10CFR2.206 ML20210E9151999-07-23023 July 1999 Discusses Evaluation of Recirculation Line Weld 32-WD-050 Indication Found During 1997 Refueling Outage (RFO14) at NMPNS Unit 1.Requests Notification of Decision to Retain Category F Classification Until Listed Conditions Satisfied ML20196J6421999-06-30030 June 1999 Discusses Completion of Licensing Action for GL 96-01, Testing of Safety-Related Logic Circuits, Issued on 960110 ML20196K6461999-06-29029 June 1999 Discusses Ofc of Investigations Rept 1-98-33 Re Unqualified Senior Reactor Operator Assuming Position of Assistant Station Shift Supervisor at Unit 1 on 980616.One Violation Being Cited as Described in Encl NOV ML20212J4431999-06-25025 June 1999 Discusses Responses to RAI Re GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20195F9971999-06-11011 June 1999 Discusses 990513 Fax Which Forwarded Copy of an Open Ltr to Central New York on Nine Mile One Nuclear Reactor, & Petition to NRC Re Nine Mile Point One Core Shroud Insp, Signed by 187 People ML20195G9661999-06-11011 June 1999 Ack Receipt of Petition Requesting Action Under 10CFR2.206 Sent to W Travers on 990524.Petition Requested That NRC Suspend Operating License Issued to NMP for Nine Mile Point Unit 1.Staff Reviewing Issues & Concerns Raised in Petition ML20207H1021999-06-10010 June 1999 Advises That Info Re Theoretical Basis for Shear & Torsional Spring Constants in Holtec Sf Rack, Submitted in & Affidavit ,marked Proprietary,Will Be Withheld from Public Disclosure,Per 10CFR2.790(b)(5) ML20207G5281999-06-0909 June 1999 Ack Receipt of Expressing Concern for Reactor Core Shroud for Plant,Unit 1.NRC Staff Requested to Conduct Insp of Reactor Shroud,Including Areas Outside Core Shroud Welds & Publicly Disclose Results 1 Wk Before Plant Restart ML20137S9381999-06-0909 June 1999 Ack Receipt of Petition Requesting Action Under 10CFR2.206 Sent to W Travers on 990405.Petition Requested That NRC Take EA Against Util & Senior Nuclear & Corporate Mgt ML20207G2171999-06-0707 June 1999 Forwards SE Accepting Proposed Mod to Each of Four Core Shroud Stabilizers for Implementation During Current 1999 Refueling Outage for Plant,Unit 1 ML20207H3961999-06-0707 June 1999 Informs That NRC NRR Reorganized,Effective 990328. Organization Chart Encl ML20195D5001999-06-0404 June 1999 Discusses NMPC Request That GE-NE-523-B13-01869-113, Assessment of Crack Growth Rates Applicable to Nine Mile Point I Vertical Indications, Rev 0 Be Withheld from Public Disclosure.Determined Info Proprietary & Will Be Withheld ML20207D3141999-05-28028 May 1999 Ack Receipt of 981203,990325 & 0415 Ltrs,Which Presented Several Concerns & Comments Re Operation of Nmp,Plant,Unit 1 During Last Operating Cycle ML20207E8131999-05-28028 May 1999 Responds to Re Concern for Core Shroud Insp Plan for Plant,Unit 1.Insp Results Cannot Be Made Available Before Plant Restarts ML20207A4881999-05-20020 May 1999 Discusses Expressing Concern Re Core Shroud at NMPNS Unit 1 & Indicating Desire to See Further Testing of Any Cracks & Release of Rept to Public Before Unit Restarted ML20207B0171999-05-18018 May 1999 Forwards Safety Evaluation Accepting Rept TR-107285, BWR Vessel & Internals Project,Bwr Top Guide Insp & Flaw Evaluation Guidelines (BWRVIP-26), Dtd December 1996 ML20206U5191999-05-17017 May 1999 Forwards SE Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant,Units 1 & 2 ML20206N6881999-05-12012 May 1999 Forwards Copy of NMP Ltr of 990430,responding to 990325 & 0415 Ltrs Re Core Shroud Evaluations for Plant Unit 1 ML20206M2041999-05-10010 May 1999 Requests Util Provide Written Comments to NRC Addressing Petitioners Expressed Concerns That Involve Licensee