|
|
Line 32: |
Line 32: |
| ~P0029 PDR ADo 8/p-' | | ~P0029 PDR ADo 8/p-' |
| 4i U.S.Nuclear Regulator Commission Page 2 December 6, 1995 Enclosure c'c (Enclosure): | | 4i U.S.Nuclear Regulator Commission Page 2 December 6, 1995 Enclosure c'c (Enclosure): |
| INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, Georgia 30339 Paul Krippner American Nuclear Insurers Town Center, Suite 300S 29 South Main Street West Hartford, Connecticut 06107 NRC Resident Inspector Browns Ferry Nuclear Plant 10833 Shaw Road Athens, Alabama 35611 Regional Administrator U.S.Nuclear Regulatory Commission Region II 101 Marietta Street;NW, Suite 2900 Atlanta, Georgia 30323 Mr.Z.F.Williams, Project Manager U.S.Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike-Rockville, Maryland 20852 | | INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, Georgia 30339 Paul Krippner American Nuclear Insurers Town Center, Suite 300S 29 South Main Street West Hartford, Connecticut 06107 NRC Resident Inspector Browns Ferry Nuclear Plant 10833 Shaw Road Athens, Alabama 35611 Regional Administrator U.S.Nuclear Regulatory Commission Region II 101 Marietta Street;NW, Suite 2900 Atlanta, Georgia 30323 Mr.Z.F.Williams, Project Manager U.S.Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike-Rockville, Maryland 20852 |
| :4k ig)/1 NRC FORH 366 (5-92)~S.NUCLEAR REGULATORY CQSIISSION ROVED BY (RIB NO.3150-0104 EXPIRES 5/31/95 LZCENSEE EVENT REPORT (LER)(See reverse for required naker of digits/characters for each block)ESTIHATED BURDEN PER RESPONSE TO COHPLY IIITH THIS INFORHATION COLLECTION REQUEST: 50.0 HRS FORMARD COHHENTS REGARDING BURDEN ESTIHATE TO THE INFORHATIOH AND RECORDS HANAGEHENT BRANCH (HNBB 7714)~U.ST NUCLEAR REGULATORY COHHISSION, NASHINGTOH, DC 20555-0001 AND TO THE PAPERMORK REDUCTION PROJECT (3140-0104), OFFICE OF HANAGEHENT AMD BUDGET UASHIMGTON DC 20503.FACILITY IWK (1>Browns Fer Nuclear Plant BFN Unit.3 DOCKET NINRIER (2)05000296 PAGE (3)1 OF 5 TITLE (4>Unplanned Engineered Safety Feature Actuation following transfer of 480V RHOV Board 38 to its normal power supply after the replacement of a temporary normal supply breaker.EVENT DATE 5 REP(XIT DATE 7 OTHER FACILITIES INVOLVED 8 MONTH DAY YEAR'EQUENTIAL NUMBER'EVISIOM NUHBER HONTH DAY FACILITY NAHE N/A YEAR DOCKET NUMBER 11 08 GYRATING INX)E (9)LEVEL (10)95'5 007 00 THIS REPIXIT IS SUBMITTED PURSUANT 20.402(b)20.405(a)(1)(i) 000: 20.405(a)(1)(i i)20 405(a)(1)(iii) | | :4k ig)/1 NRC FORH 366 (5-92)~S.NUCLEAR REGULATORY CQSIISSION ROVED BY (RIB NO.3150-0104 EXPIRES 5/31/95 LZCENSEE EVENT REPORT (LER)(See reverse for required naker of digits/characters for each block)ESTIHATED BURDEN PER RESPONSE TO COHPLY IIITH THIS INFORHATION COLLECTION REQUEST: 50.0 HRS FORMARD COHHENTS REGARDING BURDEN ESTIHATE TO THE INFORHATIOH AND RECORDS HANAGEHENT BRANCH (HNBB 7714)~U.ST