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| number = ML18128A232
| number = ML18128A232
| issue date = 05/08/2018
| issue date = 05/08/2018
| title = Oyster Creek Nuclear Generating Station-Integrated Inspection Report 05000219-2018001 and Exercise of Enforcement Discretion
| title = Integrated Inspection Report 05000219-2018001 and Exercise of Enforcement Discretion
| author name = Pelton D L
| author name = Pelton D
| author affiliation = NRC/RGN-I/DRP
| author affiliation = NRC/RGN-I/DRP
| addressee name = Hanson B
| addressee name = Hanson B
Line 9: Line 9:
| docket = 05000219
| docket = 05000219
| license number = DPR-16
| license number = DPR-16
| contact person = Young M R
| contact person = Young M
| case reference number = EA-18-007
| case reference number = EA-18-007
| document report number = IR 2018001
| document report number = IR 2018001
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=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:May 8, 2018
 
==SUBJECT:==
OYSTER CREEK NUCLEAR GENERATING STATION - INTEGRATED INSPECTION REPORT 05000219/2018001 AND EXERCISE OF ENFORCEMENT DISCRETION
 
==Dear Mr. Hanson:==
On March 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Oyster Creek Nuclear Generating Station. On April 4, 2018, the NRC inspectors discussed the results of this inspection with Mr. Timothy Moore, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.
 
NRC inspectors documented one Severity Level IV violation with no associated finding. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.
 
In addition, the NRC reviewed Licensee Event Report 05000219/2017-005-00, which described the circumstances associated with a failed electrical ring lug on the No. 2 emergency diesel generator. It was recognized that the No. 2 emergency diesel generator was inoperable for a period of time that exceeded the allowed outage time of seven days detailed in Technical Specification 3.7.C.2.b, and therefore, is a violation of technical specifications. Regional staff performed a risk evaluation and determined the issue was of low to moderate safety significance (White).
 
Although this issue constitutes a violation of NRC requirements, the NRC determined that the electrical ring lug failure which caused the No. 2 emergency diesel generator to be inoperable was not within Exelons ability to reasonably foresee and correct. As a result, the NRC did not identify a performance deficiency associated with this condition. The NRCs assessment considered Exelons maintenance practices, industry operating experience, vendor and industry maintenance and testing recommendations, and Exelons corrective actions to prevent recurrence of the issue.
 
Based on the results of the NRCs inspection and assessment, I have been authorized, after consultation with the Director, Office of Enforcement, to exercise enforcement discretion in accordance with NRC Enforcement Policy Section 2.2.4, Exceptions to Using Only the Operating Reactor Assessment Program, and Section 3.10, Reactor Violations with No Performance Deficiency. The Region I Regional Administrator was also consulted regarding enforcement discretion for this issue. If you contest the non-cited violation in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at Oyster Creek Nuclear Generating Station.
 
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRCs Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390, Public Inspections, Exemptions, Requests for Withholding.
 
Sincerely,
/RA/
 
David L. Pelton, Director Division of Reactor Projects
 
Docket Number: 50-219 License Number: DPR-16
 
===Enclosure:===
Inspection Report 05000219/2018001
 
==Inspection Report==
Docket Number:
 
50-219
 
License Number:
 
DPR-16
 
Report Number:
 
05000219/2018001
 
Enterprise Identifier:
I-2018-001-0078
 
Licensee:
 
Exelon Nuclear
 
Facility:
 
Oyster Creek Nuclear Generating Station
 
Location:
 
Forked River, New Jersey
 
Inspection Dates:
 
January 1, 2018 to March 31, 2018
 
Inspectors:
 
A. Patel, Senior Resident Inspector
 
E. Andrews, Resident Inspector
 
F. Arner, Senior Reactor Analyst
 
J. Furia, Senior Health Physicist
 
J. Kulp, Senior Reactor Inspector
 
J. Schoppy, Senior Reactor Inspector
 
Approved By:
 
David L. Pelton, Director
 
Division of Reactor Projects
 
=SUMMARY=
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Exelons performance at
 
Oyster Creek Nuclear Generating Station by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors.
 
Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC identified and self-revealing findings, violations, and additional items are summarized in the table below.
 
