ML20082B590

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Special Rept:On 950301,Unit 0 DG Tripped Due to Reverse Power.Unit 0 DG Trip May Have Been Caused by Voltage Fluctuation on Offsite Power Grid.Lasalle Operating Surveillance LOS-DG-SA1 Being Reviewed
ML20082B590
Person / Time
Site: LaSalle  Constellation icon.png
Issue date: 03/31/1995
From: Ray D
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9504050230
Download: ML20082B590 (1)


Text

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' l.a5alle Generatmg station e 2(dll North list Road i Wrseillew. ll. 61.4 41-9T Tei 8is.tsN, cii l

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March 31,1995 U. S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, D. C. 20555 This special report is sutmtted in accordance with LaSalle Units 1 and 2 Operating Ucenses NPF-11 and NPF-18, Appendix A, and Technical Specification Sections 4.8.1.1.3 and 6.6.c regarding Unit 0 Diesel Generator (DG, ODG01K), manufactured by Electro-Motive Division of General Motors Corporation (Model EMD 20-645E4).

j On March 1,1995, with LaSalle Unit 1 at power and LaSalle Unit 2 defueled, the Unit 0 Diesel Generator (DG) was operating in accordance with LaSalle Operating Surveillance LOS-DG-SA1, 'O Diesel Generator Test with Response Time". After performing a one-hour full load run synchronized with offsite power through the Unit i System Auxiliary Transformer (SAT), the Nuclear Station Operation (NSO) synchronized the 0 DG through i the Unit 2 SAT. At this time, the O DG tripped due to reverse power. This failure is not a l valid failure in accordance with Regulatory Guide 1.108 and Technical Specification ]

l 4.8.1.1.3. l l

l The breaker closed without incident, but as the NSO began to reopen the breaker, the 0 DG tripped on Reverse Power. The O DG trip may have been caused by a voltage fluctuation on the offsite power grid. LOS-DG-SA1 is being reviewed to ensure it provides proper instructions to minimize the possibility of motorizing the generator.

The surveillance was subsequently completed satisfactorily on March 1,1995.

Sinceroy, Os'

.D D.J. Ray Station Manager LaSalie County Station i

DJR/CTK/lja cc: NRC Region lli Administrator NRC Senior Resident inspector INPO - Records Center IDNS Resident inspector Nuclear Ucensing Administrator 9504050230 950331 PDR ADOCK 05000373 PDR I S

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