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| {{#Wiki_filter:j.Mj.~kc.j. | | {{#Wiki_filter:j.Mj.~kc.j.I'Y<Accr LERATr D RIDs proc!'.sslic REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9410270370 DOC.DATE: 94/10/17 NOTARIZED: |
| I'Y<AccrLERATrDRIDsproc!'.sslic REGULATORY INFORMATION DISTRIBUTION SYSTEM(RIDS)ACCESSION NBR:9410270370 DOC.DATE: | | NO FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G AUTH.NAME AUTHOR AFFILIATION ST MARTIN,J.T. |
| 94/10/17NOTARIZED: | | Rochester Gas&Electric Corp.MECREDY,R.C. |
| NOFACIL:50-244 RobertEmmetGinnaNuclearPlant,Unit1,Rochester GAUTH.NAMEAUTHORAFFILIATION STMARTIN,J.T.
| | Rochester Gas&Electric Corp.RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000244 P |
| Rochester Gas&ElectricCorp.MECREDY,R.C. | |
| Rochester Gas&ElectricCorp.RECIP.NAME RECIPIENT AFFILIATION DOCKET05000244P | |
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| ==SUBJECT:== | | ==SUBJECT:== |
| LER94-011-00:on 940917,indicating lampon"B"trainsafeguards initiation cabinetfailed.Causedbylossof125VDCcontrolpower.Burnedoutindicating lamp&blownfusereplaced.W/941017 ltr.DISTRIBUTION CODE:IE22TCOPIESRECEIVED:
| | LER 94-011-00:on 940917,indicating lamp on"B" train safeguards initiation cabinet failed.Caused by loss of 125 VDC control power.Burned out indicating lamp&blown fuse replaced.W/941017 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED: LTR I ENCL i SIZE: l TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). |
| LTRIENCLiSIZE:lTITLE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.NOTES:License Expdateinaccordance with10CFR2,2.109(9/19/72).
| | R 05000244 RECIPIENT ID CODE/NAME PD1-3 PD INTERNA EOD/~OA'B/D FILE CMTER 02 E EMEB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DSSA/SPLB NRR/PMAS/IRCB-E RGN1 FILE 01 EXTERNAL EG&G BRYCE I J~H NOAC MURPHY,G.A NRC PDR COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 RECIPIENT ID CODE/NAME JOHNSON,A AEOD/SPD/RRAB NRR/DE/EELB NRR/DORS/OEAB NRR/DRCH/HICB NRR/DRSS/PRPB NRR/DSSA/SRXB RES/DSIR/EIB L ST LOBBY WARD NOAC POORE,W.NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 D~ff z-o745/2~~U YOTE TO ALL"RIDS" RECIPIENTS: |
| R05000244RECIPIENT IDCODE/NAME PD1-3PDINTERNAEOD/~OA'B/D FILECMTER02EEMEBNRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DSSA/SPLB NRR/PMAS/IRCB-E RGN1FILE01EXTERNALEG&GBRYCEIJ~HNOACMURPHY,G.A NRCPDRCOPIESLTTRENCL112211111111111111221111RECIPIENT IDCODE/NAME JOHNSON,A AEOD/SPD/RRAB NRR/DE/EELB NRR/DORS/OEAB NRR/DRCH/HICB NRR/DRSS/PRPB NRR/DSSA/SRXB RES/DSIR/EIB LSTLOBBYWARDNOACPOORE,W.NUDOCSFULLTXTCOPIESLTTRENCL1111111111221111111111D~ffz-o745/2~~UYOTETOALL"RIDS"RECIPIENTS:
| | PLEASE HELP US TO RFDUCE iVASTE!CONTACT'I'I IE DOCl'iIEiT CONTROL DESk.ROOXI Pl-37 (EXT.504-20S3)TO FLIXIliATE O'OI:R XAXILZ FROiI DISTRIBUTION LIS'I'S I'OR l)OCl iIEi'I'S 5'OL')Oi"I''L'I'.II)! |
| PLEASEHELPUSTORFDUCEiVASTE!CONTACT'I'I IEDOCl'iIEiT CONTROLDESk.ROOXIPl-37(EXT.504-20S3)TOFLIXIliATE O'OI:RXAXILZFROiIDISTRIBUTION LIS'I'SI'ORl)OCliIEi'I'S5'OL')Oi"I''L'I'.II)!
| | FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 26 ENCL 26 |
| FULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:
| | ~v~v I~v I soac 7 s1<TC ROCHESTER GAS AND ELECTRIC CORPORATION |
| LTTR26ENCL26
| | ~89-EAST AVENUE, ROCHESTER N.Y.14649.0001 ROBERTC MECRfOY Vice President Cinna Nuclear Producrion TELEPHONE AREA CODE 716 546 2700 October 17, 1994 U.S.Nuclear Regulatory Commission Document Control Desk Attn: Allen R.Johnson PWR Project Directorate I-3 Washington, D.C.20555 |
| ~v~vI~vIsoac7s1<TCROCHESTER GASANDELECTRICCORPORATION | |
| ~89-EASTAVENUE,ROCHESTER N.Y.14649.0001 ROBERTCMECRfOYVicePresident CinnaNuclearProducrion TELEPHONE AREACODE7165462700October17,1994U.S.NuclearRegulatory Commission DocumentControlDeskAttn:AllenR.JohnsonPWRProjectDirectorate I-3Washington, D.C.20555 | |
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| ==Subject:== | | ==Subject:== |
| LER94-011,ShortCircuitinIndicating LampCausesBlownFuse,Resulting inDisabling ofAutomatic Actuation ofEngineered SafetyFeaturesActuation Systemfor"B"Safeguards LogicTrainComponents R.E.GinnaNuclearPowerPlantDocketNo.50-244Inaccordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(i)(B),whichrequiresareportof,"anyoperation orcondition prohibited bytheplant'sTechnical Specifications",
| | LER 94-011, Short Circuit in Indicating Lamp Causes Blown Fuse, Resulting in Disabling of Automatic Actuation of Engineered Safety Features Actuation System for"B" Safeguards Logic Train Components R.E.Ginna Nuclear Power Plant Docket No.50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(i)(B), which requires a report of,"any operation or condition prohibited by the plant's Technical Specifications", the attached Licensee Event Report LER 94-011 is hereby submitted. |
| theattachedLicenseeEventReportLER94-011isherebysubmitted.
| | This event has in no way affected the public's health and safety.Very truly yours, Robert C.Me edy xc: U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector svrQ L)~~gir7~Z O~p>r>4@~9410270370 941017 PDR ADDCK 05000244 S PDR NRC FORH 366 (5-92)U.S.NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO.3150-0104 EXPIRES 5/31/95 LICENSEE EVENT REPORT (LER)(See reverse for required number of digits/characters for each block)ESTIMATED BURDEN PER RESPONSE TO COHPLY WITH THIS INFORHATION COLLECTION REQUEST: 50.0 BR'ORWARD COMHENTS REGARDING BURDEN ESTIMATE TO THE INFORHATIOH AND RECORDS HANAGEHENT BRANCH (HNBB 7714), U.S.NUCLEAR REGULATORY COHHISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150.0104), OFFICE OF HANAGEHENT AND BUDGET WASHINGTON DC 20503.FACILITY NAME (1)R.E~Ginna Nuclear Power Plant DOCKET NUMBER (2)05000244 PAGE (3)1 OF 9 TITLE (4)Short Circuit in Indicating Lamp Causes Blown Fuse, Resulting in Disabling of Automatic Actuation of Engineered Safety Features Actuation System for"B" Safeguards Logic Train Components MONTH DAY YEAR EVENT DATE (5)YEAR LER NUHBER (6)SEQUENTIAL NUHBER REVISION NUHBER MONTH DAY YEAR REPORT DATE (7)OTHER FACILITIES INVOLVED (8)DOCKET HUHBER FACILITY NAHE 09 17 94 94--011--00 10 17 94 FACILITY NAME DOCKET NUHBER OPERATING HODE (9)POMER LEVEL (10)N 098 THIS REPORT IS SUBMIlTED PURSUANT 20.402(b)20.405(a)(l)(i)20.405(a)(1)(ii) 20.405(a)(l)(iii) 20.405(a)(1)(iv) 20.405(a)(1)(v) 20.405(c)50.36(c)(1) 50.73(a)(2)(iv) 50.73(a)(2)(v) 73.71(b)73.71(c)50.36(c)(2) 50.73(a)(2)(I) 50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 50.73(a)(2)(x) |
| Thiseventhasinnowayaffectedthepublic'shealthandsafety.Verytrulyyours,RobertC.Meedyxc:U.S.NuclearRegulatory Commission RegionI475Allendale RoadKingofPrussia,PA19406GinnaUSNRCSeniorResidentInspector svrQL)~~gir7~ZO~p>r>4@~9410270370 941017PDRADDCK05000244SPDR NRCFORH366(5-92)U.S.NUCLEARREGULATORY COMMISSION APPROVEDBYOMBNO.3150-0104 EXPIRES5/31/95LICENSEEEVENTREPORT(LER)(Seereverseforrequirednumberofdigits/characters foreachblock)ESTIMATED BURDENPERRESPONSETOCOHPLYWITHTHISINFORHATION COLLECTION REQUEST:50.0BR'ORWARD COMHENTSREGARDING BURDENESTIMATETOTHEINFORHATIOH ANDRECORDSHANAGEHENT BRANCH(HNBB7714),U.S.NUCLEARREGULATORY COHHISSION, WASHINGTON, DC20555-0001, ANDTOTHEPAPERWORK REDUCTION PROJECT(3150.0104),
