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| {{#Wiki_filter:}} | | {{#Wiki_filter:REGULA .. Y INFORMATION DISTR IBUTl YSTEM (R IDS) |
| | ACCESSION NBR 8707220579 DOC. DATE: 87/07/14 NOTARIZED: NO DOCKET N FACIL: 50-315 Donald C. Cook Nuclear Power Planti Unit iI Indiana 5 05000315 AUTH. NAME AUTHOR AFFILIATION ALLARDIJ. D. Indiana u~ Michigan Electric Co. |
| | SMITHS W. G. Indiana 8< Michigan Electric Co. |
| | RECIP. NAME RECIPIENT AFFILIATION |
| | |
| | ==SUBJECT:== |
| | LER 85-023-01: on 850502I auxiliary bldg crane traveled over spent fuel pool w/heavy loadI contrary to Tech Spec 3. 9. 7. |
| | Caused bg misinterpretation of NUREG-0612 .definition of "heavy load. " Tech Spec 3. 9. 7 revised. W/870502 ltr. |
| | DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR 1 ENCL TITLE: 50. 73 Licensee Event Report (LER)I Incident j |
| | Rpti . |
| | SIZE: |
| | etc. |
| | 5 NOTES: |
| | REC IP IFNT COPIES REC IP IENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-3 LA 1 PD3-3 PD 1 1 WIGGINGTQNI D 1 1 INl ERNAL: ACRS MICHELSON ACRS MOELLER 2 2 AEOD/DQ* AEOD/DSP INAS 1 AEOD/DSP/ROAB 2 2 AEOD/DSP /TPAB 1 1 DEDRO 1 1 NRR/DEST/ADE 1 0 NRR/DEBT/ADS 1 0 NRR/DEST/CEB ~ 1 1 NRR/DEBT/ELB 1 1 NRR/DESTI ICBB 1 1 NRR/DEBT/MEB 1 1 I NRR DEBT/MTB 1 1 NRR/DEBT/PBB 1 NRR/DEST/RSB 1 NRR/DEBT/SGB 1 1 NRR/DLPG/HFB 1 1 NRR/DLPG/GAB 1 NRR/DQEA/EAB 1 1 NRR /DR EP /R AB 1 NRR/DREP /RPB 2 2 N NA LRB 1 NRR/PMAS/PTSB 1 1 G - 02 1 1 RES DEPY GI 1 1 RES TELFQRDI J 1 RES/DE/EIB 1 1 RQN3 F ILE 01 1 EXTERNAL: EGD<<G GROH> 5 5 5 H BT LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC HARRISI J 1 1 NSIC MAYBI Q 1 1 TOTAL NUMBER OF COPIES REQUIRED: LTTR 45 ENCL 43 |
| | |
| | NRC Form 355 US. NUCLEAR REOULATORY COMMISSION (943) |
| | APPROVED OMB NO. 3)600101 EXPIRES: 5/31/SS LICENSEE EVENT REPORT (LER) |
| | FAClLITY NAME (Il DOCKET NUMBER (2) PA E 3 D. C. Cook Nuclear Plant, Unit 1 o s o o o 315 >0F 4 TITLE (CI Travel of Heavy Load over Spent Fuel due to NUREG 0612 misinterpretation EVENT DATE IS) LER NUMBER (5) REPORT DATE (7) OTHER FACILITIES INVOLVED (5) |
| | MONTH DAY YEAR YEAR NI SEQUENTIAL CNS NUMBER RB~ |
| | NUMBER MONTH OAY YEAR FACILITYNAMES DOCKET NUMBER(S) |
| | D. C. Cook Unit 1 o s o o o3 16 0 5 2 8 585 0 2 3 010 714 87 0 s 0 0 0 OPERATINO THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR ()t (Chock ons or mors ol Ills Iollortlnp) (11) |
| | MODE (9) 20.C02(B) 20.405(c) 50.73(x)(2) (Ir) 73.71(B) |
| | POWER 20.COS( ~ ) (I )(B SOW(c)(I) 50.734) (2) (vl 73.71(cl LEVEL II0) p p 0 20A05(s) (1)(Bl 50.35(cl(2) 50.73(s) (2) (rB) OTHER (Spsclly ln Aors'sct arty "3 (Nlotrsnd In TsxL HRC Form Sr'jc 20.sos(s) (1)(III) 50.73(s) (2)(I) 9),73(s) (2) (rIB)(A) 3SSAJ 20AOS(s) (1)(lv) 50.73(s)(2)(B) 50.73(s) (2) (rIII)(5) |
| | ,I).. 0, .ks~~'t:: Sc 20.405(v)(1) (v) 50.73(s) (2) BII) 50,73( ~ )12)(x) |
| | LICENSEE CONTACT FOR THIS LER (12) |
| | NAME TELEPHONE NUMBER AREA CODE J. D. Allard, Maintenance Superintendent 6 16 465 -5 901 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT I'13) |
| | CAUSE SYSTEM COMPONENT MANUFAC-TURER-EPORTABLE TO NPRDS r~: CAVSE SYSTEM COMPONENT MANUFAC. |
| | TURER TO NPRDS . x .. g: |
| | I xos |
| | , cL x x |
| | '.,...,. |
| | SUPPLEMENTAL REPORT EXPECTED (IC) MONTH DAY YEAR EXPECTED SUBMISSION DATE (15) |
