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{{#Wiki_filter:ACCELERANT DOCUMENT DIST VTION SYSTEM REGULAT Y INFORMATION DISTRIBUTIO SYSTEM (RIDS)'ACCESSION NBR:9303050185 DOC.DATE: 93/02/26 NOTARIZED:
{{#Wiki_filter:ACCELERANT                 DOCUMENT DIST                         VTION SYSTEM REGULAT     Y   INFORMATION DISTRIBUTIO             SYSTEM (RIDS)
NO FACIL:50-389 St.Lucie Plant, Unit 2, Florida Power&Light Co.AUTH.NAME AUTHOR.AFFILIATION HURCHALLA,J.A.
'ACCESSION NBR:9303050185             DOC.DATE:   93/02/26     NOTARIZED: NO           DOCKET FACIL:50-389 St. Lucie Plant, Unit 2, Florida                 Power & Light Co.       05000389 AUTH. NAME           AUTHOR. AFFILIATION HURCHALLA,J.A.       Florida   Power & Light Co.
Florida Power&Light Co.SAGER,D.A.
SAGER,D.A.           Florida   Power & Light Co.
Florida Power&Light Co.RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000389
RECIP.NAME           RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
LER 93-002-00:on 921201,missed surveillance on RCS pressure isolation check valves due to procedural deficiency.
LER     93-002-00:on 921201,missed surveillance on RCS pressure isolation   check valves due to procedural deficiency.                               D Deficiencies in       SR   corrected'to include precautions in "procedure.W/930226         ltr.
Deficiencies in SR corrected'to include precautions in"procedure.W/930226 ltr.DISTRIBUTION CODE: ZE22T COPIES RECEIVED:LTR L ENCL~SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES: D RECIPIENT ID CODE/NAME PD2-2 LA NORRIS,J INTERNAL: ACNW AEOD/DOA AEOD/ROAB/DSP NRR/DE/EMEB NRR/DRCH/HHFBHE NRR/DRCH/HOLB NRR/DRSS/PRPB NRR/DSSA/SRXB RES/DSIR/EIB EXTERNAL: EG&G BRYCEgJ.H NRC PDR NSIC POORE,W.COPIES LTTR ENCL 1 1 1 1 2 2 1 1 2 2 1 1 1 1 1 1 2 2 1 1 1 1 2 2 1 1 1 1 RECIPIENT ID CODE/NAME PD2-2 PD ACRS AEOD/DSP/TPAB NRR/DE/EELB NRR/DORS/OEAB NRR/DRCH/HICB NRR/DRIL/RPEB R SPLB EG FILE 02 RGN2 FILE 01 L ST LOBBY WARD NSIC MURPHYgG.A NUDOCS FULL TXT COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 D D D NOTE TO ALL"RIDS" RECIPIENTS PLEASE HELP US TO REDUCE WASTEI CONTACT THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT.504-2065)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!D*1 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 32 ENCL 32 P.O.Box 128, Ft.Pierce, FL 34954-0128 February 26, 1993 L-93-053 10 CFR 50.73 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Re: St.Lucie Unit 2 Docket No.50-389 Reportable Event: 93-002 Date of Event: February 3;1993 Missed Surveillance on Reactor Coolant System'ressure Isolation Check Valves due to Procedural Deficienc The attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.Very truly yours, D.A..er Vice r sident St.Lucz.e Plant DAS/JWH/kw
DISTRIBUTION CODE: ZE22T           COPIES RECEIVED:LTR         L ENCL     ~ SIZE:
'Attachment cc: Stewart D.Ebneter, Regional Administrator, USNRC Region II Senior Resident Inspector, USNRC, St.Lucie Plant DAS/PSL 8867-93 050029 9303050185
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
'rr3022b PDR ADQCK 05000389 S PDR an FPL Group company I gpss~
NOTES:
FPL FOCErrrr'Io or NRC ForrTT S6S/AS)U.S.NUCLEAR REGULATORY COMMrSSION LICENSEE EVENT REPORT (LER)pppNorro olw w1$1$041 Ol ETPTPEINAOOTT TET PIATT 0 TAPE N PEN TEWTCNCE TO OOWET WITH T I4$0PCINIATIOM COUl CTION TECAESTI SOD f000 TOAWAITC COANNNT0 TEOAIEPNO TAATXN EETNAATE TO TIO f0 COfOO NET TE PCITTS IININX ANNT TTTANCN TP4$00 OO MACEENl IN TTNATCITT 00044$0NPA WAWNIOT CN.OO TO f00 NO TO TIN 0ETEWIW$00 TEOOC TKN PNOE CT p1$041WEOf f ICE OP NANAIXINNT AI0$TEOCET WAWNICTTTA OC TI00$FACILITY NAME (1)St.Lucie Unit 2 DOCKET NUMBER (2)PAGE 3 050003891 0 3'~(4)Missed Surveillance on Reactor Coolant System Pressure Isolation Check Valves Due to Procedural Deficiency EVENT DATE (5)DAY YEAR YEAR LER NUMBER (6)S IAL REPORT DATE (7)MONTH DAY YEAR FACILITY NAMES N/A" DOCKET NUMBER(S)OTHER FACILITIES INVOLVED (8)1 2 0 1 9 2 9 3 0 0 2 0 0 0 2 2 6 9 3 N/A 05 0 0 0 OPERATING MODE (9)POWER LEVEL (10)0 0 0 20.402(b)20.405(a)(1)(i) 20.405(a)(1)(ii) 20.405(c)50.36(c)(1) 50.36(c)(2) 50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii) 20.405(a)(1)(iii)
RECIPIENT              COPIES              RECIPIENT           COPIES ID CODE/NAME            LTTR ENCL          ID CODE/NAME       LTTR ENCL          D PD2-2 LA                     1    1      PD2-2 PD                  1    1 NORRIS,J                     1    1                                                  D INTERNAL:   ACNW                         2      2    ACRS                      2    2 AEOD/DOA                     1      1    AEOD/DSP/TPAB              1    1 AEOD/ROAB/DSP               2      2    NRR/DE/EELB                1    1 NRR/DE/EMEB                 1      1    NRR/DORS/OEAB              1    1 NRR/DRCH/HHFBHE             1      1    NRR/DRCH/HICB              1    1 NRR/DRCH/HOLB               1      1    NRR/DRIL/RPEB              1    1 NRR/DRSS/PRPB               2      2        R          SPLB        1    1 NRR/DSSA/SRXB               1      1        EG  FILE        02    1    1 RES/DSIR/EIB                 1      1    RGN2      FILE      01    1    1 EXTERNAL: EG&G BRYCEgJ.H                 2      2    L ST LOBBY WARD            1    1 NRC PDR                     1      1    NSIC MURPHYgG.A            1    1 NSIC POORE,W.               1     1     NUDOCS FULL TXT            1     1 D
X 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) 20.405(a)(1
D NOTE TO ALL"RIDS" RECIPIENTS PLEASE HELP US TO REDUCE WASTEI CONTACT THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
)(iv)20.405(a)(1)(v) 50.73(a)(2)(ii) 50.73(a)(2)(iii)
* 1 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR                 32    ENCL       32
LICENSEE CONTACT FOR THIS LER 12 50.73(a)(2)(viii)(B) 50.73(a)(2)(x)
 
THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR: Check one or more of the followin (11)73.71(b)73.71(c)OTHER (Specify in Abstract below and in Text NRC Eorm 366A)NAME James A.Hurchalla, Shift Technical Advisor TELEP ONE NUMBER AREA CODE 4 0 7 465-3550 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13 CAUSE SYSTEM COMPONENT MANUFAC-REPORTABLE TURER TO NPRDS CAUSE SYSTEM COMPONENT MANUFAC-'fURER REPORTABLE TO NPRDS I I I SUPPLEMENTAL REPORT EXPECTED 14 YES (If yes, complete EXPECTED SUBMISSION DATE)X NO EXPECTED MONTH DAY YEAR SUBMISSION DATE (15)ABSTRACT (Limit to 1400 spaces.i.e.
P.O. Box 128, Ft. Pierce, FL 34954-0128 February 26, 1993 L-93-053 10 CFR 50.73 U. S. Nuclear Regulatory Commission Attn:      Document Control Desk Washington, D. C. 20555 Re:  St. Lucie Unit          2 Docket No. 50-389 Reportable Event: 93-002 Date of Event: February 3; 1993 Missed Surveillance on Reactor Coolant Isolation Check Valves            System'ressure due    to Procedural Deficienc The  attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.
approximately fifteen single-space typewritten lines)(16)The root cause of the missed surveillances was procedural deficiency.
Very  truly yours, D. A..       er Vice r sident St. Lucz.e Plant DAS/JWH/kw
There was no note or caution in the Plant Heatup Procedure as exists in the Prestart Check-Off List on the necessity of testing the valves as required by Technical Specification 4.4.6.2.2.d.
'Attachment cc: Stewart D. Ebneter, Regional Administrator, USNRC Region                                II Senior Resident Inspector, USNRC, St. Lucie Plant DAS/PSL 8867-93 050029 9303050185 'rr3022b                                                                                I ADQCK 05000389 PDR S                        PDR an FPL Group company gpss~
The corrective actions were to ensure current surveillance requirements on the Sl header check valves were met satisfactorily and to change the Plant Heatup Procedure OP 2-0030121 to identify the surveillance requirements following recirculation of the Sl headers during plant heatup.This event is not applicable to Unit 1 due to differences in design.On January 30, 1993 St.Lucie Unit 2 was in Mode 3 implementing the Plant Heatup Procedure OP 2-0030121.
 
