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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6631994-05-0303 May 1994 LER 94-003-00:on 940405,loss of Shutdown Cooling Occurred Due to an Inadvertent High Reactor Pressure Isolation Signal.Corrective Action:Operations Department Procedure Used to Restore Shutdown Cooling isolations.W/940503 Ltr ML20029C7501994-04-20020 April 1994 LER 94-001-01:on 940305,ESF Actuation/Isolation & Loss of Shutdown Cooling Occurred.Caused by Personnel Error. Technician counseled.W/940420 Ltr ML20045B4761993-06-14014 June 1993 LER 93-004-00:on 930516,component Failure in EHC Sys Resulted in Generator/Turbine Trip & Reactor Scram.Failed Components Replaced & Addl Monitoring Devices Installed on EHC sys.W/930614 Ltr ML20045B2861993-06-0909 June 1993 LER 93-003-00:on 930513,plant Transient Initiated When 13.8 Kv Pothead Failed,Inducing Voltage Drop & Phase Differential Relay Actuation Due to Loss of Offsite Power on 2 of 4 Vital Buses.Failed Pothead replaced.W/930609 Ltr ML20029C2071991-03-21021 March 1991 LER 91-005-00:on 910219,reactor Scram Relay Malfunction Resulted in Startup Level Control Valve Failing Closed. Caused by Failure of Relay Controlling Position of Rfw 12 Startup Level Control Valve.Relay replaced.W/910321 Ltr ML20029A6441991-02-25025 February 1991 LER 91-003-00:on 910125,channel C Primary Containment Isolation Sys Actuated,Resulting in Trip of Radwaste Area Supply & Exhaust Fans.Caused by Design Deficiency Re Steam Leak Detection Sys Cabinets.Fuse replaced.W/910225 Ltr ML20028H8531991-01-23023 January 1991 LER 90-035-00:on 901227,pipe Section on Svc Water Sys (Ssws) a Loop Developed Minor Through Wall Flaw.Caused by Pipe Corrosion.Pipe Section on Ssws Will Be Replaced Prior to Restart from Current Refueling outage.W/910123 Ltr ML20028H6781991-01-16016 January 1991 LER 90-025-01:on 901104,leak Discovered on Weld on Reactor Recirculation Instrument Line While Investigating Source of Drywell Leakage.Caused by Crack at Welded Joint Due to vibration-induced Fatigue.Line replaced.W/910116 Ltr ML20043F4521990-06-11011 June 1990 LER 90-007-00:on 900517,control Room Received Indication of Half Scram & Isolation of Inboard Reactor Water Cleanup Isolation Valve.Caused by Spurious Trip of Channel a Reactor Protection Sys Epa.Design Change implemented.W/900611 Ltr ML20043F6121990-06-11011 June 1990 LER 90-006-00:on 900512,filtration,recirculation & Ventilation Sys Recirculation Fan E Discovered Running by Nuclear Control Operator.Cause Not Determined.Work Orders Initiated to Inspect Flow switches.W/900611 Ltr ML20043A8691990-05-16016 May 1990 LER 90-004-00:on 900418,ground Fault on Motor Control Ctr Feeder Breaker Occurred & Resulted in de-energization of Reactor B Protection Sys.Cause Not Determined.Feeder Breaker & Trip Device replaced.W/900516 Ltr ML20043A9091990-05-16016 May 1990 LER 90-005-00:on 900419,determined That Inoperability of Liquid Radwaste Discharge Monitor Not Reported in Recent Radioactive Effluent Release Rept.Caused by Procedural Deficiency.Effluent Rept revised.W/900516 Ltr ML20012C5991990-03-15015 March 1990 LER 89-026-01:on 891231,leak from Weld on 1-inch Reactor Recirculation Sys Elbow Tap Flow Transmitter Instrument Line Joint Discovered.Caused by Equipment Failure Due to Installation Deficiency During Plant const.W/900315 Ltr ML20006F8651990-02-19019 February 1990 LER 90-002-00:on 900119,HPCI Outboard Steam Supply Isolation Valve Auto Closed on High Room Differential Temp Signal. Caused by Inoperative Temp Control Loop.Troubleshooting of Loop Initiated to Determine malfunction.W/900219 Ltr ML20011E3931990-02-0505 February 1990 LER 90-001-00:on 900106,turbine Trip on Moisture Separator High Level Resulted in Reactor Scram.Caused by Combination of Equipment Failure & Cognitive Personnel Errors.Moisture Separator Drain Control Instrumentation tuned.W/900205 Ltr ML20006C2571990-01-30030 