===List of Findings and Violations===
Untimely Licensee Event Report for Reportable Conditions Associated with the No. 2 Emergency Diesel Generator Cornerstone Severity Cross-Cutting Aspect Report Section Not Applicable Severity Level IV, NCV 05000219/2018001-01 Closed Not Applicable 71153 The inspectors identified a non-cited, Severity IV violation of 10 CFR 50.73(a)(1) for a failure to submit a licensee event report (LER) within 60 days after the discovery of an event requiring a report. Specifically, on October 9, 2017, Exelon determined that the No. 2 emergency diesel generator was inoperable for longer than the allowed outage time, which is reportable as a condition prohibited by technical specifications. Exelon did not submit an LER for this event until January 3, 2018.
 
===Additional Tracking Items===
Type Issue Number Title Report Section Status LER 05000219/2017-005-00 No. 2 emergency diesel generator inoperable 71153 Closed
 
=PLANT STATUS=
 
Oyster Creek began the inspection period at 100 percent power. On January 6, 2018, operators lowered power to 70 percent due to low intake levels. Operators returned the unit to 100 percent on January 8, 2018. The unit remained at or near 100 percent power for the remainder of the inspection period.
 
==INSPECTION SCOPES==
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html.
 
Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter 2515, Light-Water Reactor Inspection Program - Operations Phase.
 
The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensees performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
 
==REACTOR SAFETY==
==71111.01 - Adverse Weather Protection==
===Impending Severe Weather (2 Samples)===
The inspectors evaluated readiness for impending adverse weather conditions for a blizzard warning issued on January 4, 2018, and for low intake levels on January 6, 2018.
 
===External Flooding (1 Sample)===
The inspectors evaluated protection from external flooding prior to and during high winds and heavy rain on March 2, 2018.
 
==71111.04 - Equipment Alignment==
===Partial Walkdown (6 Samples)===
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
: (1) No. 1 emergency diesel generator while No. 2 emergency diesel generator was inoperable on January 3, 2018
: (2) Emergency service water pumps during low intake level on January 6, 2018
: (3) A isolation condenser during emergent unavailability of the B isolation condenser on February 12, 2018
: (4) Core spray system II during planned unavailability of core spray system I on February 20, 2018
: (5) B isolation condenser during shell side makeup on March 5, 2018
: (6) B isolation condenser during emergent work on A isolation condenser on March 12, 2018
 
===Complete Walkdown (1 Sample)===
The inspectors evaluated system configurations during a complete walkdown of the standby liquid control system on February 15-16, 2018.
 
==71111.05Q - Fire Protection Quarterly==
===Quarterly Inspection (9 Samples)===
The inspectors evaluated fire protection program implementation in the following selected areas:
: (1) No. 1 emergency diesel generator room on January 24, 2018
: (2) No. 2 emergency diesel generator room on January 24, 2018
: (3) Reactor building 95 elevation on February 21, 2018
: (4) Reactor building 75 elevation on February 21, 2018
: (5) Reactor building 23 elevation on February 21, 2018
: (6) C 125 VDC battery room on February 28, 2018
: (7) A and B 4kV switchgear room on February 28, 2018
: (8) New cable spreading room on March 1, 2018
: (9) Recirculation pump motor generator set room on March 1, 2018
 
==71111.06 - Flood Protection Measures==
===Internal Flooding (1 Sample)===
The inspectors evaluated internal flooding mitigation protections in turbine building switchgear area on February 22, 2018.
 
==71111.07 - Heat Sink Performance==
===Heat Sink (1 Sample)===
The inspectors evaluated Exelons monitoring and maintenance of B isolation condenser performance on March 5, 2018.
 
==71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance==
===Operator Requalification (2 Samples)===
The inspectors observed and evaluated a crew of licensed operators in the plants simulator during licensed operator requalification training on January 23, 2018, and March 13, 2018.
 
===Operator Performance (1 Sample)===
The inspectors observed licensed operator performance during the Notice of Unusual Event on January 6, 2018.
 