As part of this procedure, the Safety Injection (Sl)headers were recirculated causing six Reactor Coolant System (RCS)pressure isolation check valves to be exercised.
U.S. NUCLEAR REGULATORY COMMrSSION                                pppNorro olw w1 $ 1 $ 041 Ol FPL FOCErrrr'Io or                                                                                                              ETPTPEINAOOTT NRC ForrTT S6S                                                                                  TETPIATT 0 TAPE N PEN TEWTCNCE TO OOWET WITH T I4$ 0PCINIATIOMCOUlCTION
These valves are then required to be tested per Technical Specifications.
/AS)
The Technical Staff was advised of this and the valves were subsequently tested satisfactorily within the required time interval.A Technical Staff supervisor realized that there was not an adequate procedurally addressed method to ensure performance of surveillance requirements of this evolution during heatups.A review was initiated to address past startups to ensure this requirement had not been previously missed.On February 3, 1993 a Technical Staff pump and valve specialist performing the review discovered only two instances on 12/1/92 and 12/7/92 in which the required surveillances of the RCS pressure isolation check valves had not been performed within the appropriate time interval during past plant heatups.FPL Facsimile of NRC Form 366 (6-89)
LICENSEE EVENT REPORT (LER)                                        TECAESTI SOD f000 TOAWAITCCOANNNT0 TEOAIEPNO TAATXNEETNAATE TO TIO f0 COfOO NET TE PCITTS IININXANNT TTTANCNTP4$ 00 OO MACEENl INTTNATCITT 00044$ 0NPA WAWNIOTCN . OO TO f00 NO TO TIN 0ETEWIW$00 TEOOC TKN PNOE CT f
FPL FTCSlrrils OI NRC Form S66 (6 SS)U.S.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION AffRONTD CAST NOl 011001 Sr STTSSS:ACCST SSITAAT TD TAROT N ff R IRSACNTS TO CCADAT WIN DTS Sf CISlA DON OCIAT C TION TSCSRST: lf 0 f0TS I ORfrffO COIRNNT 0 TSCIRDNO IMTXN TSTSN OS TO TIR ISCOfOS Are TSTORI0 NANATS ASNr SRANCNTA CTCA ITS IAICTSAR IDIRAATORT
p1$ 041WEOf ICE OP NANAIXINNTAI0$ TEOCET WAWNICTTTAOC TI00$
~WADNIOTON.
FACILITYNAME (1)                                                                                               DOCKET NUMBER (2)                         PAGE 3 St. Lucie Unit 2 050003891                                          0 3
DC TCMR AIO TO TlC SAITRWOTN TSOVCTDN fROSCT TT11001 ffg Cf f TCS Of IAINAIXIRNT ffO TAIOCST, WADNICIDfr DC rlÃrfA FACILITY NAME (1)St.Lucie Unit 2 DOCKET NUMBER (2)YEAR LER NUMBER (6)EQUENTIAL NUMBER'EVISIO NUMBER PAGE (3)05000389 TEXT (/f more spaceis required, use additional NRC Form 366A's)(17)9 3 0 0 2 0 0 0 2 0 3 On January 30, 1993 St.Lucie Unit 2 was in Mode 3 implementing the Plant Heatup Procedure OP 2-00301 21.As part of this procedure, the Safety Injection (Sl)(EIIS: BP)headers were recirculated to equalize their boron concentration with the Reactor Coolant System (RCS)(EIIS: AB).This , evolution caused six RCS pressure isolation check valves (EIIS: BP)to be exercised.
  '~    (4)      Missed Surveillance on Reactor Coolant System Pressure Isolation Check Valves Due to Procedural Deficiency EVENT DATE (5)                  LER NUMBER (6)                  REPORT DATE (7)                   OTHER FACILITIES INVOLVED(8)
This required the valves to be verified closed per Technical Specifications (TS)within 24 hours and leak rate tested within 31 days.The Technical Staff was advised of this and the valves were subsequently tested satisfactorily within the required time interval.A Technical Staff supervisor realized there was not an adequate procedurally addressed method to ensure the required pressure isolation check valve testing during plant heatups.A review was initiated to address past startups to investigate as to whether this requirement had been previously missed.On February 3, 1993 a Technical Staff pump and valve specialist performing the review discovered instances in which the required surveillances had not been performed within the appropriate time interval during past heatups.subsequent to recirculating the Sl Headers.During plant heatups on 12/1/92 and on 12/7/92 the surveillance data sheet for these valves was not performed.
IAL                                            FACILITYNAMES                          DOCKET NUMBER(S)
This resulted in missing the 24 hour requirement on four Sl header valves and both the 24 hour and 31 day requirements on two Hot Leg Injection valves.The review discovered no other such instances during startups from 1985 until the present.The root cause of the event was inadequate procedural guidance.The check valves which are exercised in the Sl recirculation portion of OP 2-0030121 are required to be verified in their shut position against flow from the Reactor Coolant System per TS 4.4.6.2.2.d within 24 hours and leak tested within 31 days.However, no guidance is provided referencing this requirement.
DAY YEAR YEAR S                                    MONTH DAY        YEAR N/A" 1      2     0    1  9 2  9 3       0    0     2    0    0    0    2 2 6 9 3                          N/A                       05          0 0 0 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR:
The surveillance requirements of these valves is addressed in the Prestart Check-Off List procedure OP 2-0030120 but it does not adequately address the suweillance requirement of an evolution which may take place at any time over the course of several days.There were no unusual characteristics of the work location which contributed to this event.This event is reportable under 10 CFR 50.73.a.2.i.b, as a missed surveillance required by Technical Specifications.
OPERATING                   Check one or more of the followin    (11)
Technical Specification 4.4.6.2.2.b states that the Reactor Coolant System pressure isolation check valves shall be demonstrated operable by verifying leakage to be within its limit upon actuation or initiation of flow through the valve by verifying valve closure within 24 hours and leak rate testing within 31 days.The bases for this Technical Specification requirement is to provide additional assurance of valve integrity thereby reducing the possibility of an intersystem Loss of Coolant Accident (LOCA).FPL Facsimile of NRC Form 366 (6-69)
MODE (9)                                                                                                                            73.71(b) 20.402(b)                     20.405(c)                  50.73(a)(2)(iv)
F PL I Scsim(s o(NRC Form S66 (('P89)U.S.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROIEO ODO NCI$174 4 1 fl EAPIIE4 IC00 I'STDIATIO RAIS(N PER IESPCNIE TOO(SNIT WITH TIDS SEOISIATCN C(SAECTION IE(SECT: 000 IRS, IORWAISI C(SSRNT0 IECARCNC IAASNN ESTIIIAIE TO(IN IECOIIS AIR IEPCRT 0 SANA(E DE NT 4 RANCH (PDI(4 IA4 IAICAEAR IE(ADA(CRY
POWER                                                                                      50.73(a)(2)(v)                             73.71(c) 20.405(a)(1)(i)              50.36(c)(1)
~WAR NAITCN, CC RSI4 AIO TO TIE PPEINI(Ã0(IEOVC RON PRON CT (I'I DAD I III Of f ICE CP IIANA(XIEIIT Afo IRANRT.WAR CACTOID OC tfff(A FACILITY NAME (1)St.Lucie Unit 2 DOCKET NUMBER (2)YEAR LER NUMBER (6)EQUENTIAL REVISIO NUMBER NUMBER PAGE (3)0 500 0369 9 3 TEXT (ff more spaceis required, use additional NRC Form 366A's)(17)002-0003 0 3 The six check valves cycled in the recirculation of the Sl header all have redundant check valves between them and the RCS which act as the first pressure boundary.These redundant valves are not cycled as part of the Sl Loop recirculation and were within their surveillance requirements at all times.Should any of these redundant valves not have closed or had leaked excessively it would have become apparent by a low SIT level alarm, high Sl loop header pressure alarm, or by RCS inventory balance.Other suweillance requirements of Technical Specification (TS)4.4.6.2.2 within the Prestart Check-Off List have insured that the surveillances were performed in past plant heatups within the 24 hour.and the 31 day required time intervals.
LEVEL (10)           0  0  0      20.405(a)(1)(ii)             50.36(c)(2)                 50.73(a)(2)(vii)                           OTHER (Specify in Abstract 20.405(a)(1)(iii)     X     50.73(a)(2)(i)             50.73(a)(2)(viii)(A)                         below and in Text 20.405(a)(1 )(iv)                                         50.73(a)(2)(viii)(B)                          NRC Eorm 366A) 50.73(a)(2)(ii) 20.405(a)(1)(v)               50.73(a)(2)(iii)           50.73(a)(2)(x)
During the latest series of plant heatups on Unit 2 the other requirements were no longer applicable as the short period of time between heatups meant that these surveillances need not be performed per the other criteria of TS 4.4.6.2.2.
LICENSEE CONTACT FOR THIS LER 12 NAME                                                                                                                      TELEP ONE NUMBER AREA CODE James A. Hurchalla, Shift Technical Advisor                                                      4 0 7                465 -3550 COMPLETE ONE LINE FOR EACH COMPONENT            FAILURE  DESCRIBED    IN  THIS    REPORT            13 MANUFAC- REPORTABLE                                                                  MANUFAC- REPORTABLE CAUSE SYSTEM COMPONENT                     TURER       TO NPRDS               CAUSE SYSTEM COMPONENT                           'fURER                 TO NPRDS I     I       I SUPPLEMENTAL REPORT EXPECTED 14                                                   EXPECTED                    MONTH              DAY YEAR SUBMISSION YES (Ifyes, complete EXPECTED SUBMISSION DATE)                   X NO                               DATE (15)
Records of testing resulting from other evolutions previous and subsequent to these missed suweillances showed that the cycled valves had been performing as required.Therefore, the health and safety of the public was not affected by this event.1)A review was conducted by the Technical Staff pump and valve specialist to determine if during past heatups the required surveillances of the RCS Pressure Isolation Check Valves had been performed.
ABSTRACT (Limit to 1400 spaces.i.e. approximately fifteen single-space typewritten lines) (16)
Two heatups involved missed surveillances while all the rest were satisfactory.
On January 30, 1993 St. Lucie Unit 2 was in Mode 3 implementing the Plant Heatup Procedure OP 2-0030121.
2)Deficiencies in surveillance requirement guidance in the Unit 2 Plant Heatup Procedure OP 2-0030121 were corrected to include precautions in the procedure stating tlie required surveillance when the Sl recirculation is performed.
As part of this procedure, the Safety Injection (Sl) headers were recirculated causing six Reactor Coolant System (RCS) pressure isolation check valves to be exercised. These valves are then required to be tested per Technical Specifications. The Technical Staff was advised of this and the valves were subsequently tested satisfactorily within the required time interval. A Technical Staff supervisor realized that there was not an adequate procedurally addressed method to ensure performance of surveillance requirements of this evolution during heatups. A review was initiated to address past startups to ensure this requirement had not been previously missed. On February 3, 1993 a Technical Staff pump and valve specialist performing the review discovered only two instances on 12/1/92 and 12/7/92 in which the required surveillances of the RCS pressure isolation check valves had not been performed within the appropriate time interval during past plant heatups.
Unit 1 is not affected since the safety injection design is slightly different between the units and these check valves do not exist.There were no component failures.The following LERs were on missed surveillances due to procedural deficiencies:
The root cause of the missed surveillances was procedural deficiency. There was no note or caution in the Plant Heatup Procedure as exists in the Prestart Check-Off List on the necessity of testing the valves as required by Technical Specification 4.4.6.2.2.d.
The corrective actions were to ensure current surveillance requirements on the Sl header check valves were met satisfactorily and to change the Plant Heatup Procedure OP 2-0030121 to identify the surveillance requirements following recirculation of the Sl headers during plant heatup. This event is not applicable to Unit 1 due to differences in design.
FPL Facsimile of NRC Form 366 (6-89)
 
