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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J3301994-10-0707 October 1994 LER 94-011-00:on 940908,manual Reactor Trip Initiated Due to MSIV Failure During part-stroke Test.Solenoid Valve & Number of Pins Replaced & MSIVs Tested satisfactorily.W/941007 Ltr ML20024J3291994-10-0303 October 1994 LER 94-027-00:on 940903,determined That Channel B Linear Range Nuclear Instrument Inoperable as Result of Connector J6 Being Disconnected from Jack.Connector J6 Reinstalled.W/ 941003 Ltr ML20029E5291994-05-13013 May 1994 LER 94-007-00:on 940414,determined That Valve Stroke Time Acceptance Criterion Exceeded System Response Time.Caused by Programmatic Error During Initial Startup.Corrective Action: Stroke Time Acceptance Has Been reduced.W/940513 Ltr ML20029E1361994-05-11011 May 1994 LER 94-007-00:on 940412,CRAC & Ebfs Were Inoperable Due to Previous Charcoal Testing Performed to Industry Std Different than Ts.Corrective Actions:Ts Changed to Reflect Newest Charcoal Testing procedure.W/940511 Ltr ML20029D8491994-05-0202 May 1994 LER 94-006-00:on 940407,plant Did Not Meet Requirements of LCO 3.7.6.1 Re Two Independent Control Room Emergency Ventilation Sys.Caused by Inadequate Work Organization. Corrective Action:Revised OP 2315A.W/940502 Ltr ML20029D6221994-04-29029 April 1994 LER 94-005-00:on 940401,determined That Both Facilities of Ebfs Had Never Been Tested in Accordance W/Ts.Caused by Program Failure/Personnel Error.Corrective Action: Surveillance Was Completed satisfactorily.W/940429 Ltr ML20029D2531994-04-28028 April 1994 LER 94-008-00:on 940329,discovered That Data in OPS Form 2604P-2,was Recorded Incorrectly.Caused by Program Failure, Procedure Deficiencies & Technical Error.Corrective Action: Recalculated ESF Equipment Circuit response.W/940428 Ltr ML20046C7771993-08-0606 August 1993 LER 93-010-00:on 930707,reactor Trip Input to Turbine Trip Portion of ESFAS Declared Inoperable Due to Inadequate Surveillance Testing.Test to Verify Operability Written & performed.W/930806 Ltr ML20046C2161993-08-0303 August 1993 LER 93-017-00:on 930701,possible Inoperability of Power Operated Relief Valve Blocking Valves Caused by Original Design Basis.Changed Designs & Performed tests.W/930803 Ltr ML20046B0311993-07-23023 July 1993 LER 93-012-01:on 930524,turbine & Reactor Tripped During Mussel Cook (Thermal Backwash) Due to Lack of Heat Removal Capabilities from Main Generator Stator Water Cooling Sys. Installed Thermoconductivity filler.W/930723 Ltr ML20045H8991993-07-15015 July 1993 LER 93-009-00:on 930617,determined That Suppl Leak Collection & Release Sys May Have Been Inoperable During Certain Weather Periods in Past.Caused by Failure to Account for Chimney Effect.Suppl Will Be sent.W/930715 Ltr ML20045H4021993-07-0909 July 1993 LER 93-007-00:on 930611,plant Mgt Discovered Reduction in EDG Fuel Oil Storage Capacity Per SER & Fsar,Constituting Event Outside Design Basis of Plant.Caused by Inadequate Design Interface.Temporary Tanker utilized.W/930709 Ltr ML20045H8921993-07-0909 July 1993 LER 93-005-01:on 930311,discovered That Automatic RPS Actuation Occurred on 930222 & Not Immediately Reported to Nrc.Caused by Personnel Error.Memo Sent to All Licensed Operators/Personnel Re Reporting requirements.W/930709 Ltr ML20045H8571993-07-0909 July 1993 LER 93-008-00:on 930614,one Channel of Electrical Environmentally Qualified Temp Monitor for Main Steam Valve Bldg Found Indicating Improperly.Caused by Personnel Error. Manual Logging of Temp initiated.W/930709 Ltr ML20045F5891993-07-0202 July 1993 LER 93-013-00:on 930603,noted That Main Turbine Generator EHC Sys Caused an Increase in Pressurizer Pressure,Resulting in Reactor Trip,Due to Closing of Intercept & Cv.Operators Performed EOP & Sys Performed as expected.W/930702 Ltr ML20045F6881993-07-0202 July 1993 LER 93-004-02:on 930222,reactor Trips on SG Low Water Level Occurred.Caused by Automatic Trip of MFW Pump B on Low Suction Pressure Due to High FW Flow Rates.Classroom Training on Main & Afwc Received by Licensed Operators ML20045D9041993-06-23023 June 1993 LER 93-012-00:on 930524,reactor Trip Occurred Due to Turbine Trip & Malfunction Caused Feedwater Regulating Valve a to Stay Approx 56% Open.Caused by Lack of Heat Removal Capabilities.Hand Wheels secured.W/930623 Ltr ML20045D8601993-06-21021 June 1993 LER 93-006-00:on 930525,two HPSI Discharge Check Valves Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Personnel Error.Test Written & Performed to Demonstrate Valve operability.W/930621 Ltr ML20045D9031993-06-21021 June 1993 LER 92-003-01:on 920207,discovered Potential Barrier Breach Via Direct Openings Around Main Feedwater Bypass Line Penetrations.On 920130,plant Entered Mode 4 W/O Encl Bldg Integrity.Erosion/Corrosion Exam Procedure Modified ML20045D3091993-06-18018 June 1993 LER 93-005-00:on 930520,cold Over Pressure Protection Sys Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Mgt Deficiency.Overlap Task Force Will Continue to Review Procedures Associated W/Reactor trip.W/930618 Ltr ML20045A4491993-06-0404 June 1993 LER 93-009-00:on 930506,inlet & Outlet skid-mounted Isolation Valves to Radiation Monitor Found Shut.Caused by Procedure Noncompliance by I&C Personnel.Personnel Will Review & Edit Radiation procedures.W/930604 Ltr ML20045A2321993-06-0101 June 1993 LER 93-008-00:on 930505,determined That Electrical Starter for Both Charging Pumps Inoperable.Caused by Program Failure.Administrative