January 1990 LER 89-026-00:on 891231,leak from Weld on Reactor Recirculation Sys Flow Transmitter Instrument Line Joint Discovered.Cause Not Stated.Instrument Line Cut Out & Replaced W/New Section of piping.W/900130 Ltr ML20011E1301990-01-29029 January 1990 LER 89-025-00:on 891230,turbine Trip Occurred During Performance of Main Turbine Thrust Bearing Wear Detector Surveillance.Caused by Malfunction of Limit Switch.Design Change Implemented for Keylock Bypass switch.W/900129 Ltr ML20005E2401989-12-28028 December 1989 LER 89-024-00:on 891129,determined That Surveillance Frequency for Safety Auxiliaries Cooling Sys Valve EG-HV-2302B Should Have Been Increased.Caused by Data Recording Error.Personnel counseled.W/891228 Ltr ML20005E2421989-12-27027 December 1989 LER 89-021-01:on 891013,concluded That Class 1E Electrical Separation Criteria Not Met in Reactor Protection Sys Panel. Caused by Inadequate Review of 1986 Design Change Package. Nonconforming Power Supplies removed.W/891227 Ltr ML19332E7931989-12-0606 December 1989 LER 89-022-01:on 891016,reactor Protection Sys Electric Protection Assemblies Opened,Resulting in Loss of RHR B Which Had Been Operating in Shutdown Cooling Mode.Caused by Low Voltage Output.Assemblies reset.W/891206 Ltr ML19332E8131989-12-0404 December 1989 LER 89-023-00:on 891104,full Reactor Protection Sys Signal Inadvertently Generated While Pressurizing Drywell,Resulting in Full Scram Signal.Caused by Procedural Deficiency. Integrated Leak Rate Test Procedure revised.W/891204 Ltr ML19327C2561989-11-15015 November 1989 LER 89-022-00:from 891016-27,scrams Experienced on Channel B Reactor Protection Sys Electric Assemblies & Nuclear Steam Supply Shutdown Sys Isolated,Resulting in Loss of Shutdown Cooling.Assemblies & Output Voltages reset.W/891115 Ltr ML19327C2701989-11-13013 November 1989 LER 89-020-00:on 891011,pressure Spike in Reactor Vessel Ref Leg Resulted in ESF Actuation During Filling & Venting of Pressure Transmitter.Caused by Personnel Error.Technicians Counseled & Retrained in Venting procedures.W/891113 Ltr ML19327C2711989-11-13013 November 1989 LER 89-021-00:on 891013,review of GE Transient Analysis Recording Sys Determined That Class 1E Electrical Separation Criteria Not Met in Two Reactor Protection Sys Panels. Nonconforming Power Supplies removed.W/891113 Ltr ML19354D4411989-11-0303 November 1989 LER 89-019-00:on 891004,inadequate Instrumentation Used on Core Spray Pumps for ASME Section XI Testing.Caused by Inadequate Design Change Package.Event Reviewed W/Station Inservice Testing engineer.W/891103 Ltr ML19325E8811989-11-0202 November 1989 LER 89-018-00:on 891003,determined That Two Tech Spec Required Readings Not Taken as Required When Vent Monitoring Sys Inoperable on 890929.Caused by Lack of Adequate Communication.Personnel Involved counseled.W/891102 Ltr 1994-05-03
[Table view] Category:RO)
MONTHYEARML20029D6631994-05-0303 May 1994 LER 94-003-00:on 940405,loss of Shutdown Cooling Occurred Due to an Inadvertent High Reactor Pressure Isolation Signal.Corrective Action:Operations Department Procedure Used to Restore Shutdown Cooling isolations.W/940503 Ltr ML20029C7501994-04-20020 April 1994 LER 94-001-01:on 940305,ESF Actuation/Isolation & Loss of Shutdown Cooling Occurred.Caused by Personnel Error. Technician counseled.W/940420 Ltr ML20045B4761993-06-14014 June 1993 LER 93-004-00:on 930516,component Failure in EHC Sys Resulted in Generator/Turbine Trip & Reactor Scram.Failed Components Replaced & Addl Monitoring Devices Installed on EHC sys.W/930614 Ltr ML20045B2861993-06-0909 June 1993 LER 93-003-00:on 930513,plant Transient Initiated When 13.8 Kv Pothead Failed,Inducing Voltage Drop & Phase Differential Relay Actuation Due to Loss of Offsite Power on 2 of 4 Vital Buses.Failed Pothead replaced.W/930609 Ltr ML20029C2071991-03-21021 March 1991 LER 91-005-00:on 910219,reactor Scram Relay Malfunction