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| number = ML18024B534
| number = ML18024B534
| issue date = 05/07/1979
| issue date = 05/07/1979
| title = Responds to NRC 790413 Ltr Re Violations Noted in IE Insp Repts 50-413/79-05 & 50-414/79-05.Corrective Actions: Nitrogen Blanket Placed on Heat Exchanger & Personnel Instructed Re Nonconforming Item Rept
| title = Responds to NRC Re Violations Noted in IE Insp Repts 50-413/79-05 & 50-414/79-05.Corrective Actions: Nitrogen Blanket Placed on Heat Exchanger & Personnel Instructed Re Nonconforming Item Rept
| author name = Dail L
| author name = Dail L
| author affiliation = DUKE POWER CO.
| author affiliation = DUKE POWER CO.
Line 11: Line 11:
| contact person =  
| contact person =  
| document report number = NUDOCS 7906180741
| document report number = NUDOCS 7906180741
| title reference date = 04-13-1979
| package number = ML18024B535
| package number = ML18024B535
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE, UTILITY TO NRC
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE, UTILITY TO NRC
Line 17: Line 18:


=Text=
=Text=
{{#Wiki_filter:~S RE0II,                               UNITED STATES fpO
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                    ~i               NUCLEAR REGULATORY COMMISSION ce ee                  fl                          REGION II P
ce
I                                          101 MARIETTASTREET, N.W, Cl O~
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ATLANTA,GEORGIA 30303
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        +a*++
UNITEDSTATES NUCLEAR REGULATORYCOMMISSION REGION II 101 MARIETTASTREET, N.W, ATLANTA,GEORGIA 30303 Report Nos. 50-259/79-08, 50-260/79-06, and 50-296/79-08 Licensee:
Report Nos. 50-259/79-08, 50-260/79-06, and 50-296/79-08 Licensee:           Tennessee Valley Authority 500A Chestnut Street Tower       II Chattanooga, Tennessee 37401 Facility Name:             Browns Ferry Nuclear Plant Docket Nos. DPR-33, DPR-52, and DPR-68 Inspection at Browns erry Site near Athens, Alabama Inspector:
Tennessee Valley Authority 500A Chestnut Street Tower II Chattanooga, Tennessee 37401 Facility Name:
            ~R.         F. Su   ivan                                               Date Signed Approved by:
Browns Ferry Nuclear Plant Docket Nos. DPR-33, DPR-52, and DPR-68 Inspection at Browns erry Site near Athens, Alabama Inspector:~R. F. Su ivan Approved by:
                              '
>dI H. C. Dance, ection Chief, RONS Branch Date Signed 3 2+ 7f Date Signed
                                    >dI                                             3 2+    7f H. C. Dance,     ection Chief,   RONS Branch                 Date Signed


==SUMMARY==
==SUMMARY==
Inspection on February 5 - March 2, 1979
~A This inspection involved 83 resident inspector-hours in the areas of report-able occurrences, review plant operation, on-site review function, fire protection system and plant physical protection.
Results Of the five areas inspected, no apparent items of noncompliance or deviations were identified.
79081 50p/g


Inspection on February           5 -  March 2, 1979
4 DETAILS Persons Contacted J.
~A This inspection involved 83 resident inspector-hours in the areas of report-able occurrences, review plant operation, on-site review function, fire protection system            and plant physical protection.
J.
Results Of the five areas inspected, no apparent items                 of noncompliance or deviations were identified.
R.
79081 50 p/g
J.
M.
R.
D.
."., R.
Licensee Em lo ees l
J.
G. Dewease, Plant Superintendent H. L. Abercrombie, Assistant Plant Superintendent L. Harness, QA Supervisor B. Studdard, Operations Supervisor Hunkapillar, Assistant, Operations Supervisor A. Teague, Assistant Maintenance Supervisor, Electrical A. Haney, Assistant Maintenance Supervisor, Mechanical G. Metke, Results Section Supervisor J. L. Harness, Quality Assurance Supervisor J.
R. Pittman, Instrument Engineer G. T. Jones, Outage Director S.
G. Bugg, Health Physics Supervisor W.
C. Thomison, Chemical Engineer A. L. Burnett, Shift Engineer J.
D. Glover, Shift Engineer Thompson, Electrical Engineer
: Cole, QA Site. Representative, Office of Power
~Other licensee employees contacted included operators, craftsmen, technicians, public safety officers, QA personnel and engineering personnel.
'I h
Mana ement Interviews Management interviews were conducted on February 9, 16, 23 and March 2, 1979 with the Plant Superintendent and selected members of his staff.
The inspector summarized the scope 'nd findings of his inspection activities.
The licensee was informed that no items of noncompliance or deviations were identified.
3.
Licensee Action on Previous Ins ection Findin s Not inspected.
4, Unresolved Items No unresolved items were identified during this inspection.