Controls Have Been Established to Ensure Minimum TS requirements.W/930601 Ltr ML20044C9191993-05-0707 May 1993 LER 93-002-01:on 930206 & 07,Train a & Train B CR Pressurization Sys Failed 18-month Surveillance Test, Respectively.Caused by Moisture in Air Banks & Pressure Oscillations.Air Banks purged.W/930507 Ltr ML20044C9331993-04-30030 April 1993 LER 91-002-01:on 910118,engineering Evaluation Determined That Operation of Four Vital 120-volt Ac Buses,On Alternate Sources,Unsatisfactory.Caused by Failure to Update TS to Reflect Configuration.Inverter Sys replaced.W/930430 Ltr ML19346B2411992-08-20020 August 1992 LER 92-018-00:on 920722,both RHR Trains Rendered Inoperable Due to Procedure Deficiency.Both Trains of RHR Restored to Operable Condition & Surveillance Procedures for Both Trains revised.W/920820 Ltr ML20024H3241991-05-24024 May 1991 LER 91-001-01:on 910110,electro-hydraulic Control Sys Failure Occurred,Causing Reactor Trip.Caused by Turbine Trip.Both EHC Pump Discharge Filters Changed Out & Pump B Replaced W/Spare pump.W/910524 Ltr ML20029C1281991-03-18018 March 1991 LER 91-004-00:on 910216,unexpected Trip of 'B' Steam Generator Feed Pump & Subsequent Manual Reactor Trip Occurred.Cause Unknown.Monitoring Capability Added to Sgfp Circuitry & Design Change made.W/910318 Ltr ML20029B6001991-03-0707 March 1991 LER 91-004-00:on 910205,leakage Found During Local Leak Rate Testing for Four Containment Isolation Valves.Caused by Improper Valve Seating.Valve Removed from Svc & Sent to Mfg for overhaul.W/910307 Ltr ML20029B6031991-03-0404 March 1991 LER 91-002-00:on 910202,setpoint Drift Identified During Testing of Main Steam Safety Valves.Caused by Inadequate Design.Nine out-of-tolerance Valves Reset within Specified +1% Tolerance ML20029B5981991-03-0404 March 1991 LER 91-003-00:on 910203 & 16,spurious Control Bldg Isolation Signals Received from Train a Control Bldg Ventilation Inlet Radiation Monitor.Caused by Equipment Malfunction.Detector replaced.W/910304 Ltr ML20029A6501991-02-19019 February 1991 LER 91-001-00:on 910117,discovered That Source Check Surveillance Procedure to Verify Operability of Beta Scintillation Radiation Detectors Did Not Meet TS Requirements.Surveillance Procedure revised.W/910219 Ltr ML20028H4261990-12-27027 December 1990 LER 89-005-01:on 890330,intermittent Connection While Sliding Module Into Position Caused Automatic Test Insertion Circuit to Send Signals Greater than Normal Pulse Thus Allowing Three SIAS Modules to actuate.W/901227 Ltr ML20028H4391990-12-27027 December 1990 LER 90-015-01:on 900919,inadvertent Isolation of Containment Isolation Valves Occurred.On 900920,inadvertent Actuation of Sias,Containment Isolation Actuation Sys & Encl Bldg Filtration Sys occurred.W/901227 Ltr ML20028H4271990-12-27027 December 1990 LER 90-021-00:on 901127,LCO Paragraph 3.0.3 Entered.Caused by Poor Communications.Mgt Reviewed Event & Events Leading Up to Incident & Concluded That Increased Awareness W/ Respect to Sys Status Must Be pursued.W/901227 Ltr ML20028H4401990-12-24024 December 1990 LER 90-019-00:on 900606,automatic Reactor Trip from Negative Flux Rate Signal Occurred Due to Dropped Control Rod.Caused by Broken Connection in Gripper Coil Power Cable.Connector Replaced & Power Loop checked.W/901224 Ltr ML20028G9421990-09-26026 September 1990 LER 90-012-00:on 900827,automatic Reactor Trip Occurred During Bypass Switch Operations.Caused by Operator Error. Procedure Sp 2601D Revised to Incorporate Separate Section on Performing calibrs.W/900926 Ltr ML20028G9111990-09-18018 September 1990 LER 89-008-01:on 891002,determined That Plant Failed to Perform Functional Check of Control Board Annunciators During Channel Functional Tests.Caused by Personnel Error. Procedures Revised Re Annuciator testing.W/900918 Ltr ML20044B0441990-07-10010 July 1990 LER 90-007-00:on 900611,discovered That Surveillance Procedure 2609E Re Encl Bldg Filtration Sys Testing - Refueling Not Performed Prior to Entering Mode 4.Caused by Personnel Error.Missed Surveillance performed.W/900710 Ltr ML20044A1581990-06-18018 June 1990 LER 90-017-00:on 900518,loss of Both Trains of HPSI Occurred.Caused by Cognitive Failure by Licensed Operator. Personnel Counseled on Causes of Event & Importance of Recognizing When Event reportable.W/900618 Ltr ML20043H2021990-06-15015 June 1990 LER 90-005-00:on 900503,identified Potential for High Energy Line Break in Auxiliary Steam Sys That Could Degrade Plant Areas Determined as Mild Environs.Probably Caused by Incorrect Conclusions from Analysis in 1973.W/900615 Ltr ML20043G1031990-06-12012 June 1990 LER 90-016-00:on 900513,steam Generator B lo-lo Signal Generated Reactor Trip Signal,Causing Automatic Start of motor-driven Auxiliary Feedwater Pumps a & B.Caused by Inadequate Guidance.Procedure revised.W/900612 Ltr ML20043G3921990-06-11011 June 1990 LER 90-014-00:on 900519,manual Reactor Trip Initiated as Result of Anticipated Turbine Trip Due to Condenser Vacuum. Caused by Design Deficiency in That Traveling Screen Capacity Inadequate.Traveling Screen modified.W/900611 Ltr ML20043F7021990-06-11011 June 1990 LER 90-015-00:on 900512,feedwater Isolation Occurred While Opening Msivs.Caused by MSIV 2 Opening Faster than Other Msivs,Resulting in Swell in Steam Generator 2.Steam Generator Level Restored to normal.W/900611 Ltr ML20043F8261990-06-0707 June 1990 LER 90-006-00:on 900508,reactor Manually Tripped When Decreasing Levels Noted in Steam Generator 1 & Feedwater Regulating Valve Indicated Full Open.Caused by Valve Stem Separating from Plug.Feedwater Flow restored.W/900607 Ltr ML20043D4711990-05-30030 May 1990 LER 85-002-01:on 850302 & 25,unplanned Actuation of Containment Purge Valve Isolation Occurred.Caused by Personnel Error.Caution Signs Placed on Radiation Monitors & Reset Button on Monitor Made inaccessible.W/900530 Ltr ML20043A7841990-05-16016 May 1990 LER 90-013-00:on 900416,manual Reactor Trip Initiated Due to Imminent Loss of Condenser Vaccum.Caused by Inadequate Administrative Guidance When Debris Collected on Trash Rack. Severe Weather Procedure revised.W/900516 Ltr ML20042G7201990-05-0707 May 1990 LER 90-012-00:on 900406,review of Steam Generator Blowdown Monitor High Radiation Alarm Setpoint Revealed That Setpoint Was Nonconservative.Caused by Administrative Deficiency. Correct Setpoint installed.W/900507 Ltr ML20042E6751990-04-20020 April 1990 LER 90-002-00:on 900322,Tech Spec Action Statement 3.3.3.10 Not Entered for Out of Svc Stack Gas & Particulate Radiation Monitor.No Particulate Radiation Increases Detected.Caused by Personnel error.W/900420 Ltr ML20042E1621990-04-0909 April 1990 LER 90-009-00:on 900309,automatic Turbine Trip W/Subsequent Reactor Trip Occurred Due to High Stator Cooling Water Temp. Caused by Failure of Mechanical Linkage on Fisher & Portor Controller.Controller Replaced w/spare.W/900409 Ltr ML17223A7901990-04-0202 April 1990 LER 89-009-01:on 891025,radiation Monitor RM 8262 Inlet Valve (2-AC-82) Found Closed.Caused by Personnel Error. Isolation Valve Opened,Sample Flow Restored & Radiation Monitor Restored to Operable status.W/900402 Ltr 1994-05-02
[Table view] Category:RO)
MONTHYEARML20024J3301994-10-0707 October 1994 LER 94-011-00:on 940908,manual Reactor Trip Initiated Due to MSIV Failure During part-stroke Test.Solenoid Valve & Number of Pins Replaced & MSIVs Tested satisfactorily.W/941007 Ltr ML20024J3291994-10-0303 October 1994 LER 94-027-00:on 940903,determined That Channel B Linear Range Nuclear Instrument Inoperable as Result of Connector J6 Being Disconnected from Jack.Connector J6 Reinstalled.W/ 941003 Ltr ML20029E5291994-05-13013 May 1994 LER 94-007-00:on 940414,determined That Valve Stroke Time Acceptance Criterion Exceeded System Response Time.Caused by Programmatic Error During Initial Startup.Corrective Action: Stroke Time Acceptance Has Been reduced.W/940513 Ltr ML20029E1361994-05-11011 May 1994 LER 94-007-00:on 940412,CRAC & Ebfs Were Inoperable Due to Previous Charcoal Testing Performed to Industry Std Different than Ts.Corrective Actions:Ts Changed to Reflect Newest Charcoal Testing procedure.W/940511 Ltr ML20029D8491994-05-0202 May 1994 LER 94-006-00:on 940407,plant Did Not Meet Requirements of LCO 3.7.6.1 Re Two Independent Control Room Emergency Ventilation Sys.Caused by Inadequate Work Organization. Corrective Action:Revised OP 2315A.W/940502 Ltr ML20029D6221994-04-29029 April 1994 LER 94-005-00:on 940401,determined That Both Facilities of Ebfs Had Never Been Tested in Accordance W/Ts.Caused by Program Failure/Personnel Error.Corrective Action: Surveillance Was Completed satisfactorily.W/940429 Ltr ML20029D2531994-04-28028 April 1994 LER 94-008-00:on 940329,discovered That Data in OPS Form 2604P-2,was Recorded Incorrectly.Caused by Program Failure, Procedure Deficiencies & Technical Error.Corrective Action: Recalculated ESF Equipment Circuit response.W/940428 Ltr ML20046C7771993-08-0606 August 1993 LER 93-010-00:on 930707,reactor Trip Input to Turbine Trip Portion of ESFAS Declared Inoperable Due to Inadequate Surveillance Testing.Test to Verify Operability Written & performed.W/930806 Ltr ML20046C2161993-08-0303 August 1993 LER 93-017-00:on 930701,possible Inoperability of Power Operated Relief Valve Blocking Valves Caused by Original Design Basis.Changed Designs & Performed tests.W/930803 Ltr ML20046B0311993-07-23023 July 1993 LER 93-012-01:on 930524,turbine & Reactor Tripped During Mussel Cook (Thermal Backwash) Due to Lack of Heat Removal Capabilities from Main Generator Stator Water Cooling Sys. Installed Thermoconductivity filler.W/930723 Ltr ML20045H8991993-07-15015 July 1993 LER 93-009-00:on 930617,determined That Suppl Leak Collection & Release Sys May Have Been Inoperable During Certain Weather Periods in Past.Caused by Failure to Account for Chimney Effect.Suppl Will Be sent.W/930715 Ltr ML20045H4021993-07-0909 July 1993 LER 93-007-00:on 930611,plant Mgt Discovered Reduction in EDG Fuel Oil Storage Capacity Per SER & Fsar,Constituting Event Outside Design Basis of Plant.Caused by Inadequate Design Interface.Temporary Tanker utilized.W/930709 Ltr ML20045H8921993-07-0909 July 1993 LER 93-005-01:on 930311,discovered That Automatic RPS Actuation Occurred on 930222 & Not Immediately Reported to Nrc.Caused by Personnel Error.Memo Sent to All Licensed Operators/Personnel Re Reporting requirements.W/930709 Ltr ML20045H8571993-07-0909 July 1993 LER 93-008-00:on 930614,one Channel of Electrical Environmentally Qualified Temp Monitor for Main Steam Valve Bldg Found Indicating Improperly.Caused by Personnel Error. Manual Logging of Temp initiated.W/930709 Ltr ML20045F5891993-07-0202 July 1993 LER 93-013-00:on 930603,noted That Main Turbine Generator EHC Sys Caused an Increase in Pressurizer Pressure,Resulting in Reactor Trip,Due to Closing of Intercept & Cv.Operators Performed EOP & Sys Performed as expected.W/930702 Ltr ML20045F6881993-07-0202 July 1993 LER 93-004-02:on 930222,reactor