| | YES (II yct, complctt EXPECTED SUBMISSIDIY DATEI NO ABSTRACT (Limit to lc00 tpscst, Is., spproxlmstsly 5!tscn tlnplscpscs typsrrrlttsn linctl HB) |
| | On May 2, 1985 with the Unit 1 Reactor in Mode 6 (Refueling) and Unit 2 Reactor in Mode 1 (Power Operation) at 100 percent thermal power, the Auxiliary Building Crane traveled, unloaded, over the Spent Fuel Pool. |
| | This condition was contrary to Technical Specification 3.9.7 in that the crane's load block was at that time defined as a heavy load. |
| | The cause of this event has been determined to be the failure of Plant Personnel to recognize that the main load block on the Auxiliary Building Crane constituted a heavy load. It was believed that heavy loads were applicable to items being transported by the crane and not components of the crane. |
| | The corrective action taken was to change Technical Specification 3.9-7 by adding a footnote which defines the conditions necessary in order to place the main load block over the Spent Fuel Pool. 'The preventive actions were to impose restrictions on the crane and provide training to the operators. |
| | 8707220579 870714 PDR ADOCK 05000315 S PDR NRC Form 355 tBWBI |
| | |
| | NRC Fono 38SA US. NUCLEAR REOULATORY COMMISSION (94)3) |
| | LICENSEE E ENT REPORT (LER) TEXT CONTINUAT ON APPROVED OMS NO. 3180-0104 EXPIRES: 8/31/88 FACILITYNAME ll) OOCKET NUMBER (3) LER NUMSER (8) PACE (3) |
| | YEAR +~i SEQVSNTIAL '~j'EVISION |
| | '..: |
| | 'I)xI/ NVMSSR NVM SR D. C. Cook Nuclear Plant, Unit 1 0 S 0 0 0 3 15 85 0 2 3 0 1 0 2OF0 TEXT /$ 44>>>> <<>>c>> SI /4)MS'>>o aSSM>>o/NRC F>>RII 38M 3/ (17) |
| | Conditions Prior to Occurrence Unit One Mode 6 (refueling) at 0 Percent Reactor Thermal Power Unit Two Mode 1 (power operation) at 100 Percent Reactor Thermal Power Descri tion of Event I |
| | On May was 2, 1985 during a review of NUREG 0612 requirements, determined that on occasion, between June 1982 and April 1985, the it Auxiliary Building Crane's interlocks (EIIS/33) were defeated, allowing the Auxiliary Building Crane's main load block (EIIS/CRN) to travel over spent fuel assemblies in the Spent Fuel Pit (EIIS/RK). This condition was contrary to Technical Specification (T.S.) 3.9.7. The interlocks had been bypassed by the key-operated bypass switch (EIIS/HS) in order to allow the Auxiliary Building Crane to be used for normal maintenance activities such as retrieval of refueling tools (EIIS/FHM) from storage and maintenance of lighting fixtures over the Spent, Fuel Pit. |
| | At no time was any load carried over the Spent Fuel Pit on the main hook. |
| | During operations which resulted in traversing of the main hook over the pit area, virtually the same conditions subsequently required by the footnotes to T.S. 3.9.7 were in effect. Although the main hoist breaker (EIIS/BKR) was not open, the hoist mechanism was never operated, therefore, it remained de-energized. |
| | There were no other inoperable structures, components or systems that contributed to this event. |
| | Cause of Event The cause of this event has been determined to be the failure of Plant Personnel to recognize that the main load block on the Auxiliary Building Crane constituted a heavy load. It was believed that heavy loads were applicable to items being transported by the crane and not components of the crane. |