                                                                                                                                                    ~
FPL FTCSlrrils OI                                     U.S. NUCLEAR REGULATORYCOMMISSION                              AffRONTDCAST NOl 011001 Sr NRC Form S66                                                                                                                STTSSS:ACCST (6 SS)                                                                                                      ff SSITAATTD TAROTN R IRSACNTS TO CCADATWIN DTS SfCISlA DON OCIATC TION LICENSEE EVENT REPORT (LER)                                      TSCSRST: lf     I 0 f0TS ORfrffO COIRNNT0 TSCIRDNO IMTXNTSTSN OS TO TIR ISCOfOS Are TSTORI0 NANATSASNr SRANCNTACTCA ITS IAICTSARIDIRAATORT TEXT CONTINUATION                                                                                                            f WADNIOTON.DC TCMR AIOTO TlC SAITRWOTN TSOVCTDN fROSCT TT11001 ffgCf TCS Of IAINAIXIRNTffO TAIOCST, WADNICIDfrDC rlÃrfA FACILITYNAME (1)                                                 DOCKET NUMBER (2)               LER NUMBER (6)                                     PAGE (3)
YEAR          EQUENTIAL 'EVISIO NUMBER                 NUMBER St. Lucie Unit 2 05000389 366A's) 9 3            0      0        2          0          0  0 2            0 3 TEXT (/f more spaceis required, use additional NRC Form                     (17)
On January 30, 1993 St. Lucie Unit 2 was in Mode 3 implementing the Plant Heatup Procedure OP 2-00301 21. As part of this procedure, the Safety Injection (Sl) (EIIS: BP) headers were recirculated to equalize their boron concentration with the Reactor Coolant System (RCS) (EIIS: AB). This
                  , evolution caused six RCS pressure isolation check valves (EIIS: BP) to be exercised. This required the valves to be verified closed per Technical Specifications (TS) within 24 hours and leak rate tested within 31 days. The Technical Staff was advised of this and the valves were subsequently tested satisfactorily within the required time interval. A Technical Staff supervisor realized there was not an adequate procedurally addressed method to ensure the required pressure isolation check valve testing during plant heatups. A review was initiated to address past startups to investigate as to whether this requirement had been previously missed. On February 3, 1993 a Technical Staff pump and valve specialist performing the review discovered instances in which the required surveillances had not been performed within the appropriate time interval during past heatups.
subsequent to recirculating the Sl Headers. During plant heatups on 12/1/92 and on 12/7/92 the surveillance data sheet for these valves was not performed. This resulted in missing the 24 hour requirement on four Sl header valves and both the 24 hour and 31 day requirements on two Hot Leg Injection valves. The review discovered no other such instances during startups from 1985 until the present.
The root cause of the event was inadequate procedural guidance. The check valves which are exercised in the Sl recirculation portion of OP 2-0030121 are required to be verified in their shut position against flow from the Reactor Coolant System per TS 4.4.6.2.2.d within 24 hours and leak tested within 31 days. However, no guidance is provided referencing this requirement. The surveillance requirements of these valves is addressed in the Prestart Check-Off List procedure OP 2-0030120 but it does not adequately address the suweillance requirement of an evolution which may take place at any time over the course of several days. There were no unusual characteristics of the work location which contributed to this event.
This event is reportable under 10 CFR 50.73.a.2.i.b, as a missed surveillance required by Technical Specifications.
Technical Specification 4.4.6.2.2.b states that the Reactor Coolant System pressure isolation check valves shall be demonstrated operable by verifying leakage to be within its limit upon actuation or initiation of flow through the valve by verifying valve closure within 24 hours and leak rate testing within 31 days. The bases for this Technical Specification requirement is to provide additional assurance of valve integrity thereby reducing the possibility of an intersystem Loss of Coolant Accident (LOCA).
FPL Facsimile of NRC Form 366 (6-69)
 
