ML19274D150

From kanterella
Revision as of 17:48, 1 February 2020 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 78-076/03L-0 on 781202:during Routine Check Noted That Recorder for Chloride Intrusion Monitor Channel CO-CIS-3075- 1 Was Not Indicating.Cause Not Determined at This Time,Will Be Investigated During Next Condensate Sys Outage
ML19274D150
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 01/05/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19274D145 List:
References
LER-78-076-03L, LER-78-76-3L, NUDOCS 7901150103
Download: ML19274D150 (1)


Text

stetvtN HEF i y CONTROL BLOCK: l

, I l l l l lh t)

(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIOM

!0 1 NlC BlElP 2 @l0l0l-l0 0 0 0 l0 -

0 l 0 23l@lsti4 1LICENSE l 1 l1T YPE l 1JJl@lb7 l @

7 8 9 LICENSW COJE a 14 15 LICENSE NUMbEH CAIb8 CON'T 0 1 8

5[R[C tol L l@l61 0 l 5 l 0 l - l 0 l 3 l 2 468l@l6)1 l 2EVENT 2 7 l 874 l@l0 l 0 l DATE 75 l1REPORT l0 l DATE 5 l 7 l980 @

l DOCAET NUMBER EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h o 2 l During a routine panel check on 12/2/78, the Control Operator noticed that the recor- 1 o 3 der for chloride intrusion monitor channel CO-CIS-3075-1 (Condensate Pump Discharge)  !

o .: lwas not indicating. Further investigation revealed that the detector was malfunction-l o 5 ling. Technical Specification 3.3.5.6.

IO 6 l l 0 7 l i-~iT1 I _l

/ 8 9 80 SYSTEY CAUSE CAUSE C OY P. VALVE CCOE CODE SUSCOCE CCYPONENT CODE SUBcCDE SUBCCCE J

o 9 8

l 11 l 11 l @ l E l@ l Xl @ lI lN l Sl Tl Rl Ul@

9 10 11 12 13 18 19 Rl@ 2U zl@

._ SE OJE NT! AL CCCURAENCE REPORT REVISION LE A AO EVENT YEI.R H E PCHT No. CCDE TYPE h. C .

@ gEP, l 7l 8l _l l0 7 l6 l l/l l0l3l lLl 30

_l l0l 32

_ 21 22 23 24 iG 21 2d 23 31 ACTION FJTuaE EFFECT SHUTDOa v ATT AC H V E N T N P R O.4 PRIVE cOVP. COMPONENT TAKEN ACTION ON PLANT U E T H r.,D HOURS o SUBY1TTED FORMbVB. SUPPLI E R MANUFACTURER Iz JJ l@lc l@L.

I35 z l@ Iz l@

., o al l o 10 10 lo l 40 I nl@

41 42 xl@ l43A l@ lLl1l3lol@

44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i o l Since the condensate system must be out of service to remove the detector. it will be1 1 i l removed during the next condensate system o'itace . The mode of failure vill be invoe I

, , j tigated at that time and the need for any further corrective action determined. [

}1 3 l A I I ii 7 8 9 80 ST 5 *,PC/v E H OTHER STATUS ISC V FY DISCOVERY DESCRIPTION

i 5 W@ l0 l6 l7 lQ N l B l@l Operator observation l A TiVITY CONTENT one AsE D Cm u AsE uOuNT OF ACTiviTv @ LOCATION OF RHEASE @

i e I z I @ Iz l@l NA l NA l

/ 8 9 l ') 11 44 45 80 F E ASON NE L E X POSUHE.S N UY d E ri TYFE C E SC FD P TI ON li 7 10l0 Oj @ l z @ l NA l 7 8 9 11 12 13 80 PERSONNEL INJUHtES NUYBE R DESCRIPTION 1

i a 8 9 0l0l0l@l 11 12 NA 80 l

LOSS CF CR DAYAGE TO FACILITY TvPE DE SL R:PTION 1 9 lz NA l PUBLt TV NRC USE ONLY

  • 4 %; E D NA 2 o I Z lhlDESCRIPTI JN l 68 69 llllllllll l l'l }

80 5

/ a 9 to

~

NAYE OF PREPARER PHONE: