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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:RO)
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17284A9001999-10-31031 October 1999 Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3371998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for WNP-2.W/980409 Ltr ML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B2911998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for WNP-2.W/980313 Ltr ML17284A7971998-02-17017 February 1998 Rev 28 to Operational QA Program Description, WPPSS-QA-004.With Proposed Rev 29 ML17292B3591998-02-12012 February 1998 WNP-2 Cycle 14 Reload Design Rept. 1999-09-30
[Table view] |
Text
ACCELERATED DISTRIBUTION DEMONSTRATION SYSTEM
~
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9112300333 DOC.DATE: 91/12/19 NOTARIZED: NO DOCKET FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH. NAME AUTHOR AFFILIATION BAKER,J.W. Washington Public Power Supply System SWANK,D.A. Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION'UBJECT:
LER 91-033-00:on 911120,250 volt DC bus inoperable due to lack of adequate fuse coordination. Caused by less than D adequate design analysis. Fuses replaced.W/911120 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR Q ENCL TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
g SIZE:
NOTES:
RECIPIENT COPIES . 'ECIPIENT COPIES D
ID CODE/NAME LTTR ENCL
. ID CODE/NAME LTTR ENCL PD5 LA 1 1 PD5 PD 1 1 ENG,P.L. 1 1 D INTERNAL: ACNW 2 2, ACRS 2 2 S 1'
AEOD/DOA 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DS P 2 NRR/DET/ECMB 9H 1 1 NRR/DET/EMEB 7E 1 1 NRR/DLPQ/LHFB10 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB 1 1' NRR/DREP/PRPBll 2 2 NRR/DST/SELB 8D 1 NRR/DST/SICB8H3 '1 1 NRR DSTjSPLB8D1 1 1 NRR/DST/SRXB 8E 1 1 RE FILE~- "QQ 1 1 RES/DSIR/EIB 1 1 RGN ICE M~ 1 1 EXTERNAL: EGGG BRYCE,J.H 3 3 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHY,G.A 1 1
NSIC POORE,W. 1 1 NUDOCS FULL TXT 1 1 R
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NOTE TO ALL "RIDS" RECIPIEYIS:
PLEASE HELP US TO REDUCE DIVAS fE! CONTACT THE DOCUivIEiiT CONTROL DESK, ROO'v1 P 1-37 (EXT. 20079) TO ELI!vflNATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUivlENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES .REQUIRED:- LTTR 33 ENCL 33
ai WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ "3000 George 1Vashington 1Vay ~ Richland, )Vashington 99352 December 19, 1991 G02-91-232 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555
Subject:
NUCLEAR PLANT NO. 2 LICENSEE EVENT REPORT NO.91-033
Dear Sir:
Transmitted herewith is Licensee Event Report No.91-033 for the WNP-2 Plant. This report is submitted in response to the report requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, atid action taken -to preclude recurrence.
Very truly yours,
. W. Baker WNP-2 Plant Manager JWB:ac Enclosure e:
Licensee Event Report No.91-033 cc: Mr. John B. Martin, NRC Region V Mr. C. Sorensen, NRC Resident Inspector (M/D 901A)
INPO Records Center Alanta, GA Ms. Dottie Sherman, ANI Mr. D. L. Williams, BPA (M/D 399)
NRC Resident Inspector walk over copy qg<f
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I NRC FORM366 U.S. NUCLEAR REGULATORY COMMISSION (6419) APPROVEO OMB NO. 31604)104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUESTt 60.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (F630), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, OC 20556, AND TO THE PAPERWORK REDUCTION PROJECT 13(600104). OFFICE OF MANAGEMENTANO BUDGET, WASHINGTON, DC 20603.
FACILITY NAME (1) DOCKET NUMBER (2) IIA E 3 TITLE ( ~ )
Washington Nuclear Plant Unit 2 050003971OF 250 Volt DC Bus Inoperable Due to Lack of Adequate Fuse Coordination EVENT DATE IS) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (6)
MONTH DAY YEAR g~'EOUENTIAL ~a~ REVsl~ DAY YEAR FACILITYNAMES DOCKET NUMBER($)
YEAR NUMBER rX8 NUMBER MONTH 0 5 0 0 0 112 0 9 1 9 1 03 '3 0 0 1 2 1 9 0 5 0 0 0 OPERATING THIS REPORT IS SUBMITTED PUASUANT T 0 THE REQUIREMENTS OF 10 CFR (): IChach ona or morc ot tha fotiorrinPI (Ill MODE (9) 20.402(h) 20.405(c) 50,7 3 Ial l2) I(a) 73.71(ir)
POWER 20.406 (~ ) llI (0 50.36(a)ill 50.73(al(2)(rl 73.71(c)
LFYEL I'I0) 0 0 20.405(a) 0 l(6) 50.36(cl(2l 50.73(a N2)(rill OTHER ISpacity In Ahstract "jigicppoar 'r 20.405 (a I (1 l(i(D 50.73(al(2)(I) 50.73(a) (2) (rill)(A)
Below anti In Text, HRC Form 366AI 9'. 20.406(a) IlI I Ix) 50.73( ~ )l2)(6) 60.73( ~ ) (2)(a(I(I(BI rr 20.406(al(ll(r) 60.734)(2)BII) 60.73( ~ ) I2)(a)
LICENSEE CONTACT FOR THIS LER (121 NAME TELEPHONE NUMBER AREA CODE D, A. Swank, Compliance Engineer 5 093 77- 45 1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFAC TUAER CAUSE SYSTEM COMPONENT MANUFAC TUREA (0 NPArr )ass+(.