4 DETAILS Persons  Contacted Licensee  Em  lo  ees l
Plant erations The inspector kept informed on a daily basis on the overall plant operating status and any significant safety matters related to plant operations.
J. G. Dewease, Plant Superintendent H. L. Abercrombie, Assistant Plant Superintendent J. L. Harness, QA Supervisor J. B. Studdard, Operations Supervisor R. Hunkapillar, Assistant, Operations Supervisor J. A. Teague, Assistant Maintenance Supervisor, Electrical M. A. Haney, Assistant Maintenance Supervisor, Mechanical R. G. Metke, Results Section Supervisor J. L. Harness, Quality Assurance Supervisor J. R. Pittman, Instrument Engineer G. T. Jones, Outage Director S. G. Bugg, Health Physics Supervisor W. C. Thomison, Chemical Engineer A. L. Burnett, Shift Engineer J. D. Glover, Shift Engineer D. Thompson, Electrical Engineer
Daily discussions were held with plant management and members of the operations staff.
  ."., R. Cole, QA Site. Representative,    Office of  Power
Selected portions of the various daily operating journals and data sheets were reviewed on at least a
      ~ Other licensee employees contacted included operators, craftsmen, technicians, public safety officers, QA personnel and engineering personnel.              'I h
weekly basis during the report period.
Mana ement    Interviews Management interviews were conducted on February 9, 16, 23 and March 2, 1979 with the Plant Superintendent and selected members of his staff.
The inspector made plant tours on the following dates:
The inspector summarized the scope      'nd  findings of his inspection activities. The licensee was informed      that  no items of noncompliance or deviations were identified.
2/8, 2/16, 2/22, 2/27 and 2/28.
: 3.      Licensee Action on Previous Ins ection Findin      s Not inspected.
Selected areas of the turbine building, reactor buildings and outside areas were visited.
4,      Unresolved Items No unresolved items were    identified during this inspection.
The control rooms were visited on a
 
more frequent basis than other areas of the plant.
Plant    erations The   inspector kept informed on a daily basis on the overall plant operating status and any significant safety matters related to plant operations. Daily discussions were held with plant management and members of the operations staff. Selected portions of the various daily operating journals and data sheets were reviewed on at least a weekly basis during the report period.
Observations included work activities in progress, valve positions, status of operating and standby safety
The   inspector made plant tours on the following dates: 2/8, 2/16, 2/22, 2/27 and 2/28. Selected areas of the turbine building, reactor buildings and outside areas were visited. The control rooms were visited on a more frequent basis than other areas of the plant.
: systems,
Observations included work activities in progress, valve positions, status of operating and standby safety systems, >nubbers, instrument readings and recordings, panel indications, housekeeping and vital areas controls.
>nubbers, instrument readings and recordings, panel indications, housekeeping and vital areas controls.
The tour of 2/28 was in the company of the plant electrical engineer whose responsibilities include overview of the       fire protection alarm and automatic initiation systems.     Emphasis was placed on valve line ups and operability of alarms and automatic controls for protection of safety-related equipment.
The tour of 2/28 was in the company of the plant electrical engineer whose responsibilities include overview of the fire protection alarm and automatic initiation systems.
I           H Informal discussions were held with operators and other personnel on work activities in progress and status of safety-related equipment or systems.     The inspector's questions were satisfactorily answered.
Emphasis was placed on valve line ups and operability of alarms and automatic controls for protection of safety-related equipment.
Shift change was observed in the control rooms on 2/7 and,2/21. On the latter date shutdown of Unit 2 was observed in the control room.
I H
On 2/27 startup operations including subcritical rod withdrawal and bringing the reactor critical were witnessed by the inspector. An unannounced visit to observe operations was also made on 2/19 which was a holiday.     On all the above occasions, the Technical Specifica-tions staffing requirements were met.
Informal discussions were held with operators and other personnel on work activities in progress and status of safety-related equipment or systems.
No item of noncompliance or deviations were identified by the inspector.
The inspector's questions were satisfactorily answered.
Re ortable Occurrences Review The below     listed licensee event reports were reviewed to determine   if the information provided met NRC reporting requirements. The determi-nation included adequacy of event description and corrective action taken or planned, existence of potential generic problems and the relative safety significance.
Shift change was observed in the control rooms on 2/7 and,2/21.
On the latter date shutdown of Unit 2 was observed in the control room.
On 2/27 startup operations including subcritical rod withdrawal and bringing the reactor critical were witnessed by the inspector.
An unannounced visit to observe operations was also made on 2/19 which was a holiday.
On all the above occasions, the Technical Specifica-tions staffing requirements were met.
No item of noncompliance or deviations were identified by the inspector.
Re ortable Occurrences Review The below listed licensee event reports were reviewed to determine if the information provided met NRC reporting requirements.
The determi-nation included adequacy of event description and corrective action taken or planned, existence of potential generic problems and the relative safety significance.


LER No.
LER No.
                    \
Date
Date              Event 259/7837           32/29/78         Check valve in HPCE faile4 in open position Drywell oxygen concentration greater'han
\\
                '
259/7837 32/29/78 260/7817 10/25/78 Event Check valve in HPCE faile4 in open position Drywell oxygen concentration greater'han 4 percent 260/7822 12/22/78
260/7817          10/25/78 4 percent 260/7822           12/22/78       'efueling floor ventilation     monitor inoperative 260/791       "
'efueling floor ventilation monitor inoperative 260/791 2/8/79 HPC I inoperable 260/792 296/791 3/1/79 Fire protection panel 25-326 in the control room inoperative 1/30/79 Reactor water level switch inoperative 296/791
2/8/79   .        HPC I inoperable 260/792           3/1/79           Fire protection panel 25-326 in the control room inoperative 296/791            1/30/79           Reactor water level switch inoperative 296/791     '/6/79                   Automatic   initiation of protection inoperative one zone in fire Corrective action taken or implemented         on the above events was deter-mined to be adequate.       No items of noncompliance or deviations were identified.
'/6/79 Automatic initiation of one zone in fire protection inoperative Corrective action taken or implemented on the above events was deter-mined to be adequate.
: 7. Plant     erations Review Committee       (PORC)
No items of noncompliance or deviations were identified.
The functions and activities of the PORC, which serves as the onsite review committee, -were reviewed for the period September 6,- 1978 through February 15, 1979 to determine conformance to Technical Speci-fications requirements and the Charter described in the Operational Quality Assurance Manual. Meeting minutes confirmed that meetings were conducted with a quorum of qualified members present           within the required frequency. Items coming before the Committee included among other things, new procedures, procedure revisions, corrective section reports, Licensee Events Reports, Scram Reports, Work Plans, Proposed Technical Specification changes, License Amendments, nonconforming items, test reports and noncompliance items.
7.
Plant erations Review Committee (PORC)
The functions and activities of the PORC, which serves as the onsite review committee, -were reviewed for the period September 6,- 1978 through February 15, 1979 to determine conformance to Technical Speci-fications requirements and the Charter described in the Operational Quality Assurance Manual.
Meeting minutes confirmed that meetings were conducted with a quorum of qualified members present within the required frequency.
Items coming before the Committee included among other things, new procedures, procedure revisions, corrective section
: reports, Licensee Events Reports, Scram Reports, Work Plans, Proposed Technical Specification
: changes, License Amendments, nonconforming items, test reports and noncompliance items.
8.
Xn addition to reviewing the records of PORC the inspector interviewed various members of the Committee on selected topics. All the inspector's question were satisfactorily answered.
Xn addition to reviewing the records of PORC the inspector interviewed various members of the Committee on selected topics. All the inspector's question were satisfactorily answered.
: 8. Plant Dewaterin     S stem E
Plant Dewaterin S stem E
Repairs "and modifications to the plant dewatering system, which were accomplished during the report period, were followed by the inspector.
Repairs "and modifications to the plant dewatering
: system, which were accomplished during the report period, were followed by the inspector.
Simultaneous failure of both dewatering pumps had led to building in-leakage problems as described in a previous inspection report (lE Report 50-259/79-4).
Simultaneous failure of both dewatering pumps had led to building in-leakage problems as described in a previous inspection report (lE Report 50-259/79-4).