==71111.12 - Maintenance Effectiveness==
===Routine Maintenance Effectiveness (4 Samples)===
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
: (1) Periodic 10 CFR 50.65(a)(3) evaluation on January 17, 2018
: (2) Service air system on January 22, 2018
: (3) Start-up transformers on February 21, 2018
: (4) Reactor recirculation system on March 5, 2018
 
==71111.13 - Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13|count=6}}
 
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
: (1) Notice of Unusual Event declaration due to low intake levels on January 6, 2018
: (2) Planned maintenance on the A isolation condenser on January 9, 2018
: (3) Planned maintenance on the B isolation condenser on January 18, 2018
: (4) Planned maintenance on core spray system I on February 20, 2018
: (5) Planned maintenance on core spray system II on March 14, 2018
: (6) Planned maintenance on the No. 2 emergency diesel generator on March 26, 2018
 
==71111.15 - Operability Determinations and Functionality Assessments==
{{IP sample|IP=IP 71111.15|count=7}}
 
The inspectors evaluated the following operability determinations and functionality assessments:
: (1) Emergency service water pumps during low intake level on January 6, 2018
: (2) Standby liquid control poison tank low level on January 29, 2018
: (3) B isolation condenser elevated temperatures on February 16, 2018
: (4) Control rod 34-43 slow five percent scram time on March 5, 2018
: (5) B isolation condenser lowering shell side level on March 6, 2018
: (6) A isolation condenser steam leak on March 12, 2018
: (7) No. 2 emergency diesel generator elevated lead levels in oil sample on March 15, 2018
 
==71111.18 - Plant Modifications==
{{IP sample|IP=IP 71111.18|count=1}}
 
The inspectors evaluated the following temporary or permanent modifications:
 
Engineering Change 620725, Refuel Bridge Software Modification to Allow Offloading Fuel from a Cask
 
==71111.19 - Post Maintenance Testing==
{{IP sample|IP=IP 71111.19|count=8}}
 
The inspectors evaluated post maintenance testing for the following maintenance/repair activities:
: (1) A recirculation pump relay replacement on January 22, 2018
: (2) B isolation condenser valve, V-14-37, following valve repair on February 13, 2018
: (3) A core spray pump relay replacement on February 20, 2018
: (4) Average power range monitor 7 restoration to an operable condition on February 22, 2018
: (5) B isolation condenser remote shutdown panel level indication following emergent inoperability on February 22, 2018
: (6) Main generator exciter direct current (DC) brush inspection and replacement on March 1, 2018
: (7) 1-8 sump control logic following fuse replacement on March 27, 2018
: (8) No. 2 emergency diesel generator following biannual overhaul on March 28, 2018
 
==71111.22 - Surveillance Testing==
The inspectors evaluated the following surveillance tests:
 
===Routine===
{{IP sample|IP=IP 71111.22|count=6}}
: (1) 636.4.013, Diesel Generator 2 Load Test on January 3, 2018
: (2) 609.3.003, Isolation Condenser Automatic Actuation Sensor Calibration and Test on January 18, 2018
: (3) 607.4.016, Containment Spray and Emergency Service Water System I Pump Operability and Quarterly Inservice Test on January 23, 2018
: (4) 604.3.001, Reactor Building to Torus Power Vacuum Breaker Test and Calibration on February 8, 2018
: (5) 602.3.004, Electromatic Relief Valve Pressure Sensor Test and Calibration on March 6, 2018
: (6) 651.4.003, Standby Gas Treatment System 15-minute Run - System 2 on March 17, 2018
 
===Inservice (2 Samples)===
: (1) 612.4.001, A Standby Liquid Control Pump and Valve Operability and In-service Test on January 9, 2018
: (2) 610.4.003, Core Spray Valve Operability and In-Service Test on March 12, 2018
 
==71114.06 - Drill Evaluation==
===Emergency Planning Drill (1 Sample)===
The inspectors evaluated the conduct of a routine Exelon emergency planning drill on March 13, 2018.
 
===Drill/Training Evolution (1 Sample)===
The inspectors observed a simulator training evolution for licensed operators on January 23,
 
==RADIATION SAFETY==
==71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,==
and Transportation
 
===Radioactive Material Storage===
{{IP sample|IP=IP 71124.08|count=1}}
 
The inspectors observed radioactive waste container storage areas and verified the postings and controls and that Exelon had established a process for monitoring the impact of long-term storage of the waste.
 