NUCLEAR REGULATORY COHHISSION, NASHINGTOH, DC 20555-0001 AND TO THE PAPERMORK REDUCTION PROJECT (3140-0104), OFFICE OF HANAGEHENT AMD BUDGET UASHIMGTON DC 20503.FACILITY IWK (1>Browns Fer Nuclear Plant BFN Unit.3 DOCKET NINRIER (2)05000296 PAGE (3)1 OF 5 TITLE (4>Unplanned Engineered Safety Feature Actuation following transfer of 480V RHOV Board 38 to its normal power supply after the replacement of a temporary normal supply breaker.EVENT DATE 5 REP(XIT DATE 7 OTHER FACILITIES INVOLVED 8 MONTH DAY YEAR'EQUENTIAL NUMBER'EVISIOM NUHBER HONTH DAY FACILITY NAHE N/A YEAR DOCKET NUMBER 11 08 GYRATING INX)E (9)LEVEL (10)95'5 007 00 THIS REPIXIT IS SUBMITTED PURSUANT 20.402(b)20.405(a)(1)(i) 000: 20.405(a)(1)(i i)20 405(a)(1)(iii) |
| !cist 4+i,%,'xwg4~clj'c';isa";> | | !cist 4+i,%,'xwg4~clj'c';isa";> |
|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:RO)
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML20199F2791998-12-0303 December 1998 Bfnp Unit 3 Cycle 8 ASME Section XI NIS-2 Data Rept ML20198D9621998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bfn,Units 1,2 & 3. with ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr 1999-09-30
[Table view] |
Text
j.Mj.~&(.j.'I Y 1 ACCELERATED RIDS PROCI'.SSIiG)
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR 9512110280 DOC DATE: 95/12/06 NOTARIZED-NO.DOCKET FACIL:50-296 Browns Ferry Nuclear Power Station, Unit 3, Tennessee 05000296 AUTH.NAME AUTHOR AFFILIATION WALLACE,J.E.
'ennessee Valley Authority MACHON,R.D.
Tennessee Valley Authority RECIP.NAME
, RECIPIENTAFFILIATION'UBJECT:
LER 95-007-00:on 951108,unplanned ESFA occurred following transfer of 480V.RMOV board 3B to.normal power supply after temporary normal supply'breaker was replaced.Caused by faulty amptector trip actuator.W/951206 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE TITLE: 50.73/50.9 Licensee Event Report (LER), ncident Rpt, etc.NOTES: RECIPIENT I D CODE/NAME PD2-3-PD INTERNAL: ACRS.AEOD/S PD/RRAB NRR/DE/ECGB.NRR/DE/EME B NRR/DRCH/HI CB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DSIR/EIB EXTERNAL: L ST LOBBY WARD NOAC MURPHY,G.A NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1'1 1 1'1 1 1 1 1 RECIPIENT ID CODE/NAME WILLIAMS,J.
I LE CEN~gh DE/EELB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPM/PECB NRR/DSSA/SRXB RGN2 FILE Ol LITCO BRYCE i J H NOAC POORE,W.NUDOCS FULL TXT COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1~1 1 1 1 1 2 2 1 1 1 1 VOTE TO ALL"RI DS" RECIPIENTS:
PLEASE ICELP US TO REDUCE 4VKSTE!CONTACT'I'I IE DOLL'i!CiT COiTROI.DESk, ROOil Pl-37 (I'.XT.04-~OS'TO I;Ll%Ill:%TE 5'OI.'R iAiIL I ROil DIS I'Rl DU I'IOi LIS'I'S I'OR DOCI'XII'.i'I'S YOU lmi"I'I I'.I)!FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 26 ENCL 26
Tennessee vattey Autronty.post office Box 2000.Decatur.Alabaina 35609.2000 R.D.(Rick)Machon Vice PresiCent.
