ML17252A845: Difference between revisions
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| issue date = 02/26/1974 | | issue date = 02/26/1974 | ||
| title = Report of an Inadvertent Safety Injection Signal Was Generated Which by Design, Caused the Accumulator Discharge Stop Valves to Open | | title = Report of an Inadvertent Safety Injection Signal Was Generated Which by Design, Caused the Accumulator Discharge Stop Valves to Open | ||
| author name = Cobean W | | author name = Cobean W | ||
| author affiliation = Consolidated Edison Co of New York, Inc | | author affiliation = Consolidated Edison Co of New York, Inc | ||
| addressee name = O'Reilly J | | addressee name = O'Reilly J | ||
| addressee affiliation = US Atomic Energy Commission (AEC) | | addressee affiliation = US Atomic Energy Commission (AEC) | ||
| docket = 05000247 | | docket = 05000247 | ||
Revision as of 04:20, 19 June 2019
| ML17252A845 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 02/26/1974 |
| From: | Cobean W Consolidated Edison Co of New York |
| To: | O'Reilly J US Atomic Energy Commission (AEC) |
| References | |
| AO 4-2-9 | |
| Download: ML17252A845 (1) | |
Text
Mr. James P. O'Reilly, Director Regulatory Operations, Region I u. S. Atomic Energy Commission 631 Park Avenue February 26, 1974 Re: Indian Point Unit No. 2 AEC Docket No. 50-247 Operating License DPR-26 A.O. 4-2-9 King of Prussia, Pennsylvania 19406 '
Dear Mr. O'Reilly:
In accordance with the requirements of Section 6.12.2(a) of the Technical Specifications of Facility Operating License No. DPR-26, the following report is submitted!
In the course of perforrning
.. periodic surveillance test PT-Mll, "Steam Line Pressure Analog .Channel Functional Test" on February 22, 1974, an inadvertent safety injection signal was generated which, by design, caused the accumulator discharge stop valves to open. At-the time of the occurrence, the reactor was in the cold shutdown condition with the Heat Removal System in service and a reactor coolant pressure and temperature of 150 psig and ll50F respectively.
Since the reactor coolant system was ing operated in the solid mode, opening of the accumulator valves pressurized the system to about 560 psig which was slightly in excess of the Technical Specification limit 'of 500 -psig for dicated temperatures at or below 2200F. The pressure was promptly reduced below the 500 psig limit by operator action. There was no damage incurred to any system or component as a result of the pressure transient of this magnitude nor was there any reason to expect any.* . Mr. Anthony Fasano of your office was informed of this occurrence by Mr. John M. Makepeace on February 22, 1974. Very truly yours, . L.Uo ..
12_ .... t , Warren R. Cobean, Jr * .Manager Nuclear Power Generation Depart. cc: John F. O'Leary l