===Radioactive Waste System Walkdown (1 Sample)===
The inspectors walked down the following:
* Accessible portions of liquid and solid radioactive waste processing systems to verify current system alignment and material condition
* Abandoned in place radioactive waste processing equipment to review the controls in place to ensure protection of personnel
* Changes made to the radioactive waste processing systems since the last inspection
* Processes for mixing and transferring radioactive waste resin and/or sludge discharges into shipping/disposal containers
* Current methods and procedures for dewatering waste
 
===Waste Characterization and Classification (1 Sample)===
The inspectors identified radioactive waste streams and reviewed radiochemical sample analysis results to support radioactive waste characterization. The inspectors reviewed the use of scaling factors and calculations to account for difficult-to-measure radionuclides.
 
===Shipment Preparations (1 Sample)===
The inspectors reviewed the records of shipment packaging, surveying, labeling, marking, placarding, vehicle checks, emergency instructions, disposal manifest, shipping papers provided to the driver, and Exelons verification of shipment readiness.
 
===Shipment Records (1 Sample)===
The inspectors reviewed selected non-excepted package shipment records.
 
==OTHER ACTIVITIES - BASELINE==
==71152 - Problem Identification and Resolution==
===Annual Follow-up of Selected Issues (1 Sample)===
The inspectors reviewed Exelons implementation of its corrective action program related to the following issues:
 
No. 2 Emergency Diesel Generator Ring Lug Failure
 
===71153 - Follow-up of Events and Notices of Enforcement Discretion
 
Events===
{{IP sample|IP=IP 71153|count=1}}
 
The inspectors evaluated response to the following events:
 
Notice of Usual Event due to low intake levels on January 6, 2018
 
===Licensee Event Reports (1 Sample)===
The inspectors evaluated the following LERs which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:
 
LER 05000219/2017-005-00 and -01, Failure of the Emergency Diesel Generator #2, During Surveillance Testing due to a Broken Electrical Connector, on February 14,
 
==INSPECTION RESULTS==
Enforcement Discretion Enforcement Action (EA)-18-007: No. 2 Emergency Diesel Generator Ring Lug Failure 71152
 
=====Description:=====
On October 9, 2017, during a routine surveillance load test, the No. 2 emergency diesel generator failed approximately 5 minutes into the run due to a broken ring lug on a current transformer. Laboratory analysis of the broken ring lug determined that the ring lug failed due to fatigue cracking that was initiated due to stresses caused by bending and twisting of the electrical lug. Exelon last conducted a load surveillance on the No. 2 emergency diesel generator on September 25, 2017.
 
Corrective Actions: Corrective actions included replacement on the broken ring lug on the No. 2 emergency diesel generator, extent of condition inspections on the No. 1 and No. 2 emergency diesel generators for additional bent or twisted ring lug connectors, and revision to the electrical ring lug installation and emergency diesel generator procedures to include inspection for bent or twisted ring lugs.
 
Corrective Action Reference(s): Issue report 4060815
 
=====Enforcement:=====
Violation: Oyster Creek Technical Specification 3.7.C.2.b states, in part, that if one diesel generator becomes inoperable during power operation, the reactor may remain in operation for a period not to exceed 7 days.
 
Contrary to the above, on October 9, 2017, it was recognized that one diesel generator was inoperable for greater than the technical specification allowed outage time of 7 days, and Oyster Creek continued power operation. Specifically, on October 9, 2017, No. 2 emergency diesel generator failed to run during a routine surveillance test due to a broken ring lug on a current transformer, which resulted in a total inoperability time of 6.5 months.
 
Severity/Significance: For violations warranting enforcement discretion, Inspection Manual Chapter 0612 does not require a detailed risk evaluation, however, safety significance characterization is appropriate. A Region I Senior Reactor Analyst (SRA) performed a best estimate analysis of the safety significance using the Oyster Creek Standardized Plant Analysis Risk (SPAR) model, Version 8.50 and Systems Analysis Programs for Hands-On Integrated Reliability Evaluations (SAPHIRE). The evaluation estimated the total (internal and external events risk) increase in core damage frequency (CDF) to be in the mid to high E-6/yr range, or a low to moderate safety significance. The SRA evaluated the internal events risk contribution due to the inoperability of the No. 2 emergency diesel generator for an approximate 6.5 month exposure time. The exposure time relative to when the No. 2 emergency diesel generator was no longer capable of meeting its 24 hour mission time is uncertain due to the effect of vibration induced fatigue, and therefore the method prescribed within the RASP handbook guidance was used.
 