| | ~ t)RC FORM 3>>SA ~USOPO:IOS(LO83A.S38/SSSIN |
| | "(883) |
| | |
| | NRC Form 388A US. NUCLEAR REOULATORY COMMISSION |
| | )883) |
| | LICENSEE E NT REPORT (LER) TEXT CONTINUAT N APPROVED OM8 NO. 3160&104 EXPIRES: 8/31/88 FACILITYNAME 11) DOCKET NUMBER I2) LER NUMBER )8) PACE 13) |
| | YEAR .'san 8EOUENTIAL 'Nr IIEVISION |
| | ~ |
| | %%1 NUM SII N U M 8 8 II D. C. Cook Nuclear Plant, Unit 1 o s o o o 31 58 5 023 0 1 0 30F 04 TEXT 13//Noro deco 8 ro0rkord Iso akN5wo/H/IC %%drIII 38/A8/ OT) |
| | Anal sis of Event lt is concluded that this event is reportable per 10CFR50.73(a) (2) (i) (B). |
| | Technical Specification 3.9.7 prohibited loads in excess of 2500 pounds to travel over fuel assemblies stored in the Spent Fuel Pit. The Auxiliary Building Crane's load block weighs 4.25 tons. The immediate preventive actions taken were to place additional administrative controls on the movement of the crane. The main hoist breaker was de-energized and a clearance permit taken to prevent operation of the hoist or the key operated bypass switch. Training sessions were held for all crane operators to reinforce the requirements of NURZG 0612 and T.S. 3.9.7. |
| | Exxon Nuclear performed an analysis of a load block drop over the spent fuel assemblies and concluded that the damage to assemblies due to the drop of the load block would not cause a release of radiation exceeding the limitations imposed by 10CFR100. This load drop analysis was submitted to the NRC for review on January 9, 1987. |
| | Based on the results of the load drop analysis, Technical Specification 3.9.7 was changed by Amendments 79 and 93, adding a footnote which states; "This does not include the main load block, which weighs approximately 4.25 tons. Whenever the load block is moved over the pool, the'main hoist must be de-energized and be carrying no load." The changes made to Technical Specification 3.9.7 constitute permanent corrective measures. |
| | 'NR C'PO'RM *U.S.OPOII 0880824438/1 66 . |
| | 1883) |
| | |
| | hRC Form 3BBA US. NUCLEAR REOULATORY COMMISSION (083) |
| | LICENSEE E NT REPORT (LER) TEXT CONTINUATI N APPROVED OMB NO. 3150-0104 EXPIRES: 8/31 I(6 FACIU NAME (1) DOCKET NUMBER (3) LER NUMBER (B) PACE (3) |
| | YEAR SEOVENTIAL REVISION rIVM ER %Ã NVM ER D. C. Cook Nuclear Plant, Unit 1 0 5 0 0 0 3 l 5 8 5 023 0 1 0 4 OF 0 4 TEXT (PIRoro N>>co Jr roBMBad oro aki5ans'NRC ForIII 3(ELBE) ((7) |
| | Corrective Actions The appropriate Plant Procedures have been modified to clearly indicate that the load block of the Auxiliary Building Crane is to be considered as a heavy load. Administrative controls regarding movement of the Auxiliary Building Crane over the Spent Fuel Pit have been strengthened. |
| | Technical Specification 3.9.7 has been changed defining conditions required whenever the load block is moved over the Spent Fuel Pool, i.e. |
| | the main hoist must be de-energized and be carrying no load, Amendments No. 79 and 93. |
| | Failed Com onent Identification None Previous Similar Events None identified at this time. |
| | N)IC FORM SOBA m ().SOP(3I198()4() SI.S38/add, . |
| | BALI) |
| | |
| | er4tsn leotrlo |
| | ~ye/ INDIANA I& MICIIIGAN ELEC 78IC COMPA N Y DONALD C. COOK NUCLEAR PLANT P.O. Box 456, Brldgemen, Ml 49106 Telephone (616) 465 5901 July 14, 1987 United States Nuclear Regulatory Commission Document Control Desk Washington, D.C. |