Resulted in Startup Level Control Valve Failing Closed. Caused by Failure of Relay Controlling Position of Rfw 12 Startup Level Control Valve.Relay replaced.W/910321 Ltr ML20029A6441991-02-25025 February 1991 LER 91-003-00:on 910125,channel C Primary Containment Isolation Sys Actuated,Resulting in Trip of Radwaste Area Supply & Exhaust Fans.Caused by Design Deficiency Re Steam Leak Detection Sys Cabinets.Fuse replaced.W/910225 Ltr ML20028H8531991-01-23023 January 1991 LER 90-035-00:on 901227,pipe Section on Svc Water Sys (Ssws) a Loop Developed Minor Through Wall Flaw.Caused by Pipe Corrosion.Pipe Section on Ssws Will Be Replaced Prior to Restart from Current Refueling outage.W/910123 Ltr ML20028H6781991-01-16016 January 1991 LER 90-025-01:on 901104,leak Discovered on Weld on Reactor Recirculation Instrument Line While Investigating Source of Drywell Leakage.Caused by Crack at Welded Joint Due to vibration-induced Fatigue.Line replaced.W/910116 Ltr ML20043F4521990-06-11011 June 1990 LER 90-007-00:on 900517,control Room Received Indication of Half Scram & Isolation of Inboard Reactor Water Cleanup Isolation Valve.Caused by Spurious Trip of Channel a Reactor Protection Sys Epa.Design Change implemented.W/900611 Ltr ML20043F6121990-06-11011 June 1990 LER 90-006-00:on 900512,filtration,recirculation & Ventilation Sys Recirculation Fan E Discovered Running by Nuclear Control Operator.Cause Not Determined.Work Orders Initiated to Inspect Flow switches.W/900611 Ltr ML20043A8691990-05-16016 May 1990 LER 90-004-00:on 900418,ground Fault on Motor Control Ctr Feeder Breaker Occurred & Resulted in de-energization of Reactor B Protection Sys.Cause Not Determined.Feeder Breaker & Trip Device replaced.W/900516 Ltr ML20043A9091990-05-16016 May 1990 LER 90-005-00:on 900419,determined That Inoperability of Liquid Radwaste Discharge Monitor Not Reported in Recent Radioactive Effluent Release Rept.Caused by Procedural Deficiency.Effluent Rept revised.W/900516 Ltr ML20012C5991990-03-15015 March 1990 LER 89-026-01:on 891231,leak from Weld on 1-inch Reactor Recirculation Sys Elbow Tap Flow Transmitter Instrument Line Joint Discovered.Caused by Equipment Failure Due to Installation Deficiency During Plant const.W/900315 Ltr ML20006F8651990-02-19019 February 1990 LER 90-002-00:on 900119,HPCI Outboard Steam Supply Isolation Valve Auto Closed on High Room Differential Temp Signal. Caused by Inoperative Temp Control Loop.Troubleshooting of Loop Initiated to Determine malfunction.W/900219 Ltr ML20011E3931990-02-0505 February 1990 LER 90-001-00:on 900106,turbine Trip on Moisture Separator High Level Resulted in Reactor Scram.Caused by Combination of Equipment Failure & Cognitive Personnel Errors.Moisture Separator Drain Control Instrumentation tuned.W/900205 Ltr ML20006C2571990-01-30030 January 1990 LER 89-026-00:on 891231,leak from Weld on Reactor Recirculation Sys Flow Transmitter Instrument Line Joint Discovered.Cause Not Stated.Instrument Line Cut Out & Replaced W/New Section of piping.W/900130 Ltr ML20011E1301990-01-29029 January 1990 LER 89-025-00:on 891230,turbine Trip Occurred During Performance of Main Turbine Thrust Bearing Wear Detector Surveillance.Caused by Malfunction of Limit Switch.Design Change Implemented for Keylock Bypass switch.W/900129 Ltr ML20005E2401989-12-28028 December 1989 LER 89-024-00:on 891129,determined That Surveillance Frequency for Safety Auxiliaries Cooling Sys Valve EG-HV-2302B Should Have Been Increased.Caused by Data Recording Error.Personnel counseled.W/891228 Ltr ML20005E2421989-12-27027 December 1989 LER 89-021-01:on 891013,concluded That Class 1E Electrical Separation Criteria Not Met in Reactor Protection Sys Panel. Caused by Inadequate Review of 1986 Design Change Package. Nonconforming Power Supplies removed.W/891227 Ltr ML19332E7931989-12-0606 December 1989 LER 89-022-01:on 891016,reactor Protection Sys Electric Protection Assemblies