ML19296A954

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Monthly Operating Rept for Jan 1980
ML19296A954
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 01/31/1980
From: Roden J
GEORGIA POWER CO.
To:
Shared Package
ML19296A952 List:
References
NUDOCS 8002190521
Download: ML19296A954 (6)


Text

4 OPERATING DATA REPORT DOCKETNO ._

DiTE (- _

CO31PLETED BY >

TELEFliONE : -~ __

OPERATING STATUS i

Hatch 2 Notes

1. Unir Nsme:
2. Reporting Period: January 1980
3. Licensed Thermal Power (NIWt): 2436 MWt

-4. Nameplate Rating (Gross NIWe): - 817.0 Gross MWe ,

5. Design Electrical Rating (Net 31We): 784.0 flet MWe ,
6. 51aximum Dependable Capacity (Gross 51We): 805.7 Gross MWe

~

Slaximum Dependable Capacity (Net 51We): 772.7 fiet MWe ,

S. If Changes Occur in Capacity Ratings (!! ems Number 3 Through 7) Since Last Report. Give Reasons:

ch,ncad flat M0r from 740 to 772.7 to reflect new utility --- '_

9. Power Level To hhich Restricted. If Any (Net S!We):
10. Reasons For Restrictions,if Any:

This 51onth Yr..t o.Da t e Cumum:.

I1. Hours In Reporting Period 744 744 357-

12. Number Of Hours Reactor Was Criticai 684.1 684.1 33a7 n
13. Reactor Reserve Shutdown Hours 0.0 0.0
14. Hours Generator on-Line 661.2 661.2 30;
15. Unit Resene Shutdown Hours 0.0 0.0
16. Gross Thermal Energy Generated (51WH) 1471890 1471890 696595:
17. Gross Electrical Energy Generated ('.1WH) 49.9_79._0_ _ _, 499790 233575G -

IS. Net Electrieal Energy Generated (.'.tWH) 478796 478796 22359 "

19. Unit Senice Factor 88.9 88.9 . .. . . n
20. Unit Availability Factor 88.9 88.9 0
21. Unit Capacity Factor (Using SIDC Net) 83.3 83.3 i
22. Unit Capacity Factor (Using DER Net) 82.I 82.1 7: -
23. Unit Forced Outage Rate 0.0 0.0
24. Shutdowns Scheduled Oser Next 6.\1onths (Type. Date,and Duration of Each):

Vont Headpr naflector and Surveillanca Outage. March 1 to Aoril 13

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation): Forecast Achiewu INITIA L CRITICALITY INITl4 L ELECTRICITY Coil %1ERCI A L OPERATION 8002.I9Og

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. Y-UNIT "!_ _.

D \TE 2.

C05tPLETED BY U- ~~ '"

TELEPflONE 9IA - -

510NTil January DAY AVERAGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEV:L (Niwe-Net) (51We-Net :

1 800 17 792 2 800 is 789 3 801 i9 662 4 800 :o 786 5 77a 796 21 .

6 774 22 796 7 799 23 799 8 795 24 801 9 793 25 771 10 796 26 15 11 789 27 -7

440 23 -7 i3 680 29 29 i4 787 3o 204 15 794 3 507 16 795 INSTRUCTIONS On this format,!ist the average daily unit power leselin NIWe Net for each day in the reporting month. C the nearest whole megawatt.

s DOCKET NO. 50-366 UNIT S!!UIDOWNS AND POWER REDt!CllONS UNIT NAME liat cli 2 DA TE 2-10-80 COMPLE IED HY J. Lt. Rodtn REPORT MON Ill January 1 EkJPilONE 912-167-7781

i _

"o .3 h k 3Ct'n5CL* C 'F, E, CJu$c & Correttive No. 1)2tc g g g jgy Evciti a7 g7 Ati,on i,,

$3 5 ~5j Report

  • NU h' Psesent Recurreine u

Q 80-01 800111 S 0 li 4 flA ZZ C0flROD Reduction in power to perfonn turb-ine test and rod sequence exchange 80-02 800126 S 81.4 0 1 flA SA ZZZZZZ Shutdown to perfonn primary contain-ment isolation modifications ,

80-03 800129 S 01.4 B 4 flA ZZ TURBill Unit was brough off 1ine to perform turbine over. testing Oo do A

F: I onced Reason:

Method:

INintur G Instinitions y

S: Sulied uled A 1:iguipment Failure (laplain) 1. Manual fo 1 s ep.n .uion i, li o i Ital.iinteiunte on' fest J Ma n u il .';. i .n. . I niiy n!,, .:s i.o ,,i.

f-lkl u elt.y i A ni. i, .i: '

. ' . I 1: , 6.r (I i r. I 1. e.

( > :i 3ilo.r 15 i . . i i. . :i , i

!-)  : a is 'i t :i 4,4 C; i i. .I. ,E i t ; ,, , ,

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NARRATIVE REPORT UNIT 2 January 11th Reduction started for turbine test

sequence exchange January 25th Shutdown started *or TMI connitmen . . . _ _ .

Containment Isclation logic)

January 26th Generator off line 03: 43 CST January 29th Generator on line 13:06 CST Generator off line 19:50 CST for turbine tertin:

Generator on line 21:14 January 30th Reduction due to PCIOMR, CMPF There was no single release of radioactivity or single -

exoosure which accounts for more than 10% of the allowab'.

values during January of 1Q80.

k 6

N D h 9 b S

o sh 5

HATCH 2 SAFETY-RELATED MAINTENANCE REQUESTS TO BE REPORTED FOR OCTOBER 1979 NUMBER DATE COMPLETED DESCRTPTION 79-5c26 1 7-80 Reoaired stanr:- '

service water pum: -

79-5478 1-24-80 Mounted and - "

protection breaker na,- -

79-5513 12-23 79 Performed PM on  ?'" -

79-5203 1-8-80 Repaired "A" RHR S' -

79-3423 1-8-80 Repaired reactor -n-"'

control system 79-5990 1-8-80 Repaired rod bico "B"

79-5957 1-7-80 Replaced PSW 3+-

guage 79-5732 1-3-80 Tightened core s o .-

, bolts 79-4086 1-9-80 Adjusted recirc n high soeed stops 79-6004 1-2-80 Replaced bolts on -

PSW pumps 79-5948 1-4-80 Replaced inverter discharge flow india-79-5752 1-2-80 Repaired coupling an B.W. rec. tank tran e - --

79-3044 12-3-79 Installed filter circumes on reactor manual relays 79-3338 1-28-80 Inspected RPS M-G s-- v' ~

distribution panel . --w' for missing insulate.-

80-271 1-29-80 Visually inspected held devices in dr" found all to be acca-g

80-376 1-30-80 Repaired motor on .

main steam line draic 0'342 31.gg Nemov,4 then ' ' ' ~

  • e*"Us ,g
  • 00'371 28~80 Repy**ed t 0 :.
    • c o nl*'o 1 st y

.