Trips on SG Low Water Level Occurred.Caused by Automatic Trip of MFW Pump B on Low Suction Pressure Due to High FW Flow Rates.Classroom Training on Main & Afwc Received by Licensed Operators ML20045D9041993-06-23023 June 1993 LER 93-012-00:on 930524,reactor Trip Occurred Due to Turbine Trip & Malfunction Caused Feedwater Regulating Valve a to Stay Approx 56% Open.Caused by Lack of Heat Removal Capabilities.Hand Wheels secured.W/930623 Ltr ML20045D8601993-06-21021 June 1993 LER 93-006-00:on 930525,two HPSI Discharge Check Valves Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Personnel Error.Test Written & Performed to Demonstrate Valve operability.W/930621 Ltr ML20045D9031993-06-21021 June 1993 LER 92-003-01:on 920207,discovered Potential Barrier Breach Via Direct Openings Around Main Feedwater Bypass Line Penetrations.On 920130,plant Entered Mode 4 W/O Encl Bldg Integrity.Erosion/Corrosion Exam Procedure Modified ML20045D3091993-06-18018 June 1993 LER 93-005-00:on 930520,cold Over Pressure Protection Sys Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Mgt Deficiency.Overlap Task Force Will Continue to Review Procedures Associated W/Reactor trip.W/930618 Ltr ML20045A4491993-06-0404 June 1993 LER 93-009-00:on 930506,inlet & Outlet skid-mounted Isolation Valves to Radiation Monitor Found Shut.Caused by Procedure Noncompliance by I&C Personnel.Personnel Will Review & Edit Radiation procedures.W/930604 Ltr ML20045A2321993-06-0101 June 1993 LER 93-008-00:on 930505,determined That Electrical Starter for Both Charging Pumps Inoperable.Caused by Program Failure.Administrative Controls Have Been Established to Ensure Minimum TS requirements.W/930601 Ltr ML20044C9191993-05-0707 May 1993 LER 93-002-01:on 930206 & 07,Train a & Train B CR Pressurization Sys Failed 18-month Surveillance Test, Respectively.Caused by Moisture in Air Banks & Pressure Oscillations.Air Banks purged.W/930507 Ltr ML20044C9331993-04-30030 April 1993 LER 91-002-01:on 910118,engineering Evaluation Determined That Operation of Four Vital 120-volt Ac Buses,On Alternate Sources,Unsatisfactory.Caused by Failure to Update TS to Reflect Configuration.Inverter Sys replaced.W/930430 Ltr ML19346B2411992-08-20020 August 1992 LER 92-018-00:on 920722,both RHR Trains Rendered Inoperable Due to Procedure Deficiency.Both Trains of RHR Restored to Operable Condition & Surveillance Procedures for Both Trains revised.W/920820 Ltr ML20024H3241991-05-24024 May 1991 LER 91-001-01:on 910110,electro-hydraulic Control Sys Failure Occurred,Causing Reactor Trip.Caused by Turbine Trip.Both EHC Pump Discharge Filters Changed Out & Pump B Replaced W/Spare pump.W/910524 Ltr ML20029C1281991-03-18018 March 1991 LER 91-004-00:on 910216,unexpected Trip of 'B' Steam Generator Feed Pump & Subsequent Manual Reactor Trip Occurred.Cause Unknown.Monitoring Capability Added to Sgfp Circuitry & Design Change made.W/910318 Ltr ML20029B6001991-03-0707 March 1991 LER 91-004-00:on 910205,leakage Found During Local Leak Rate Testing for Four Containment Isolation Valves.Caused by Improper Valve Seating.Valve Removed from Svc & Sent to Mfg for overhaul.W/910307 Ltr ML20029B6031991-03-0404 March 1991 LER 91-002-00:on 910202,setpoint Drift Identified During Testing of Main Steam Safety Valves.Caused by Inadequate Design.Nine out-of-tolerance Valves Reset within Specified +1% Tolerance ML20029B5981991-03-0404 March 1991 LER 91-003-00:on 910203 & 16,spurious Control Bldg Isolation Signals Received from Train a Control Bldg Ventilation Inlet Radiation Monitor.Caused by Equipment Malfunction.Detector replaced.W/910304 Ltr ML20029A6501991-02-19019 February 1991 LER 91-001-00:on 910117,discovered That Source Check Surveillance Procedure to Verify Operability of Beta Scintillation Radiation Detectors Did Not Meet TS Requirements.Surveillance Procedure revised.W/910219 Ltr ML20028H4261990-12-27027 December 1990 LER 89-005-01:on 890330,intermittent Connection While Sliding Module Into Position Caused Automatic Test Insertion Circuit to Send Signals Greater than Normal Pulse Thus Allowing Three SIAS Modules to actuate.W/901227 Ltr ML20028H4391990-12-27027 December 1990 LER 90-015-01:on 900919,inadvertent Isolation of Containment Isolation Valves Occurred.On 900920,inadvertent Actuation of Sias,Containment Isolation Actuation Sys & Encl Bldg Filtration Sys occurred.W/901227 Ltr ML20028H4271990-12-27027 December 1990 LER 90-021-00:on 901127,LCO Paragraph 3.0.3 Entered.Caused by Poor Communications.Mgt Reviewed Event & Events Leading Up to Incident & Concluded That Increased Awareness W/ Respect to Sys Status Must Be pursued.W/901227 Ltr ML20028H4401990-12-24024 December 1990 LER 90-019-00:on 900606,automatic Reactor Trip from Negative Flux Rate Signal Occurred Due to Dropped Control Rod.Caused by Broken Connection in Gripper Coil Power Cable.Connector Replaced & Power Loop checked.W/901224 Ltr ML20028G9421990-09-26026 September 1990 LER 90-012-00:on 900827,automatic Reactor Trip Occurred During Bypass Switch Operations.Caused by Operator Error. Procedure Sp 2601D Revised to Incorporate Separate Section on Performing calibrs.W/900926 Ltr ML20028G9111990-09-18018 September 1990 LER 89-008-01:on 891002,determined That Plant Failed to Perform Functional Check of Control Board Annunciators During Channel Functional Tests.Caused by Personnel Error. Procedures Revised Re Annuciator testing.W/900918 Ltr ML20044B0441990-07-10010 July 1990 LER 90-007-00:on 900611,discovered That Surveillance Procedure 2609E Re Encl Bldg Filtration Sys Testing - Refueling Not Performed Prior to Entering Mode 4.Caused by Personnel Error.Missed Surveillance performed.W/900710 Ltr ML20044A1581990-06-18018 June 1990 LER 90-017-00:on 900518,loss of Both Trains of HPSI Occurred.Caused by Cognitive Failure by Licensed Operator. Personnel Counseled on Causes of Event & Importance of Recognizing When Event reportable.W/900618 Ltr ML20043H2021990-06-15015 June 1990 LER 90-005-00:on 900503,identified Potential for High Energy Line Break in Auxiliary Steam Sys That Could Degrade Plant Areas Determined as Mild Environs.Probably Caused by Incorrect Conclusions from Analysis in 1973.W/900615 Ltr ML20043G1031990-06-12012 June 1990 LER 90-016-00:on 900513,steam Generator B lo-lo Signal Generated Reactor Trip Signal,Causing Automatic Start of motor-driven Auxiliary Feedwater Pumps a & B.Caused by Inadequate Guidance.Procedure revised.W/900612 Ltr ML20043G3921990-06-11011 June 1990 LER 90-014-00:on 900519,manual Reactor Trip Initiated as Result of Anticipated Turbine Trip Due to Condenser Vacuum. Caused by Design Deficiency in That Traveling Screen Capacity Inadequate.Traveling Screen modified.W/900611 Ltr ML20043F7021990-06-11011 June 1990 LER 90-015-00:on 900512,feedwater Isolation Occurred While Opening Msivs.Caused by MSIV 2 Opening Faster than Other Msivs,Resulting in Swell in Steam Generator 2.Steam Generator Level Restored to normal.W/900611 Ltr ML20043F8261990-06-0707 June 1990 LER 90-006-00:on 900508,reactor Manually Tripped When Decreasing Levels Noted in Steam Generator 1 & Feedwater Regulating Valve Indicated Full Open.Caused by Valve Stem Separating from Plug.Feedwater Flow restored.W/900607 Ltr ML20043D4711990-05-30030 May 1990 LER 85-002-01:on 850302 & 25,unplanned Actuation of Containment Purge Valve Isolation Occurred.Caused by Personnel Error.Caution Signs Placed on Radiation Monitors & Reset Button on Monitor Made inaccessible.W/900530 Ltr ML20043A7841990-05-16016 May 1990 LER 90-013-00:on 900416,manual Reactor Trip Initiated Due to Imminent Loss of Condenser Vaccum.Caused by Inadequate Administrative Guidance When Debris Collected on Trash Rack. Severe Weather Procedure revised.W/900516 Ltr ML20042G7201990-05-0707 May 1990 LER 90-012-00:on 900406,review of Steam Generator Blowdown Monitor High Radiation Alarm Setpoint Revealed That Setpoint Was Nonconservative.Caused by Administrative Deficiency. Correct Setpoint installed.W/900507 Ltr ML20042E6751990-04-20020 April 1990 LER 90-002-00:on 900322,Tech Spec Action Statement 3.3.3.10 Not Entered for Out of Svc Stack Gas & Particulate Radiation Monitor.No Particulate Radiation Increases Detected.Caused by Personnel error.W/900420 Ltr ML20042E1621990-04-0909 April 1990 LER 90-009-00:on 900309,automatic Turbine Trip W/Subsequent Reactor Trip Occurred Due to High Stator Cooling Water Temp. Caused by Failure of Mechanical Linkage on Fisher & Portor Controller.Controller Replaced w/spare.W/900409 Ltr ML17223A7901990-04-0202 April 1990 LER 89-009-01:on 891025,radiation Monitor RM 8262 Inlet Valve (2-AC-82) Found Closed.Caused by Personnel Error. Isolation Valve Opened,Sample Flow Restored & Radiation Monitor Restored to Operable status.W/900402 Ltr 1994-05-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20211A6631999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level,Operating Data Rept & Unit Shutdowns & Power Reductions B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17807, Monthly Operating Rept for May 1999 for Mnps,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 1.With ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206J8351999-05-0707 May 1999 Rev 20,Change 7 to QAP-1.0, Northeast Utls QA Program (Nuqap) Tr ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 B17782, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With ML20205R3531999-04-30030 April 1999 Addendum 4 to Annual Rept, B17775, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With ML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20206E2971999-04-30030 April 1999 Rev 1 to Millstone Nuclear Power Station,Unit 2 COLR - Cycle 13 B17777, Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with ML20205Q5891999-04-0909 April 1999 Rev 20,change 6 to QAP-1.0,Northeast Utils QA Program TR ML20205R8751999-04-0909 April 1999 Provides Commission with Staff Assessment of Issues Related to Restart of Millstone Unit 2 & Staff Recommendations Re Restart Authorization for Millstone Unit 2 ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 B17747, Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With 1999-09-30
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. l NORTHEAST tmLITIES oenere' = ces saenS"eet Beran connecocut l
3 w sin 7/aIsIenYk tUE1e cC an7 P.O. BOX 270
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N[r$r*I[$InNYery a c7c*Nuany
' Northeast Nuc' ear Erggy Company e
HARTFORD, CONNECTICUT 06141-0270 (203)665-5000 l
1 July 23, 1993 MD-93-590 .
Re: 10CFR50.73(a)(2)(iv) 10CFR50.73(a)(2)(ii)(B) i l
U.S. Nuclear Regulatory Commission l Document Control Desk Washington, D.C. 20555
Reference:
Facility Operating License No. DPR-65 Docket No. 50-336 Licensee Event Report 93-012-01 Gentlemen: l l
This letter forwards an update to Licensee Event Report 93--012-01. ;
Very tru.'y yours, i NORTHEAST NUCLEAR ENERGY COMPANY FOR: Stephen E. Scace Vice President - Millstone S*ation
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BY: Harry F. ( 'i ) ne.
