IR 05000220/1995023

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Ack Receipt of 951221 Ltr Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-220/95-23 & 50-410/95-23
ML20149L252
Person / Time
Site: Nine Mile Point  Constellation icon.png
Issue date: 02/15/1996
From: Conte R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Sylvia B
NIAGARA MOHAWK POWER CORP.
References
NUDOCS 9602260001
Download: ML20149L252 (2)


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  • i February 15, 1996 Mr. B. Ralph Sylvia Executive Vice President - Generation Business Group Niagara Mohawk Power Corporation-(NMPC)

Nine Mile Point Nuclear Station P. O. Box 63 Lycoming, NY 13093 SUBJF.CT: NRC COMBINED INSPECTION REPORT NOS. 50-220/95-23 AND 50-410/95-23

Dear Mr. Sylvia:

This acknowledges receipt of your letter dated December 21, 1995, which was in response w a Notice of Violation (Notice) contained in the subject inspection report, dated November 22, 1995. The Notice dealt with the identification of a Unit 1 primary containment isolation valve which was required to be locked closed, but which was found unlocked by an NRC inspector on October 13, 1995.

Thank you for informing us of the corrective and preventive actions documented in your letter. We have reviewed this matter in accordance with NRC ,

Inspection Manual Procedure 92901, " Followup - Plant Operations." Our preliminary assessment indicates that your response was timely and acceptable, and that your apparent root cause of " poor work practice" is correct. You stated in your letter that this was not a generic concern, and your basis was verifying that all other accessible primary containment isolation valves were properly secured. However, we note that at least two differact operators verified that the valve was locked; and although the problen ,wy :.9t be generic, it was not an isolated condition. The NRC staff will continue to monitor your ability to maintain control of the equipment configuration and assess if the actions to prevent recurrence were adequate.

The inspection report also discussed other events related, in part, to procedural weaknesses or inadequacies. We asked you to address our concern about the effectiveness of the procedure periodic review program and how well personnel provided input for procedure problems. You discussion with respect to why the periodic review process would not have prevented each of the three examples is acceptable. And, although you admit that opportunities did exist to improve the procedures, you did not dets.il specifically what your plans were to capture those opportunities and inprovements. A detailed review of your procedure development and maintenance program will be included as part of the upcoming IPAP (Integrated Performance Assessment Program) inspection.

Your cooperation with us is appreciated.

Sincerely, Original Signed By:

230079 Richard J. Conte, Lhief Projects Branch 5 Division of Reactor Projects l

Docket Nos. 50-220 50-410 9602260001 960215 // }l PDR ADOCK 05000220 /

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B. Ralph Sylvia 2

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, R. Abbott, Vice President-Nuclear Generation C. Terry, Vice President-Nuclear Engineering 4 M. McCormick, Vice President - Safety Assessment and Support

! N. Rademacher, Unit 1 Plant Manager J. Conway, Unit 2 Plant Manager (acting)

D. Wolniak, Manager, Licensing cc w/cy Licensee Response Letter:

J. Warden, New York Consumer Protection Branch G. Wilson, Senior Attorney H. Wetterhahn, Winston and Strawn

Director, Energy & Water Division, Department of Public Service, State of'

New York ,

C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law J. Vinquist, MATS, Inc.

P. Eddy, Power Division, Derartment of Public Service, State of New York l State of New York SLO Designee Distribution w/ enc 1:

D. Screnci, PA0 (2)

Region I Docket Room (with concurrences)

2 Nuclear Safety Information Center (NSIC)

PUBLIC NRC Resident Inspector R. Conte, DRP H. Eichenholz, DRP C. O'Daniell, DRP

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DOCUMENT NAME: G:\U1952301.ACK Ta h a copy of this dooumont. Indosts in me box: "C" = Copy without attachment / enclosure T = Copy with attachment / enclosure "N" = No copy 0FFICE RI/DRP Rl/DRP /1 JL / l NAME BNORRIS W RCONTE/'/)'

DATE 02/15/96 / 02/ /t-196 02/ /96 02/ /96 02/ /96 I 0FFICIAL RECORD COPY

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M V NIAGARA R U MOHAWK HIA0 ARA MOHAWK POWER CORPORATION,tHNE MILE POINT NUCLEAR STAfloN, P.o. 80X 63, LYcOMING, N.Y.13093JEL (315) 34S1812 FAX (315)3494417 NCHAND B. AB80rr Vlos Preeldent December 21,1995 w oenneman NMPIL 1017 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555

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RE: Nine Mile Point Unit 1 Docket No. 50-220 DPR-63 Subject: RESPONSE TO NOTICE OF VIOLATION NRC Inspection Report No. 50-220/95-23 and 50-410/95-23 Gentlemen:

Niagara Mohawk Power Corporation's response to the Notice of Violation contained in the subject Inspection Report dated November 22,1995 is enclosed as Attachment A.

Attachment B addresses the NRC's concern about the effectiveness of the NMPC periodic review program also expressed in the Inspection Report.