Browns Ferry Huctear Pant December 6, 1995 U..S.Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C.20555
Dear Sir:
10 CFR 50.73 BROWNS PERRY NUCLEAR PLANT (BFN)-UNZTS 1g.2g AND 3-DOCKET NOS~'50-259~50-260~AND 50-296-FACILITY OPERATING LICENSE DPR-33~52~AND 68-LZCENSEE EVENT.REPORT 50-296/95007 The enclosed report provides details concerning the unplanned Engineered Safety Feature (ESF)actuation resulting from the transfer of 480V Reactor Motor Operated Valve Board 3B from its alternate power supply to its normal power supply.This report is submitted in accordance with 10 CFR 50.73(a)(2)(iv) as an event or condition that resulted in an automatic actuation of an ESF.Sincerel R.D.Machon Enclosure cc: See page 2 9512ii0280
~P0029 PDR ADo 8/p-'
4i U.S.Nuclear Regulator Commission Page 2 December 6, 1995 Enclosure c'c (Enclosure):
INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, Georgia 30339 Paul Krippner American Nuclear Insurers Town Center, Suite 300S 29 South Main Street West Hartford, Connecticut 06107 NRC Resident Inspector Browns Ferry Nuclear Plant 10833 Shaw Road Athens, Alabama 35611 Regional Administrator U.S.Nuclear Regulatory Commission Region II 101 Marietta Street;NW, Suite 2900 Atlanta, Georgia 30323 Mr.Z.F.Williams, Project Manager U.S.Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike-Rockville, Maryland 20852
- 4k ig)/1 NRC FORH 366 (5-92)~S.NUCLEAR REGULATORY CQSIISSION ROVED BY (RIB NO.3150-0104 EXPIRES 5/31/95 LZCENSEE EVENT REPORT (LER)(See reverse for required naker of digits/characters for each block)ESTIHATED BURDEN PER RESPONSE TO COHPLY IIITH THIS INFORHATION COLLECTION REQUEST: 50.0 HRS FORMARD COHHENTS REGARDING BURDEN ESTIHATE TO THE INFORHATIOH AND RECORDS HANAGEHENT BRANCH (HNBB 7714)~U.ST NUCLEAR REGULATORY COHHISSION, NASHINGTOH, DC 20555-0001 AND TO THE PAPERMORK REDUCTION PROJECT (3140-0104), OFFICE OF HANAGEHENT AMD BUDGET UASHIMGTON DC 20503.FACILITY IWK (1>Browns Fer Nuclear Plant BFN Unit.3 DOCKET NINRIER (2)05000296 PAGE (3)1 OF 5 TITLE (4>Unplanned Engineered Safety Feature Actuation following transfer of 480V RHOV Board 38 to its normal power supply after the replacement of a temporary normal supply breaker.EVENT DATE 5 REP(XIT DATE 7 OTHER FACILITIES INVOLVED 8 MONTH DAY YEAR'EQUENTIAL NUMBER'EVISIOM NUHBER HONTH DAY FACILITY NAHE N/A YEAR DOCKET NUMBER 11 08 GYRATING INX)E (9)LEVEL (10)95'5 007 00 THIS REPIXIT IS SUBMITTED PURSUANT 20.402(b)20.405(a)(1)(i) 000: 20.405(a)(1)(i i)20 405(a)(1)(iii)
!cist 4+i,%,'xwg4~clj'c';isa";>
<'xiPxy+~20 e 405 (a)(1)(i v)12 06 FACILITY NAHE N/A 95 DOCKET NUMBER 20.405(c)50.36(c)(1) 50.36(c)(2) 50.73(a)(2)(i)(B) 50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(iv) 50.73(a)(2)(v) 73.71(b)73.71(c)OTHER 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A>(Specify in 5073()(2)(vf I I)(B)Abstract hei ou and in Text, 50.73(a)(2)(x)
MRC Form 366A TO THE REQUIREMENTS OF 10 CFR": Check one or'more 11 LICENSEE CONTACT'FOR THIS LER 12 NAHE TELEPHONE NUHBER (Include Area Code)James E.Wallace, Compliance Engineer (205)729-7874 C(SIPLETE ONE LINE'FOR EACH IXNPONENT FAILURE DESCRIBED IN THIS REPORT'13 CAUSE SYSTEH X EC COHPONENT BKR HANUFACTURER TO NPRDS G080 CAUSE SYSTEH COMPONENT HANUFACTURER REPORTABLE TO NPRDS SUPPLEMENTAL REPIXIT EXPECTED 14 YES (I f,yes, complete EXPECTED SUBHISSION DATE).EXPECTED SUBHI SSI Ql DATE (15)HOMTH DAY YEAR ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten Lines)~(16)On November 8, 1995, at approximately 1347 hours0.0156 days <br />0.374 hours <br />0.00223 weeks <br />5.125335e-4 months <br /> Central Standard Time (CST), Unit 3 480V Reactor Motor Operated Valve (RMOV)Board 3B was transferred from its normal power supply to i.ts alternate power supply to support the installation of the permanent normal supply breaker.At 1357 hours0.0157 days <br />0.377 hours <br />0.00224 weeks <br />5.163385e-4 months <br />, after the permanent supply breaker was installed, an attempt to transfer 480V RMOV Board 3B back to i.ts permanent normal supply breaker resulted i.n the board de-energizing.
