ENS 40349
ENS Event | |
---|---|
05:53 Nov 22, 2003 | |
Title | Valid Actuation of the "a" Emergency Diesel Generator During Testing |
Event Description | The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73.
On November 21, 2003, at approximately 22:53 Mountain Standard Time, Palo Verde Nuclear Generating Station Unit 2 experienced a valid actuation (start) of the 'A' Emergency Diesel Generator (EDG). Unit 2 had been performing testing of the capability to parallel the EDG 'A' with the Gas Turbine Generator #1 (alternate AC Power source for station blackout.) The Train 'A' 4.16 Kv bus had been successfully transferred to the EDG and loads carried by the EDG for approximately 5 minutes. When the EDG speed control was taken from 'droop' mode (load sharing) to 'isochronous' mode (fixed frequency,) the EDG output breaker tripped opened, resulting in a valid Loss of Power (LOP) signal based on undervoltage on the Train 'A' bus. The EDG resupplied the bus in the LOP mode. Offsite power remained available to both safety buses throughout the event. The other (Train 'B') safety bus is being supplied by offsite power and its EDG is operable. The offsite electrical grid is stable. Palo Verde Unit 2 is shutdown and defueled in its 11th refueling outage. No other ESF actuations occurred and none were required. There were no structures, systems, or components that were inoperable at the time of discovery that contributed to this condition. There were no failures that rendered a train of a safety system inoperable and no failures of components with multiple functions were involved. The event did not result in the release of radioactivity to the environment and did not adversely affect the safe operation of the plant or health and safety of the public. Troubleshooting will be conducted to determine the cause of the EDG output breaker opening. The licensee has notified the NRC Resident Inspector. |
Where | |
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Palo Verde Arizona (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000529/LER-2003-002 |
Time - Person (Reporting Time:+-1.38 h-0.0575 days <br />-0.00821 weeks <br />-0.00189 months <br />) | |
Opened: | John Gunn 04:30 Nov 22, 2003 |
NRC Officer: | Gerry Waig |
Last Updated: | Nov 22, 2003 |
40349 - NRC Website
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WEEKMONTHYEARENS 570472024-03-24T23:34:00024 March 2024 23:34:00
[Table view]10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Specified System Actuations of Unit 2 Train B Emergency Diesel Generator and Train B Auxiliary Feedwater ENS 565512023-06-02T11:05:0002 June 2023 11:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 564592023-04-09T04:44:0009 April 2023 04:44:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Reactor Coolant Pumps ENS 560442022-08-15T00:02:00015 August 2022 00:02:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuations of Unit 1 and Unit 3 Emergency Diesel Generators and Unit 1 Auxiliary Feedwater Pump ENS 558782022-05-05T02:55:0005 May 2022 02:55:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuation of Unit 2 and Unit 3 Emergency Diesel Generators and Unit 3 Auxiliary Feedwater Pump ENS 555342021-10-20T21:46:00020 October 2021 21:46:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Specified System Actuations of Unit 1 and Unit 3 Emergency Diesel Generators ENS 542242019-08-16T15:21:00016 August 2019 15:21:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip ENS 534772018-06-27T07:00:00027 June 2018 07:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Low Steam Generator Water Level ENS 466332011-02-22T03:01:00022 February 2011 03:01:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Auto Start and Load of Edgs on Units 1&3 Following Loss of Start-Up Transformer ENS 465562011-01-20T01:41:00020 January 2011 01:41:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Main Feedwater Pump Trip ENS 429382006-10-27T06:53:00027 October 2006 06:53:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Power to the Unit 1 and Unit 3 Train B Safety Buses with Emergency Diesel Generator Actuation ENS 426092006-05-30T15:13:00030 May 2006 15:13:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Power to Train "a" 4 Kv Safety Bus ENS 425592006-05-06T23:35:0006 May 2006 23:35:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuation of Emergency Diesel Generator Due to Low Voltage Condition ENS 424682006-04-03T03:54:0003 April 2006 03:54:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Trip During Testing ENS 413792005-02-07T05:19:0007 February 2005 05:19:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Start Due to Bus Deenergization ENS 413042004-12-31T17:42:00031 December 2004 17:42:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Plant Had Auto Start and Loading of Two Emergency Diesel Gererators ENS 408162004-06-14T14:44:00014 June 2004 14:44:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Due to Reactor Trip Due to Loss of Off Site Power ENS 408152004-06-14T14:44:00014 June 2004 14:44:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Reactor Trip Due to Loss of Off Site Power ENS 408142004-06-14T14:44:00014 June 2004 14:44:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Alert Declared - Reactor Trip Due to Loss of Off Site Power ENS 403492003-11-22T05:53:00022 November 2003 05:53:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuation of the "a" Emergency Diesel Generator During Testing 2024-03-24T23:34:00 | |