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Very truly yours, h $ cr '

R. B. Abbott Vice President - Nuclear Generation RBA/TWR/Imc Attachment

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xc: Regional Administrator, Region I Mr. B. S. Norris, Senior Resident Inspector l Mr. L. B. Marsh, Director, Project Directorate I-1, NRR Mr. G. E. Edison, Senior Project Manager, NRR Records Management

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, A'ITACHMENT A l

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NIAGARA MOHAWK POWER CORPORATION j NINE MILE POINT UNIT 1 DOCKET NO. 50-220

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DPR-63 1

l " RESPONSE TO NOTICE OF VIOLATION," AS CONTAINED IN i- INSPECTION REPORT 54220/95-23 AND 54410/95-23 l

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VIOLATION 50 220/95-23 01 During an NRC inspection conducted from September 3 through October 14,1995, a violation of NRC requirements was identified. In accordance with the NRC " General ;

Statement of Policy and Procedure for NRC Enforcement Actions" (Enforcement Policy),

NUREO 1600, (60 FR 34381; June 30,1995), the violation is listed below: 1
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The Nine Mile Point Nuclear Power Station Technical Specifications Section f

6.8.1, requires procedures to be established and implemented.

e 4 Procedure N1-PM-V16, " Reactor Startup and Shutdown Prerequisite Verifications," requires the service water primary containment outside isolation

valve be locked closed.

Contrary to the above

On October 13,1995, a Unit 1 service water containment outside isolation valve (72-479)

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locking chain was not locked. (This resulted in the valve being closed but not locked.)

i This is a Severity Level IV violation (Supplement I).

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I. THE REASON FOR THE VIOLATION i

Niagara Mohawk admits to the violation as stated in Inspection Report 50-220/95-23.

An apparent cause analysis was performed in accordance with Nuclear Interface Procedure l NIP-ECA-01, " Deviation / Event Report." The cause for the valve being inadequately secured

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with a locking device was determined to be poor work practice.

On April 2,1995, valve 72-479 was lined up in accordance with N1-OP-18, " Service Water

< System," and independently verified closed. The procedure did not specify this valve as

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having to be locked which was consistent with the Piping and Instrumentation drawing

. (P&ID). On April 3,1995, Form III of Procedure N1-PM-V16, " Reactor Startup and

Shutdown Prerequisite Verification," was completed. Step 6.0 of this procedure required-verification that valve 72-479 was locked closed. The Operator that performed the step

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verified the valve was closed and placed a locking device on the valve. However, the locking device did not engage the valve in a manner to secure it. Specifically, the cable was not looped through the valve yoke and only went through the handwheel. On April 11, 1995, Form III of Procedure N1-PM-V16 was performed again. A different Operator performed the verification that valve 72-479 was locked closed. The Operator performing this verification determined the valve was closed and that a lock was on the valve. The Operator, however, did not detect that the lock was not securing the valve, because by casual visual observation, it appeared to be locked.

The cause for the discrepancy between procedure N1-PM-V16, procedure N1-OP-18, and the P&ID is ineffective procedure development. A review of the licensing and design bases reveals there are no requirements that valve 72-479 be locked; locking of the valve was a management decision implemented in the early 1980's as a prudent measure above and beyond regulatory requirements. 1 N1-PM-V16 currently consists of plant startup checks which had previously been included in plant startup procedure N1-OP-43. In 1993, N1-PM-V16 was developed to remove the checks from the startup procedure; this change was administrative in nature and included reformatting to standards of the procedure writers manual. Because the relocation of the startup checks to another procedure was primarily an administrative change, a review of the i technical content of the procedures was not adequately performed.

While operating procedure N1-OP-18 was reconciled against the design bases to eliminate the requirement to lock the valve, an opportunity was missed to similarly reconcile N1-PM-V16 at the time that procedure was developed. At the time of discovery of the inadequate securing of the valve, N1-PM-V16 was at Jhe revision 00 level and had not yet undergone the technical review associated with the periodic review process.

Procedure N1-PM-V16 is used as a prerequisite verification for plant startup or shutdown.

Although procedure N1-PM-V16, Form III, did not require an independent verification for valve 72-479, Form II of this procedure required verification of system valve / electrical lineups per the applicable Operating Procedures, including N1-OP-18. N1-OP-18 specified l

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independent verification for valve 72-479 which had been reconciled with the P& ids.

Procedure N1-PM-V16 was not reconciled in the same manner when it was developed in November of 1993. l II. CORRECTIVE ACTIONS TAKRN AND RESULTS ACHIEVED A Deviation / Event Report (DER) was initiated to identify and document corrective actions for this event. These actions include:

1. Operations personnel immediately properly locked closed valve 72-479.

2. To ensure that the inadequate work practices associated with improper locking of valves was not a generic concern, -ible manual primary containment valves required to be locked closed were verified to be properly secured in accordance with applicable procedures. No other valves were found to be improperly secured.

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ATTACHMENT B

d SupplementalIgonnation In addition to the specific violation, the NRC expressed the following concern:

I j "As a, result of those findings, we are concerned about the effectiveness of ,

! your procedure periodic review program and how well personnel provide input for procedure problems."