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Millstone UnJt 1 irector !
SES/ZH:bjo
Attachment:
LER 93-012-01 cc: T. T. Martin. Region 1 Administrator P. D. Swetland, Senior Resident inspector, Millstone Unit Nos.1, 2 and 3 G. S. Vissing, NRC Project Manager, Millstone Unit No. 2 n
s DR ADO [ ,
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NRC FO'm 360 US nucle AR REGULATORY COMM:SS10N APPROVED OMB NO 3160-0104 8 i
@ 89) E.xPtRES 4 /30/B2 Estimated bs oen per response to compty w!n te ns {
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informa1 eor coue: tion reavest . 50 C rn Forwarc a comments rer,arding buroen estimate to tne r<eco ds LICENSEE EVENT REPORT (LER) ana Reports Manager =nt e enen m-sact u s Navear Rega:atory Comm:suon Wasmngton DC 20f,55, and to tw Paperwom Recuction Prorect (3150-0104i Office et Management anc Bsapet. Aasnmgton DC 20503 f F ACILrrY NAME (t j DOCKE I NUM68 (21 CV- -
l Nidlstone Nuclear Power Stanon Unit 2 ofsiololol3l3is 1 lod 0l5 i T;TLE i4)
Turbine and Reactor Tnp Dunng N1ussel Cook (Thermal Backwash) eve NT oiTE (5 - L E A NUMPEG @ AFDOAT D ATE m OT HE A F A01UTIE S INvot vFO @
VONTF DAY VEAR VEAA y [g* MONTH DAY VEAq F ACluTY NAME5 '
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0l5 2l4 9 3 ol.3 ol1l2 ol i ol7 2 l3 9l 3 olslolofof l l OPE R/, TING T45 AEPORT 15 BEING SJOCTED PURSUANT TO THE PEQJREME NTS OF 10 CFA 6: (Cheo one or rnye c41% fonowng)(11) 20 4;2(c) 2; 402;c) V SD 73(al f21 hv) 73 71 4) pOwpp 2:: 405: a : (11 t o 60 36scir11 50 73(al(2;M 73 71gc)
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OTHEA f 5pecW m Aostract timow anc 'n e :: C5ialf t lim 50 73(alt ro 50 73la)(211vao t Ai l ext. NRC Forrn 366 A) 20 405:a!(liev N 50 73:a] Teit0 50 73!ali2i f wo Gs J 4Wat P1 t 3 SC 73(a6:2)imi 53 73f alf2) f N UCENSEE CON'ACT COA TH 9 LEP Im NAME TE LEPHONE NUMBER AREA CODi Zan Hogland. Engmeer. X 4725 2l0l3 4l4l7l-l1l7l9l1 COMPLETE ONE UNE FOR E ACM COMPDNENT F AtiUAE DE SOA BED rN TH'S REPOAT tt3) [
CAUSE S Y S T E PJ CoupONENT Th[ QMI CAUSE SYSTEM C OMPONE NT $$ ,p,Yg l l II I I I I II I I I I l i I l l I I 1 II 1 I I I SJPP .EMEV AL 8;E PO47 EXPECTED 114)
MONTH DAY YEAR suevassioN
] vE S gg ves wwete E XPEcED SUEMSStON C ATE) NO l l l ABSTRACT pm:t tc 14D0 En::es as. notommatch 5*4eq singesrace twewntter tines) (SE)
On Niav 24,1993. at 0043 hours4.976852e-4 days <br />0.0119 hours <br />7.109788e-5 weeks <br />1.63615e-5 months <br />, wnh the p! ant m N1 ode 1 at 100G power. a reactor inp occurred due to a turbine tnp. The turbine inp was caused by high generator stator cooling water temperature resulting from mussel cookmg (thermal backwash) operanons on the 'B' condenser waterbox. During the subsequent transient, a malfunction caused the 'A' feedwater regulating salve to stay at approximately 569 open which caused the #1 steam generator water lesel to increase to the high level setpomt. The reactor operator tripped the running feedwater pump bated on the high steam generator water level. Steam generator water levels were subsequently controlled usmg the auxiliar> feedwater system. Operators performed Emergency Operating Procedure 2525.
" Standard Post Tnp Acuansf All safety related equipment. wnh the exception of the mam feedwater regulating valves, responded as expected and the umt was pl3:ed in a stable condmon. Durmg the event investigauon subsequent to the inp, n was discosered that during the muuel cook, Reactor Buildmg Closed Cochng Water
( R BCCW ) temperatures momentan13 exceeded 55'F which potentially resulted in the plant bemp outside of its design b.eis. RBCCW temperatures immedmteh returned to normal.
l These everm are being reported pursuant to the requirements of Paragraph 50.73(a)(2)(iv) and Paragraph 50.73(a)(2(ii)(B) reporung any event or cond;uon that resuhed m manual or automauc actuation of any l Enpneered Safety Feature Ss stem mcluding the Reactor Protection system and to report an event or condition that potennall) resuhed m the nuclear power plant bemp in a condition outside the design basis of the plant. l NH C V orm 366 1 (649) )
I 1
FAC Fo-m 366A U.S. NvCLE AR REGLL ATORY CoMM:SSION APPROVED OMB NO 3 ' 50-O Kae r6-69i EWRE S. C30 92 Estenatec becer, per resconse to compty wetn this
'"'o"""
- 5 * * 'd LICENSEE EVENT REPORT (LER) Comme"'s rega' ding buroen est msie to the RecorCS TEXT CONTINUATION ana secons Maragemed Enncn p530L U S Nacw Regulatory Commission A a smngton Dc 20555 and to tne Paperwork Aecsctcon Project (3150-01041 Ottice et Management anc Buapet. Wasmngton DC 20503 FACIUTV NAMEqT) DoCdI NUMeER (2) !(' A NUf GF Q @ PAGE (31 VEAR mem NUWm Millstone Nuclear Power Stauon Unil -
0l5l0l0l0l3l3l6 9l3 0l1l2 0l 1 0l 2 OF 0l5 TE AT P' more scace rs 'ewee use aci tions' NRc Form 3R A si il7)
- 1. Descrmnon of Esem On May 24,1993, at 0920, with the plant at 1009 power, mussel cooking (thermal backwash) operanons on the 'B' waterbox w ere imnated. At approximately 0940 hours0.0109 days <br />0.261 hours <br />0.00155 weeks <br />3.5767e-4 months <br />, the ume hmit for elevated temperature m the 'B' waterbox was sausf ed and restoration of the waterbox was underuay.