Activities.Petitioner Asserts That Util Actions Resulted in Placement of Confidential & Fraudulent Employee Evaluation ML20206K1681999-05-10010 May 1999 Forwards RAI Re 981116 Request for License Amend to Change TSs Re Implementation of Sys for Detection & Suppression of Coupled neutronic/thermal-hydraulic Instabilities in Reactor at Plant,Unit 1.Response Requested by 990621 ML20206L3981999-04-30030 April 1999 Responds to Requesting Addl Info to Either Respond to Apparent Violation,Or Prepare for Predecisional Enforcement Conference Re Apparent Violation of NRC Requirements Identified by OI in Rept 1-98-033 ML20205Q6471999-04-13013 April 1999 Discusses OI Report 1-1998-033.Purpose of Investigation Was to Determine Whether SRO Willfully Violated Conditions of SRO License by Assuming Assistant Station Shift Supervisor Position After Failing Requalification Scenario Evaluation ML20205N0591999-04-12012 April 1999 Forwards RAI Re Which Describes Proposed Core Shroud Repair for Core Shroud Vertical Welds at Plant,Unit 1.Response Requested by 990414 ML20205J3761999-04-0808 April 1999 Final Response to FOIA Request for Documents.App a Records Already Available in PDR IA-99-179, Final Response to FOIA Request for Documents.App a Records Already Available in PDR1999-04-0808 April 1999 Final Response to FOIA Request for Documents.App a Records Already Available in PDR ML20207L0111999-03-11011 March 1999 Forwards RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves, for Nine Mile Point Nuclear Station,Units 1 & 2 ML20207L5711999-03-0404 March 1999 Informs That Info Submitted with 990203 Application Marked as Proprietary Will Be Withheld from Public Disclosure Per 10CFR.790 & Section 103(b) of Atomic Energy Act of 1954,as Amended ML20207K3701999-03-0303 March 1999 Forwards NRC PRB Meeting Summary Re Recipient Ltr of 981214, Expressing Concern for Degraded Core Shroud & Vessel Internals at Nine Mile Point Unit 1 ML20203E7281999-02-11011 February 1999 Responds to to W Travers & Submitted Pursuant to 10CFR2.206,requesting That NRC Convene Public Hearing to Consider Revocation of Operating License for Nine Mile Point Nuclear Station,Unit 1.Petition Does Not Meet Criteria ML20203B4671999-02-0808 February 1999 Informs That Licensee 990111 Application & Affidavit Submitting HI-961584,HI-971667,HI-92801 & HI-89330 Will Be Marked as Proprietary & Will Be Withheld from Public Disclosure Pursuant to 10CFR2.790(b)(5) & Section 103(b) ML20206R8331999-01-14014 January 1999 Advises That, Licensing Rept for Reracking Nine Mile,Unit 1 Spent Fuel Pool, Will Be Withheld from Public Disclosure, Per 10CFR2.790 ML20199E2701999-01-14014 January 1999 Ltr Contract:Mod 1 to Task Order 235, Review & Evaluation of Nine Mile 2 Nuclear Plant Application for Conversion to Improved TSs - Electrical Sys, Under Contract NRC-03-95-026 ML20206R6161999-01-12012 January 1999 Informs That on 981124 Licensee Submitted Revs to TSs Bases for Plant,Unit 1.Revs Update Listed Bases to Incorporate Design Changes Affecting Reactor Fuel,Reactor Vessel Water Level Instrumentation & Drywell Leak Detection Sys ML20199D2801999-01-12012 January 1999 Informs That on 981204,NMP Submitted Rev to TSs Bases for NMPNS Unit 1.Rev Update Bases for 3.6.2 & 4.6.2 Protective Instrumentation. Forwards Modified Pages for NMP Unit 1 TS Bases for Insertion Into TSs ML20206R0831999-01-0404 January 1999 Informs That Privacy Info Re Investigation Rept Entitled, Results of Independent Team Investigation of Concerns Involving Erosion & Corrosion of Flow Elements, Will Be Withheld from Public Disclosure,Per 10CFR2.790 ML20198L1971998-12-24024 December 1998 Informs That Based Upon Conclusion That Current Design & Licensing Basis Does Not Credit Containment Overpressure to Ensure Adequate NPSH to Core Spray & Containment Spray Pumps,Nrc Considers GL 97-04 Closed Per 980807 RAI ML20198L3831998-12-23023 December 1998 Forwards Insp Repts 50-220/98-15 & 50-410/98-15 on 980927-1121.No Violations Noted.Notes Challenges Faced by Unit 2 Operators Due to Equipment Performance Problems 1999-09-30