This loss of power to the 480V RMOV Board caused Reactor Protection System Bus 3B to de-energize, resulting in the initiation of the standby gas treatment system, control room emergency, venti.lation, system, and primary contai.nment isolation.
At the time of this event, Unit 3 was in cold shutdown and in the refueling mode.Unit 2 was operating at 100 percent power.Unit 1 was shutdown and defueled.The root cause of this event was a faulty Westinghouse Amptector Tri.p Actuator on the permanent normal supply breaker.Corrective acti.ons included replacing the faulty trip actuator and forwarding the faulty trip actuator to Westinghouse for failure analysis.This report is submitted in accordance wi.th 10 CFR 50.73(a)(2)(iv) as an event or condition that resulted in automatic actuation of an Engineered Safety Feature.HRC FORH ()
0ll ts, NRC FORH 366A (5-92)U.S.ISICLEAR REGIRATORY C(SSIISS ION IsICENSEE EVENT REPORT TEXT'ONTZNUATZON APPROVED SY aNI NO.3150-0104 EXPIRES 5/31/95 ESTIHATED BURDEN'PER RESPONSE TO CDHPLY WITH THIS INFORHATION COLLECT ION REQUEST: 50.0 HRS.FORWARD COHHENTS REGARDING BURDEN EST IHATE TO THE INFORMATION AMD RECORDS HAMAGEHENT BRANCH (HMBS 77N)~U.S.NUCLEAR REGULATORY CDHHISSIONg WASNINGTOM, DC 20555-0001
~AMD TO THE PAPERWORK REDUCI'ION PROJECT (3150-0104), OFFICE OF HANAGEHENT AND BUDGET, WASHINGTON DC 20503 FACILITY NAIE C1)Browne Ferry Unit 3 DocKET NIsmER (2)05000296 TEAR 95 LER NISISER C6)SEQUENTIAL MUHBER2 2 007 REVISION NUHBER 00 PAGE C3)2 of 5 TEXT If more s ce is r ired use addi lone(c ies of MRC Form 366A C17)I~PLANT CONDITIONS At the time of this event, Unit 3 was in cold shutdown and in the refueling mode.Unit 2, was operating at 100 percent power.Unit 1 was shutdown and defueled.II'ESCRIPTION OF EVENT ho Events B~On November 8, 1995, at approximately 1347 hours0.0156 days <br />0.374 hours <br />0.00223 weeks <br />5.125335e-4 months <br /> Central Standard Time (CST),'Unit 3 480V Reactor Motor Operated Valve (RMOV)Board (BD)3B[ED]was transferred from its normal power supply to its alternate power supply to allow the replacement of the temporary normal supply breaker with the permanent normal supply breaker.At 1357 hours0.0157 days <br />0.377 hours <br />0.00224 weeks <br />5.163385e-4 months <br />, after the permanent normal supply breaker was installed, an attempt to transfer 480V RMOV BD 3B back to its normal supply resulted in the board de-energi.zi.ng because the permanent normal supply breaker failed to latch closed (tripped free).The board was re-energized by its alternate power supply.This loss of power to 480V RMOV BD 3B resulted in the Reactor Protecti.on System (RPS)[JC]Bus 3B de-energizing, which caused a half scram in channel B.This also resulted in primary containment i.solation
[JM]system groups 2[BO], 3[CE], and 6[VB]isolations, and standby gas treatment system[BH]and control room emergency ventilation system[VZ]actuations.
At 1403 hours0.0162 days <br />0.39 hours <br />0.00232 weeks <br />5.338415e-4 months <br />, the half scram was reset, the.RPS was re-energi.zed and the ESF systems were returned to standby readiness.
At 1443 hours0.0167 days <br />0.401 hours <br />0.00239 weeks <br />5.490615e-4 months <br />, the temporary normal supply breaker was installed and placed in service without any additional problems.This event is reportable in accordance with 10 CFR 50.73 (a)(2)(iv) as an event or condition that resulted in an unplanned actuation of an engineered safety feature (ESF).Ino erable Structures Cam nents or S stems that Contributed to the Events A trip actuator for a Westinghouse Amptector 1A solid state trip devi.ce installed in a General Electric AK type breaker.