By the end   of this report period, "B" well       had a new stainless steel liner installed inside the concrete casing and the electric pump had been rebuilt with subsequent satisfactory performance.           A new larger-diameter well, also with a stainless steel liner, had been sunk nearby.
By the end of this report period, "B" well had a new stainless steel liner installed inside the concrete casing and the electric pump had been rebuilt with subsequent satisfactory performance.
This well currently has a diesel driven pump installed which test operated satisfactorily. Final determination of the type of pump for this well has not been made. This well has been designated as standby to "B" well. "A" well which had suffered casing damage will be aban-doned due to reluctance to attempt clean-out because of its close proximity to "B" well.
A new larger-diameter well, also with a stainless steel liner, had been sunk nearby.
A program   of test well drilling is under consideration to learn more about the underground water paths and the advisability of sinking additional dewatering wells. Recent experience following a heavy rainstorm has demonstrated that no in-leakage problem developed with the current system.
This well currently has a diesel driven pump installed which test operated satisfactorily.
: 9. Plant Ph sical Protection The inspector observed on a routine basis personnel badging, searching, escort, and vehicle and escort control practices. Vital area controls were also observed.             No items of noncompliance or deviations were identified.
Final determination of the type of pump for this well has not been made.
t                                           4
This well has been designated as standby to "B" well.
              ~ 44 ~ 4 tt tat ~   ~ t 4
"A" well which had suffered casing damage will be aban-doned due to reluctance to attempt clean-out because of its close proximity to "B" well.
                        /4}}
A program of test well drilling is under consideration to learn more about the underground water paths and the advisability of sinking additional dewatering wells.
Recent experience following a heavy rainstorm has demonstrated that no in-leakage problem developed with the current system.
9.
Plant Ph sical Protection The inspector observed on a routine basis personnel badging, searching,
: escort, and vehicle and escort control practices.
Vital area controls were also observed.
No items of noncompliance or deviations were identified.
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Latest revision as of 04:15, 7 January 2025

Responds to NRC Re Violations Noted in IE Insp Repts 50-413/79-05 & 50-414/79-05.Corrective Actions: Nitrogen Blanket Placed on Heat Exchanger & Personnel Instructed Re Nonconforming Item Rept
ML18024B534
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 05/07/1979
From: Dail L
DUKE POWER CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18024B535 List:
References
NUDOCS 7906180741
Download: ML18024B534 (5)


Text

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~i ee flP ICl O~

+a*++

UNITEDSTATES NUCLEAR REGULATORYCOMMISSION REGION II 101 MARIETTASTREET, N.W, ATLANTA,GEORGIA 30303 Report Nos. 50-259/79-08, 50-260/79-06, and 50-296/79-08 Licensee:

Tennessee Valley Authority 500A Chestnut Street Tower II Chattanooga, Tennessee 37401 Facility Name:

Browns Ferry Nuclear Plant Docket Nos. DPR-33, DPR-52, and DPR-68 Inspection at Browns erry Site near Athens, Alabama Inspector:~R. F. Su ivan Approved by:

>dI H. C. Dance, ection Chief, RONS Branch Date Signed 3 2+ 7f Date Signed

SUMMARY

Inspection on February 5 - March 2, 1979

~A This inspection involved 83 resident inspector-hours in the areas of report-able occurrences, review plant operation, on-site review function, fire protection system and plant physical protection.

Results Of the five areas inspected, no apparent items of noncompliance or deviations were identified.

79081 50p/g

4 DETAILS Persons Contacted J.

J.

R.

J.

M.

R.

D.

."., R.

Licensee Em lo ees l

J.

G. Dewease, Plant Superintendent H. L. Abercrombie, Assistant Plant Superintendent L. Harness, QA Supervisor B. Studdard, Operations Supervisor Hunkapillar, Assistant, Operations Supervisor A. Teague, Assistant Maintenance Supervisor, Electrical A. Haney, Assistant Maintenance Supervisor, Mechanical G. Metke, Results Section Supervisor J. L. Harness, Quality Assurance Supervisor J.

R. Pittman, Instrument Engineer G. T. Jones, Outage Director S.

G. Bugg, Health Physics Supervisor W.

C. Thomison, Chemical Engineer A. L. Burnett, Shift Engineer J.

D. Glover, Shift Engineer Thompson, Electrical Engineer

Cole, QA Site. Representative, Office of Power

~Other licensee employees contacted included operators, craftsmen, technicians, public safety officers, QA personnel and engineering personnel.

'I h

Mana ement Interviews Management interviews were conducted on February 9, 16, 23 and March 2, 1979 with the Plant Superintendent and selected members of his staff.

The inspector summarized the scope 'nd findings of his inspection activities.

The licensee was informed that no items of noncompliance or deviations were identified.