The analyst used the guidance in Section 2.5 of the Handbook, Revision 2.0, to estimate the exposure time of 6.5 months based on the cumulative 24 hour summation of the No. 2 emergency diesel generator surveillance test proven run time. This approach is appropriate for periodically operated components that degrade during operation (i.e. vibration induced fatigue only occurs while the emergency diesel generator is in-service/operating). Given this approach, the dominant internal events, loss of offsite power were evaluated for the estimated internal risk increase. This contribution was estimated at 2E-6/yr increase in CDF. The dominant sequences involved loss of offsite power events with a concurrent failure of the No. 1 emergency diesel generator, failure of the combustion turbines, and failure to recover offsite power or recover an emergency diesel generator prior to core damage.
 
The SRA performed various modeling changes after a review of revised calculations for DC battery life:
 
Analysis noted that Oyster Creek Generating Station recirculation pump seals are similar in design to those tested in reports generated for Nine Mile Point Unit 1 with the use of CAN2A seals. Therefore, the failure probability of the seals in the station blackout sequence was adjusted from 0.1 to 5E-2 similar to Nine Mile Point Unit 1 SPAR model 8.50.
 
The failure to load shed action (DCP-XHE-XM-LSHED) in the model was calculated using the SPAR-H method and revised to 1.2E-2 versus being assumed to always fail (TRUE).
* Failure probabilities for 1, 2, or 3 stuck open electromatic relief valves were revised to be consistent with the previous model version 8.22 because of the isolation condenser design at Oyster Creek Generating Station which limits cycling and significantly reduces the probability of a failed open electromatic relief valve due to isolation condensers controlling pressure.
* The depressurization function using electromatic relief valves, if required, was calculated through SPAR-H to be 1E-2 for sequences where total seal failure is assumed (DEPSEALFAIL) (conservatively assumed limited time available).
* The diesel driven firewater pumps are both available and were set to calculated fault tree failure probabilities instead of always failed in the previous model. These are 2,000 gallons per minute pumps with a large supply of water and relatively simple operator actions to inject to the reactor pressure vessel. The firewater was assumed to fail at 0.1 when a total recirculation seal failure occurs due to assumed time constraints.
* The offsite power and the emergency diesel generator required recovery time events were increased to 24 hours for events where DC load shedding was successful, without seal failures and isolation condenser success along with diesel driven firewater success.
 
The SRA noted the No. 2 emergency diesel generator was recoverable. In fact, the diagnosis of the failed condition was performed in a nominal 8-10 hours from the failure. Therefore, a probability of failure to recover event for the conditional case was developed. The SRA used SPAR-H as simple guidance, which conservatively supported a reasonable assumption of a 0.10 conditional probability of failure to recover the emergency diesel generator within 24 hours. The base case utilized a calculation within SPAR of 0.33 failure to recover probability for 24 hour sequences.
 
To estimate the external risk contribution, the SRA identified that the most significant external risk contribution was from fire events. Seismic, external flooding, and high wind events were not significant contributors for the issue.
 
From discussions with Oyster Creek Fire probabilistic risk analysts and a review of this failure condition, the increase in CDF due to the failed No. 2 emergency diesel generator for the assumed 6.5 month exposure time was estimated at 4.5E-6/yr [(8.5E-5/yr-4.5E-5/yr) x (6.5/12 months) x 0.2].
 
The DC safety-related battery life would be at least a nominal 14 hours and longer if DC bus stripping occurred, this allows for extended isolation condenser or electromatic relief valve function, with injection from diesel driven firewater. Given the time considerations and characteristics of the failure, an assumed recovery at a failure probability of 0.2 (slightly higher than internal due to less time) was applied for the No. 2 emergency diesel generator, which was a best estimate determined through SPAR-H insights. The dominant fire sequence was a fire affecting the A and B 4kV switchgear rooms, where combustion turbine support would be lost, with failure of the No. 1 emergency diesel generator breaker to close, and failure of locally operating the isolation condenser due to eventual loss of power. The SRA noted that FLEX credit was not quantified and would result in a lower risk estimation likely in the low E-6/yr range. Combining internal and external risk contributions, the total increase in CDF was 6.5E-6/yr, or low to moderate safety significance. The SRA determined that Exelon uses a Large Early Release Frequency (LERF) factor value of 8E-2. This value takes into consideration operator action for those relevant high pressure vessel breach scenarios (fuel-coolant interaction, liner-melt-through, and direct containment heating). This also credits procedure strategies where other mitigating actions are taken such as flooding the drywell.
 