                                                                                                                                                        ~
F PL I Scsim(s o(                                 U.S. NUCLEAR REGULATORY COMMISSION                                 APPROIEO ODO NCI $ 174 4 1 fl NRC Form S66                                                                                                                EAPIIE4 IC00 I
(('P89)
                                                                                        'STDIATIORAIS(N PER IESPCNIE TOO(SNIT WITH TIDS SEOISIATCN C(SAECTION LICENSEE EVENT REPORT (LER)                                      IE(SECT: 000 IRS, IORWAISIC(SSRNT0 IECARCNC IAASNN ESTIIIAIETO(IN IECOIIS AIR IEPCRT 0 SANA(EDE NT 4 RANCH (PDI(4 IA4 IAICAEARIE(ADA(CRY TEXT CONTINUATION                                          WARNAITCN,CC RSI4 AIO TO TIE PPEINI(Ã0( IEOVCRON PRON CT (I'IDADI IIIOf fICE CP IIANA(XIEIITAfo IRANRT.WARCACTOID OC tfff(A FACILITYNAME (1)                                             DOCKET NUMBER (2)                   LER NUMBER (6)                                         PAGE (3)
YEAR            EQUENTIAL REVISIO NUMBER                    NUMBER St. Lucie Unit 2 0   500 0369             9 3              002-0003                                                    0 3 TEXT (ff more spaceis required, use additional NRC Form 366A's) (17)
The six check valves cycled in the recirculation of the Sl header all have redundant check valves between them and the RCS which act as the first pressure boundary. These redundant valves are not cycled as part of the Sl Loop recirculation and were within their surveillance requirements at all times. Should any of these redundant valves not have closed or had leaked excessively it would have become apparent by a low SIT level alarm, high Sl loop header pressure alarm, or by RCS inventory balance.
Other suweillance requirements of Technical Specification (TS) 4.4.6.2.2 within the Prestart Check-Off List have insured that the surveillances were performed in past plant heatups within the 24 hour.
and the 31 day required time intervals. During the latest series of plant heatups on Unit 2 the other requirements were no longer applicable as the short period of time between heatups meant that these surveillances need not be performed per the other criteria of TS 4.4.6.2.2. Records of testing resulting from other evolutions previous and subsequent to these missed suweillances showed that the cycled valves had been performing as required. Therefore, the health and safety of the public was not affected by this event.
: 1) A review was conducted by the Technical Staff pump and valve specialist to determine if during past heatups the required surveillances of the RCS Pressure Isolation Check Valves had been performed. Two heatups involved missed surveillances while all the rest were satisfactory.
: 2) Deficiencies in surveillance requirement guidance in the Unit 2 Plant Heatup Procedure OP 2-0030121 were corrected to include precautions in the procedure stating tlie required surveillance when the Sl recirculation is performed. Unit 1 is not affected since the safety injection design is slightly different between the units and these check valves do not exist.
There were no component failures.
The following LERs were on missed surveillances due to procedural deficiencies:
LER 335-90-006 Missed surveillance on Control Element Assemblies Due to Procedural Deficiency LER 33543-016 Inadequate Procedure for Boric Acid Flow Path Surveillance LER 369-91-002 Missed Technical Specification Surveillance Due to Procedural Error FPL Facsimile of NRC Form 366 (6-89)}}
LER 335-90-006 Missed surveillance on Control Element Assemblies Due to Procedural Deficiency LER 33543-016 Inadequate Procedure for Boric Acid Flow Path Surveillance LER 369-91-002 Missed Technical Specification Surveillance Due to Procedural Error FPL Facsimile of NRC Form 366 (6-89)}}