$ (EE-SUPPLEMENTAL REPORT EXPECTED (1 ~ ) MONTH OAY YEAR EXPECTED SUB MISS 10 N DATE I'IS)
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As part of the Supply System effort to upgrade the design calculations for WNP-2, a fuse coordination calculation is being prepared for the Class lE Direct Current ('DC) power systems, including the 250 volt (250VDC) system. Development of this calculation revealed that tlie time-current minimum melting curve for the Class lE 250VDC bus battery main fuse, an 800 amp fuse, crosses over the time-current clearing curve for the downstream branch circuit fuse that supplies non-Class lE loads, a 400 amp fuse. This means that it was possible, under the postulated fault conditions, that the Class lE battery main fuse could have melted prior to the downstream branch circuit fuse clearing, isolating the 250VDC battery from the bus. Had this event occurred the 250VDC bus would have been supplied by the battery charger, but this is not considered a stable long-term condition and is not credited in the accident analyses. Because of the lack of selective coordination, the 250VDC system has been technically inoperable since the time of initial Plant startup in 1983. Operation with the 250VDC system inoperable was a condition prohibited by the Plant's Technical Specifications and is reportable pursuant to the requirements of 10CFR50.73(a)(2)(i)(B). This condition, lack of selective coordination on the 250VDC bus, was outside the design basis of .the Plant and is reportable in accordance with 10CFR50.73(a)(2)(ii).
NRC Form 366 164)9r
0 I
'P
(669)'S.
NAC FOAM 386A LICENSEE E TEXT CONTINUATION T REPORT (LER)
NUCLEAR REGULATORY COMMISSION
~
APPROVE'0 0MB NO. 31500)04 EXPIRES: 4/30/92 IMATED BURDEN PEA RESPONSE TO COMPLY WTH THIS FORMATION COLLECTION REQUEST: 50XI HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND AEPOATS MANAGEMENT BRANCH (P4)30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, ANO TO 1HE PAPERWORK REDUCTION PROJECT (31504104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, OC 20503.
FACILITY NAME I'l DOCKET NUMBER (2) LEA NUMBER (6) PAGE (3)
SEQVENTIAL Ref( REVISION NVMSEII Ng~: NVMEER Washington Nuclear Plant Uni't 2 p e p p p 9 9 1 033 0 0 0 2oF 0 5 TEXT /I/moro g>>co /I rooulod, u>> 464IE/or>>/ HRC Form 366A9/ () 2)
Because the Plant was shut down when this condition was discovered, the immediate corrective action for this event was to replace the fuses in question with new fuses that meet the selective coordination and other applicable design requirements. The root cause of this event was a less than adequate design analysis. A coordination cd culatlon was not previously performed, and resulted in selection of improper components.
For this event to have affected the Plant, a line-to-line fault would have had to occur.
'The more common line-to-ground faults are annunciated on the ungrounded 250VDC system, The loss of the 250VDC system would not, however, significantly impact the Plant since the safety-related equipment served by this bus is either not credited, in the WNP-2 design basis accident analyses, or the equipment is backed up by redundant equipment served from a different safety-related bus. Additionally, a fault would have caused the downstream fuse to blow in addition to the upstream fuse, isolating the fault and allowing Plant personnel to replace the main upstream fuse to restore the Class 1E portion of the 250VDC system to service. The main upstream fuse has a blown fuse indicator with annunciation. Therefore, this event is deemed to have minimal safety significance. This event posed no threat to the health and safety of either the public or Plant personnel.
Plant Mode 4 (Cold Shutdown)
Power Level 0%
Ev D As part of- the Supply System effort to upgrade the design calculations at WNP-2, a calculation is being performed to document fuse coordination for the Class lE busses, including the 250VDC system. This 250VDC bus is a non-redundant bus serving both Class lE and non-lE loads. The'esign criteria for the 250VDC system is described in the WNP-2 FSAR and includes a requirement to provide isolation of non-class lE equipment from Class 1E equipment using Class lE isolation devices.