The SRA review of the dominant sequences and time to core damage affirmed that LERF did not increase the risk over that determined from the increase in CDF.
 
Basis for Discretion: The inspectors determined that the ring lug failure was not within Exelons ability to foresee and prevent. As a result, no performance deficiency was identified.
 
The inspectors assessment considered:
 
===1. Exelons review of emergency diesel maintenance performed in 2015 checked all===
connections of the current transformer for tightness. The inspectors did not identify any gaps or deficiencies in the 2015 inspections. Inspectors also reviewed completed biennial inspections of the connection dating back to 1991 and did not identify any gaps.
 
===2. At the time of the failure, the current transformer connections did not have a time===
directed replacement frequency recommended by the Emergency Diesel Generator Owners Group. The inspectors did not identify any additional vendor or industry recommendations specific to the failed component or considerations specific to the failed component that existed prior to the failure.
 
===3. Industry operating experience information available to Exelon did not identify the===
potential for the fatigue cracking of the bent wire ring lug that was experienced.
 
===4. The bent ring lug failure was not the result of a failure on the part of Exelon staff; no===
standards existed on bending of the lug during installation and is considered skill of the craft.
 
The NRC determined that it was not reasonable for Exelon to have been able to foresee and prevent this violation of NRC requirements, and as such, no performance deficiency existed.
 
Therefore, the NRC has decided to exercise enforcement discretion in accordance with Sections 2.2.4 and 3.10 of the NRC Enforcement Policy and refrain from issuing enforcement action for the violation of technical specifications (EA-18-007). Further, because Exelons actions did not contribute to this violation, it will not be considered in the assessment process or the NRC Action Matrix.
 
Observation 71152 Exelons equipment corrective action program evaluation report (ECAPE) determined that the ring lug failed on the No. 2 emergency diesel generator as a result of fatigue cracking, which was initiated due to excessive stress caused by bending and twisting of the ring lug beyond limits specified in industry guidelines. The inspectors noted that the ECAPE did not provide supporting information regarding how the ring lug was bent and twisted beyond industry guidelines. Specifically, industry guidance states that ring lugs can be bent up to 90 degrees.
 
The broken ring lug found in the No. 2 emergency diesel generator was bent at approximately 45-55 degrees per the ECAPE, which was within industry guidelines. Additionally, the ECAPE did not include specific guidance on twisting allowances for ring lugs. Exelon documented the inspectors observation in Issue Report 4089829. As a result of the inspectors observation, Exelon revised the ECAPE to say the ring lug failed on the No. 2 emergency diesel generator as a result of fatigue cracking, which was initiated due to excessive stress caused by bending and twisting of the ring lug.
 
Untimely Licensee Event Report for Reportable Conditions Associated with the No. 2 Emergency Diesel Generator Cornerstone Severity Cross-Cutting Aspect Report Section Not Applicable Severity Level IV, NCV 05000219/2018001-01 Opened/Closed Not Applicable 71153 The inspectors identified a Severity IV non-cited violation of 10 CFR 50.73(a)(1) for a failure to submit an LER within 60 days after the discovery of an event requiring a report.
 
Specifically, on October 9, 2017, Exelon determined that the No. 2 emergency diesel generator was inoperable for longer than the allowed outage time, which is reportable as a condition prohibited by technical specifications. Exelon did not submit an LER for this event until January 3, 2018.
 
=====Description:=====
On October 9, 2017, the No. 2 emergency diesel was operated for its bi-weekly load surveillance. Approximately five minutes into the run, the main control room received LKOUT RELAY TRIP and EDG 2 DISABLED alarms. Following an automatic shutdown of the No. 2 emergency diesel generator, Exelon staff discovered a ring lug of a current transformer had broken. The last time the No. 2 emergency diesel generator was operated for its bi-weekly load surveillance was on September 25, 2017. Oyster Creek Technical Specification 3.7.C.2 states, in part, that if one diesel generator becomes inoperable during power operation, the reactor may remain in operation for a period not to exceed 7 days.
 
Details regarding the broken lug on the No. 2 emergency diesel generator can be found in Section 71152.
 
On December 9, 2017, the inspectors identified that the No. 2 emergency diesel generator was inoperable for longer than its technical specification allowed outage time of 7 days, which is reportable to the NRC. 10 CFR 50.73 states, in part, that the licensee shall report any operation or condition which was prohibited by the plants technical specifications. Exelon had not submitted an LER within the 60 day requirement because they did not consider the inoperable No. 2 emergency diesel generator as an event that required an LER as specified in 10 CFR 50.73.
 
Corrective Action(s): Exelon submitted the required LER on January 3, 2018.
 
Corrective Action Reference: Issue Report 4092328
 
=====Performance Assessment:=====
__________________________________________________________________________
Performance Deficiency: The inspectors determined that the failure to report a condition which is prohibited by technical specifications within the time frame required by 10 CFR 50.73(a)(1) was a performance deficiency.
 
Screening: Traditional enforcement applies because a failure to report an event in a timely manner has the potential to impact the NRCs ability to perform its regulatory function.
 
Significance: The finding was determined to be a Severity Level IV violation consistent with Section 6.9.d.9 of the NRC Enforcement Policy.
 
Cross-Cutting Aspect: No cross-cutting aspect was assigned to this finding because it was screened under the traditional enforcement process.
 
=====Enforcement:=====
Severity: The ROPs significance determination process does not specifically consider the regulatory process impact in its assessment of licensee performance. Therefore, it is necessary to address this violation which impedes the NRCs ability to regulate using traditional enforcement to adequately determine non-compliance.
 
The inspectors determined that the violation was a Severity Level IV, which is a more than minor violation, which is a concern that resulted in no or relatively inappreciable potential safety or security consequence. The untimely LER was not used to make an unacceptable change to the facility nor did it impact a licensing or safety decision by the NRC.
 
Violation: 10 CFR 50.73(a)(1) requires, in part, that a licensee submit an LER for any event of the type described in this paragraph within 60 days after the discovery of the event.
 
10 CFR 50.73(a)(2)(i)(B) requires, in part, that the licensee report any event or condition prohibited by the plants technical specifications. Contrary to the above, on December 9, 2017, Exelon failed to submit an LER within 60 days after the discovery that the No. 2 emergency diesel generator was inoperable for longer than its technical specification allowed outage time of 7 days. This event occurred on October 9, 2017, and Exelon submitted the LER on January 3, 2018, which exceeded the 10 CFR 50.73(a)(11) 60 day requirement.
 
Exelon entered this issue into their corrective action program in issue report 4092328.
 
Enforcement Action(s): This Severity Level IV violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the NRC Enforcement Policy.
 
==EXIT MEETINGS AND DEBRIEFS==
Inspectors verified no proprietary information was retained or documented in this report.
* On February 9, 2018, the inspectors presented the radiation safety inspection results to Mr. Michael Gillin, Plant Manager, and other members of the Oyster Creek staff.
* On April 4, 2018, the inspectors presented the quarterly resident inspector inspection results to Mr. Timothy Moore, Site Vice President, and other members of the Oyster Creek staff.
 
=DOCUMENTS REVIEWED=
 
71111.01: Adverse Weather Protection
Procedures
ABN 18, Service Water Failure Response, Revision 7
ABN-31, High Winds, Revision 21
ABN 32, Abnormal Intake Level, Revision 30
OP-AA-108-111-1001, Severe Weather and Natural Disaster Guidelines, Revision 16
OP-OC-108-109-1001, Severe Weather Preparation T&RM for Oyster Creek, Revision 38
Issue Reports
4110580
71111.04: Equipment Alignment
Drawings
GE 885D781 Sh.1, Core Spray System Flow Diagram, Revision 76
GE 148F262 Sh.1, Emergency Condenser Flow Diagram, Revision 56
Issue Reports
1619946
4102875
4108748
4108767
4109454
71111.05: Fire Protection
Procedures
101.2, Oyster Creek Site Fire Protection Program, Revision 73
ABN 29, Plant Fires, Revision 32
ER-AA-600-1069, High Risk Fire Area Identification, Revision 4
OP-OC-201-008, Oyster Creek Pre-fire Plans, Revision 26
OP-OC-201-012-1001, On-line Fire Risk Management, Revision 4
Issue Reports
3971381
4059012
71111.06: Flood Protection Measures
Miscellaneous
OP-PSA-012, Internal Flood Evaluation Summary Notebook, dated May 2014
OC-PSA-022, Internal Flood Walkdown Notebook, dated May 2014
71111.11: Licensed Operator Requalification Program
Procedures
EP-AA-1010, Addendum 3, Exelon Nuclear Emergency Action Levels for Oyster Creek Station,
Revision 2
71111.12: Maintenance Effectiveness
Procedures
ER-AA-310, Implementation of the Maintenance Rule, Revision 11
ER-AA-310-1004, Maintenance Rule - Performance Monitoring, Revision 14
ER-AA-310-1005, Maintenance Rule - Dispositioning Between (a)(1) and (a)(2), Revision 7
 