41 0 HRC FORH 366A (5-92)U.S.WCLEAR REGULATORY COHIISSIOH LICENSEE EVENT REPORT TEXT CONTINUATION APPROVED BY QS NO.3150-0104 EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPOHSE TO COHPLY llITH THIS INFORHATION COLLECTION REOUEST: 50.0 HRS.FORMARD COHHENTS REGARD IHG BURDEN EST IHATE TO THE INFORNATI ON AND RECORDS HANAGEHENT BRANCH (HNBB 7714)~U.S.NUCLEAR REGULATORY COHHISSION, NASH INGTOH, DC 20555-0001
~AND TO THE PAPERUORK REDUCTION PROJECT'(3150-0104), OFFICE OF HANAGEHENT AND BN)GET~IIASHINGTON DC 20503 FACILITY HA%(1)Browns Ferry Unit 3 DOCKET HQSER (2)05000296 LER HISSER (6)YEAR SEQUENTIAL REVISION NUHBER3 3 HUHBER 95 007'00 PAGE (3)3 of 5 TEXT If more s ce is r ired use sdditionsl co ies of NRC Form 366A (17)Co Dates and A roximate Times of Ma or Occurrencest November 8, 1995 at 1347 hours0.0156 days <br />0.374 hours <br />0.00223 weeks <br />5.125335e-4 months <br />, CST at 1357 hours0.0157 days <br />0.377 hours <br />0.00224 weeks <br />5.163385e-4 months <br />, CST at 1403 hours0.0162 days <br />0.39 hours <br />0.00232 weeks <br />5.338415e-4 months <br />, CST Transferred 480V RMOV BD 3B to its alternate.power supply to replace the temporary normal supply breaker with the permanent normal supply breaker.Attempt to transfer 480V RMOV BD 3B back to its normal power supply resulted in the board de-energizing.
The board was re-energized from its alternate power supply-Reset the half scram, re-energized the RPS, and returned ESF, systems to standby readiness.
at 1443 hours0.0167 days <br />0.401 hours <br />0.00239 weeks <br />5.490615e-4 months <br />, CST Re-installed the temporary normal supply breaker and placed 480V RMOV BD 3B on its normal power supply.Do Other S stems'or Seconds Functions Affecteds None.Xethod of Discove I This condition was discovered when the Unit Operator[utility, 1'icensed]
received the half scram on RPS Bus 3B, which initiated the ESFs.erator Actionst The RPS was re-energized, and the ESF systems were returned to standby readiness.
Safet S stem Res onsess Safety systems responded as designed for this type of event.
41 4~yf h NRC F(RH 366A (5.92)LICENSEE BVENT REPORT TEXT CONTINUATION FACILITY'AIK (1)DOCKET NINBER (2)0 S.IRICLEAR REGUIAT(XIY CQHISSImi APPROVED BY (NNI NO.3150-0104 EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY llITH THIS INFORHATION COLLECTION REQUEST: 50.0 HRS.FORNARD COHHENTS REGARDING BURDEN EST IHATE TO THE INFORHAT I ON AND RECORDS HAMAGEHENT BRANCH (HNBB 7714), U.S.NUCLEAR REGULATORY COHHISS IONg NASHINGTON, DC 20555 0001, AMD TO THE PAPERNORK REDUCTIOH , PROJECT.(3150-0104)
~OFFICE OF HANAGEHENT AND BUDGET, NASHINGTON DC 20503 LER RIBBER (6)PAGE (3)YEAR SEQUENTIAL REVISION.NUHBER4 4 NUHBER Browns Ferry Unit 3 05000296 95 007 00 4 of 5 TEXT If more s ce is r ired use additional co ies of NRC Form 366A (17)ZIZ~CAUSE OF THE EVENT Immedi.ate Causet B During the transfer of the 480V RMOV BD 3B from its alternate to its normal power supply, the permanent normal supply breaker for 480V RMOV BD 3B failed to latch closed (tripped free).'oot Causet The root cause of this event was a faulty breaker trip actuator.Specifically, a magnet that was glued to the trip actuator became unglued resulting in an unplanned operation of the trip device.ZVo ANALYSIS OF THE BVENT'The systems affected during this event are designed to shutdown the reactor, to contain and process any radioactive releases, and to fulfill their safety functions upon loss of initiation logic power.The systems responded correctly to the loss of power;therefore, plant safety was not adversely affected.The plant's safe shutdown capabilities would not have been diminished had Unit 3 been in power operation.