Opened,Resulting in Loss of RHR B Which Had Been Operating in Shutdown Cooling Mode.Caused by Low Voltage Output.Assemblies reset.W/891206 Ltr ML19332E8131989-12-0404 December 1989 LER 89-023-00:on 891104,full Reactor Protection Sys Signal Inadvertently Generated While Pressurizing Drywell,Resulting in Full Scram Signal.Caused by Procedural Deficiency. Integrated Leak Rate Test Procedure revised.W/891204 Ltr ML19327C2561989-11-15015 November 1989 LER 89-022-00:from 891016-27,scrams Experienced on Channel B Reactor Protection Sys Electric Assemblies & Nuclear Steam Supply Shutdown Sys Isolated,Resulting in Loss of Shutdown Cooling.Assemblies & Output Voltages reset.W/891115 Ltr ML19327C2701989-11-13013 November 1989 LER 89-020-00:on 891011,pressure Spike in Reactor Vessel Ref Leg Resulted in ESF Actuation During Filling & Venting of Pressure Transmitter.Caused by Personnel Error.Technicians Counseled & Retrained in Venting procedures.W/891113 Ltr ML19327C2711989-11-13013 November 1989 LER 89-021-00:on 891013,review of GE Transient Analysis Recording Sys Determined That Class 1E Electrical Separation Criteria Not Met in Two Reactor Protection Sys Panels. Nonconforming Power Supplies removed.W/891113 Ltr ML19354D4411989-11-0303 November 1989 LER 89-019-00:on 891004,inadequate Instrumentation Used on Core Spray Pumps for ASME Section XI Testing.Caused by Inadequate Design Change Package.Event Reviewed W/Station Inservice Testing engineer.W/891103 Ltr ML19325E8811989-11-0202 November 1989 LER 89-018-00:on 891003,determined That Two Tech Spec Required Readings Not Taken as Required When Vent Monitoring Sys Inoperable on 890929.Caused by Lack of Adequate Communication.Personnel Involved counseled.W/891102 Ltr 1994-05-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F1501999-10-12012 October 1999 Special Rept:On 990929,south Plant Vent (SPV) Range Ng Monitor Was Inoperable.Monitor Was Inoperable for More than 72 H.Caused by Electronic Noise Generated from Noise Suppression Circuit.Replaced Circuit ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20217N6531999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Hope Creek Generating Station,Unit 1.With ML20217M0211999-09-20020 September 1999 Part 21 Rept Re Possible Deviation of NLI Dc Power Supply Over Voltage Protection Circuit Actuation.Caused by Electrical Circuit Conditions Unique to Remote Engine Panel. Travelled to Hope Creek to Witness Startup Sequence of DG ML20211N5531999-09-0808 September 1999 Safety Evaluation Supporting Amend 121 to License NPF-57 ML20211B3781999-08-13013 August 1999 Special Rept 99-002:on 990730,NPV Radiation Monitoring Sys Was Declared Inoperable.Caused by Voltage Induced in Detector Output by Power Cable to Low Range Sample Pump. Separated Cables & Secured in Place to Prevent Recurrence ML20210U4721999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8331999-07-26026 July 1999 Safety Evaluation Concluding That Licensee IPEEE Complete Re Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given HCGS Design,Operation & History ML20216D8721999-07-26026 July 1999 Review of Submittal in Response to USNRC GL 88-20,Suppl 4: 'Ipeees,' Fire Submittal Screening Review Technical Evaluation Rept:Hope Creek Rev 1:980518 ML20210F3331999-07-22022 July 1999 Safety Evaluation Granting Relief Requests RR-B1,RR-C1,RR-D1 & RR-B3.Finds That Proposed Alternative for RR-B3 Provides Acceptable Level of Quality & Safety & Authorizes Alternative Pursuant to 10CFR50.55a(a)(3)(i) ML20210C4731999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8901999-06-30030 June 1999 IPEEEs Technical Evaluation Rept High Winds,Floods & Other External Events ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML20196A1511999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Hope Creek Generating Station,Unit 1.With ML20206Q4731999-05-14014 May 1999 SER Accepting Response to GL 