| | OTHER (Specify in Abstract below and in Text, NRC Form 366A)TO THE RE UIREMENTS OF 10 CFR 5: (Check one or more)(11)LICENSEE CONTACT FOR THIS LER (12)~NAHE John T.St.Hartin-Director, Operating Experience TELEPHONE NUHBER (Include Area Code)(315)524-4446 COHPLETE ONE LINE FOR EACH COHPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEH COMPONENT HANUFACTURER XOOO REPORTABLE TO NPRDS CAUSE SYSTEM COHPONENT MANUFACTURER REPORTABLE TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14)YES (If yes, complete EXPECTED SUBHISSION DATE).X NO EXPECTED SUBMISSION DATE (15)MONTH DAY YEAR ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines)(16)On September 17, 1994, at approximately 1224 EDST, with the reactor at approximately 98%steady state power, an indicating lamp on the"B" train safeguards initiation cabinet failed in a manner that caused a short circuit that blew a 10 ampere fuse in the 125 VDC control power circuit.This disabled the automatic actuation of"B" train safeguards components. |
| OFFICEOFHANAGEHENT ANDBUDGETWASHINGTON DC20503.FACILITYNAME(1)R.E~GinnaNuclearPowerPlantDOCKETNUMBER(2)05000244PAGE(3)1OF9TITLE(4)ShortCircuitinIndicating LampCausesBlownFuse,Resulting inDisabling ofAutomatic Actuation ofEngineered SafetyFeaturesActuation Systemfor"B"Safeguards LogicTrainComponents MONTHDAYYEAREVENTDATE(5)YEARLERNUHBER(6)SEQUENTIAL NUHBERREVISIONNUHBERMONTHDAYYEARREPORTDATE(7)OTHERFACILITIES INVOLVED(8)DOCKETHUHBERFACILITYNAHE09179494--011--00101794FACILITYNAMEDOCKETNUHBEROPERATING HODE(9)POMERLEVEL(10)N098THISREPORTISSUBMIlTED PURSUANT20.402(b) 20.405(a)(l)(i)20.405(a)(1)(ii) 20.405(a)(l)(iii) 20.405(a)(1)(iv) 20.405(a)(1)(v) 20.405(c) 50.36(c)(1) 50.73(a)(2)(iv) 50.73(a)(2)(v) 73.71(b)73.71(c)50.36(c)(2) 50.73(a)(2)(I) 50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 50.73(a)(2)(x)
| | Immediate corrective action was to replace the burned out indicating lamp and blown fuse.The underlying cause of the event was determined to be a shorting out of the low resistance leads that connect the indicating lamp base to the lamp filaments. |
| OTHER(SpecifyinAbstractbelowandinText,NRCForm366A)TOTHEREUIREMENTS OF10CFR5:(Checkoneormore)(11)LICENSEECONTACTFORTHISLER(12)~NAHEJohnT.St.Hartin-Director, Operating Experience TELEPHONE NUHBER(IncludeAreaCode)(315)524-4446COHPLETEONELINEFOREACHCOHPONENT FAILUREDESCRIBED INTHISREPORT(13)CAUSESYSTEHCOMPONENT HANUFACTURER XOOOREPORTABLE TONPRDSCAUSESYSTEMCOHPONENT MANUFACTURER REPORTABLE TONPRDSSUPPLEMENTAL REPORTEXPECTED(14)YES(Ifyes,completeEXPECTEDSUBHISSION DATE).XNOEXPECTEDSUBMISSION DATE(15)MONTHDAYYEARABSTRACT(Limitto1400spaces,i.e.,approximately 15single-spaced typewritten lines)(16)OnSeptember 17,1994,atapproximately 1224EDST,withthereactoratapproximately 98%steadystatepower,anindicating lamponthe"B"trainsafeguards initiation cabinetfailedinamannerthatcausedashortcircuitthatblewa10amperefuseinthe125VDCcontrolpowercircuit.Thisdisabledtheautomatic actuation of"B"trainsafeguards components. | | This event is NUREG-1022 Cause Code"B".Corrective action to preclude repetition is outlined in Section V.B.NRC FORM 366 (5-92) |
| Immediate corrective actionwastoreplacetheburnedoutindicating lampandblownfuse.Theunderlying causeoftheeventwasdetermined tobeashortingoutofthelowresistance leadsthatconnecttheindicating lampbasetothelampfilaments. | |
| ThiseventisNUREG-1022 CauseCode"B".Corrective actiontoprecluderepetition isoutlinedinSectionV.B.NRCFORM366(5-92)
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| NRCFORH366A(5-92)U.S.NUCLEARREGULATORY COHHISSION LICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBYOHBNO.3150-0104 EXPIRES5/31/95ESTIMATED BURDENPERRESPONSETOCOHPLYWITHTHISINFORMATION COLLECTION REQUEST:50.0NRS.FORWARDCOHMENTSREGARDING BURDENESTIHATETOTHEINFORHATION ANDRECORDSMANAGEMENT BRANCH(HNBB7714),U.STNUCLEARREGULATORY COHHISSION, WASHINGTON, DC20555-0001 ANDTOTHEPAPERWORK REDUCTION PROJECT(3110-0104),
| | NRC FORH 366A (5-92)U.S.NUCLEAR REGULATORY COHHISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY OHB NO.3150-0104 EXP I RES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COHPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 NRS.FORWARD COHMENTS REGARDING BURDEN ESTIHATE TO THE INFORHATION AND RECORDS MANAGEMENT BRANCH (HNBB 7714), U.ST NUCLEAR REGULATORY COHHISSION, WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (3110-0104), OFFICE OF HANAGEMENT AND BUDGET WASHINGTON DC 20503.FACILITY NAHE (1)R.E.Ginna Nuclear Power Plant'OCKET NUHBER (2)05000244 LER NUHBER (6)YEAR E 94--011--REVISION 00 PAGE (3)2 OF 9 TEXT (tf more space is required, use additionat copies of NRC Form 366A)(17)PRE-EVENT PLANT CONDITIONS The plant was at approximately 98~steady state reactor power with no major operational activities in progress.While making a routine tour of the Relay Room, a licensed reactor operator observed that a normally lit indicating lamp for"Safeguard DC Failure", on the"Safeguards Initiation SI-B2" cabinet, was extinguished. |
| OFFICEOFHANAGEMENT ANDBUDGETWASHINGTON DC20503.FACILITYNAHE(1)R.E.GinnaNuclearPowerPlant'OCKET NUHBER(2)05000244LERNUHBER(6)YEARE94--011--REVISION00PAGE(3)2OF9TEXT(tfmorespaceisrequired, useadditionat copiesofNRCForm366A)(17)PRE-EVENT PLANTCONDITIONS Theplantwasatapproximately 98~steadystatereactorpowerwithnomajoroperational activities inprogress.
| | He noted that another normally lit indicating lamp on this cabinet was illuminated, and concluded that power was still available to this cabinet.Since replacement of burned out light bulbs for these indicating lamps is a normal responsibility of the licensed operators, he made preparations to replace the lamp.II.DESCRIPTION OF EVENT A.DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES: |
| WhilemakingaroutinetouroftheRelayRoom,alicensedreactoroperatorobservedthatanormallylitindicating lampfor"Safeguard DCFailure",
| | o September 17, 1994, 1224 EDST: Event date and time.0 September 17, 1994, 1224 EDST: Discovery date and time.li September 17, 1994, 1346 EDST: Indicating lamp and fuses replaced and"B" train of Engineered Safety Features Actuation System (ESFAS)components restored to operable status.B.EVENT: On September 17, 1994, at approximately 1224 EDST, with the reactor at approximately 98%steady state reactor power, the licensed reactor operator had returned to the Relay Room with a new indicating lamp for replacement of the burned out lamp.As he unscrewed the burned out lamp from the'socket, he observed a flash.He also saw that the other indicating lamp (that had been illuminated) was now extinguished. |
| onthe"Safeguards Initiation SI-B2"cabinet,wasextinguished.