Dunny the course of the restoranon, the elevated temperature in the 'B' circulaung water intake bay was affecung the sernce water temperature and Turbme Building Closed Cochng Water temperature. It was deterrmned that the service water mlet isolanon vahes for the Turbme Buildmg Closed Cochng Water (TBCCW) heat exchangers were restnctmg the flow and heat removal capabihues. The service water l inlet solanon valves were then opened from 30 degrees to 40 degrees open m response to elevated TBCCW temperatures.
Approximate!) 0940 hours0.0109 days <br />0.261 hours <br />0.00155 weeks <br />3.5767e-4 months <br />. a common alarm for the mam generator stator cochng cabinet was annunciated m the Control Room. A Plant Equipment Operator was dispatched to invesupate this alarm.
l The mam generator stator wmdmg inlet temperature was found to be 51 degrees Celsius, which was I abose the alarm setpomt of 47 degrees Celsius. This condmon was reported to the Shift Superusor by l the Plant Equipment Operator. When the Plant Equipment Operator returned to the mam generator l stator coolmp cabinet, the " Generator Protecuan Tnp Circuit Energized" alarm uas observed to be l
annunciated followed shortly b3 the turbine tnp. When the alarm energized, the process computer mdicated that the stator coolmg water heat exchanger outlet temperature was 75 degrees Celsius. The setpoint for the " Generator Protecuon Tnp Circu t Energized" is 81 depees Celsius.
l
! The feedwater reculatmc vahes receive a ramp close signal as part of the normal inp response. During l the subsequent transient. a malfunction caused the 'A' feedwater regulatmg valve to stay at approximately 5(M open causmg the #1 stearn generator water lesel to increase to the high level setpomt. In response to this condmon, the reactor operator closed the bypass valve and the blockmg valve for the 'A' i feedwater regulating vahes. Then the 'B' steam generator lesel went high. The 'B' feedwater regulating I valve mdicated 109 open. The bvpass vahe and the blocking vahe for the 'B' feedwater regulatmg vahes were closed. Additionally, the reactor operator tnpped the running feedwater pump based on the l high steam generator water level. Steam generator water levels were subsequently controlled usm; the auxihary feedwater system. Operators performed Emergency Operatmg Procedure 2525, " Standard Post Tnp Actions All safety related eqwpment responded as expected unh the exception of the main feedwater regulaung valves and the umt was placed in a stable condition. j l
j Durmg tha transient, the Reactor Buildmg Closed Cooling Water (RBCCW System reached a l
temperature of 9 ' degrees Fahrenhen. The maximum normal operation RBCCW discharge temperature o 85 degrees Fahrenhen when the RBCCW heat exchangers are cooled by semce water up to a ,
maximum temperature of '5 degrees Fahrenheit.
l
- 11. Q use of Twent l 1. The reactor trip was caused by a turbme trip. The root cause of the turbine inp was the lack of heat removal capabihues from the Mam Generator Stator Water Coolmg System. The warm water bemg dscharged through the 'B' circulating water pump into the 'B' intake bay was being recirculated to the 'A' and 'C' intake bay s, causing an increased sernce water temperatures. The tide nas a significant f actor in the high semte water temperature. The low mcoming tide allowed the 'B' intake bay's high temperature to cause an aggravated ef fect on the adjacent bays. Some temperature stratification m the adiacent bays has been observed on prenous mussel cooks. The low tide placed the higher temperature water at the suction of the Serace Water pumps.
1 During the mussel cooking operations, all components cooled by the TBCCW System experienced j l elevated temperatures. The Mam Generator Stator Coohng Water outlet temperature increased )
greater than the tamperature switch setpoint. 81 degrees telwus, for greater than 70 seconds which resuhed in a Turbine tnp.
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- a We Form 36f A L' s Nv0LE AR RE G.L A10RV COMM;55:ON APPAOVED Or4 NL 3150-0104 b fG E x r4RE S : 4 30'92 Estmatec bercea te recorre to comp <y w'tn tms M m a W " C& e:U m ro sest 500ms Forware LICENSEE EVENT REPORT (LER) 9 " * * * * '
TEXT CONTINUATION ""
and' Rep
'*"a'r*a"ge Y1s M 6'nent
""* t (D-630)
- ' U S. N eear Peg.f atyy Comm%ori. W asnergtor. De PD$$5 and te the I"aDEvwork Recetton Ptoie:1 ;3150.-0104). c>tf ace et Management and 6scQet, W psmnyo% DC PD533 F ACUT v NAME (1; DOCC NW8E A 2 t r =; pf u:g r.; f i PACd (3, v:- , v n m nat avism usets co m Milktone Nuclear Power Station U t-0lSl0l0l0l3l3l6 ol3 0l1l2 0l1 0l 3 OF Oj5 w o, .we i.e ee 4 , ewe: ma=e #cro-r- 3cea s ; 72 2 The root cause of the ' A' feedwater regulating valve was vibrauon which caused the valve to go mio local manual controh The 'B' feedwater regulaung valve was 109 open due to the vahe stroke being out uf cabrrauon.
- 3. The root cause of the hich RBCCW temperatures was a lack of procedural go dance to address the 65 degrees Fahrenhen RBCCW temperature hmnanon.