97-05, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant ML20206U1571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8451999-04-30030 April 1999 Rev 1, Submittal-Only Screening Review of Hope Creek Unit 1 IPEEE (Seismic Portion). Finalized April 1999 ML20206C8481999-04-22022 April 1999 SER Authorizing Pse&G Proposed Relief Requests Associated with Changes Made to Repair Plan for Core Spray Nozzle Weld N5B Pursuant to 10CFR50.55a(a)(3)(i) LR-N990157, Special Rept 99-001:on 990315, C EDG Valid Failure Occurred During Surveillance Testing.Testing Resulted in Unsuccessful Loading Attempt,Due to Failure EDG Output Breaker to Close.Faulty Card Replaced1999-04-12012 April 1999 Special Rept 99-001:on 990315, C EDG Valid Failure Occurred During Surveillance Testing.Testing Resulted in Unsuccessful Loading Attempt,Due to Failure EDG Output Breaker to Close.Faulty Card Replaced ML20205R5901999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Hope Creek Generating Station,Unit 1.With ML20205G6051999-03-19019 March 1999 SER Accepting Relief Request Re Acme Code Case N-567, Alternate Requirements for Class 1,2 & 3 Replacement Components,Section Xi,Div 1 ML20205F8911999-03-18018 March 1999 Safety Evaluation Authorizing Licensee Requests for Second 10-year Interval for Pumps & Valves IST Program ML20204F7951999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Hope Creek Generating Station,Unit 1.With ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML20202F6861999-01-26026 January 1999 Engine Sys,Inc Part 21 (10CFR21-0078) Rept Re Degradation of Synchrostat Model ESSB-4AT Speed Switches Resulting in Heat Related Damage to Power Supply Card Components.Caused by Incorrect Sized Resistor.Notification Sent to Customers ML18107A1871998-12-31031 December 1998 PSEG Annual Rept for 1998. ML20199E7271998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Hope Creek Generating Station,Unit 1.With ML18107A1881998-12-31031 December 1998 PECO 1998 Annual Rept. LR-N980580, Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With ML20198N4161998-11-12012 November 1998 MSIV Alternate Leakage Treatment Pathway Seismic Evaluation LR-N980544, Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with ML20155J9861998-10-31031 October 1998 Non-proprietary TR NEDO-32511, Safety Review for HCGS SRVs Tolerance Analyses LR-N980491, Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils LR-N980439, Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With LR-N980401, Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 1 ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps LR-N980354, Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 1 ML20236E9491998-06-30030 June 1998 Rev 0 to non-proprietary Rept 24A5392AB, Lattice Dependent MAPLHGR Rept for Hope Creek Generating Station Reload 7 Cycle 8 ML18106A6821998-06-24024 June 1998 Revised Charting Our Future. ML18106A6681998-06-17017 June 1998 Charting the Future. LR-N980302, Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 1 ML20248C7381998-05-22022 May 1998 Rev 0 to Safety Evaluation 98-015, Extension of Allowed Out of Service Time for B Emergency Diesel Generator LR-N980247, Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 1 LR-N980196, Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 1 ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML18106A5851998-03-0303 March 1998 Emergency Response Graded Exercise,S98-03. Nuclear Business Unit Salem,Hope Creek Emergency Preparedness, 980303 1999-09-08
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DIMG Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge. New Jersey 08038 Hope Creek Generating Station June 11, 1990
- U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
- HOPE CREEK GENERATING STATION DOCKET NO. 50-354 UNIT NO. 1 LICENSEE EVENT REPORT 90-007-00 This Licensee . Event Report 'is being submitted pursuant to the requirements of 10CFR50.73(a) (2) (iv) .