| | He immediately proceeded to the Control Room.NRC FORH 366A (5-92) |
| Henotedthatanothernormallylitindicating lamponthiscabinetwasilluminated, andconcluded thatpowerwasstillavailable tothiscabinet.Sincereplacement ofburnedoutlightbulbsfortheseindicating lampsisanormalresponsibility ofthelicensedoperators, hemadepreparations toreplacethelamp.II.DESCRIPTION OFEVENTA.DATESANDAPPROXIMATE TIMESOFMAJOROCCURRENCES:
| | NRC FORM 366A (5.92)U.S.NUCLEAR REGULATORY COHHISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY OHB NO.3150-0104 EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY WITH THIS IHFORHATIOH COLLECTION REQUEST: 50.0 HRS.FORWARD COHHEHTS REGARDING BURDEN ESTIHATE TO THE INFORHATIOH AHD RECORDS HAHAGEHEHT BRANCH (HNBB 7714), U.S NUCLEAR REGULATORY COHHISSION, WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTIOH PROJECT (3140-0104), OFFICE OF HANAGEHENT AND BUDGET WASHINGTON DC 20503.FACILITY NAHE (1)R.E.Ginna Nuclear Power Plant DOCKET NUHBER (2)YEAR 05000244 94 LER NUHBER (6)SEQUENTIAL 011 REVISION 00 PAGE (3)3 OF 9 TEXT (tf more space is required, use additional copies of NRC Form 366A)(17)The Control Room operators were immediately made aware of the problem when Main Control Board (MCB)Annunciator L-31,"Safeguard DC Failure", alarmed.The Control Room operators immediately performed the appropriate actions of Alarm Response procedure AR-L-31, and also reviewed appropriate electrical drawings to determine the effect on the plant.They concluded that 125 VDC control power had been lost to a part of the"Safeguards Initiation SI-B2" cabinet.Loss of this DC control power resulted in the disabling of the"B" safeguards logic train, which would prevent the automatic actuation of engineered safety features (ESF)components for the"B" safeguards logic train.However, the components remained capable of being manually operated by operator action at the Main Control Board or by local operator action in the field.The plant's Technical Specifications (TS)were reviewed, and the Control Room operators did not locate an applicable specification or Limiting Condition for Operation (LCO)that had been exceeded.However, the Control Room operators recognized that LCOs existed for components which are actuated by ESFAS signals.The Shift Supervisor then made a conservative decision to enter TS 3.0', and directed that actions be initiated to place the plant in hot shutdown.An Instrument and Control (IIC)technician responded to the announcement of the event.The ISC technician and Shift Technical Advisor assisted the Control Room operators in troubleshooting the event.Operations procedure P-ll,"Electrical Distribution Panel Reference Manual", was consulted, and the Control Room operators also referred to Equipment Restoration procedure ER-ELEC.2,"Recovery From Loss of A or B DC Bus", for guidance.It was determined'hat a 125 VDC 10 ampere fuse (FUSIB1/SIBF1-P on the positive leg of the DC circuit)had blown.This fuse caused the disabling of 125 VDC control power to the"B" safeguards logic train.The burned out lamp was replaced, and the blown fuse (and the other 10 ampere fuse FUSIB1/SIBF2-N on the negative leg of the DC circuit)was replaced.When the fuses were replaced, Annunciator L-31 cleared.The"B" train of ESFAS components was restored to operable status at approximately 1346 EDST.NRC FORH 366A (5-92) |
| oSeptember 17,1994,1224EDST:Eventdateandtime.0September 17,1994,1224EDST:Discovery dateandtime.liSeptember 17,1994,1346EDST:Indicating lampandfusesreplacedand"B"trainofEngineered SafetyFeaturesActuation System(ESFAS)components restoredtooperablestatus.B.EVENT:OnSeptember 17,1994,atapproximately 1224EDST,withthereactoratapproximately 98%steadystatereactorpower,thelicensedreactoroperatorhadreturnedtotheRelayRoomwithanewindicating lampforreplacement oftheburnedoutlamp.Asheunscrewed theburnedoutlampfromthe'socket,heobservedaflash.Healsosawthattheotherindicating lamp(thathadbeenilluminated) wasnowextinguished.
| | NRC FORH 366A (5-92)U.S.NUCLEAR REGULATORY COHHISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY OHB NO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COHPLY WITH THIS INFORMATION COLLECTIOH REQUEST: 50.0 HRS.FORWARD COHMENTS REGARDING BURDEN ESTIHATE TO THE IHFORHATION AHD RECORDS MANAGEMENT BRANCH (HHBB 7l'14), U-S.NUCLEAR REGULATORY COHHISSIOH, WASHINGTON, DC 20555-0001 AHD TO THE PAPERWORK REDUCTION PROJECT (3140-0104), OFFICE OF HANAGEHENT AND BUDGET WASHINGTON DC 20503.FACILITY NAHE (1)R.E.Ginna Nuclear Power Plant DOCKET NUHBER (2)05000244 YEAR 94 011 00 LER NUMBER (6)SEQUENTIAL REVISION PAGE (3)4 OF 9 TEXT (If more space is required, use additional copies of HRC Form 366A)(17)C INOPERABLE STRUCTURES I COMPONENTS I OR SYSTEMS THAT CONTRIBUTED TO THE EVENT: None D.OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED: Train"B" ESFAS components would not actuation signals from approximately September 17, 1994.However, manual components by Control Room operators and local operation of components in have actuated from ESF 1224 EDST to 1346 EDST on" operation of individual at the Main Control Board the field was not affected.E.METHOD OF DISCOVERY: |
| Heimmediately proceeded totheControlRoom.NRCFORH366A(5-92)
| | This event was immediately apparent to the Control Room operators due to receipt of Annunciator L-31,"Safeguard DC Failure".F.OPERATOR ACTION: The Control Room operators responded to Annunciator L-31 and performed the actions of Alarm Response procedure AR-L-31.The Control Room operators reviewed'he TS and did not locate an applicable specification or LCO that had been exceeded.However, the Control Room operators recognized that LCOs existed for components which are actuated by ESFAS signals.The Shift Supervisor made a conservative decision to enter TS 3.0.1, and directed that actions be initiated to place the plant in hot shutdown prior to 1924 EDST on September 17, 1994, as required by TS 3.0.1.The Control Room operators consulted Operations procedure P-11 for the effect of the blown fuse on the plant.Equipment Restoration procedure ER-ELEC.2 was referred to for additional guidance.HRC FORH 366A (5-92) |
| NRCFORM366A(5.92)U.S.NUCLEARREGULATORY COHHISSION LICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBYOHBNO.3150-0104 EXPIRES5/31/95ESTIHATED BURDENPERRESPONSETOCOHPLYWITHTHISIHFORHATIOH COLLECTION REQUEST:50.0HRS.FORWARDCOHHEHTSREGARDING BURDENESTIHATETOTHEINFORHATIOH AHDRECORDSHAHAGEHEHT BRANCH(HNBB7714),U.SNUCLEARREGULATORY COHHISSION, WASHINGTON, DC20555-0001 ANDTOTHEPAPERWORK REDUCTIOH PROJECT(3140-0104),
| | NRC FORM 366A (5.92)U.S.NUCLEAR REGULATORY CONIISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY OMB NO.3150~0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.FORHARD COMMENTS REGARDIHG BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRAHCH (MHBB 7714), UPS.NUCLEAR REGULATORY COMMISSION, llASHIHGTON, DC 20555-0001 AHD TO THE PAPERHORK REDUCTION PROJECT (3140 0104), OFFICE OF MAHAGEHEHT AND BUDGET llASHIHGTOH DC 20503.FACILITY NAME (1)R.E.Ginna Nuclear Power Plant DOCKET NUMBER (2)05000244 YEAR 94 LER NUMBER (6)SEQUENTIAL |
| OFFICEOFHANAGEHENT ANDBUDGETWASHINGTON DC20503.FACILITYNAHE(1)R.E.GinnaNuclearPowerPlantDOCKETNUHBER(2)YEAR0500024494LERNUHBER(6)SEQUENTIAL 011REVISION00PAGE(3)3OF9TEXT(tfmorespaceisrequired, useadditional copiesofNRCForm366A)(17)TheControlRoomoperators wereimmediately madeawareoftheproblemwhenMainControlBoard(MCB)Annunciator L-31,"Safeguard DCFailure",
| | --011--REVISION 00 PAGE (3)5 OF 9 TEXT (If more space is required, use additionaL copies of HRC Form 366A)(17)When the cause of Annunciator L-31 was determined and corrective actions to replace the fuse were in progress, the Shift Supervisor discussed the situation with plant management. |
| alarmed.TheControlRoomoperators immediately performed theappropriate actionsofAlarmResponseprocedure AR-L-31,andalsoreviewedappropriate electrical drawingstodetermine theeffectontheplant.Theyconcluded that125VDCcontrolpowerhadbeenlosttoapartofthe"Safeguards Initiation SI-B2"cabinet.LossofthisDCcontrolpowerresultedinthedisabling ofthe"B"safeguards logictrain,whichwouldpreventtheautomatic actuation ofengineered safetyfeatures(ESF)components forthe"B"safeguards logictrain.However,thecomponents remainedcapableofbeingmanuallyoperatedbyoperatoractionattheMainControlBoardorbylocaloperatoractioninthefield.Theplant'sTechnical Specifications (TS)werereviewed, andtheControlRoomoperators didnotlocateanapplicable specification orLimitingCondition forOperation (LCO)thathadbeenexceeded. | | A decision was made to continue to take appropriate actions to place the plant in hot shutdown by 1924 EDST, but actual reduction of reactor power was deferred, pending the imminent replacement of the fuses.At approximately 1545 EDST on September 16, 1994, the Shift Supervisor notified the NRC per 10CFR 50.72 (b)(2)(iii)(D).G.SAFETY SYSTEM RESPONSES: |
| However,theControlRoomoperators recognized thatLCOsexistedforcomponents whichareactuatedbyESFASsignals.TheShiftSupervisor thenmadeaconservative decisiontoenterTS3.0',anddirectedthatactionsbeinitiated toplacetheplantinhotshutdown. | | None III.CAUSE OF EVENT A.IMMEDIATE CAUSE: The immediate cause of the disabling of the"B" safeguards logic train from any ESF actuation signal was loss of 125 VDC control power due to a blown fuse in the 125 VDC control power circuit.B.INTERMEDIATE CAUSE: The intermediate cause of the blown fuse was a short circuit in the burned out indicating lamp.HRC FORM 366A (5-92) ll NRC FORH 366A (5.92)U.S.NUCLEAR REGULATORY COHHISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY OHB NO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEH PER RESPONSE TO COMPLY WITH THIS INFORMATIOH COLLECTION REQUEST: 50.0 HRS~FORWARD COMHENTS REGARDIHG BURDEN ESTIHATE TO THE INFORHATIOH AND RECORDS HAHAGEMENT BRANCH (MHBB 7714), U.S.NUCLEAR REGULATORY COHMISSION, WASNIHGTOH, DC 20555-0001 AHD TO THE PAPERWORK REDUCTION PROJECT (3140-0104), OFFICE OF MANAGEMENT AND BUDGET WASHIHGTOH DC 20503.FACILITY NAHE (1)DOCKET NUHBER (2)LER NUHBER (6)YEAR SEQUEHTIAL REVISION PAGE (3)R.E.Ginna Nuclear Power Plant 05000244 94 011--00 6 OF 9 TEXT (If more space is required, use additional copies of HRC Form 366A)(17)C.ROOT CAUSE: The underlying cause of the short circuit in the burned out indicating lamp was the internal shorting out of the low resistance leads that connect the lamp base to the lamp filament.This occurred when the licensed operator was removing the burned out lamp from the socket.The low resistance caused increased current in the lamp, which resulted in sufficient current to blow the 10 ampere fuse.This event is NUREG-1022 Cause Code"B", Design, Manufacturing, Construction |
| AnInstrument andControl(IIC)technician responded totheannouncement oftheevent.TheISCtechnician andShiftTechnical AdvisorassistedtheControlRoomoperators introubleshooting theevent.Operations procedure P-ll,"Electrical Distribution PanelReference Manual",wasconsulted, andtheControlRoomoperators alsoreferredtoEquipment Restoration procedure ER-ELEC.2, "Recovery FromLossofAorBDCBus",forguidance.
| |
| Itwasdetermined'hat a125VDC10amperefuse(FUSIB1/SIBF1-P onthepositivelegoftheDCcircuit)hadblown.Thisfusecausedthedisabling of125VDCcontrolpowertothe"B"safeguards logictrain.Theburnedoutlampwasreplaced, andtheblownfuse(andtheother10amperefuseFUSIB1/SIBF2-N onthenegativelegoftheDCcircuit)wasreplaced.
| |
| Whenthefuseswerereplaced, Annunciator L-31cleared.The"B"trainofESFAScomponents wasrestoredtooperablestatusatapproximately 1346EDST.NRCFORH366A(5-92)
| |
| NRCFORH366A(5-92)U.S.NUCLEARREGULATORY COHHISSION LICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBYOHBNO.3150-0104 EXPIRES5/31/95ESTIMATED BURDENPERRESPONSETOCOHPLYWITHTHISINFORMATION COLLECTIOH REQUEST:50.0HRS.FORWARDCOHMENTSREGARDING BURDENESTIHATETOTHEIHFORHATION AHDRECORDSMANAGEMENT BRANCH(HHBB7l'14),U-S.NUCLEARREGULATORY COHHISSIOH, WASHINGTON, DC20555-0001 AHDTOTHEPAPERWORK REDUCTION PROJECT(3140-0104),
| |
| OFFICEOFHANAGEHENT ANDBUDGETWASHINGTON DC20503.FACILITYNAHE(1)R.E.GinnaNuclearPowerPlantDOCKETNUHBER(2)05000244YEAR9401100LERNUMBER(6)SEQUENTIAL REVISIONPAGE(3)4OF9TEXT(Ifmorespaceisrequired, useadditional copiesofHRCForm366A)(17)CINOPERABLE STRUCTURES ICOMPONENTS IORSYSTEMSTHATCONTRIBUTED TOTHEEVENT:NoneD.OTHERSYSTEMSORSECONDARY FUNCTIONS AFFECTED:
| |
| Train"B"ESFAScomponents wouldnotactuation signalsfromapproximately September 17,1994.However,manualcomponents byControlRoomoperators andlocaloperation ofcomponents inhaveactuatedfromESF1224EDSTto1346EDSTon"operation ofindividual attheMainControlBoardthefieldwasnotaffected. | |
| E.METHODOFDISCOVERY: | |
| Thiseventwasimmediately apparenttotheControlRoomoperators duetoreceiptofAnnunciator L-31,"Safeguard DCFailure".
| |
| F.OPERATORACTION:TheControlRoomoperators responded toAnnunciator L-31andperformed theactionsofAlarmResponseprocedure AR-L-31.TheControlRoomoperators reviewed'he TSanddidnotlocateanapplicable specification orLCOthathadbeenexceeded. | |
| However,theControlRoomoperators recognized thatLCOsexistedforcomponents whichareactuatedbyESFASsignals.TheShiftSupervisor madeaconservative decisiontoenterTS3.0.1,anddirectedthatactionsbeinitiated toplacetheplantinhotshutdownpriorto1924EDSTonSeptember 17,1994,asrequiredbyTS3.0.1.TheControlRoomoperators consulted Operations procedure P-11fortheeffectoftheblownfuseontheplant.Equipment Restoration procedure ER-ELEC.2 wasreferredtoforadditional guidance. | |
| HRCFORH366A(5-92)
| |
| NRCFORM366A(5.92)U.S.NUCLEARREGULATORY CONIISSION LICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBYOMBNO.3150~0104EXPIRES5/31/95ESTIMATED BURDENPERRESPONSETOCOMPLYWITHTHISINFORMATION COLLECTION REQUEST:50.0HRS.FORHARDCOMMENTSREGARDIHG BURDENESTIMATETOTHEINFORMATION ANDRECORDSMANAGEMENT BRAHCH(MHBB7714),UPS.NUCLEARREGULATORY COMMISSION, llASHIHGTON, DC20555-0001 AHDTOTHEPAPERHORK REDUCTION PROJECT(31400104),OFFICEOFMAHAGEHEHT ANDBUDGETllASHIHGTOH DC20503.FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKETNUMBER(2)05000244YEAR94LERNUMBER(6)SEQUENTIAL
| |
| --011--REVISION00PAGE(3)5OF9TEXT(Ifmorespaceisrequired, useadditionaL copiesofHRCForm366A)(17)WhenthecauseofAnnunciator L-31wasdetermined andcorrective actionstoreplacethefusewereinprogress, theShiftSupervisor discussed thesituation withplantmanagement. | |
| Adecisionwasmadetocontinuetotakeappropriate actionstoplacetheplantinhotshutdownby1924EDST,butactualreduction ofreactorpowerwasdeferred, pendingtheimminentreplacement ofthefuses.Atapproximately 1545EDSTonSeptember 16,1994,theShiftSupervisor notifiedtheNRCper10CFR50.72(b)(2)(iii)(D).G.SAFETYSYSTEMRESPONSES:
| |
| NoneIII.CAUSEOFEVENTA.IMMEDIATE CAUSE:Theimmediate causeofthedisabling ofthe"B"safeguards logictrainfromanyESFactuation signalwaslossof125VDCcontrolpowerduetoablownfuseinthe125VDCcontrolpowercircuit.B.INTERMEDIATE CAUSE:Theintermediate causeoftheblownfusewasashortcircuitintheburnedoutindicating lamp.HRCFORM366A(5-92) ll NRCFORH366A(5.92)U.S.NUCLEARREGULATORY COHHISSION LICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBYOHBNO.3150-0104 EXPIRES5/31/95ESTIMATED BURDEHPERRESPONSETOCOMPLYWITHTHISINFORMATIOH COLLECTION REQUEST:50.0HRS~FORWARDCOMHENTSREGARDIHG BURDENESTIHATETOTHEINFORHATIOH ANDRECORDSHAHAGEMENT BRANCH(MHBB7714),U.S.NUCLEARREGULATORY COHMISSION, WASNIHGTOH, DC20555-0001 AHDTOTHEPAPERWORK REDUCTION PROJECT(3140-0104),
| |
| OFFICEOFMANAGEMENT ANDBUDGETWASHIHGTOH DC20503.FACILITYNAHE(1)DOCKETNUHBER(2)LERNUHBER(6)YEARSEQUEHTIAL REVISIONPAGE(3)R.E.GinnaNuclearPowerPlant0500024494011--006OF9TEXT(Ifmorespaceisrequired, useadditional copiesofHRCForm366A)(17)C.ROOTCAUSE:Theunderlying causeoftheshortcircuitintheburnedoutindicating lampwastheinternalshortingoutofthelowresistance leadsthatconnectthelampbasetothelampfilament.
| |
| Thisoccurredwhenthelicensedoperatorwasremovingtheburnedoutlampfromthesocket.Thelowresistance causedincreased currentinthelamp,whichresultedinsufficient currenttoblowthe10amperefuse.ThiseventisNUREG-1022 CauseCode"B",Design,Manufacturing, Construction
| |
| /Installation. | | /Installation. |
| ThislossofpowerdoesnotmeettheNUMARC93-01,"Industry Guideline forMonitoring theEffectiveness ofMaintenance atNuclearPowerPlants",definition ofa"Maintenance Preventable Functional Failure".
| | This loss of power does not meet the NUMARC 93-01,"Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants", definition of a"Maintenance Preventable Functional Failure".IV.ANALYSIS OF EVENT: This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(i)(B), in'that the disabling of the automatic actuation of ESF components for the"B" safeguards logic train resulted in two HEPA filter units and associated recirculation fan coolers being inoperable, which is more than allowed by the LCO for TS 3'.2.2.a.This is a condition prohibited by TS 3.3.2.2.An assessment was performed considering both the safety consequences and-implications of this event with the following results and conclusions: |
| IV.ANALYSISOFEVENT:Thiseventisreportable inaccordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(i)(B),in'thatthedisabling oftheautomatic actuation ofESFcomponents forthe"B"safeguards logictrainresultedintwoHEPAfilterunitsandassociated recirculation fancoolersbeinginoperable, whichismorethanallowedbytheLCOforTS3'.2.2.a.Thisisacondition prohibited byTS3.3.2.2.Anassessment wasperformed considering boththesafetyconsequences and-implications ofthiseventwiththefollowing resultsandconclusions: | | o During this event, automatic actuation of ESF components for the"B" safeguards logic train was disabled.However, the components were still capable of being manually operated by operator action at the Main Control Board and also locally in the field at the appropriate Motor Control Center and/or 480 Volt bus.HRC FORM 366A (5-92) |
| oDuringthisevent,automatic actuation ofESFcomponents forthe"B"safeguards logictrainwasdisabled.
| | NRC FORH 366A (5-92).S.NUCLEAR REGULATORY COHHISSIOH PROVED BY OHB NO.3150~0104 EXPIRES 5/3'I/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY WITH THIS IHFORHATION COLLECTION REQUEST: 50.0 NRS.FORWARD COHHEHTS REGARDING BURDEN ESTIHATE TO THE INFORHATION AHD RECORDS HANAGEHENT BRANCH (HNBB 7714), U.ST NUCLEAR REGULATORY COHHISSION, WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (3140-0104), OFFICE OF HANAGEHENT AND BUDGET WASHINGTON DC 20503.LICENSEE EVENT REPORT (LER)TEXT CONTINUATION PAGE (3)DOCKET NUHBER (2)LER NUHBER (6)REVISION SEQUENTIAL YEAR pp 7 OF 9 05000244 94--011--FACILITY NAHE (1)R.E.Ginna Nuclear Power Plant TEXT (If more space is required, use additional copies of HRC Form 366A)(17)0 The ESFAS is intended to provide protection against the release of radioactive materials in the event of a loss of coolant accident (LOCA)or secondary line break.The ESFAS provides actuation of the following functions (or components): |
| However,thecomponents werestillcapableofbeingmanuallyoperatedbyoperatoractionattheMainControlBoardandalsolocallyinthefieldattheappropriate MotorControlCenterand/or480Voltbus.HRCFORM366A(5-92) | | safety injection (SI), containment (CNMT)isolation, CNMT spray, auxiliary feedwater (AFW), diesel generators, and main steam and main feedwater isolation. |
| NRCFORH366A(5-92).S.NUCLEARREGULATORY COHHISSIOH PROVEDBYOHBNO.3150~0104EXPIRES5/3'I/95ESTIHATED BURDENPERRESPONSETOCOHPLYWITHTHISIHFORHATION COLLECTION REQUEST:50.0NRS.FORWARDCOHHEHTSREGARDING BURDENESTIHATETOTHEINFORHATION AHDRECORDSHANAGEHENT BRANCH(HNBB7714),U.STNUCLEARREGULATORY COHHISSION, WASHINGTON, DC20555-0001 ANDTOTHEPAPERWORK REDUCTION PROJECT(3140-0104),
| | The loss of'fuse FUSIBl/SIBF1-P caused the loss of automatic actuation of the following items: o SI train"B" o CNMT spray train"B" o CNMT isolation train"B" 0 0 o Main steam and main feedwater isolation (one of two channels for each isolation and/or bypass valve)The"B" Emergency diesel generator (D/G)and"B" motor-driven AFW pump train would still actuate from signals such as undervoltage or low steam generator level.However, the loss of automatic actuation of SI train"B" prevented the"B" Emergency D/G and"B" motor-driven AFW pump train from starting due to an SI signal.As shown above, the loss of fuse FUSIB1/SIBF1-P resulted in the loss of one multi-function train;however, the redundant train was available if an accident were to occur during the approximately one and one half hours that the single train'was inoperable. |
| OFFICEOFHANAGEHENT ANDBUDGETWASHINGTON DC20503.LICENSEEEVENTREPORT(LER)TEXTCONTINUATION PAGE(3)DOCKETNUHBER(2)LERNUHBER(6)REVISIONSEQUENTIAL YEARpp7OF90500024494--011--FACILITYNAHE(1)R.E.GinnaNuclearPowerPlantTEXT(Ifmorespaceisrequired, useadditional copiesofHRCForm366A)(17)0TheESFASisintendedtoprovideprotection againstthereleaseofradioactive materials intheeventofalossofcoolantaccident(LOCA)orsecondary linebreak.TheESFASprovidesactuation ofthefollowing functions (orcomponents):
| | The loss of a single train is considered in the design of the ESFAS, which utilizes independent trains and channels for each function.This independence is maintained from the process sensors to the signal output relays and includes the channel power supplies.Thus, no single failure can cause the loss of function.0 The Standard Technical Specifications for Westinghouse reactors (NUREG-1431) allows six hours to restore an inoperable channel to operable status before requiring a plant shutdown.Entering TS 3.0~1 is more conservative than following the requirements of NUREG-1431, since the redundant trains were available to perform their intended function.Based on the above, it can be concluded that the public's health and safety was assured at all times.NRC FORH 366A (5 92) |
| safetyinjection (SI),containment (CNMT)isolation, CNMTspray,auxiliary feedwater (AFW),dieselgenerators, andmainsteamandmainfeedwater isolation.
| | NRC FORM 366A (5-92)U.S.NUCLEAR REGULATORY COHHISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY OMB NO.3150.0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPOHSE TO COMPLY IIITN THIS INFORHATIOH COLLECTIOH REQUEST: 50.0 MRS'ORHARD COHHEHTS REGARDIHG BURDEN ESTIMATE TO THE INFORMATION AND RECORDS HANAGEHEHT BRANCH (HHBB 7714), U.ST NUCLEAR REGULATORY COHHISSION, IIASHINGTOH, DC 20555-0001 AND TO THE PAPERNORK REDUCTION PROJECT (3140-0104), OFFICE OF HAHAGEHEHT AND BUDGET IIASHIHGTON DC 20503.FACILITY NAHE (1)R.E.Ginna Nuclear Power Plant DOCKET NUHBER (2)05000244 YEAR 94--011--00 LER NUHBER (6)SEQUENTIAL REVISION PAGE (3)8 OF 9 TEXT (If more space is required, use additional copies of HRC Form 366A)(17)V.CORRECTIVE ACTION A.ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS: o The burned out indicating lamp was replaced.o The blown fuse (and associated negative fuse)were replaced.B.ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE: |
| Thelossof'fuseFUSIBl/SIBF1-P causedthelossofautomatic actuation ofthefollowing items:oSItrain"B"oCNMTspraytrain"B"oCNMTisolation train"B"00oMainsteamandmainfeedwater isolation (oneoftwochannelsforeachisolation and/orbypassvalve)The"B"Emergency dieselgenerator (D/G)and"B"motor-driven AFWpumptrainwouldstillactuatefromsignalssuchasundervoltage orlowsteamgenerator level.However,thelossofautomatic actuation ofSItrain"B"prevented the"B"Emergency D/Gand"B"motor-driven AFWpumptrainfromstartingduetoanSIsignal.Asshownabove,thelossoffuseFUSIB1/SIBF1-P resultedinthelossofonemulti-function train;however,theredundant trainwasavailable ifanaccidentweretooccurduringtheapproximately oneandonehalfhoursthatthesingletrain'wasinoperable.
| | o Operations supervision notified all operations personnel not to change any indicating lamps on the cabinets in the Relay Room.Operators are to submit a trouble report for IEC to change the lamps.o All 120 Volt indicating lamps on site are being replaced with 155 Volt lamps.When a 120 Volt lamp requires replacement, it will be replaced with a 155 Volt lamp.This is intended to increase the life of these lamps, and decrease the frequency of replacement. |
| Thelossofasingletrainisconsidered inthedesignoftheESFAS,whichutilizesindependent trainsandchannelsforeachfunction.
| | o NRC Information Notice 94-68,"Safety-Related Equipment Failures Caused by Faulted Indicating Lamps", will be assessed as part of the Operational Assessment program.VI.ADDITIONAL INFORMATION A.FAILED COMPONENTS: |
| Thisindependence ismaintained fromtheprocesssensorstothesignaloutputrelaysandincludesthechannelpowersupplies.
| | The burned out indicating lamp was a Sylvania incandescent lamp, Model 6S6 120V, with a design rating of 6 watts.HRC FORM 366A (5-92) |
| Thus,nosinglefailurecancausethelossoffunction. | | NRC FORH 366A (5-92)U.S.NUCLEAR REGULATORY COHHISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY OHB NO.3150.0104 EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORHATIOH COLLECTION REQUEST: 50.0 HRS.FORWARD COHHENTS REGARDIHG BURDEH ESTIHATE TO THE INFORHATIOH AHD RECORDS HANAGEHENT BRANCH (MHBB 7714), U.S.NUCLEAR REGULATORY COMMISSION, WASHIHGTON, DC 20555-0001 AHD TO THE PAPERWORK REDUCTION PROJECT (31/0-0104), OFFICE OF MANAGEMENT AND BUDGET'WASHINGTON DC 20503.FACILITY NAME (I)R.E.Ginna Nuclear Power Plant DOCKET NUMBER (2)05000244 94 011 00 LER NUHBER (6 YEAR SEQUENTIAL REVISION PAGE (3)9 OF 9 TEXT (If more space is required, use additional copies of HRC Form 366A)(17)B.PREVIOUS LERs ON SIMILAR EVENTS: A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Nuclear Power Plant could be iden-tified.C.SPECIAL COMMENTS: This event of September 17, 1994 is similar to events described in NRC Information Notice 94-68, which is dated September 27, 1994, and was received by Rochester Gas 6 Electric on October 4, 1994.HRC FORM 366A (5-92)}} |
| 0TheStandardTechnical Specifications forWestinghouse reactors(NUREG-1431) allowssixhourstorestoreaninoperable channeltooperablestatusbeforerequiring aplantshutdown.
| |
| EnteringTS3.0~1ismoreconservative thanfollowing therequirements ofNUREG-1431, sincetheredundant trainswereavailable toperformtheirintendedfunction.
| |
| Basedontheabove,itcanbeconcluded thatthepublic'shealthandsafetywasassuredatalltimes.NRCFORH366A(592)
| |
| NRCFORM366A(5-92)U.S.NUCLEARREGULATORY COHHISSION LICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBYOMBNO.3150.0104 EXPIRES5/31/95ESTIMATED BURDENPERRESPOHSETOCOMPLYIIITNTHISINFORHATIOH COLLECTIOH REQUEST:50.0MRS'ORHARD COHHEHTSREGARDIHG BURDENESTIMATETOTHEINFORMATION ANDRECORDSHANAGEHEHT BRANCH(HHBB7714),U.STNUCLEARREGULATORY COHHISSION, IIASHINGTOH, DC20555-0001 ANDTOTHEPAPERNORK REDUCTION PROJECT(3140-0104),
| |
| OFFICEOFHAHAGEHEHT ANDBUDGETIIASHIHGTON DC20503.FACILITYNAHE(1)R.E.GinnaNuclearPowerPlantDOCKETNUHBER(2)05000244YEAR94--011--00LERNUHBER(6)SEQUENTIAL REVISIONPAGE(3)8OF9TEXT(Ifmorespaceisrequired, useadditional copiesofHRCForm366A)(17)V.CORRECTIVE ACTIONA.ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENT NORMALSTATUS:oTheburnedoutindicating lampwasreplaced.
| |
| oTheblownfuse(andassociated negativefuse)werereplaced.
| |
| B.ACTIONTAKENORPLANNEDTOPREVENTRECURRENCE: | |
| oOperations supervision notifiedalloperations personnel nottochangeanyindicating lampsonthecabinetsintheRelayRoom.Operators aretosubmitatroublereportforIECtochangethelamps.oAll120Voltindicating lampsonsitearebeingreplacedwith155Voltlamps.Whena120Voltlamprequiresreplacement, itwillbereplacedwitha155Voltlamp.Thisisintendedtoincreasethelifeoftheselamps,anddecreasethefrequency ofreplacement.
| |
| oNRCInformation Notice94-68,"Safety-Related Equipment FailuresCausedbyFaultedIndicating Lamps",willbeassessedaspartoftheOperational Assessment program.VI.ADDITIONAL INFORMATION A.FAILEDCOMPONENTS:
| |
| Theburnedoutindicating lampwasaSylvaniaincandescent lamp,Model6S6120V,withadesignratingof6watts.HRCFORM366A(5-92)
| |
| NRCFORH366A(5-92)U.S.NUCLEARREGULATORY COHHISSION LICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBYOHBNO.3150.0104 EXPIRES5/31/95ESTIHATED BURDENPERRESPONSETOCOMPLYWITHTHISINFORHATIOH COLLECTION REQUEST:50.0HRS.FORWARDCOHHENTSREGARDIHG BURDEHESTIHATETOTHEINFORHATIOH AHDRECORDSHANAGEHENT BRANCH(MHBB7714),U.S.NUCLEARREGULATORY COMMISSION, WASHIHGTON, DC20555-0001 AHDTOTHEPAPERWORK REDUCTION PROJECT(31/0-0104),
| |
| OFFICEOFMANAGEMENT ANDBUDGET'WASHINGTON DC20503.FACILITYNAME(I)R.E.GinnaNuclearPowerPlantDOCKETNUMBER(2)050002449401100LERNUHBER(6YEARSEQUENTIAL REVISIONPAGE(3)9OF9TEXT(Ifmorespaceisrequired, useadditional copiesofHRCForm366A)(17)B.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistorical searchwasconducted withthefollowing results:Nodocumentation ofsimilarLEReventswiththesamerootcauseatGinnaNuclearPowerPlantcouldbeiden-tified.C.SPECIALCOMMENTS:
| |
| ThiseventofSeptember 17,1994issimilartoeventsdescribed inNRCInformation Notice94-68,whichisdatedSeptember 27,1994,andwasreceivedbyRochester Gas6ElectriconOctober4,1994.HRCFORM366A(5-92)}}
| |
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Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
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j.Mj.~kc.j.I'Y<Accr LERATr D RIDs proc!'.sslic REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9410270370 DOC.DATE: 94/10/17 NOTARIZED:
NO FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G AUTH.NAME AUTHOR AFFILIATION ST MARTIN,J.T.
Rochester Gas&Electric Corp.MECREDY,R.C.
Rochester Gas&Electric Corp.RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000244 P
SUBJECT:
LER 94-011-00:on 940917,indicating lamp on"B" train safeguards initiation cabinet failed.Caused by loss of 125 VDC control power.Burned out indicating lamp&blown fuse replaced.W/941017 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED: LTR I ENCL i SIZE: l TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
R 05000244 RECIPIENT ID CODE/NAME PD1-3 PD INTERNA EOD/~OA'B/D FILE CMTER 02 E EMEB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DSSA/SPLB NRR/PMAS/IRCB-E RGN1 FILE 01 EXTERNAL EG&G BRYCE I J~H NOAC MURPHY,G.A NRC PDR COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 RECIPIENT ID CODE/NAME JOHNSON,A AEOD/SPD/RRAB NRR/DE/EELB NRR/DORS/OEAB NRR/DRCH/HICB NRR/DRSS/PRPB NRR/DSSA/SRXB RES/DSIR/EIB L ST LOBBY WARD NOAC POORE,W.NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 D~ff z-o745/2~~U YOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO RFDUCE iVASTE!CONTACT'I'I IE DOCl'iIEiT CONTROL DESk.ROOXI Pl-37 (EXT.504-20S3)TO FLIXIliATE O'OI:R XAXILZ FROiI DISTRIBUTION LIS'I'S I'OR l)OCl iIEi'I'S 5'OL')Oi"IL'I'.II)!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 26 ENCL 26
~v~v I~v I soac 7 s1<TC ROCHESTER GAS AND ELECTRIC CORPORATION
~89-EAST AVENUE, ROCHESTER N.Y.14649.0001 ROBERTC MECRfOY Vice President Cinna Nuclear Producrion TELEPHONE AREA CODE 716 546 2700 October 17, 1994 U.S.Nuclear Regulatory Commission Document Control Desk Attn: Allen R.Johnson PWR Project Directorate I-3 Washington, D.C.20555
Subject:
LER 94-011, Short Circuit in Indicating Lamp Causes Blown Fuse, Resulting in Disabling of Automatic Actuation of Engineered Safety Features Actuation System for"B" Safeguards Logic Train Components R.E.Ginna Nuclear Power Plant Docket No.50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(i)(B), which requires a report of,"any operation or condition prohibited by the plant's Technical Specifications", the attached Licensee Event Report LER 94-011 is hereby submitted.
This event has in no way affected the public's health and safety.Very truly yours, Robert C.Me edy xc: U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector svrQ L)~~gir7~Z O~p>r>4@~9410270370 941017 PDR ADDCK 05000244 S PDR NRC FORH 366 (5-92)U.S.NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO.3150-0104 EXPIRES 5/31/95 LICENSEE EVENT REPORT (LER)(See reverse for required number of digits/characters for each block)ESTIMATED BURDEN PER RESPONSE TO COHPLY WITH THIS INFORHATION COLLECTION REQUEST: 50.0 BR'ORWARD COMHENTS REGARDING BURDEN ESTIMATE TO THE INFORHATIOH AND RECORDS HANAGEHENT BRANCH (HNBB 7714), U.S.NUCLEAR REGULATORY COHHISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150.0104), OFFICE OF HANAGEHENT AND BUDGET WASHINGTON DC 20503.FACILITY NAME (1)R.E~Ginna Nuclear Power Plant DOCKET NUMBER (2)05000244 PAGE (3)1 OF 9 TITLE (4)Short Circuit in Indicating Lamp Causes Blown Fuse, Resulting in Disabling of Automatic Actuation of Engineered Safety Features Actuation System for"B" Safeguards Logic Train Components MONTH DAY YEAR EVENT DATE (5)YEAR LER NUHBER (6)SEQUENTIAL NUHBER REVISION NUHBER MONTH DAY YEAR REPORT DATE (7)OTHER FACILITIES INVOLVED (8)DOCKET HUHBER FACILITY NAHE 09 17 94 94--011--00 10 17 94 FACILITY NAME DOCKET NUHBER OPERATING HODE (9)POMER LEVEL (10)N 098 THIS REPORT IS SUBMIlTED PURSUANT 20.402(b)20.405(a)(l)(i)20.405(a)(1)(ii) 20.405(a)(l)(iii) 20.405(a)(1)(iv) 20.405(a)(1)(v) 20.405(c)50.36(c)(1) 50.73(a)(2)(iv) 50.73(a)(2)(v) 73.71(b)73.71(c)50.36(c)(2) 50.73(a)(2)(I) 50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 50.73(a)(2)(x)
OTHER (Specify in Abstract below and in Text, NRC Form 366A)TO THE RE UIREMENTS OF 10 CFR 5: (Check one or more)(11)LICENSEE CONTACT FOR THIS LER (12)~NAHE John T.St.Hartin-Director, Operating Experience TELEPHONE NUHBER (Include Area Code)(315)524-4446 COHPLETE ONE LINE FOR EACH COHPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEH COMPONENT HANUFACTURER XOOO REPORTABLE TO NPRDS CAUSE SYSTEM COHPONENT MANUFACTURER REPORTABLE TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14)YES (If yes, complete EXPECTED SUBHISSION DATE).X NO EXPECTED SUBMISSION DATE (15)MONTH DAY YEAR ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines)(16)On September 17, 1994, at approximately 1224 EDST, with the reactor at approximately 98%steady state power, an indicating lamp on the"B" train safeguards initiation cabinet failed in a manner that caused a short circuit that blew a 10 ampere fuse in the 125 VDC control power circuit.This disabled the automatic actuation of"B" train safeguards components.