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- i February 15, 1996 Mr. B. Ralph Sylvia Executive Vice President - Generation Business Group Niagara Mohawk Power Corporation-(NMPC)
Nine Mile Point Nuclear Station P. O. Box 63 Lycoming, NY 13093 SUBJF.CT: NRC COMBINED INSPECTION REPORT NOS. 50-220/95-23 AND 50-410/95-23
Dear Mr. Sylvia:
This acknowledges receipt of your letter dated December 21, 1995, which was in response w a Notice of Violation (Notice) contained in the subject inspection report, dated November 22, 1995. The Notice dealt with the identification of a Unit 1 primary containment isolation valve which was required to be locked closed, but which was found unlocked by an NRC inspector on October 13, 1995.
Thank you for informing us of the corrective and preventive actions documented in your letter. We have reviewed this matter in accordance with NRC ,
Inspection Manual Procedure 92901, " Followup - Plant Operations." Our preliminary assessment indicates that your response was timely and acceptable, and that your apparent root cause of " poor work practice" is correct. You stated in your letter that this was not a generic concern, and your basis was verifying that all other accessible primary containment isolation valves were properly secured. However, we note that at least two differact operators verified that the valve was locked; and although the problen ,wy :.9t be generic, it was not an isolated condition. The NRC staff will continue to monitor your ability to maintain control of the equipment configuration and assess if the actions to prevent recurrence were adequate.
The inspection report also discussed other events related, in part, to procedural weaknesses or inadequacies. We asked you to address our concern about the effectiveness of the procedure periodic review program and how well personnel provided input for procedure problems. You discussion with respect to why the periodic review process would not have prevented each of the three examples is acceptable. And, although you admit that opportunities did exist to improve the procedures, you did not dets.il specifically what your plans were to capture those opportunities and inprovements. A detailed review of your procedure development and maintenance program will be included as part of the upcoming IPAP (Integrated Performance Assessment Program) inspection.
Your cooperation with us is appreciated.
Sincerely, Original Signed By:
230079 Richard J. Conte, Lhief Projects Branch 5 Division of Reactor Projects l
Docket Nos. 50-220 50-410 9602260001 960215 // }l PDR ADOCK 05000220 /
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B. Ralph Sylvia 2
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, R. Abbott, Vice President-Nuclear Generation C. Terry, Vice President-Nuclear Engineering 4 M. McCormick, Vice President - Safety Assessment and Support
! N. Rademacher, Unit 1 Plant Manager J. Conway, Unit 2 Plant Manager (acting)
D. Wolniak, Manager, Licensing cc w/cy Licensee Response Letter:
J. Warden, New York Consumer Protection Branch G. Wilson, Senior Attorney H. Wetterhahn, Winston and Strawn
- Director, Energy & Water Division, Department of Public Service, State of'
New York ,
C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law J. Vinquist, MATS, Inc.