Sincerely,
.J. H Jan Gener Manager -
Hope Creek Operations RBC/
Attachment SORC Mtg.90-051 C Distribution 9006150026 900611 PDR ADOCK 05000354 S PDC
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, EXP18't$ 4'30'92 N8 eMATs0N C L (CT ON 8 0 Ett 60 0 H $ FOR AK UCENSEE EVENT REPORT (LER) g u,t,N4sy c,A,ao;= g t g T;M,A,T g Tgt g APE RWOke Rt TION JC (3 0 IC OF MAN AGEMENT AND CUDGET m AlmiNGTON DC 20503 poCati aspesesR 43: eaus i:s, 81CILITV NAast 96 Fort Calhoun Station Unit No. 1 015101010191 A lei 1 IoFln I c; I t#)gt top Potential for Overpressurization of Auxiliary Feedwater Pinino IVINT Daf t 191 Lth humastR sel AGPORT oaf t (?) OTHER f ACILITit$ INVOLWs0 a01 MONTH DAY vtAR vtAR "MU '*, 6 ",8j,$ MONTH DAY vtAR 8Aci6rtv hAwes DOCS.t T NUMethisi N 015l01010 1 1 I 1
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CAult SylT E M COMPONENT C A$'o {,ta ns CAUse $vsttu COMPONtNT "'%$C 0 en k' l I I I I I I I I I f I I I l l 1 I I i l l l I I I I I MONTH OAv vtAR SUPPLEMilNT AgtPORT G RPtCit01941 4tS ll* ree sonwete tKPLCtlO SUOnel3SION CA Til ko l l l ASSTR ACT itsev, M I400 aseres a e , asPremnaemir Areeea s'ap e asete typeweerma maest 06:
Accident scenarios have been identified by which the Auxiliary Feedwater piping from the discharge of turbine driven Auxiliary Feedwater pum) FW-10 can be overpressurized. The scenarios require FW-10 to be running in tie recirculation mode, with no injection to the steam generr.cors, a coincident loss of instrument air, and a single active failure of the pump's speed limiting governor. In accordance with 10 CFR 50.72 tb)(2)(i), this potential for overpressurization was reported to the NRC On May 11, 1990 at 1725 hours0.02 days <br />0.479 hours <br />0.00285 weeks <br />6.563625e-4 months <br /> CDT as a condition outside the design basis.
A design deficency during plant construction which eliminated the specification for an overspeed trip on FW-10 has been determined to be the cause of this condition.
An engineering analysis of tne pump's failure mode has determined that, although the maximum pump discharge pressure will exceed the piping design pressure, catastro) hic failure of the piping or associated components will not occur. Based on tiis analysis, Safety Analysis for Operability 90-012 was approved on May 13, 1990, to justify acceptability of plant operation.
A permanent resolution to the concern for overpressurization of the auxiliary feedwater piping from overspeeding of FW-10 will be completed during the 1991 Refueling and Maintenance Outage.