| | 20555'perating License DPR-58 Docket No. 50-315 Document Control Manager: |
| | In accordance with the criteria established by 10 CFR 50.73 entitled Licensee Event Re ortin S stem, the following report is being submitted: |
| | 85-023-01 Sincerely, W. G. Smith, Jr. |
| | Plant Manager WGS:afh Attachments cc: A. B. Davis, Region R. C. Callen, MPSC III D. Hahn, MDPH G. Charnoff, Esq. |
| | Dottie Sherman, ANI Library D. L. Wigginton, NRC Records Center, INPO J. E. Dolan M. P. Alexich R. W. Jurgensen H. B. Brugger NRC Resident Inspector PNSRC A. A. Blind R. F. Kroeger File J. G. Feinstein/B. P. Lauzau}} |
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[Table view] Category:RO)
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Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors ML17335A5171999-02-11011 February 1999 LER 99-002-00:on 990112,determined That RCS Pressurizer PORVs Had Not Been Tested,Per Ts.Caused by Inadequate Scheduling Controls Allowing Personnel Error.Surveillance Procedure Was Completed & Updated LER Will Be Submitted ML17335A5141999-02-10010 February 1999 LER 99-001-00:on 990106,noted That GE Hfa Relays Installed in EDGs May Not Meet Seismic Qualification.Caused by Operating Experience Info Incorrectly Dispositioned in 1985. Updated LER Will Be Submitted by 990405 ML17335A5011999-02-0101 February 1999 LER 98-060-00:on 981231,identified That Rt Sys Response Time Testing Did Not Comply with TS Definition.Caused by Inadequate Procedures.Corrective Actions Will Be Developed & Update to LER Will Be Submitted by 990415.With 990201 Ltr ML17335A4951999-01-29029 January 1999 LER 98-059-00:on 981230,interim LER -single Failure in Containment Spray Sys Could Result in Containment Spray Ph Outside Design Occurred.Investigation Into Condition Continuing.Update Will Be Submitted by 990514 Ltr ML17335A4961999-01-27027 January 1999 LER 98-057-00:on 981228,discovered That AFW Valves Were Not Tested IAW Inservice Testing Program.Caused by Failure to Recognize Design Bases Features Re Afws by Personnel. Updated LER Will Be Submittted by 990415.With 990127 Ltr ML17335A4921999-01-19019 January 1999 LER 98-052-01:on 981128,no Analysis for NSR Sc Manual Loader for Tdafwp Could Be Found in Original Design.Cause Due to All Failure Modes Not Considered When Compressed Air Sys Originally Designed.Performed Review of Components ML17335A4721999-01-0606 January 1999 LER 98-055-00:on 981207,potential for Condition Outside of Design Bases for Rod Control Sys Was Noted.Caused by Calibration Error Coupled with Single Rod Failure.Condition Rept Investigation Is Ongoing ML17335A4691999-01-0606 January 1999 LER 98-056-00:on 981211,hot Leg Nozzle Gaps Resulted in Plant Being in Unanalyzed Condition.Analyses Are Being Performed by W to Resolve Problem.Updated LER Will Be Submitted by 990211.With 990106 Ltr ML17335A4661999-01-0505 January 1999 LER 98-049-00:on 981020,emergency Boron Injection Flow Path Was Inoperable.Caused by Original Design Deficiency. Engineering Evaluation of Event Is Continuing ML17335A4631999-01-0404 January 1999 LER 98-054-00:on 981202,discovered That at Least One MSSV Had Not Been Reset as Required by Ts.Engineering Is Continuing Review of Extent of Condition for