P. Eddy, Power Division, Derartment of Public Service, State of New York l State of New York SLO Designee Distribution w/ enc 1:
D. Screnci, PA0 (2)
Region I Docket Room (with concurrences)
2 Nuclear Safety Information Center (NSIC)
PUBLIC NRC Resident Inspector R. Conte, DRP H. Eichenholz, DRP C. O'Daniell, DRP
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DOCUMENT NAME: G:\U1952301.ACK Ta h a copy of this dooumont. Indosts in me box: "C" = Copy without attachment / enclosure T = Copy with attachment / enclosure "N" = No copy 0FFICE RI/DRP Rl/DRP /1 JL / l NAME BNORRIS W RCONTE/'/)'
DATE 02/15/96 / 02/ /t-196 02/ /96 02/ /96 02/ /96 I 0FFICIAL RECORD COPY
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M V NIAGARA R U MOHAWK HIA0 ARA MOHAWK POWER CORPORATION,tHNE MILE POINT NUCLEAR STAfloN, P.o. 80X 63, LYcOMING, N.Y.13093JEL (315) 34S1812 FAX (315)3494417 NCHAND B. AB80rr Vlos Preeldent December 21,1995 w oenneman NMPIL 1017 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555
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RE: Nine Mile Point Unit 1 Docket No. 50-220 DPR-63 Subject: RESPONSE TO NOTICE OF VIOLATION NRC Inspection Report No. 50-220/95-23 and 50-410/95-23 Gentlemen:
Niagara Mohawk Power Corporation's response to the Notice of Violation contained in the subject Inspection Report dated November 22,1995 is enclosed as Attachment A.
Attachment B addresses the NRC's concern about the effectiveness of the NMPC periodic review program also expressed in the Inspection Report.
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Very truly yours, h $ cr '
R. B. Abbott Vice President - Nuclear Generation RBA/TWR/Imc Attachment
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xc: Regional Administrator, Region I Mr. B. S. Norris, Senior Resident Inspector l Mr. L. B. Marsh, Director, Project Directorate I-1, NRR Mr. G. E. Edison, Senior Project Manager, NRR Records Management
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, A'ITACHMENT A l
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NIAGARA MOHAWK POWER CORPORATION j NINE MILE POINT UNIT 1 DOCKET NO. 50-220
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DPR-63 1
l " RESPONSE TO NOTICE OF VIOLATION," AS CONTAINED IN i- INSPECTION REPORT 54220/95-23 AND 54410/95-23 l
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- VIOLATION 50 220/95-23 01 During an NRC inspection conducted from September 3 through October 14,1995, a violation of NRC requirements was identified. In accordance with the NRC " General ;
Statement of Policy and Procedure for NRC Enforcement Actions" (Enforcement Policy),
- NUREO 1600, (60 FR 34381; June 30,1995), the violation is listed below: 1
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The Nine Mile Point Nuclear Power Station Technical Specifications Section f
- 6.8.1, requires procedures to be established and implemented.
e 4 Procedure N1-PM-V16, " Reactor Startup and Shutdown Prerequisite Verifications," requires the service water primary containment outside isolation
valve be locked closed.
- Contrary to the above
On October 13,1995, a Unit 1 service water containment outside isolation valve (72-479)
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locking chain was not locked. (This resulted in the valve being closed but not locked.)
i This is a Severity Level IV violation (Supplement I).
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I. THE REASON FOR THE VIOLATION i
Niagara Mohawk admits to the violation as stated in Inspection Report 50-220/95-23.
An apparent cause analysis was performed in accordance with Nuclear Interface Procedure l NIP-ECA-01, " Deviation / Event Report." The cause for the valve being inadequately secured
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with a locking device was determined to be poor work practice.
On April 2,1995, valve 72-479 was lined up in accordance with N1-OP-18, " Service Water
< System," and independently verified closed. The procedure did not specify this valve as
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having to be locked which was consistent with the Piping and Instrumentation drawing
. (P&ID). On April 3,1995, Form III of Procedure N1-PM-V16, " Reactor Startup and
- Shutdown Prerequisite Verification," was completed. Step 6.0 of this procedure required-verification that valve 72-479 was locked closed. The Operator that performed the step
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verified the valve was closed and placed a locking device on the valve. However, the locking device did not engage the valve in a manner to secure it. Specifically, the cable was not looped through the valve yoke and only went through the handwheel. On April 11, 1995, Form III of Procedure N1-PM-V16 was performed again. A different Operator performed the verification that valve 72-479 was locked closed. The Operator performing this verification determined the valve was closed and that a lock was on the valve. The Operator, however, did not detect that the lock was not securing the valve, because by casual visual observation, it appeared to be locked.
The cause for the discrepancy between procedure N1-PM-V16, procedure N1-OP-18, and the P&ID is ineffective procedure development. A review of the licensing and design bases reveals there are no requirements that valve 72-479 be locked; locking of the valve was a management decision implemented in the early 1980's as a prudent measure above and beyond regulatory requirements. 1 N1-PM-V16 currently consists of plant startup checks which had previously been included in plant startup procedure N1-OP-43. In 1993, N1-PM-V16 was developed to remove the checks from the startup procedure; this change was administrative in nature and included reformatting to standards of the procedure writers manual. Because the relocation of the startup checks to another procedure was primarily an administrative change, a review of the i technical content of the procedures was not adequately performed.
While operating procedure N1-OP-18 was reconciled against the design bases to eliminate the requirement to lock the valve, an opportunity was missed to similarly reconcile N1-PM-V16 at the time that procedure was developed. At the time of discovery of the inadequate securing of the valve, N1-PM-V16 was at Jhe revision 00 level and had not yet undergone the technical review associated with the periodic review process.
Procedure N1-PM-V16 is used as a prerequisite verification for plant startup or shutdown.
Although procedure N1-PM-V16, Form III, did not require an independent verification for valve 72-479, Form II of this procedure required verification of system valve / electrical lineups per the applicable Operating Procedures, including N1-OP-18. N1-OP-18 specified l
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independent verification for valve 72-479 which had been reconciled with the P& ids.
Procedure N1-PM-V16 was not reconciled in the same manner when it was developed in November of 1993. l II. CORRECTIVE ACTIONS TAKRN AND RESULTS ACHIEVED A Deviation / Event Report (DER) was initiated to identify and document corrective actions for this event. These actions include:
1. Operations personnel immediately properly locked closed valve 72-479.
2. To ensure that the inadequate work practices associated with improper locking of valves was not a generic concern, -ible manual primary containment valves required to be locked closed were verified to be properly secured in accordance with applicable procedures. No other valves were found to be improperly secured.
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ATTACHMENT B
d SupplementalIgonnation In addition to the specific violation, the NRC expressed the following concern:
I j "As a, result of those findings, we are concerned about the effectiveness of ,
! your procedure periodic review program and how well personnel provide input for procedure problems."
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! Ffectiveness of the Periodic Review Process The periodic review process encompasses three basic areas; 1) future Procedure Change j Evaluations (PCEs), 2) immediate PCEs, and 3) source documents for changes or performance of a technical review as specified in " Preparation and Review of Technical Procedures" (NIP-PRO-03). Future PCEs are evaluated for impact and if determined to significantly enhance the procedure, they are incorporated at the time of periodic review.
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Immediate PCEs (already incorporated) are reviewed for human factors and accuracy.
l Source documents are reviewed to determine if changes that would affect the procedure have
- occurred since the last review or revision.
l At Nine Mile Point few problems have been experienced with the periodic review process
{ related to the technical correctness of the procedures. This performance has led to the i submittal of a Proposed Change to the Quality Assurance Topical Report which would
- replace the biennial review process with an alternative commitment to review procedures ;
i upon identification of new or revised source material that could affect procedures. l Personnel Input to Piecedures .