NRC. - =.iu.,
9 LIONSIE B7NT RElWT FACIIIlY NAME (1) DOGET NUMBER (2) PAGE (3)
IDPE CRHX GENERATING ETATIm 0 5 0 0 0 3 5 4 1 7 4 TITLE (4): INGINEDD SAIElY IB1URIE (ESP) ACIVATIm (RFAC10R WA1TR CLEANUP ISXATIm) IIJE 101 RIPPING OF REACIUR IWITLTIm SYS11N OIANNEL "A" IIICIRICAL IWITLTIm ASSINBLY f% TNT DA1E (5) IIR NLMBER (6) RDWT M1E (7) OnlIR FACILITIES INVOLATD (8)
Unl IAY ** NLMBER ** Umi iTAR YEAR YEAR REV DAY FACILITY NAME(S) DOCKET NUMRER(S) 0 5 1 7 9 0 9 0 -
0 0 7 -
0 0 0 6 1 1 9 0 OPERATING 1 BIIS RDWT IS SUIMITITD IURSUAVI 10 UIE REULHRfMENPS OF 100R: (OIDCK (NE OR P0RE HE10W)(11)
KI10 (9) 20.402(b) , _ 20.405(c) , X_X 50.73(a)(2)(iv) _ _73.71 (b)
KWIR 20.405(a)(1)(1) 50.36(c) (1) __50.73(a)(2) (v) 73.71(c)
._cnER (Specify in IET7L 1 0 0 _
50.36(c) (2) ._
20.405(a)(1)(ii) 20.405(a)(1)(iii) ._ ._50.73(a)(2)(1) ._50.73(t)(2)(vii)Abstract below
\\\\\\\\\\\\\\\\\__ _20.405(a)(1)(iv) ._50.73(a)(2)(ii) ._50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) and in Text) 50.73(a)(2)(iii)
\\\\\\\\\\\\\\\\\ 20.405(a)(1)(v) 50.73(a) (2) (x)
LIONSEI GWTACT FOR 11[IS IIR _(12)
NAME 1T117WNE NUMBER Richant Cowles, Senior Stafi Engineer - Tedmical 60 9 3 3 9 3 4 3 1 (IMPIEIE ONE IJNE 10R FA010:MKNINT FAlll3RE N0 LID IN DlIS RDORT (13)
CAUSE SYSUM EMKNENT MANUFAC- RE2 W TABLE \\\\\\\ CAUSE SYElIM GMfWINT MANUIRC- RDMTABLE 1URIR 10 NPRDS? \\\\\\\ 1URER 10 NPRDS?
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SUPPIIMFNTAL RUMT EXPfURD? (14) YELL I NDlXX DALE 11PErnD (15) Uni DAY YEAR \\\\\\\\\\\\\\\\\\
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ABS 1RAct (16)
On 5/17/90 at 1353, the control room received indication of a half scram and isolation of the inboard Reactor Water Cleanup (RWCU) isolation valve.
The above actions occurred as a result of a loss of the power supply to the Channel "A" Reactor Protection System (RPS) electrical bus when the normal power supply' Electrical Protection Assembly (EPA) experienced a spurious trip. The Channel "A" RPS bus was re-powered from its alternate power source, and the half scram and RWCU isolation were reset. Followup troubleshooting by the Maintenance Department could not determine a definitive reason for the trip of the EPA, however, it is suspected that the trip resulted from an EPA performance problem similar to those noted in General Electric Service Information Letter (SIL) 496. Corrective actions include scheduling of modifications to all RPS EPAs as described in SIL-496.
EPA Manufacturer: General Electric Type: TFJ Part Number: 184C449P001
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LIGNSEE EVENT RDWT (IDt) 'IIXT ONTDIUATim FACILITY NME (1) DOLET NUMBER (2) 11R NUMBER (6) PME (3) J iTAR ** NLDWER ** REV HOPE CRED: GENERATDG STATEN 05000354 )
90 -
0 0 7 -
0 0 0 2 CF 0 4 1
PLANT AND SYSTEM IDENTIFICATION j General Electric - Boiling Water Reactor (BWR/4)
Reactor Protection System (EIIS Deaignation: JC)
Reactor Water Cleanup System (F11S Designation: CE)
IDENTIFICATION OF OCCURRENCE Engineered Safety Features (ESP) Actuation (Reactor Water Cleanup Isolation) Due to Tripping Of Reactor Protection System ;
Channel "A" Electrical Protection Assembly Event Date: 5/17/90 Event Time: 1353 This LER was initiated by Incident Report No.90-050 CONDITIONS PRIOR TO OCCURRENCE Plant in OPERATIONAL CONDITION 1 (Power Operation), reactor power 100%, unit load 1110MWe.