Immediate corrective action was to replace the burned out indicating lamp and blown fuse.The underlying cause of the event was determined to be a shorting out of the low resistance leads that connect the indicating lamp base to the lamp filaments.
This event is NUREG-1022 Cause Code"B".Corrective action to preclude repetition is outlined in Section V.B.NRC FORM 366 (5-92)
NRC FORH 366A (5-92)U.S.NUCLEAR REGULATORY COHHISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY OHB NO.3150-0104 EXP I RES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COHPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 NRS.FORWARD COHMENTS REGARDING BURDEN ESTIHATE TO THE INFORHATION AND RECORDS MANAGEMENT BRANCH (HNBB 7714), U.ST NUCLEAR REGULATORY COHHISSION, WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (3110-0104), OFFICE OF HANAGEMENT AND BUDGET WASHINGTON DC 20503.FACILITY NAHE (1)R.E.Ginna Nuclear Power Plant'OCKET NUHBER (2)05000244 LER NUHBER (6)YEAR E 94--011--REVISION 00 PAGE (3)2 OF 9 TEXT (tf more space is required, use additionat copies of NRC Form 366A)(17)PRE-EVENT PLANT CONDITIONS The plant was at approximately 98~steady state reactor power with no major operational activities in progress.While making a routine tour of the Relay Room, a licensed reactor operator observed that a normally lit indicating lamp for"Safeguard DC Failure", on the"Safeguards Initiation SI-B2" cabinet, was extinguished.
He noted that another normally lit indicating lamp on this cabinet was illuminated, and concluded that power was still available to this cabinet.Since replacement of burned out light bulbs for these indicating lamps is a normal responsibility of the licensed operators, he made preparations to replace the lamp.II.DESCRIPTION OF EVENT A.DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
o September 17, 1994, 1224 EDST: Event date and time.0 September 17, 1994, 1224 EDST: Discovery date and time.li September 17, 1994, 1346 EDST: Indicating lamp and fuses replaced and"B" train of Engineered Safety Features Actuation System (ESFAS)components restored to operable status.B.EVENT: On September 17, 1994, at approximately 1224 EDST, with the reactor at approximately 98%steady state reactor power, the licensed reactor operator had returned to the Relay Room with a new indicating lamp for replacement of the burned out lamp.As he unscrewed the burned out lamp from the'socket, he observed a flash.He also saw that the other indicating lamp (that had been illuminated) was now extinguished.
He immediately proceeded to the Control Room.NRC FORH 366A (5-92)
NRC FORM 366A (5.92)U.S.NUCLEAR REGULATORY COHHISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY OHB NO.3150-0104 EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY WITH THIS IHFORHATIOH COLLECTION REQUEST: 50.0 HRS.FORWARD COHHEHTS REGARDING BURDEN ESTIHATE TO THE INFORHATIOH AHD RECORDS HAHAGEHEHT BRANCH (HNBB 7714), U.S NUCLEAR REGULATORY COHHISSION, WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTIOH PROJECT (3140-0104), OFFICE OF HANAGEHENT AND BUDGET WASHINGTON DC 20503.FACILITY NAHE (1)R.E.Ginna Nuclear Power Plant DOCKET NUHBER (2)YEAR 05000244 94 LER NUHBER (6)SEQUENTIAL 011 REVISION 00 PAGE (3)3 OF 9 TEXT (tf more space is required, use additional copies of NRC Form 366A)(17)The Control Room operators were immediately made aware of the problem when Main Control Board (MCB)Annunciator L-31,"Safeguard DC Failure", alarmed.The Control Room operators immediately performed the appropriate actions of Alarm Response procedure AR-L-31, and also reviewed appropriate electrical drawings to determine the effect on the plant.They concluded that 125 VDC control power had been lost to a part of the"Safeguards Initiation SI-B2" cabinet.Loss of this DC control power resulted in the disabling of the"B" safeguards logic train, which would prevent the automatic actuation of engineered safety features (ESF)components for the"B" safeguards logic train.However, the components remained capable of being manually operated by operator action at the Main Control Board or by local operator action in the field.The plant's Technical Specifications (TS)were reviewed, and the Control Room operators did not locate an applicable specification or Limiting Condition for Operation (LCO)that had been exceeded.However, the Control Room operators recognized that LCOs existed for components which are actuated by ESFAS signals.The Shift Supervisor then made a conservative decision to enter TS 3.0', and directed that actions be initiated to place the plant in hot shutdown.An Instrument and Control (IIC)technician responded to the announcement of the event.The ISC technician and Shift Technical Advisor assisted the Control Room operators in troubleshooting the event.Operations procedure P-ll,"Electrical Distribution Panel Reference Manual", was consulted, and the Control Room operators also referred to Equipment Restoration procedure ER-ELEC.2,"Recovery From Loss of A or B DC Bus", for guidance.It was determined'hat a 125 VDC 10 ampere fuse (FUSIB1/SIBF1-P on the positive leg of the DC circuit)had blown.This fuse caused the disabling of 125 VDC control power to the"B" safeguards logic train.The burned out lamp was replaced, and the blown fuse (and the other 10 ampere fuse FUSIB1/SIBF2-N on the negative leg of the DC circuit)was replaced.When the fuses were replaced, Annunciator L-31 cleared.The"B" train of ESFAS components was restored to operable status at approximately 1346 EDST.NRC FORH 366A (5-92)
NRC FORH 366A (5-92)U.S.NUCLEAR REGULATORY COHHISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY OHB NO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COHPLY WITH THIS INFORMATION COLLECTIOH REQUEST: 50.0 HRS.FORWARD COHMENTS REGARDING BURDEN ESTIHATE TO THE IHFORHATION AHD RECORDS MANAGEMENT BRANCH (HHBB 7l'14), U-S.NUCLEAR REGULATORY COHHISSIOH, WASHINGTON, DC 20555-0001 AHD TO THE PAPERWORK REDUCTION PROJECT (3140-0104), OFFICE OF HANAGEHENT AND BUDGET WASHINGTON DC 20503.FACILITY NAHE (1)R.E.Ginna Nuclear Power Plant DOCKET NUHBER (2)05000244 YEAR 94 011 00 LER NUMBER (6)SEQUENTIAL REVISION PAGE (3)4 OF 9 TEXT (If more space is required, use additional copies of HRC Form 366A)(17)C INOPERABLE STRUCTURES I COMPONENTS I OR SYSTEMS THAT CONTRIBUTED TO THE EVENT: None D.OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED: Train"B" ESFAS components would not actuation signals from approximately September 17, 1994.However, manual components by Control Room operators and local operation of components in have actuated from ESF 1224 EDST to 1346 EDST on" operation of individual at the Main Control Board the field was not affected.E.METHOD OF DISCOVERY:
This event was immediately apparent to the Control Room operators due to receipt of Annunciator L-31,"Safeguard DC Failure".F.OPERATOR ACTION: The Control Room operators responded to Annunciator L-31 and performed the actions of Alarm Response procedure AR-L-31.The Control Room operators reviewed'he TS and did not locate an applicable specification or LCO that had been exceeded.However, the Control Room operators recognized that LCOs existed for components which are actuated by ESFAS signals.The Shift Supervisor made a conservative decision to enter TS 3.0.1, and directed that actions be initiated to place the plant in hot shutdown prior to 1924 EDST on September 17, 1994, as required by TS 3.0.1.The Control Room operators consulted Operations procedure P-11 for the effect of the blown fuse on the plant.Equipment Restoration procedure ER-ELEC.2 was referred to for additional guidance.HRC FORH 366A (5-92)
NRC FORM 366A (5.92)U.S.NUCLEAR REGULATORY CONIISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY OMB NO.3150~0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.FORHARD COMMENTS REGARDIHG BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRAHCH (MHBB 7714), UPS.NUCLEAR REGULATORY COMMISSION, llASHIHGTON, DC 20555-0001 AHD TO THE PAPERHORK REDUCTION PROJECT (3140 0104), OFFICE OF MAHAGEHEHT AND BUDGET llASHIHGTOH DC 20503.FACILITY NAME (1)R.E.Ginna Nuclear Power Plant DOCKET NUMBER (2)05000244 YEAR 94 LER NUMBER (6)SEQUENTIAL
--011--REVISION 00 PAGE (3)5 OF 9 TEXT (If more space is required, use additionaL copies of HRC Form 366A)(17)When the cause of Annunciator L-31 was determined and corrective actions to replace the fuse were in progress, the Shift Supervisor discussed the situation with plant management.