Current limiting fuses are rated at two current squared times time (I2t) values; total clearing and minimum melting. These values are used for evaluating coordination in the current limiting range. The clearing I2t value is the value where the fuse interrupts current, while the minimum melting I~t value is the value where the element begins to melt. For fault currents below the current limiting range, coordination is determined by comparing the clearing time-current curve of the downstream branch fuse with the melting time-current curve of the upstream main fuse. For each fuse model and size, the clearing and melting curves and I2t values are developed by the manufacturer. The goal of the design, as described above, is to have the downstream fuse clear before the upstream fuse melts. This is commonly termed "selective fuse coordination." Two methods are considered acceptable for fuse coordination work, either the use of the manufacturer provided fuse time-current curves and I2t data, or use of the manufacturer provided fuse-coordination tables. The fuse-coordination tables from a given manufacturer provide the upstream/downstream fuse size ratio when using various models .from that manufacturer. By using the curves and I2t values, fuses from different manufacturers can be compared and utilized while maintainin ro er coordination'AC Fono368A (669)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (SJ)9) APPROVEO 0MB NO. 3)500)04 EXPIRES: 4/30/92 IMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE E T REPORT {LER) INFORMATION COLLECTION REQUEST: 60.0 HRS. FORWARD COMMFNTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31504104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON. DC 20503.
FACILITY NAME ll) DOCKET NUMBER 12) LER NUMBER (6) PAGE (3)
SEOVENTrAL NQ REVISK>N YEAR gg NVMSErr &A NVMSER Washington Nuclear Plant Unit 2 o s o o o 9 1 033 0 0 0 3oF 0 5 TEXT ///moro s/>>oo/s n /rr/ror/ rrso /r/o'oro/HRC Forrrr 366AS/ ill)
During the performance of the 250VDC bus coordination calculation it was determined that under certain extreme conditions, the clearing characteristics of the fuse serving the non-Class 1E motor control center (HCC), MC-S2-1B, were such that this fuse could fail to clear the MCC circuit prior to melting of'the 250VDC main supply fuse from the battery.
The conditions which could cause this to occur would be either a line-to-line fault of the ungrounded 250VDC bus or a fault of the backup DC-driven main turbine lube oil pump motor, with a fault'current in excess of 8500 amperes; This crossing of the clearing/melting curves for the two fuses, and an I2t clearing value for the downstream fuse that is higher than the I2t melting value of the upstream fuse, does not satisfy the WNP-2 design requirements.
I m rr v A I n The non-coordinated fuses were replaced with fuses that satisfied both the coordination and other applicable design requirements, F r h r v rr iv A Further review identified a lack of coordination existed as part of the original Plant design. Since no selective coordination calculation was previously prepared for the DC systems, it is not possible to determine why the fuses were not properly coordinated. The root cause for this event was a'ess than adequate- design analysis since no DC system coordination calculation had ever been performed, which resulted in the selection of improper components.
The DC coordination calculation has not been completed. Sufficient work has been completed, however, for Supply System Engineering to conclude that the remainder of the Plant DC systems meet the sel'.ective coordination requirements.
The lack of fuse coordination between safety-related and non-safety-related loads on the 250VDC system 'resulted in the system being technically inoperable since in.itial Plant startup in 1983. This is a condition prohibited by the WNP-2 Technical Specifications and is therefore reportable pursuant to the requirements of 10CFR50.73(a)(2)(i)(B). This condition, lack of selective'coordination on the 250VDC bus, was outside the design basis of the Plant and is reportable in accordance with 10CFR50.73(a)(2)(ii).
There were no structures, systems, 'or components inoperable prior to the start of this event that contributed to the event.
A i n Supply System Engineering will.complete the DC fuse coordination calculation that uncovered this problem, This calculation will include an analysis of the Class lE DC busses to document the required coordination.
NRC Form 366A (649)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION 164)9) APPROVEO 0MB NO. 31604104 EXPIRES: 4/30/92 LICENSEE E IMATED BURDEN PER RESPONSE TO COMPLY WTH THIS T REPORT (LER) INFORMATION COLLECTION REQUEST: 60.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH IP630), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT 131504104), OFFICE OF MANAGEMENTAND BUDGET. WASHINGTON. OC 20503.
FACILITY NAME 11) DOCKET NUMBER 12)
LER NUMBER ISI PAGE 13)
YEAR '.hM SEQUENTIAI, PN REVOION NUMEER >re'< NUM ER Hashington Nuclear Plant TEXT ///more 4/roce JI )er/reer/, Iree Unit 2
//r/ooe/HRC %%dnrr JSSA'4/ lll) osooo3 9 1 033 0 0 0 4 OF 0 5 r
A formal root cause analysis is currently being prepared to address this event. This analysis will explore the programmatic aspects of this event to determine if the processes in place today require modification.