Event.Updated LER Will Be Submitted by 990129.With 990104 Ltr ML17335A4481998-12-30030 December 1998 LER 98-053-00:on 981130,discovered Use of Inoperable Substitute Subcooling Margin Monitor.Caused by Condition Existing Since Installation of Plant Process Computer in 1992.Updated LER Will Be Submitted.With 981230 Ltr ML17335A4581998-12-28028 December 1998 LER 98-052-00:on 981128,turbine Driven AFW Pump Speed Controller Failure Mode Occurred.Caused Because Not All Failure Modes Were Considered When Compressed Air Sys Was Originally Designed.Verified Current Design Change Process ML17335A4281998-12-22022 December 1998 LER 98-051-00:on 981122,reactor Trip Signal from Manual Safety Injection Not Verified as Required by TS Surveillance,Was Discovered.Maintenance Currently Evaluating Significance & Cause of Event ML17335A4111998-12-17017 December 1998 LER 98-047-00:on 981117,potential for Increase Leakage from Reactor Coolant Pump Seals Was Identified.Util Is Working with W to Resolve Issue.Current Expectations Are to Submit Update to LER by 990215.With 981217 Ltr ML17335A4141998-12-16016 December 1998 LER 98-058-00:on 981216,postulated High Line Break Could Result in Condition Outside Design Bases for AF Occurred. Caused by Deficiencies Associated with Administration of HELB Program.Analysis of AF Will Be Completed by 990122 ML17335A4181998-12-16016 December 1998 LER 98-050-00:on 980814,ancillary Equipment Installed in Ice Condenser Was Not Designed to Withstand Design Basis Accident/Earthquake Loads.Caused by Lack of Established Design Criteria.Developed Design Criteria ML17335A3871998-12-11011 December 1998 LER 98-031-01:on 980610,potential Common Mode Failure of RHR Pumps Were Noted.Caused by Inaccurate Values.Accurate Miniflow Numbers Have Been Determined by Flow Testing ML17335A3821998-12-0808 December 1998 LER 98-039-01 Re EOP Step Conflicts with Small Break LOCA Analysis.Ler 98-039-00 Has Been Canceled.With 981208 Ltr ML17335A3781998-12-0707 December 1998 LER 98-007-00:on 981106,high Energy Line Break Effects in Auxiliary FW Sys Was Noted.Cause of Event Is Under Investigation & Will Be Completed by 990220.Updated LER Will Be Submitted by 990310.With 981207 Ltr ML17335A3771998-12-0303 December 1998 LER 98-046-00:on 981103,determined That Afs Was Unable to Meet Design Flow Requirements During Special Test.Caused by Failure to Consider All Aspects of Sys Operation in Design of Suction Basket Strainers.Sys Will Be Redesigned ML17335A3741998-12-0202 December 1998 LER 97-011-02:on 970822,operation Was Noted Outside Design Bases for ECCS & CSP for Switchover to Recirculation Sump Suction.Caused by Ineffective Change Mgt.Revised Procedure for Switchover 01(02) Ohp 4023.ES-1.3 1999-09-17
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5481999-09-30030 September 1999 Non-proprietary DC Cook Nuclear Plant Units 1 & 2 Mods to Containment Sys W SE (Secl 99-076,Rev 3). ML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors 1999-09-30
[Table view] |
Text
REGULA .. Y INFORMATION DISTR IBUTl YSTEM (R IDS)
ACCESSION NBR 8707220579 DOC. DATE: 87/07/14 NOTARIZED: NO DOCKET N FACIL: 50-315 Donald C. Cook Nuclear Power Planti Unit iI Indiana 5 05000315 AUTH. NAME AUTHOR AFFILIATION ALLARDIJ. D. Indiana u~ Michigan Electric Co.
SMITHS W. G. Indiana 8< Michigan Electric Co.