DESCRIPTION OF OCCURRENCE On 5/17/90 at 1353, control room personnel received- indication of a half screm and isolation of the inboard Reactor Water ,
Cleanup ( p' jeu) isolation valve (HV-F001).
. The Nuclear Control Operator (NCO, RO licensed) noted that an electrical protection assembly (EPA) for the Channel "A" Reactor Protection System (RPS) normal power supply had tripped. Channel "A" RPS was re-energized from its alternate power source, and the half ^
scram and RWCU isolation were reset. A work request was initiated to troubleshoot the tripped EPA, and- the Senior Nuclear Shift Supervisor (SNSS, SRO licensed) initiated a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> non-emergency report per 10CFR50.72 due to the- RWCU isolation.
APPARENT CAUSE OF OCCURRENCE This occurrence was caused by a spurious trip of a Channel "A" RPS bus EPA.
ANALYSIS OF OCCURRENCE Followup troubleshooting by the Maintenance Department could not determine a cause for the trip of the EPA. Over and under voltage trip setpoints were verified to be within tolerance, and no perturbations from the respective RPS motor generator set were noted.
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LICENSEE LVDff RDORT (IER) MT 03frDO. TIN FACILITI NN: (1) 10CKET NUMBDi (2) IIR NUER (6) PME (3)
YIAR \\ NLPEER \\ REN
- HOPE: OtEIK GENERATING STATIN 05000354 0 0 7 -
0 0 0 3 T 0 4 ANALYSIS OF OCCURRENCE. CONT'D t
Systems Engineering reviewed the event, and determined that the EPA trip exhibited characteristics of EPA performance problems similar to those identified in GE SIL-496, which was issued in
-August, 1989.- In response to SIL-496, in February, 1990, Systems Engineering initiated a design change to replace existing logic cards in all EPA's at liope Creek with upgraded logic cards as recommended by GE. This design change is expected to be implemented prior to the end of the stations third refueling outage in early 1991.
PREVIOUS OCCURRENCES ~
There have been 3 previous reportable occurrences initiated by tripping of RPS electrical protection assemblies (reference:
LERs86-007, 87-021, and 89-022). In all cases, the EPAs
, tripped on undervoltage conditions due to either undervoltage L setpoint problems or undervoltage conditions on the alternate power supplies. No " spurious" EPA trips have previously occurred at Hope Creek.
-SAFETY SIGNIFICANCE This incident had ininimal potential safety significance.
Immediately following the EPA trip, RPS channel "A" was ,
re-energized from its alternate power supply.. Technical Specifications permit operation in any operating condition for .,
up to. 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> with one RPS channel inoperable.
Had RPS channel "B" been inoperable at the time of this occurrence, a s L reactor scram would have occurred, and a reactor scram is bounded by UFSAR analysis.
EQUIPMENT / MANUFACTURER DATA EPA' Manufacturer: General Electric EPA Type: TFJ Part Number: 184C449P001 l
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. LIONSEE IVINF REKRP (IIR) 1RT ONTINATION 17CIIJlY 10ME (1) DOCKLT 10EER (2) IIR NUMIER (6) PAh (3)
YEAR \\ )UEER \\ REN ltFE OHK GENERATDC STATICH 05X)0354 90 -
0 0 7 -
0 0 0 4 OE' O 4 pORRECTIVE ACTIONS The design change as recommended by GE SIL-496 with respect to EPA logic cards will be implemented prior to the end of the stations third refueling outage.
Since ely,
.J 11 Jan Gen Manager -
Hope Creek Operations RBC/
SORC Mtg.90-051 1
1
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