Latest revision as of 21:19, 29 October 2019

LER 93-002-00:on 921201,missed Surveillance on RCS Pressure Isolation Check Valves Due to Procedural Deficiency. Deficiencies in SR Corrected to Include Precautions in procedure.W/930226 Ltr
ML17227A750
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 02/26/1993
From: Hurchalla J, Sager D
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-93-053, L-93-53, LER-93-002-02, LER-93-2-2, NUDOCS 9303050185
Download: ML17227A750 (5)


Text

ACCELERANT DOCUMENT DIST VTION SYSTEM REGULAT Y INFORMATION DISTRIBUTIO SYSTEM (RIDS)

'ACCESSION NBR:9303050185 DOC.DATE: 93/02/26 NOTARIZED: NO DOCKET FACIL:50-389 St. Lucie Plant, Unit 2, Florida Power & Light Co. 05000389 AUTH. NAME AUTHOR. AFFILIATION HURCHALLA,J.A. Florida Power & Light Co.

SAGER,D.A. Florida Power & Light Co.

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 93-002-00:on 921201,missed surveillance on RCS pressure isolation check valves due to procedural deficiency. D Deficiencies in SR corrected'to include precautions in "procedure.W/930226 ltr.

DISTRIBUTION CODE: ZE22T COPIES RECEIVED:LTR L ENCL ~ SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL D PD2-2 LA 1 1 PD2-2 PD 1 1 NORRIS,J 1 1 D INTERNAL: ACNW 2 2 ACRS 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFBHE 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRIL/RPEB 1 1 NRR/DRSS/PRPB 2 2 R SPLB 1 1 NRR/DSSA/SRXB 1 1 EG FILE 02 1 1 RES/DSIR/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: EG&G BRYCEgJ.H 2 2 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHYgG.A 1 1 NSIC POORE,W. 1 1 NUDOCS FULL TXT 1 1 D

D NOTE TO ALL"RIDS" RECIPIENTS PLEASE HELP US TO REDUCE WASTEI CONTACT THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

  • 1 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 32 ENCL 32

P.O. Box 128, Ft. Pierce, FL 34954-0128 February 26, 1993 L-93-053 10 CFR 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Re: St. Lucie Unit 2 Docket No. 50-389 Reportable Event: 93-002 Date of Event: February 3; 1993 Missed Surveillance on Reactor Coolant Isolation Check Valves System'ressure due to Procedural Deficienc The attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.

