ML19254E850

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LER 79-068/03X-1:on 790910,downscale Alarm for Average Power Range Monitor F Actuated at Less than Required Percentage. Caused by Monitor Instrument Drift.Monitor Will Be Replaced
ML19254E850
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 10/30/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19254E847 List:
References
LER-79-068-03X, LER-79-68-3X, NUDOCS 7911020401
Download: ML19254E850 (1)


Text

NRc FORM 366 . . LA R COMMI I (7 7J) C LICENSEE EVENT REPORT CONTROL BLOCK: l 1

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l B l ECODE l P l 214l@l150 0 l- l 0 l0 l O! 0l 0l - O!0l@l4l1l1 LICENSE NUMBER 25 26 1l 1 @!57 CAT LICENSE TYPE 40 l l@

58 CON'T o 1 7,"CT lLl@l0 5 l0 l- l0 3 2 1468l@l690 l 9 EVENT 1 DATE l0 7l9 @h l0l3l0 7l9 g 74 75 REPORT DATE 80 7 8 60 61 DOCKET NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h

['O 2 While performing PT 1.2.4. APRM High Fluv and Downsenle Teme. the dnuneenle ntnr, fnr O 3 l APRM "F" actuated at 27. vice the required h 37 . APRM "B" was also out of service due!

O 4 lto a detector open signal lead. I R l Technical Specification 3.3.1, 6.9.1.9a l LO_LJ l l O 7 l l 0 8  !

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33 35 36 40 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 1 O APRM "F" was out of calibration due to instrument drif t. The instrument was recali- l 1 1 lbrated and returned to service satisfactorily. APRM "B" will be reolaced durine che l i 7 lnext outage of sufficient length. As this is the first APRM calibration problem. this g lis considered an isolated event and no further action is required. l i 4 1 7 8 9 80 ST  % POWER OTHER STATUS DISCO RY DISCOVERY DESCRIPTION iTTsl U@ l o I 815 l@l NA l l B l@l Periodic Test l A TlVITY CO TENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE y y 8@

7 9 l Z l@l NA 10 11 44 l NA 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION i 7 l 0 l 0 l 0 l@l Zl@l NA _

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PERSONNE L IN;uWiES 125;? O52 NUV8ER DESCRIPTION i s l 7 8 9 l 0 l 0 l 0 l@] NA 11 12 80 l

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