RECIP. NAME RECIPIENT AFFILIATION
SUBJECT:
LER 85-023-01: on 850502I auxiliary bldg crane traveled over spent fuel pool w/heavy loadI contrary to Tech Spec 3. 9. 7.
Caused bg misinterpretation of NUREG-0612 .definition of "heavy load. " Tech Spec 3. 9. 7 revised. W/870502 ltr.
DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR 1 ENCL TITLE: 50. 73 Licensee Event Report (LER)I Incident j
Rpti .
SIZE:
etc.
5 NOTES:
REC IP IFNT COPIES REC IP IENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-3 LA 1 PD3-3 PD 1 1 WIGGINGTQNI D 1 1 INl ERNAL: ACRS MICHELSON ACRS MOELLER 2 2 AEOD/DQ* AEOD/DSP INAS 1 AEOD/DSP/ROAB 2 2 AEOD/DSP /TPAB 1 1 DEDRO 1 1 NRR/DEST/ADE 1 0 NRR/DEBT/ADS 1 0 NRR/DEST/CEB ~ 1 1 NRR/DEBT/ELB 1 1 NRR/DESTI ICBB 1 1 NRR/DEBT/MEB 1 1 I NRR DEBT/MTB 1 1 NRR/DEBT/PBB 1 NRR/DEST/RSB 1 NRR/DEBT/SGB 1 1 NRR/DLPG/HFB 1 1 NRR/DLPG/GAB 1 NRR/DQEA/EAB 1 1 NRR /DR EP /R AB 1 NRR/DREP /RPB 2 2 N NA LRB 1 NRR/PMAS/PTSB 1 1 G - 02 1 1 RES DEPY GI 1 1 RES TELFQRDI J 1 RES/DE/EIB 1 1 RQN3 F ILE 01 1 EXTERNAL: EGD<<G GROH> 5 5 5 H BT LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC HARRISI J 1 1 NSIC MAYBI Q 1 1 TOTAL NUMBER OF COPIES REQUIRED: LTTR 45 ENCL 43
NRC Form 355 US. NUCLEAR REOULATORY COMMISSION (943)
APPROVED OMB NO. 3)600101 EXPIRES: 5/31/SS LICENSEE EVENT REPORT (LER)
FAClLITY NAME (Il DOCKET NUMBER (2) PA E 3 D. C. Cook Nuclear Plant, Unit 1 o s o o o 315 >0F 4 TITLE (CI Travel of Heavy Load over Spent Fuel due to NUREG 0612 misinterpretation EVENT DATE IS) LER NUMBER (5) REPORT DATE (7) OTHER FACILITIES INVOLVED (5)
MONTH DAY YEAR YEAR NI SEQUENTIAL CNS NUMBER RB~
NUMBER MONTH OAY YEAR FACILITYNAMES DOCKET NUMBER(S)
D. C. Cook Unit 1 o s o o o3 16 0 5 2 8 585 0 2 3 010 714 87 0 s 0 0 0 OPERATINO THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR ()t (Chock ons or mors ol Ills Iollortlnp) (11)
MODE (9) 20.C02(B) 20.405(c) 50.73(x)(2) (Ir) 73.71(B)
POWER 20.COS( ~ ) (I )(B SOW(c)(I) 50.734) (2) (vl 73.71(cl LEVEL II0) p p 0 20A05(s) (1)(Bl 50.35(cl(2) 50.73(s) (2) (rB) OTHER (Spsclly ln Aors'sct arty "3 (Nlotrsnd In TsxL HRC Form Sr'jc 20.sos(s) (1)(III) 50.73(s) (2)(I) 9),73(s) (2) (rIB)(A) 3SSAJ 20AOS(s) (1)(lv) 50.73(s)(2)(B) 50.73(s) (2) (rIII)(5)
,I).. 0, .ks~~'t:: Sc 20.405(v)(1) (v) 50.73(s) (2) BII) 50,73( ~ )12)(x)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE J. D. Allard, Maintenance Superintendent 6 16 465 -5 901 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT I'13)
CAUSE SYSTEM COMPONENT MANUFAC-TURER-EPORTABLE TO NPRDS r~: CAVSE SYSTEM COMPONENT MANUFAC.