3.

Licensee Action on Previous Ins ection Findin s Not inspected.

4, Unresolved Items No unresolved items were identified during this inspection.

Plant erations The inspector kept informed on a daily basis on the overall plant operating status and any significant safety matters related to plant operations.

Daily discussions were held with plant management and members of the operations staff.

Selected portions of the various daily operating journals and data sheets were reviewed on at least a

weekly basis during the report period.

The inspector made plant tours on the following dates:

2/8, 2/16, 2/22, 2/27 and 2/28.

Selected areas of the turbine building, reactor buildings and outside areas were visited.

The control rooms were visited on a

more frequent basis than other areas of the plant.

Observations included work activities in progress, valve positions, status of operating and standby safety

systems,

>nubbers, instrument readings and recordings, panel indications, housekeeping and vital areas controls.

The tour of 2/28 was in the company of the plant electrical engineer whose responsibilities include overview of the fire protection alarm and automatic initiation systems.

Emphasis was placed on valve line ups and operability of alarms and automatic controls for protection of safety-related equipment.

I H

Informal discussions were held with operators and other personnel on work activities in progress and status of safety-related equipment or systems.

The inspector's questions were satisfactorily answered.

Shift change was observed in the control rooms on 2/7 and,2/21.

On the latter date shutdown of Unit 2 was observed in the control room.

On 2/27 startup operations including subcritical rod withdrawal and bringing the reactor critical were witnessed by the inspector.

An unannounced visit to observe operations was also made on 2/19 which was a holiday.

On all the above occasions, the Technical Specifica-tions staffing requirements were met.

No item of noncompliance or deviations were identified by the inspector.

Re ortable Occurrences Review The below listed licensee event reports were reviewed to determine if the information provided met NRC reporting requirements.

The determi-nation included adequacy of event description and corrective action taken or planned, existence of potential generic problems and the relative safety significance.

LER No.

Date

\\

259/7837 32/29/78 260/7817 10/25/78 Event Check valve in HPCE faile4 in open position Drywell oxygen concentration greater'han 4 percent 260/7822 12/22/78

'efueling floor ventilation monitor inoperative 260/791 2/8/79 HPC I inoperable 260/792 296/791 3/1/79 Fire protection panel 25-326 in the control room inoperative 1/30/79 Reactor water level switch inoperative 296/791

'/6/79 Automatic initiation of one zone in fire protection inoperative Corrective action taken or implemented on the above events was deter-mined to be adequate.

No items of noncompliance or deviations were identified.

7.

Plant erations Review Committee (PORC)

The functions and activities of the PORC, which serves as the onsite review committee, -were reviewed for the period September 6,- 1978 through February 15, 1979 to determine conformance to Technical Speci-fications requirements and the Charter described in the Operational Quality Assurance Manual.

Meeting minutes confirmed that meetings were conducted with a quorum of qualified members present within the required frequency.

Items coming before the Committee included among other things, new procedures, procedure revisions, corrective section

reports, Licensee Events Reports, Scram Reports, Work Plans, Proposed Technical Specification
changes, License Amendments, nonconforming items, test reports and noncompliance items.

8.

Xn addition to reviewing the records of PORC the inspector interviewed various members of the Committee on selected topics. All the inspector's question were satisfactorily answered.

Plant Dewaterin S stem E

Repairs "and modifications to the plant dewatering

system, which were accomplished during the report period, were followed by the inspector.

Simultaneous failure of both dewatering pumps had led to building in-leakage problems as described in a previous inspection report (lE Report 50-259/79-4).

By the end of this report period, "B" well had a new stainless steel liner installed inside the concrete casing and the electric pump had been rebuilt with subsequent satisfactory performance.

A new larger-diameter well, also with a stainless steel liner, had been sunk nearby.

This well currently has a diesel driven pump installed which test operated satisfactorily.

Final determination of the type of pump for this well has not been made.

This well has been designated as standby to "B" well.

"A" well which had suffered casing damage will be aban-doned due to reluctance to attempt clean-out because of its close proximity to "B" well.

A program of test well drilling is under consideration to learn more about the underground water paths and the advisability of sinking additional dewatering wells.

Recent experience following a heavy rainstorm has demonstrated that no in-leakage problem developed with the current system.

9.

Plant Ph sical Protection The inspector observed on a routine basis personnel badging, searching,

escort, and vehicle and escort control practices.

Vital area controls were also observed.

No items of noncompliance or deviations were identified.

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