Accordingly, this event did not affect the health and safety of plant personnel or the public.Vs CORRBCTIVE ACTIONS Ao Immediate Corrective Actionss The.480V RMOV BD was re<<energized by its alternate power.supply.The RPS was re-energized and the ESF systems were returned to standby readiness.
The breakers and actuator had been successfully bench tested and field tested prior to installation.
i>i NRC FORM 366A (5-92)U S IN)CLEAR REGULATORY CQBII SSI IXI LICENSEE EVENT REPORT'TEXT CONTZNUATZON APPROVED BY (HEI.NO 3150-0104 EXPran 5I31/95 ESTIMATED BURDEN PER RESPONSE TO'COMPLY IJITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.FORNARD COMMENTS REGARDING BURDEN ESTIMATE TO THE'INFORHATION AND RECORDS NAMAGENENT BRANCH (HHBB 7714),.U.S.NUCLEAR REGULATORY COMMISSION, NASHIMGTON, DC 20555-0001, AMD TO THE PAPERlQRK REDUCTION PROJECT (3150-0104)
~OFFICE OF HAMAGEHENT AMD BUDGET~l!ASHINGTOM DC 20503 FACILITY NJUK (1)Browns Ferry Unit 3 DOCKET NINBER (2)05000296 LER NIHQKR (6)YEAR SEQUENTIAL REVISION NUMBERS 5 NUMBER 95 007 00 PAGE (3)5 of 5 TEXT If more s ce is r ired use additional co ies of NRC Form 366A (17)Bi Corrective Actions to Prevent Recurrencel Corrective actions included reinstalling the temporary normal supply breaker, re-energixing the board, and troubleshooting the permanent normal supply breaker.Following troubleshooting, the faulty trip actuator was disassembled, and the temporary breaker was removed from the board.After a new actuator was installed in the breaker, the'breaker was reinstalled and the board was transferred successfully.
The faulty actuator was forwarded to Westinghouse for failure analysis.Zf the results of Westinghouse's investigation significantly alter either the.cause or the coriective actions for this event, a supplemental report will be submitted.
Additionally, any further corrective actions.that are developed as a result of the investigation will be implemented in accordance with TVA's corrective action process.VZ~ADDITIONAL INFORNATZON Ao Failed Com nentsI h A trip actuator for a Westinghouse Amptector 1A solid state device installed in a General Electric AK type breaker.There are currently 11 other AK breakers with the Westinghouse amptector trip device installed in Unit 3 (none installed i.n Units 1 or 2).Prior to installati.on, these breakers were simi'larly bench tested and fi.eld tested.However, none of these breakers have experienced similar failures.Bo Previous LERs on Similar Events!LER 260/88009 addressed three separate occasions where the normal/alternate, supply breakers failed to close because of the dirty conditions of the sli.ding secondary di.sconnects in the breaker control logic.The root cause of LER 260/88009 was the lack of preventive maintenance.
LER 296/95007 was not caused:by a lack of, preventive maintenance.
VZ I~COMMITMENTS None.Energy Industry Identification System (EIIS)system and component codes are identified in the text with brackets (e.g.,[XX)).
U.S.Nuclear Regulatory Commission Page 3 December 6, 1995 PS: SAW: JEW:MTN Enclosure cc (Enclosure):
C.W.Beasley, PAB 1B-BFN P.P.Carier, BR.4G-C L.S.Clardy, CFC 1C-BFN C.T.Dexter,'BFT 3A-BFN J.A.Frost,, POB 2E-BFN O..D.Kingsley, LP 6A-C John P.Maciejewski, LP 3B-C J.Scott Martin, PMC 1D-BFN T.J.McGrath, LP 3B-C M.0.Medford, LP 3B-C G.D.Pierce, PEB 1B-BFN E.Preston, POB 2C-BFN C.M.Root, CFC 1D-BFN R.H.Shell, 0&PS 4C-SQN T.D.Shriver, PAB 1A-BFN H.L.Williams, EDB lA-BFN 0.J.Zeringue, LP 3B-C RIMS, WT 3B-K a%m85007a3 e'er Oi