In order for the lack of fuse coordination to have affected the Plant, numerous failures woul'd have had to'occur. A line-to-line fault in the non-Class lE portion of the 250VDC system would have had to occur. The 250VDC system is an ungrounded system and alarms on the occurrence of a ground. This alarm would have provided the opportunity to locate and isolate the ground, reducing the probability for a line-to-line fault. The only component which could have faulted and taken out the main bus fuse is the backup main turbine lube-oil pump. This pump is normally only used in a loss of off-si te power event when the main turbine shaft-driven lube oil pump and the non-safety-related AC-driven backup oil pump are not available.
Loss of the 250VDC battery would result, in the safety-related battery charger supplying the loads. The chargers are not designed to carry the design basis loads without the battery in service. The chargers have proven stable, however, when the Plant is shut down and the 250VDC system is not required to be operable, and the battery is taken out of service for maintenance, The battery charger is designed to serve the safety-related loads while recharging the battery in 24-hours from its discharged state.
A significant event at the Plant would have had to occur in the same time frame as the loss of the 250VOC bus which resulted in the need for the safety-related equipment supplied by the 250VDC bus. A review of the safety-related loads supplied from the 250VDC bus revealed that they are'ot credited for the prevention or mitigation of the required design-basis .accidents, or that the components serve a redundant function to components supplied from a different Class lE bus. The following is a description of the safety-related equipment that would be unavailable due to a loss of the 250VDC bus.
- 1. Numerous Reactor Core Isolation Cooling (RCIC) components would be unavailable on loss of the 250VOC system, causing the system to be unavailable. RCIC can provide high pressure injection just as the High Pressure Core Spray (HPCS) system can..
HPCS, a safety-related, diesel backed high pressure injection source, is not affected by this postulated event. In addition, three of the RCIC valves supplied from the 250VDC bus provide a containment isolation function that is backed up by a check valve providing the same function.
E 2'. Residual'Heat Removal (RHR) RHR-V-8, Shutdown Cooling Suction Isolation Valve.
Shutdown Cooling is not required to prevent or mitigate. the consequences of an accident. Normally closed Residual Heat Removal (RHR) valve RHR-V-23, Reactor Head Spray Isolation Valve. The isolation function for this line is al,so accomplished by check valve RHR-V-19. The Reactor Head Spray and Shutdown Cooling functions of RHR are not credited in design-basis accident analyses. The Low Pressure Core Injection and Suppression Pool Cooling functions of RHR are not affected by the loss of RHR-V-23 and RHR-V.-S.
NRC Form 366A (64)9)
NRC FORM 36SA (SJ)9) '
LICENSEE E TEXT CONTINUATION S. NUCLEAR REGULATORY COMMISSION REPORT (LER) l APPROVED OMB NO. 3)600)OE EXPIRES: E/30/92 MATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST: 60.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P630), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31604104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (11 DOCKET NUMBER Il) LER NUMBER (5) PAGE (3)
SEOUENTIAL 1I)g REVISION NUMBER ~g NUMSER Hashington Nuclear Plant Unit 2 p p p p p 3 9 7 9 1 033 0 0 5 OF TEXT //fmoro opoco /E /I//rior/ Iroo aAAbnd HRC Rorrn 366A3/ l(7)
- 3. Reactor Hater Cleanup (RHCU) valve RHCU-V-4, an outside containment isolation valve.
Containment isolation is also provided by inside containment isolation valve RHCU-V-1 which is powered from a different Class 1 source. The reactor water cleanup function is not required for accident prevention or mitigation.
The loss of the 250VDC bus due to a fault in the non-Class lE portion of the system is considered a very low probability event. Had the postulated loss of the 250VDC system occurred, however, redundant equipment is available for the prevention and mitigation of the design basis accidents. Additionally, Plant personnel could have rapidly restored the Class 1 portion of the 250VDC system to service by replacing the battery main fuse.
Therefore, this event is deemed to have had minimal safety significance.
r~l HNP-2 Licensee Event Report (LER)84-048 reported a problem with improper fuse application on the 250VDC NCCs. The manufacturer recommended that the a new fuse type be used, rated at 600V instead of 250V, to provide an acceptable level of protection for the 250VDC HCCs. The corrective action for that LER was the replacement of the identified fuses with fuses rated at 600V instead of 250V. The downstream fuse in this event'as changed out as part of the corrective action for LER 84-048, and resulted in improved coordination.
5mtem Camuunmi 250 Volt DC EI FU'D Hain Turbine Lube Oil P Reactor Core Isolation Cooling BN High Pressure Core Spray BG Residual Heat Removal BO ISV Reactor Hater Clean Up CE ISV NRC Form 366A (689)
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