TURER TO NPRDS . x .. g:
I xos
, cL x x
'.,...,.
SUPPLEMENTAL REPORT EXPECTED (IC) MONTH DAY YEAR EXPECTED SUBMISSION DATE (15)
YES (II yct, complctt EXPECTED SUBMISSIDIY DATEI NO ABSTRACT (Limit to lc00 tpscst, Is., spproxlmstsly 5!tscn tlnplscpscs typsrrrlttsn linctl HB)
On May 2, 1985 with the Unit 1 Reactor in Mode 6 (Refueling) and Unit 2 Reactor in Mode 1 (Power Operation) at 100 percent thermal power, the Auxiliary Building Crane traveled, unloaded, over the Spent Fuel Pool.
This condition was contrary to Technical Specification 3.9.7 in that the crane's load block was at that time defined as a heavy load.
The cause of this event has been determined to be the failure of Plant Personnel to recognize that the main load block on the Auxiliary Building Crane constituted a heavy load. It was believed that heavy loads were applicable to items being transported by the crane and not components of the crane.
The corrective action taken was to change Technical Specification 3.9-7 by adding a footnote which defines the conditions necessary in order to place the main load block over the Spent Fuel Pool. 'The preventive actions were to impose restrictions on the crane and provide training to the operators.
8707220579 870714 PDR ADOCK 05000315 S PDR NRC Form 355 tBWBI
NRC Fono 38SA US. NUCLEAR REOULATORY COMMISSION (94)3)
LICENSEE E ENT REPORT (LER) TEXT CONTINUAT ON APPROVED OMS NO. 3180-0104 EXPIRES: 8/31/88 FACILITYNAME ll) OOCKET NUMBER (3) LER NUMSER (8) PACE (3)
YEAR +~i SEQVSNTIAL '~j'EVISION
'..:
'I)xI/ NVMSSR NVM SR D. C. Cook Nuclear Plant, Unit 1 0 S 0 0 0 3 15 85 0 2 3 0 1 0 2OF0 TEXT /$ 44>>>> <<>>c>> SI /4)MS'>>o aSSM>>o/NRC F>>RII 38M 3/ (17)
Conditions Prior to Occurrence Unit One Mode 6 (refueling) at 0 Percent Reactor Thermal Power Unit Two Mode 1 (power operation) at 100 Percent Reactor Thermal Power Descri tion of Event I
On May was 2, 1985 during a review of NUREG 0612 requirements, determined that on occasion, between June 1982 and April 1985, the it Auxiliary Building Crane's interlocks (EIIS/33) were defeated, allowing the Auxiliary Building Crane's main load block (EIIS/CRN) to travel over spent fuel assemblies in the Spent Fuel Pit (EIIS/RK). This condition was contrary to Technical Specification (T.S.) 3.9.7. The interlocks had been bypassed by the key-operated bypass switch (EIIS/HS) in order to allow the Auxiliary Building Crane to be used for normal maintenance activities such as retrieval of refueling tools (EIIS/FHM) from storage and maintenance of lighting fixtures over the Spent, Fuel Pit.
At no time was any load carried over the Spent Fuel Pit on the main hook.
During operations which resulted in traversing of the main hook over the pit area, virtually the same conditions subsequently required by the footnotes to T.S. 3.9.7 were in effect. Although the main hoist breaker (EIIS/BKR) was not open, the hoist mechanism was never operated, therefore, it remained de-energized.
There were no other inoperable structures, components or systems that contributed to this event.
Cause of Event The cause of this event has been determined to be the failure of Plant Personnel to recognize that the main load block on the Auxiliary Building Crane constituted a heavy load. It was believed that heavy loads were applicable to items being transported by the crane and not components of the crane.
~ t)RC FORM 3>>SA ~USOPO:IOS(LO83A.S38/SSSIN
"(883)
NRC Form 388A US. NUCLEAR REOULATORY COMMISSION
)883)
LICENSEE E NT REPORT (LER) TEXT CONTINUAT N APPROVED OM8 NO. 3160&104 EXPIRES: 8/31/88 FACILITYNAME 11) DOCKET NUMBER I2) LER NUMBER )8) PACE 13)
YEAR .'san 8EOUENTIAL 'Nr IIEVISION
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%%1 NUM SII N U M 8 8 II D. C. Cook Nuclear Plant, Unit 1 o s o o o 31 58 5 023 0 1 0 30F 04 TEXT 13//Noro deco 8 ro0rkord Iso akN5wo/H/IC %%drIII 38/A8/ OT)
Anal sis of Event lt is concluded that this event is reportable per 10CFR50.73(a) (2) (i) (B).
Technical Specification 3.9.7 prohibited loads in excess of 2500 pounds to travel over fuel assemblies stored in the Spent Fuel Pit. The Auxiliary Building Crane's load block weighs 4.25 tons. The immediate preventive actions taken were to place additional administrative controls on the movement of the crane. The main hoist breaker was de-energized and a clearance permit taken to prevent operation of the hoist or the key operated bypass switch. Training sessions were held for all crane operators to reinforce the requirements of NURZG 0612 and T.S. 3.9.7.
Exxon Nuclear performed an analysis of a load block drop over the spent fuel assemblies and concluded that the damage to assemblies due to the drop of the load block would not cause a release of radiation exceeding the limitations imposed by 10CFR100. This load drop analysis was submitted to the NRC for review on January 9, 1987.
Based on the results of the load drop analysis, Technical Specification 3.9.7 was changed by Amendments 79 and 93, adding a footnote which states; "This does not include the main load block, which weighs approximately 4.25 tons. Whenever the load block is moved over the pool, the'main hoist must be de-energized and be carrying no load." The changes made to Technical Specification 3.9.7 constitute permanent corrective measures.
'NR C'PO'RM *U.S.OPOII 0880824438/1 66 .
1883)
hRC Form 3BBA US. NUCLEAR REOULATORY COMMISSION (083)
LICENSEE E NT REPORT (LER) TEXT CONTINUATI N APPROVED OMB NO. 3150-0104 EXPIRES: 8/31 I(6 FACIU NAME (1) DOCKET NUMBER (3) LER NUMBER (B) PACE (3)
YEAR SEOVENTIAL REVISION rIVM ER %Ã NVM ER D. C. Cook Nuclear Plant, Unit 1 0 5 0 0 0 3 l 5 8 5 023 0 1 0 4 OF 0 4 TEXT (PIRoro N>>co Jr roBMBad oro aki5ans'NRC ForIII 3(ELBE) ((7)
Corrective Actions The appropriate Plant Procedures have been modified to clearly indicate that the load block of the Auxiliary Building Crane is to be considered as a heavy load. Administrative controls regarding movement of the Auxiliary Building Crane over the Spent Fuel Pit have been strengthened.
Technical Specification 3.9.7 has been changed defining conditions required whenever the load block is moved over the Spent Fuel Pool, i.e.
the main hoist must be de-energized and be carrying no load, Amendments No. 79 and 93.
Failed Com onent Identification None Previous Similar Events None identified at this time.
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~ye/ INDIANA I& MICIIIGAN ELEC 78IC COMPA N Y DONALD C. COOK NUCLEAR PLANT P.O. Box 456, Brldgemen, Ml 49106 Telephone (616) 465 5901 July 14, 1987 United States Nuclear Regulatory Commission Document Control Desk Washington, D.C.
20555'perating License DPR-58 Docket No. 50-315 Document Control Manager:
In accordance with the criteria established by 10 CFR 50.73 entitled Licensee Event Re ortin S stem, the following report is being submitted:
85-023-01 Sincerely, W. G. Smith, Jr.
Plant Manager WGS:afh Attachments cc: A. B. Davis, Region R. C. Callen, MPSC III D. Hahn, MDPH G. Charnoff, Esq.
Dottie Sherman, ANI Library D. L. Wigginton, NRC Records Center, INPO J. E. Dolan M. P. Alexich R. W. Jurgensen H. B. Brugger NRC Resident Inspector PNSRC A. A. Blind R. F. Kroeger File J. G. Feinstein/B. P. Lauzau