ML19296D354

From kanterella
Revision as of 03:20, 8 November 2019 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
Updated LER 79-030/03X-2:on 791121,during Walkdown Insp Per IE Bulletins 79-14 & 79-02,two Snubbers Found Incorrectly Installed & One Hanger Found Damaged.Cause Not Stated. Repairs Have Been Made & All Devices Are Operable
ML19296D354
Person / Time
Site: Prairie Island Xcel Energy icon.png
Issue date: 02/26/1980
From: Hunstad A
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19296D353 List:
References
IEB-79-02, IEB-79-14, IEB-79-2, LER-79-030-03X, LER-79-30-3X, NUDOCS 8003030580
Download: ML19296D354 (1)


Text

NMbrunMJCO (7-771 UPDATE REPORT LICENSEE EVENT REPORT PREVIOUS REPORT DATE 01-30-80 CONTROL BLOCK: l 1

l l l l 6

lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI l o l t8 l9 l M !LICENSEE 7

N l PCODE l I l N 14l 1 l@l 15 0 l 0 l - l LICENSE 0 l 0 NUMBEHl 0 l 0 l 0l -l 0 l 250 l@l 26 4 LICENSE l 1 l 1Tvl1l1l@l PE h bl LATb8 l@

CON'T

"

0 i 1 8 5$nN 60l L hl 061 l 5 l 0DOCK l 0 ETl NUMB 0 l zE Rl 8 l 2 68@l 691 l 1 EVENT 1 l 7 l 9 l@ 0 l 2REPOR1 12 l DATE 74 75 2 l 6 l 8 l 080 l@

D ATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 l During walkdown inspection dictated by IE Bulletin 79-14 and 79-02, two snubbers in 1 o 3 l the Cooling Nater System were found incorrectly installed and one hanger in the I o 4 l Auxiliary Feedwater System was found damaged. One hanger each in the Cooling Water,j loisl I Component Cooling Water, Reactor Coolant and Chemical and Volume Control Systems was l 0 6 Ifound to have inadequate safety factor. No effect on public health and safety. Tech.l O 7 l Spec. 3.12 applies. I o s l 7 8 9 80 SYSTEM CA US E CAUSE COVP. VALVE CODE CODE SU8 CODE COMPONENT CODE SU6 CODE SU8COQE 7

O 9 8

lWlAl@ W @ lCl@ S lU lP l0 lR lT l@ {@ ]@

9 10 11 12 13 18 19 20

_ SE QUE N TI AL OCCURPENCE REPORT REVISION LERHO [ VENT YE AR REPORT NO. CODE TYPE NO.

h RE$RTsU l7 l9 l 21 22 l-l 23 l 0l3 0l 24 26 l/

27 l0 l3 28 29 W30 l-l 31

@

32 T EN A O ON PLANT TH HOURS 22 SS8 MITT o FOR Un. SUPPLIE MAN FACT REH l33B l@l34 Z l@ WQ 35 lZ 36 l@ l0 l0 0l0 31 40 W@

41 lY 42 l@ l43A l@ lZl9 9l9l@

44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i o l Repairs have been made. All seven devices are operable. Inspection is continuinn. I li lil i i i > l 1 i illi i l i 4 l 1 7 8 9 80 STA S  % POWER OTHEH STA TUS S OV HY DISCOVERY DESCRIPTION l1 15 I [_Ej@ l0 l 6 l 5 l@ N/A l l C l@l Inspection per IE Bulletins ACTIVITY CON TE N T RE LE ASE . OF RE LE ASE AVOUNT OF ACTIVITY LOC ATION OF RE LE ASE l1 IGH 9I W @ [Z_j@l NA l l NA l 1 10 11 44 45 F,a PERSONNEL EMPOSURES NUMBE R TYPE D E SC RIP TION

[' i l i "l l' 0 [ 0 l 0 'l@l Z l@l NA l PE RSON~E'L ,NJUU,ES

" "

NouRER DESCniPTiON@

NA l i l aHl 9l 0 l 0 l 0 l@l12

  1. 11 I

80 LOSS OF OR DAVACE TO FACILITY TYPE DESCRIPTION i 9 (Zj@l NA l

7 8 'l to 80 PUBLICITV i DESCRtPTION NHC USL ONL Y rryT)[SSUEDNjgl NA l l llllllll ll 7 8 9 10 68 69 80 k NAME OF PREPARER

  • ^* ~

-

8 PH7)N E-oaoao