Very truly yours, D. A.. er Vice r sident St. Lucz.e Plant DAS/JWH/kw

'Attachment cc: Stewart D. Ebneter, Regional Administrator, USNRC Region II Senior Resident Inspector, USNRC, St. Lucie Plant DAS/PSL 8867-93 050029 9303050185 'rr3022b I ADQCK 05000389 PDR S PDR an FPL Group company gpss~

U.S. NUCLEAR REGULATORY COMMrSSION pppNorro olw w1 $ 1 $ 041 Ol FPL FOCErrrr'Io or ETPTPEINAOOTT NRC ForrTT S6S TETPIATT 0 TAPE N PEN TEWTCNCE TO OOWET WITH T I4$ 0PCINIATIOMCOUlCTION

/AS)

LICENSEE EVENT REPORT (LER) TECAESTI SOD f000 TOAWAITCCOANNNT0 TEOAIEPNO TAATXNEETNAATE TO TIO f0 COfOO NET TE PCITTS IININXANNT TTTANCNTP4$ 00 OO MACEENl INTTNATCITT 00044$ 0NPA WAWNIOTCN . OO TO f00 NO TO TIN 0ETEWIW$00 TEOOC TKN PNOE CT f

p1$ 041WEOf ICE OP NANAIXINNTAI0$ TEOCET WAWNICTTTAOC TI00$

FACILITYNAME (1) DOCKET NUMBER (2) PAGE 3 St. Lucie Unit 2 050003891 0 3

'~ (4) Missed Surveillance on Reactor Coolant System Pressure Isolation Check Valves Due to Procedural Deficiency EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED(8)

IAL FACILITYNAMES DOCKET NUMBER(S)

DAY YEAR YEAR S MONTH DAY YEAR N/A" 1 2 0 1 9 2 9 3 0 0 2 0 0 0 2 2 6 9 3 N/A 05 0 0 0 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR:

OPERATING Check one or more of the followin (11)

MODE (9) 73.71(b) 20.402(b) 20.405(c) 50.73(a)(2)(iv)

POWER 50.73(a)(2)(v) 73.71(c) 20.405(a)(1)(i) 50.36(c)(1)

LEVEL (10) 0 0 0 20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii) OTHER (Specify in Abstract 20.405(a)(1)(iii) X 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) below and in Text 20.405(a)(1 )(iv) 50.73(a)(2)(viii)(B) NRC Eorm 366A) 50.73(a)(2)(ii) 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)

LICENSEE CONTACT FOR THIS LER 12 NAME TELEP ONE NUMBER AREA CODE James A. Hurchalla, Shift Technical Advisor 4 0 7 465 -3550 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13 MANUFAC- REPORTABLE MANUFAC- REPORTABLE CAUSE SYSTEM COMPONENT TURER TO NPRDS CAUSE SYSTEM COMPONENT 'fURER TO NPRDS I I I SUPPLEMENTAL REPORT EXPECTED 14 EXPECTED MONTH DAY YEAR SUBMISSION YES (Ifyes, complete EXPECTED SUBMISSION DATE) X NO DATE (15)

ABSTRACT (Limit to 1400 spaces.i.e. approximately fifteen single-space typewritten lines) (16)

On January 30, 1993 St. Lucie Unit 2 was in Mode 3 implementing the Plant Heatup Procedure OP 2-0030121.

As part of this procedure, the Safety Injection (Sl) headers were recirculated causing six Reactor Coolant System (RCS) pressure isolation check valves to be exercised. These valves are then required to be tested per Technical Specifications. The Technical Staff was advised of this and the valves were subsequently tested satisfactorily within the required time interval. A Technical Staff supervisor realized that there was not an adequate procedurally addressed method to ensure performance of surveillance requirements of this evolution during heatups. A review was initiated to address past startups to ensure this requirement had not been previously missed. On February 3, 1993 a Technical Staff pump and valve specialist performing the review discovered only two instances on 12/1/92 and 12/7/92 in which the required surveillances of the RCS pressure isolation check valves had not been performed within the appropriate time interval during past plant heatups.

The root cause of the missed surveillances was procedural deficiency. There was no note or caution in the Plant Heatup Procedure as exists in the Prestart Check-Off List on the necessity of testing the valves as required by Technical Specification 4.4.6.2.2.d.

The corrective actions were to ensure current surveillance requirements on the Sl header check valves were met satisfactorily and to change the Plant Heatup Procedure OP 2-0030121 to identify the surveillance requirements following recirculation of the Sl headers during plant heatup. This event is not applicable to Unit 1 due to differences in design.

FPL Facsimile of NRC Form 366 (6-89)

~

FPL FTCSlrrils OI U.S. NUCLEAR REGULATORYCOMMISSION AffRONTDCAST NOl 011001 Sr NRC Form S66 STTSSS:ACCST (6 SS) ff SSITAATTD TAROTN R IRSACNTS TO CCADATWIN DTS SfCISlA DON OCIATC TION LICENSEE EVENT REPORT (LER) TSCSRST: lf I 0 f0TS ORfrffO COIRNNT0 TSCIRDNO IMTXNTSTSN OS TO TIR ISCOfOS Are TSTORI0 NANATSASNr SRANCNTACTCA ITS IAICTSARIDIRAATORT TEXT CONTINUATION f WADNIOTON.DC TCMR AIOTO TlC SAITRWOTN TSOVCTDN fROSCT TT11001 ffgCf TCS Of IAINAIXIRNTffO TAIOCST, WADNICIDfrDC rlÃrfA FACILITYNAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

YEAR EQUENTIAL 'EVISIO NUMBER NUMBER St. Lucie Unit 2 05000389 366A's) 9 3 0 0 2 0 0 0 2 0 3 TEXT (/f more spaceis required, use additional NRC Form (17)

