ML19241B772

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LER 79-029/03X-1 on 790602:during Insp Per IE Bulletin 79-07,snubbers in Core to Spray Vessel,Recirculation Pump Suction & Main Steam Line Discovered Inoperable.Caused by Low Fluid Level.Snubbers Aligned & Clamps Tightened
ML19241B772
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 07/18/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19241B756 List:
References
LER-79-029-03X, LER-79-29-3X, NUDOCS 7907230618
Download: ML19241B772 (2)


Text

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DATE 80 8 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES O'o o 2 lWhile performing an inspection of pipe supports and hangers in accordance with IE J o 3 l Bulletin 79-07, the following snubbers were found inoperable: 1) 2E21-3SS48, Core j o 4 l Spray to vessel; 2) 2B32-SSB9B, 2B Recire. pump suction; 3) 2W N-B3SS46, main steam I o s , lin e " B" ; 4) 2C41-12SS98, RHR to fuel pool cooling: 5) 2PS-3613, instrumentation top. ]

o 6 l Technical Specification 3.7.5, 6.9.1.9_.b I 0 i e 4 I I

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_ 21 22 23 24 .6 27 23 29 30 31 32 ACTION GUTURE EFFECT SHUTDOWN A TT AC HV E N T NP R O-4 PRIME C,OMP. CCMPONENT TAKEN ACTION CN PL ANT *tETHOD HOURS SU B MI TT E D FORY WB. SU PP LI E R VANUFACTURER 34 h 36 7 O O l0 O l Vl l l9 l? 0 Q l 3/ 40 41 42 43 44 47

~CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 1 o l 2B32-SSB9B, 2PSN-B3SS46, and 2PS-3613 had low fluid level due to seal leakage. These l y g [were rebuilt, functionally tested, and returned to service. 2G41 '2SS98 had a loose t

[ pipe clamp. The snubber was aligned and the clamp tightened per procedure. 2E 21- j l3SS/Q was found missing. This snubber was immediately replaced. This snubber was l 1 4 I removed and rebuilt during the performance of the drywell visurl inspection, (CON'T) l 3 3 80 TA S  % POWER OTHER STA TUS IS OV RY OlSCO"ERV CESCRiPTION 1 5 [fjh l 0 l 0 l 0 l@l NA l l Clg; tianger Inspection l ACTIVITY CC TENT DELEASED CF RELE ASE .MCUNT CF ACTIVITY LOCATION OF RELEASE i 6 NA 4 9 lZl@ to Z l@l NA l l l 11 44 45 80 PERSONNEL EXPOSURES NLY9ER TvaE D E SCRIP TIO N i NA 7

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12 13 30 PERSONNE L INJUR'ES

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/ 4 9 11 12 80 LOSS OF OR D AMAGE TO FACILITY

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LFR CONTINUATION -- RO# 2-79-029 Facility: BSEP Unit No. 2 Eveat Date: 6-2-79 PT 19.6.0.1, during the 1979 refueling outage. The snubber was to have been installed by contract auintenance personnel who were shown the proper location for reinstallation. They failed to install the snubber. Management personnel of that contract maintenance company have been informed of the seriousness of this job omission. This has also been reviewed by plent maintenance fereman and will be reviewed by all mechanics. Testing of snt.bbers will contum _ per Technical Specifications. Maintenance procedures are being revised suct that when a snubber is removed for mainterance, it will be verified reinstalled and operable.

467 320

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