A decision was made to continue to take appropriate actions to place the plant in hot shutdown by 1924 EDST, but actual reduction of reactor power was deferred, pending the imminent replacement of the fuses.At approximately 1545 EDST on September 16, 1994, the Shift Supervisor notified the NRC per 10CFR 50.72 (b)(2)(iii)(D).G.SAFETY SYSTEM RESPONSES:
None III.CAUSE OF EVENT A.IMMEDIATE CAUSE: The immediate cause of the disabling of the"B" safeguards logic train from any ESF actuation signal was loss of 125 VDC control power due to a blown fuse in the 125 VDC control power circuit.B.INTERMEDIATE CAUSE: The intermediate cause of the blown fuse was a short circuit in the burned out indicating lamp.HRC FORM 366A (5-92) ll NRC FORH 366A (5.92)U.S.NUCLEAR REGULATORY COHHISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY OHB NO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEH PER RESPONSE TO COMPLY WITH THIS INFORMATIOH COLLECTION REQUEST: 50.0 HRS~FORWARD COMHENTS REGARDIHG BURDEN ESTIHATE TO THE INFORHATIOH AND RECORDS HAHAGEMENT BRANCH (MHBB 7714), U.S.NUCLEAR REGULATORY COHMISSION, WASNIHGTOH, DC 20555-0001 AHD TO THE PAPERWORK REDUCTION PROJECT (3140-0104), OFFICE OF MANAGEMENT AND BUDGET WASHIHGTOH DC 20503.FACILITY NAHE (1)DOCKET NUHBER (2)LER NUHBER (6)YEAR SEQUEHTIAL REVISION PAGE (3)R.E.Ginna Nuclear Power Plant 05000244 94 011--00 6 OF 9 TEXT (If more space is required, use additional copies of HRC Form 366A)(17)C.ROOT CAUSE: The underlying cause of the short circuit in the burned out indicating lamp was the internal shorting out of the low resistance leads that connect the lamp base to the lamp filament.This occurred when the licensed operator was removing the burned out lamp from the socket.The low resistance caused increased current in the lamp, which resulted in sufficient current to blow the 10 ampere fuse.This event is NUREG-1022 Cause Code"B", Design, Manufacturing, Construction
/Installation.
This loss of power does not meet the NUMARC 93-01,"Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants", definition of a"Maintenance Preventable Functional Failure".IV.ANALYSIS OF EVENT: This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(i)(B), in'that the disabling of the automatic actuation of ESF components for the"B" safeguards logic train resulted in two HEPA filter units and associated recirculation fan coolers being inoperable, which is more than allowed by the LCO for TS 3'.2.2.a.This is a condition prohibited by TS 3.3.2.2.An assessment was performed considering both the safety consequences and-implications of this event with the following results and conclusions:
o During this event, automatic actuation of ESF components for the"B" safeguards logic train was disabled.However, the components were still capable of being manually operated by operator action at the Main Control Board and also locally in the field at the appropriate Motor Control Center and/or 480 Volt bus.HRC FORM 366A (5-92)
NRC FORH 366A (5-92).S.NUCLEAR REGULATORY COHHISSIOH PROVED BY OHB NO.3150~0104 EXPIRES 5/3'I/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY WITH THIS IHFORHATION COLLECTION REQUEST: 50.0 NRS.FORWARD COHHEHTS REGARDING BURDEN ESTIHATE TO THE INFORHATION AHD RECORDS HANAGEHENT BRANCH (HNBB 7714), U.ST NUCLEAR REGULATORY COHHISSION, WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (3140-0104), OFFICE OF HANAGEHENT AND BUDGET WASHINGTON DC 20503.LICENSEE EVENT REPORT (LER)TEXT CONTINUATION PAGE (3)DOCKET NUHBER (2)LER NUHBER (6)REVISION SEQUENTIAL YEAR pp 7 OF 9 05000244 94--011--FACILITY NAHE (1)R.E.Ginna Nuclear Power Plant TEXT (If more space is required, use additional copies of HRC Form 366A)(17)0 The ESFAS is intended to provide protection against the release of radioactive materials in the event of a loss of coolant accident (LOCA)or secondary line break.The ESFAS provides actuation of the following functions (or components):
safety injection (SI), containment (CNMT)isolation, CNMT spray, auxiliary feedwater (AFW), diesel generators, and main steam and main feedwater isolation.
The loss of'fuse FUSIBl/SIBF1-P caused the loss of automatic actuation of the following items: o SI train"B" o CNMT spray train"B" o CNMT isolation train"B" 0 0 o Main steam and main feedwater isolation (one of two channels for each isolation and/or bypass valve)The"B" Emergency diesel generator (D/G)and"B" motor-driven AFW pump train would still actuate from signals such as undervoltage or low steam generator level.However, the loss of automatic actuation of SI train"B" prevented the"B" Emergency D/G and"B" motor-driven AFW pump train from starting due to an SI signal.As shown above, the loss of fuse FUSIB1/SIBF1-P resulted in the loss of one multi-function train;however, the redundant train was available if an accident were to occur during the approximately one and one half hours that the single train'was inoperable.
The loss of a single train is considered in the design of the ESFAS, which utilizes independent trains and channels for each function.This independence is maintained from the process sensors to the signal output relays and includes the channel power supplies.Thus, no single failure can cause the loss of function.0 The Standard Technical Specifications for Westinghouse reactors (NUREG-1431) allows six hours to restore an inoperable channel to operable status before requiring a plant shutdown.Entering TS 3.0~1 is more conservative than following the requirements of NUREG-1431, since the redundant trains were available to perform their intended function.Based on the above, it can be concluded that the public's health and safety was assured at all times.NRC FORH 366A (5 92)
NRC FORM 366A (5-92)U.S.NUCLEAR REGULATORY COHHISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY OMB NO.3150.0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPOHSE TO COMPLY IIITN THIS INFORHATIOH COLLECTIOH REQUEST: 50.0 MRS'ORHARD COHHEHTS REGARDIHG BURDEN ESTIMATE TO THE INFORMATION AND RECORDS HANAGEHEHT BRANCH (HHBB 7714), U.ST NUCLEAR REGULATORY COHHISSION, IIASHINGTOH, DC 20555-0001 AND TO THE PAPERNORK REDUCTION PROJECT (3140-0104), OFFICE OF HAHAGEHEHT AND BUDGET IIASHIHGTON DC 20503.FACILITY NAHE (1)R.E.Ginna Nuclear Power Plant DOCKET NUHBER (2)05000244 YEAR 94--011--00 LER NUHBER (6)SEQUENTIAL REVISION PAGE (3)8 OF 9 TEXT (If more space is required, use additional copies of HRC Form 366A)(17)V.CORRECTIVE ACTION A.ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS: o The burned out indicating lamp was replaced.o The blown fuse (and associated negative fuse)were replaced.B.ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
o Operations supervision notified all operations personnel not to change any indicating lamps on the cabinets in the Relay Room.Operators are to submit a trouble report for IEC to change the lamps.o All 120 Volt indicating lamps on site are being replaced with 155 Volt lamps.When a 120 Volt lamp requires replacement, it will be replaced with a 155 Volt lamp.This is intended to increase the life of these lamps, and decrease the frequency of replacement.
o NRC Information Notice 94-68,"Safety-Related Equipment Failures Caused by Faulted Indicating Lamps", will be assessed as part of the Operational Assessment program.VI.ADDITIONAL INFORMATION A.FAILED COMPONENTS:
The burned out indicating lamp was a Sylvania incandescent lamp, Model 6S6 120V, with a design rating of 6 watts.HRC FORM 366A (5-92)
NRC FORH 366A (5-92)U.S.NUCLEAR REGULATORY COHHISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY OHB NO.3150.0104 EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORHATIOH COLLECTION REQUEST: 50.0 HRS.FORWARD COHHENTS REGARDIHG BURDEH ESTIHATE TO THE INFORHATIOH AHD RECORDS HANAGEHENT BRANCH (MHBB 7714), U.S.NUCLEAR REGULATORY COMMISSION, WASHIHGTON, DC 20555-0001 AHD TO THE PAPERWORK REDUCTION PROJECT (31/0-0104), OFFICE OF MANAGEMENT AND BUDGET'WASHINGTON DC 20503.FACILITY NAME (I)R.E.Ginna Nuclear Power Plant DOCKET NUMBER (2)05000244 94 011 00 LER NUHBER (6 YEAR SEQUENTIAL REVISION PAGE (3)9 OF 9 TEXT (If more space is required, use additional copies of HRC Form 366A)(17)B.PREVIOUS LERs ON SIMILAR EVENTS: A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Nuclear Power Plant could be iden-tified.C.SPECIAL COMMENTS: This event of September 17, 1994 is similar to events described in NRC Information Notice 94-68, which is dated September 27, 1994, and was received by Rochester Gas 6 Electric on October 4, 1994.HRC FORM 366A (5-92)