ML19354C386

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LER 80-037/03L-0:on 801025,during Routine Surveillance, Bistable Setpoint That Instates Channel D Local Power Density & Loss of Turbine Trips Found Above Required Setpoint.Caused by Normal Bistable Drift.Bistable Recalibr
ML19354C386
Person / Time
Site: Millstone Dominion icon.png
Issue date: 11/24/1980
From: Clement C
NORTHEAST NUCLEAR ENERGY CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19345B802 List:
References
LER-80-037-03L, LER-80-37-3L, NUDOCS 8012020535
Download: ML19354C386 (1)


Text

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O'RUiLl@l 0151010101313 ls J@l1 60 61 COCKET NU?.*S ER 68 69 EVENTInDATE12 k lain l@li l i 1714 l a in l@

74 75 REPCRT D ATE 80 EVENT DESCRIPTION ANo PROB ABLE CONSEouENCES h l o 121 l During routine surveillance of the reactor orotection system. tha hittible cornnin+

o 33 j l that instates Channel D local power density and loss of turbine trios *was found above i I o 1.s i I the required setpoint. The LPD and loss of turbine trips are recuired to be insta+ad _]

o isi I above 15 percent power per Table 3.3-1 (Note C) and Table 2.2-1 (Note C) of the l l0 Js j ; Technical Specifications. The plant was operated within Technical Soecification Table 1 j o l7] l 3.3-1, Action Statement 2. There have been no similar events. I I

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33 34 35 CAUSE DESCRIPTION ANo CCRRECTIVE ACTIC,iJS h tija]l During a calibration, the bistable setooint had been left at the hiah limit allo ilyJ 3,,,ji the surveillance procedure; thus, the apparent cause is nomal bistable drift. Tha I

, , , , , , bistable was recalibrated and restored to service. Technicians have been cautionad to l leave these setpoints at mid-range of allowed band. The bistable is a Gulf l f i l 31 l

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i 7 8 9 OTHER STATUS 015 O RY 0:5COVERY OESCRIPTION 5A '6PCWER NA l lBl@l Routine Surveillance l I1 I s l lE l@ l019 16 l@l ACTIVITY CC TENT LOCATION CF RELEASE

  1. ELEASE AMOUNT OF ACTIVITY NA l l t I *6*l l Z l @D
  1. ' CP RELEASE NA lZl@l"l l PERseNNEL ExPCsuREs NuuSEn TYPE CEsCRiPTiou @ l I t 171 l 0101 Ol@lZj@l NA PERSONNEL iNrlRiEs NUMBER C ESCRiPTION I

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, , , o , 7Tr@f"'"'"' ~ N4 8012 o e 05%. i i , i i i i i i i i i i ii 68 69 - go. ;

Car Clement PHONE: (203) 447-1791 (X572) {

NA?.tE oF PREPARER