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! Ffectiveness of the Periodic Review Process The periodic review process encompasses three basic areas; 1) future Procedure Change j Evaluations (PCEs), 2) immediate PCEs, and 3) source documents for changes or performance of a technical review as specified in " Preparation and Review of Technical Procedures" (NIP-PRO-03). Future PCEs are evaluated for impact and if determined to significantly enhance the procedure, they are incorporated at the time of periodic review.

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Immediate PCEs (already incorporated) are reviewed for human factors and accuracy.

l Source documents are reviewed to determine if changes that would affect the procedure have

occurred since the last review or revision.

l At Nine Mile Point few problems have been experienced with the periodic review process

{ related to the technical correctness of the procedures. This performance has led to the i submittal of a Proposed Change to the Quality Assurance Topical Report which would

replace the biennial review process with an alternative commitment to review procedures  ;

i upon identification of new or revised source material that could affect procedures. l Personnel Input to Piecedures .

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Typically, many immediate, future, and editorial procedure changes, on the order of several

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thousand per year are written against both units' procedures. Whether self-identified or

identified by others, this indicates considerable personnel input when problems or areas to j improve are identified. NMPC recognizes that user input into the procedure review and I

! revision process is vital to the success of the program and continues to encourage station j personnel to identify worthwhile changes to procedures. Specifically, our procedures are developed by user department personnel.

! 'Ihe need for procedure changes may be identified through a number of sources and at 4 various intervals. The current procedure review process at Nine Mile Point Unit 1 and Nine

Mile Point Unit 2 is dynamic, based on internal identification and external receipt of new or

, revised source material. The DER program also provides a method for personnel to report

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and correct items adverse to quality. Corrective actions may include procedural changes i deemed necessary to preclude recurrence as well as recommendations for procedural enhancements.

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Existing administrative controls specify responsibilities for proper use of procedures. If a procedn'e cannot be performed safely, cannot or should not be performed as written, is

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tech &dly incorrect, or unexpected results or conditions occur, users are directed to stop the acti%.y, r.otify supervision, and initiate a change or revision to the procedure, as appropriate.

' In addition, mechanisms exist for procedure users to recommend enhancements to improve

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procedures / processes based on experience.

Specffic Issues in Inspection Report 95-23

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With regard to the concern pertaining to the periodic review of procedure N1-PM-V16, the

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current revision at the time of this event was Rev. O. The procedure was not due for j periodic review untillate October 1995, which was after the event. Therefore, NMPC does not consider the periodic review process to be a contributing factor.

The trip of both Reactor Recirculation Pumps at Unit 2 (DER 2-95-2571) was determined not i to be due to procedural inadequacy, but rather an unanticipated interaction of systems or

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components by the persons performing the work. Hat is, personnel failed to understand the plant impact when troubleshooting this circuit. The RRCS was being de-energized in accordance with procedure (N2-OP-30B) as had been done successfully many times previous to this event. The trip of the Recirculation Pumps occurred because the procedure did not anticipate the system response with one channel in a tripped condition. Additionally, the

procedure source documents did not identify the susceptibility of the system to spuriously tripping under these conditions. When the event occurred, Operations personnel immediately revised the procedure to preclude similar conditions from causing a trip in the future, i

The failure to reopen a Unit 2 suppression pool spray valve after a test (DER 2-95-1854) was determined to be caused by a failure to follow procedure in that the Operator initialed the restoration step but failed to properly verify the step had actually been performed.

Contributing causes were difficulties due to multiple procedure implementation and

substandard procedural guidance for component position verification. That is, the Operators

involved were performing too many tasks simultaneously and the interaction of performing several procedures resulted in not having sufficiently clear guidance to restore the system appropriately.

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While opportunities exist to improve procedures, these instances do not demonstrate an inherent inadequacy of the periodic review process or personnel input to procedures.

Conclusion i Niagara Mohawk has concluded that the periodic review process is effective. Input to

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procedures is received from many sources to correct deficiencies. Through review and analysis of the three specific examples discussed in Inspection Report 95-23, it is concluded that poor personnel performance was the primary cause of these events rather than an ineffective periodic review process or inadequate personnel input to resolve procedural I problems.

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3. While no regulatory requirements exist to require locking 72-479, a management decision has been made to incorporate locking of the valve into appropriate ;

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documents; as a result, the P&ID and Operating Procedure N1-OP-18 have been revised to require valve 72-479 to be locked closed. Similarly, the P&ID and N1-OP-18 have been revised to require the inside containment valve 72-480 to be locked closed, lH. ACTIONS TAKRN TO PREVENT RECURRENCE

1. Operations Department personnel have been coached on the proper techniques for locking and verifying valves locked.  ;

2. Procedure N1-PM-V16 will be reviewed and revised by February 28,1996, to ensure:

  • compliance to the procedure writers manual for component positioning and verification standards
  • compliance to the licensing and design bases.

IV. DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED Full compliance with procedure N1-PM-V16, " Reactor Startup and Shutdown Prerequisite Verifications" was achieved on October 13,1995 when Operations personnel immediately locked valve 72-479. ,

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