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Typically, many immediate, future, and editorial procedure changes, on the order of several
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thousand per year are written against both units' procedures. Whether self-identified or
- identified by others, this indicates considerable personnel input when problems or areas to j improve are identified. NMPC recognizes that user input into the procedure review and I
! revision process is vital to the success of the program and continues to encourage station j personnel to identify worthwhile changes to procedures. Specifically, our procedures are developed by user department personnel.
! 'Ihe need for procedure changes may be identified through a number of sources and at 4 various intervals. The current procedure review process at Nine Mile Point Unit 1 and Nine
- Mile Point Unit 2 is dynamic, based on internal identification and external receipt of new or
, revised source material. The DER program also provides a method for personnel to report
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and correct items adverse to quality. Corrective actions may include procedural changes i deemed necessary to preclude recurrence as well as recommendations for procedural enhancements.
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Existing administrative controls specify responsibilities for proper use of procedures. If a procedn'e cannot be performed safely, cannot or should not be performed as written, is
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tech &dly incorrect, or unexpected results or conditions occur, users are directed to stop the acti%.y, r.otify supervision, and initiate a change or revision to the procedure, as appropriate.
' In addition, mechanisms exist for procedure users to recommend enhancements to improve
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procedures / processes based on experience.
Specffic Issues in Inspection Report 95-23
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With regard to the concern pertaining to the periodic review of procedure N1-PM-V16, the
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- current revision at the time of this event was Rev. O. The procedure was not due for j periodic review untillate October 1995, which was after the event. Therefore, NMPC does not consider the periodic review process to be a contributing factor.
The trip of both Reactor Recirculation Pumps at Unit 2 (DER 2-95-2571) was determined not i to be due to procedural inadequacy, but rather an unanticipated interaction of systems or
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components by the persons performing the work. Hat is, personnel failed to understand the plant impact when troubleshooting this circuit. The RRCS was being de-energized in accordance with procedure (N2-OP-30B) as had been done successfully many times previous to this event. The trip of the Recirculation Pumps occurred because the procedure did not anticipate the system response with one channel in a tripped condition. Additionally, the
- procedure source documents did not identify the susceptibility of the system to spuriously tripping under these conditions. When the event occurred, Operations personnel immediately revised the procedure to preclude similar conditions from causing a trip in the future, i
The failure to reopen a Unit 2 suppression pool spray valve after a test (DER 2-95-1854) was determined to be caused by a failure to follow procedure in that the Operator initialed the restoration step but failed to properly verify the step had actually been performed.
Contributing causes were difficulties due to multiple procedure implementation and
substandard procedural guidance for component position verification. That is, the Operators
- involved were performing too many tasks simultaneously and the interaction of performing several procedures resulted in not having sufficiently clear guidance to restore the system appropriately.
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While opportunities exist to improve procedures, these instances do not demonstrate an inherent inadequacy of the periodic review process or personnel input to procedures.
Conclusion i Niagara Mohawk has concluded that the periodic review process is effective. Input to
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procedures is received from many sources to correct deficiencies. Through review and analysis of the three specific examples discussed in Inspection Report 95-23, it is concluded that poor personnel performance was the primary cause of these events rather than an ineffective periodic review process or inadequate personnel input to resolve procedural I problems.
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3. While no regulatory requirements exist to require locking 72-479, a management decision has been made to incorporate locking of the valve into appropriate ;
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documents; as a result, the P&ID and Operating Procedure N1-OP-18 have been revised to require valve 72-479 to be locked closed. Similarly, the P&ID and N1-OP-18 have been revised to require the inside containment valve 72-480 to be locked closed, lH. ACTIONS TAKRN TO PREVENT RECURRENCE
1. Operations Department personnel have been coached on the proper techniques for locking and verifying valves locked. ;
2. Procedure N1-PM-V16 will be reviewed and revised by February 28,1996, to ensure:
- compliance to the procedure writers manual for component positioning and verification standards
- compliance to the licensing and design bases.
IV. DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED Full compliance with procedure N1-PM-V16, " Reactor Startup and Shutdown Prerequisite Verifications" was achieved on October 13,1995 when Operations personnel immediately locked valve 72-479. ,
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