On January 30, 1993 St. Lucie Unit 2 was in Mode 3 implementing the Plant Heatup Procedure OP 2-00301 21. As part of this procedure, the Safety Injection (Sl) (EIIS: BP) headers were recirculated to equalize their boron concentration with the Reactor Coolant System (RCS) (EIIS: AB). This

, evolution caused six RCS pressure isolation check valves (EIIS: BP) to be exercised. This required the valves to be verified closed per Technical Specifications (TS) within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and leak rate tested within 31 days. The Technical Staff was advised of this and the valves were subsequently tested satisfactorily within the required time interval. A Technical Staff supervisor realized there was not an adequate procedurally addressed method to ensure the required pressure isolation check valve testing during plant heatups. A review was initiated to address past startups to investigate as to whether this requirement had been previously missed. On February 3, 1993 a Technical Staff pump and valve specialist performing the review discovered instances in which the required surveillances had not been performed within the appropriate time interval during past heatups.

subsequent to recirculating the Sl Headers. During plant heatups on 12/1/92 and on 12/7/92 the surveillance data sheet for these valves was not performed. This resulted in missing the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> requirement on four Sl header valves and both the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and 31 day requirements on two Hot Leg Injection valves. The review discovered no other such instances during startups from 1985 until the present.

The root cause of the event was inadequate procedural guidance. The check valves which are exercised in the Sl recirculation portion of OP 2-0030121 are required to be verified in their shut position against flow from the Reactor Coolant System per TS 4.4.6.2.2.d within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and leak tested within 31 days. However, no guidance is provided referencing this requirement. The surveillance requirements of these valves is addressed in the Prestart Check-Off List procedure OP 2-0030120 but it does not adequately address the suweillance requirement of an evolution which may take place at any time over the course of several days. There were no unusual characteristics of the work location which contributed to this event.

This event is reportable under 10 CFR 50.73.a.2.i.b, as a missed surveillance required by Technical Specifications.

Technical Specification 4.4.6.2.2.b states that the Reactor Coolant System pressure isolation check valves shall be demonstrated operable by verifying leakage to be within its limit upon actuation or initiation of flow through the valve by verifying valve closure within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and leak rate testing within 31 days. The bases for this Technical Specification requirement is to provide additional assurance of valve integrity thereby reducing the possibility of an intersystem Loss of Coolant Accident (LOCA).

FPL Facsimile of NRC Form 366 (6-69)

~

F PL I Scsim(s o( U.S. NUCLEAR REGULATORY COMMISSION APPROIEO ODO NCI $ 174 4 1 fl NRC Form S66 EAPIIE4 IC00 I

(('P89)

'STDIATIORAIS(N PER IESPCNIE TOO(SNIT WITH TIDS SEOISIATCN C(SAECTION LICENSEE EVENT REPORT (LER) IE(SECT: 000 IRS, IORWAISIC(SSRNT0 IECARCNC IAASNN ESTIIIAIETO(IN IECOIIS AIR IEPCRT 0 SANA(EDE NT 4 RANCH (PDI(4 IA4 IAICAEARIE(ADA(CRY TEXT CONTINUATION WARNAITCN,CC RSI4 AIO TO TIE PPEINI(Ã0( IEOVCRON PRON CT (I'IDADI IIIOf fICE CP IIANA(XIEIITAfo IRANRT.WARCACTOID OC tfff(A FACILITYNAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

YEAR EQUENTIAL REVISIO NUMBER NUMBER St. Lucie Unit 2 0 500 0369 9 3 002-0003 0 3 TEXT (ff more spaceis required, use additional NRC Form 366A's) (17)

The six check valves cycled in the recirculation of the Sl header all have redundant check valves between them and the RCS which act as the first pressure boundary. These redundant valves are not cycled as part of the Sl Loop recirculation and were within their surveillance requirements at all times. Should any of these redundant valves not have closed or had leaked excessively it would have become apparent by a low SIT level alarm, high Sl loop header pressure alarm, or by RCS inventory balance.

Other suweillance requirements of Technical Specification (TS) 4.4.6.2.2 within the Prestart Check-Off List have insured that the surveillances were performed in past plant heatups within the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

and the 31 day required time intervals. During the latest series of plant heatups on Unit 2 the other requirements were no longer applicable as the short period of time between heatups meant that these surveillances need not be performed per the other criteria of TS 4.4.6.2.2. Records of testing resulting from other evolutions previous and subsequent to these missed suweillances showed that the cycled valves had been performing as required. Therefore, the health and safety of the public was not affected by this event.

1) A review was conducted by the Technical Staff pump and valve specialist to determine if during past heatups the required surveillances of the RCS Pressure Isolation Check Valves had been performed. Two heatups involved missed surveillances while all the rest were satisfactory.
2) Deficiencies in surveillance requirement guidance in the Unit 2 Plant Heatup Procedure OP 2-0030121 were corrected to include precautions in the procedure stating tlie required surveillance when the Sl recirculation is performed. Unit 1 is not affected since the safety injection design is slightly different between the units and these check valves do not exist.

There were no component failures.

The following LERs were on missed surveillances due to procedural deficiencies:

LER 335-90-006 Missed surveillance on Control Element Assemblies Due to Procedural Deficiency LER 33543-016 Inadequate Procedure for Boric Acid Flow Path Surveillance LER 369-91-002 Missed Technical Specification Surveillance Due to Procedural Error FPL Facsimile of NRC Form 366 (6-89)