Ill. Anah sis of Ei. en' Then esents are being repened pursuant to the requirements of Paragraph 50.73(a)f:)(iv) and Paragraph 50. 3(a n dni(B) reportmg ans event or condition that resulted m mar:ual or automatic actuauon of any Engmeered Safety Feature System. including the Reactor Protecuon System and to repon an esent or condinon that potentially resuhed in the nuclear power plant bemy in a condition outs:de the design basis of the plant.
There were no safets consequences from this reactor inp event. All safety equipment wnh the excepuon of one of the mam leeriuater regulaung vahes. responded as expected and plani operators executed appbcable Emergenc, Operaog Procedures accordmgly. All coohng water temperatures immechately returned to their normal salues.
IV. Cerrectn e Actmn
- 1. Post inp data review idenufied that the Mam Generator Stator Cochng Water outlet temperature, as monitored by a Resistance Temperature Device (RTD), only reached a maximum of the equivalent of 75 degrees Celsius, belou us computer alarm setpoint and the inp setpomt value of 81 degrees Celuus The tnp is imuated by a separate temperature swnch. Dunng the subsequent shutdown, the Mam Generator Stator Water Coohng water outlet temperature swuch calibrauon was checked and was found to operate within allowable ranges. Addiuonauy. the stator water temperature RTD cabbranon was checked it was found acceptable. It was determmed that the clearance between the RTD and the mner diameter of thermowell was excessive. This would cause a time delay for the mdicated temperature to read the actual temperature. A thermocanducuvny hUer was mstalled m the thermowen, at.d the RTD was remstaued. The presence of this gap explained the temperature chscrepancy observed between the stator coohng outlet temperature temperature sw tch, top setpomt and the stator coohng temperature. RTD. indication recorded by the process computer.
To present recurrence of this esent, procedure enhancements have been meluded m the Service Water System and the Circulaimg Water System procedures.
- 2. The feeciwater regulaung valves hand wheek were mechanicaH3 secured to prevent the large handwheel from vibrating to the manual engagement pomt. A design chance is beine evaluated for the next refuel outact i 1
On the 'B' feedwater regulatmg sahe, a cahbration of the poquoner and the pouuon indication j circu t was performed. The vahe was stroked f rom tne Control Room to verif y the stroke and the i posinon indicator. ~1 he vahe was verified sausfactors. l
- 3. Upon muuel cook restoranon. the Sernce Water temperature decreased to its normal value. To present recurrence of this condnion procedure change. have been made to secure mussel cooking if RBCCW temperature reaches greater than 83 degrees Fahrenheit.
1 NH c i or m 3ta I 16- M ) 1
NAc Norm ?S6A U. S NUOLEAR REGULATORY COMM;SSION APPROVED OMB NO 315C-01(4 f6-89) EXPIRES- 4 /30/92 .
Estimated burden per response to compiy with tnis
at* c " ct ** '*os t 60 0 h's. For ward LICENSEE EVENT REPORT (LER) Com"ments"rega'O+ng burce" n estimate to tne ReCDros e TEXT CONTINUATION a,o Reports uanagement e anen ::-sa:n u s. Nuc. ear ,
Regulatory Comrnission. Washington DC 2055E. and to l'5p PaperwD'k Reductan Pro lect (3150-01C41. Omce of Management and Buopet W ashmoton DC 20503.
FAOUTY NAME 11) DOcn.ET NUMBER (2) MP NUMArm @ PAGE [3i YEAR N N nuem m hiillstone Nuclear Power Station Unit 2
~
0l 5l 0l 0l 0l3 l3 l6 9l3 0 l 1l 2 0l1 0l 4 OF Ol5 TEXT tti more space is rewed. use accitea NRC Form 366A s) (17)
Y. Addninnal Inf ormnion Similar LERs: None .
Ells Codes for referenced components:
+
N1ain Feedwater Reculatine Valves: SJ-FCV-C635 hiam Feedwater Regulating Bypass Valves: SJ-FCV-C635 Stator Coolmg Water Outlet Temperature Switch: TJ-TS-G054 Turbine Building Closed Cooling Water Heat Exchangers KB-HX-530S Stain Feedwater Blocking Valve: SJ-ISV-C684
+
Auxihary Feedwater Pump: B A-P- 1075
+ Niain Feedwater Pump: SJ-P-1075
=
Slam Generator Stator Cochng Water Heat Exchanger: TJ-HX-G054 hiam Generator Stator Coolmg Water RTD TJ-23-GO S4 Reactor Buildmg Closed Cooling Water Heat Exchangers CC-HX-5445 1
I l
l l
i NRC Form 366 (6-t'9) l 4
. . .. . l A orm 366A U.S NUOLEAR REGJLATORY COMM:SSiCN APPROVE O BtO $0-0104 Estimated buroen per response to comply w;tm this LICENSEE EVENT REPORT (LER) g;m*,'g',cy,qt *ng,q5l,1?on,0,l(5, ,l,"n*go, TEXT CONTINUATION and Rewr:s Management Branch 1p-630L U S. Nuc1 ear Repatory Comm ssion. Washington DO 2005E. anc to the Paperwork Recuction Pro,ect (3150-01D4) Othee of Management and Bucpet, Wasnington DO 20503 F AO!UTY NAME tij DOOKET NUVEER (2) LCD tJUMBFA #6 PAGE (3',
YEAR mcm met Millstone Nuclear Power Station Unit 2 0l5l0l0]0[3l3l6 9l3 0 l 1l 2l 0l 1 0l 5 OF 0l5 TEXT in more space is reostf ac. use accitener PJRC Form 300A s) (17)
MUSSEL COOK (THERMAL BACKWASH) LINEUP Traveling Screens Traveling Screens Traveiin;; Screens Travehng Screens O O O ;
C SW Pump B SW Pump A SW Pump D C B A DC Pump CCW ump BC Pump AC Pump !
h 12C 12D LA LA l rT r3 V Y Y !
[11E { 11F {11G {11H D Condenser C Condenser B Condenser A Concenser Wateroox Waterbox Waterbox Waterbox 12B A 12A LA k/2' r, VN y V
[11D 11C
^
2, V V V To Discharge Canal
- Throttle 11 A to maintain inlet temperature of 'B' Circulating waterbox between 110 - 120 F.
geg-maa
_ - _ _ _ _ _ _ - _ _ _ - _ _ _ _ . _ _ - .