Issue Reports
0516160
0648480
0687240
1501306
1514742
2472912
23130
2536453
2537005
2572740
25933
29443
29982
2637292
2643485
2643486
2702946
2714199
2715226
2719824
3949214
3952496
4060818
4069654
4089360
4089390
4109343
Miscellaneous
Oyster Creek Generating Station Maintenance Rule Periodic (a)(3) Assessment from
July 1, 2015 - June 30, 2017, dated November 29, 2017
Maintenance Orders/Work Orders
4345665
4345669
4345671
4345673
71111.15: Operability Evaluations
Issue Reports
4111295
4111496
4111518
4111506
71111.18: Plant Modifications
Miscellaneous
EC 620725, Refuel Bridge PLC Software Modification to Allow Offloading Fuel from a Cask,
dated February 23, 2018
71111.19: Post-Maintenance Testing
Issue Reports
4070270
4103389
4104381
4106951
4107367
4110560
Maintenance Orders/Work Orders
4745244
4745324
4745979
4748691
71124.08: Radioactive Solid Waste Processing and Radioactive Material Handling,
Storage, and Transportation
Procedures
RW-AA-100, Process Control Program for Radioactive Wastes, Revision 12
RW-AA-605, 10 CFR 61 Program, Revision 8
RP-AA-600, Radioactive Material/Waste Shipments, Revision 16
RP-AA-600-1001, Exclusive Use and Emergency Response Information, Revision 9
RP-AA-600-1005, Radioactive Material and Non Disposal Site Waste Shipments, Revision 19
RP-AA-600-1006, Shipment of Category 1 Quantities of Radioactive Material or Waste
(Category 1 RAMQC), Revision 11
RP-AA-600-1009, Shipment of Category 2 Quantities of Radioactive Material or Waste
(Category 2 RAMQC), Revision 2
RP-AA-600-1010, Use and Operation of WMG Software for Creating Containers, Samples,
Waste Streams and Waste Types, Revision 2
RP-AA-600-1011, Use and Operation of WMG Software for Gross Gamma Characterization and
Generation of Shipping Paperwork, Revision 4
RP-AA-601, Surveying Radioactive Material Shipments, Revision 20
RP-AA-602, Packaging of Radioactive Material Shipments, Revision 20
RP-AA-602-1001, Packaging of Radioactive Material/Waste Shipments, Revision 17
RP-AA-603, Inspection and Loading of Radioactive Material Shipments, Revision 10
RP-AA-605, 10 CFR 61 Program, Revision 7
 
Quality Assurance
NOSA-OYS-16-04, Chemistry, Radwaste, Effluent and Environmental Monitoring Audit Report
NOSA-OYS-17-06, Radiation Protection Audit Report
Fleet Assessment T-18 Assessment Report, October 2016
Fleet Assessment T-6 Assessment Report, September 2017
Fleet Assessment Mid-Cycle Assessment Report, March 2017
CFR Part 61 Scaling Factors
Dry Active Waste, Bead Resin, Sludge, CLW Composite, Cartridge Filters
2016-2017 10 CFR 61 Waste Stream Analysis, December 2016
Assignment Reports
23501
20554
2608094
Training
HAZSEC, DOT Security Awareness and Transportation Security Plan, Revision 1
NRWSHP-1000, DOT/79-19 Training for Support of Radioactive and Asbestos Shipments,
Revision 4
Shipments
OC-3001-16 OC-4003-16 OC-3001-17 OC-3002-17 OC-3003-17
71152: Problem Identification and Resolution
Procedures
PI-AA-125, Corrective Action Program Procedure, Revision 6
PI-AA-125-1006, Investigation Techniques Manual, Revision 3
MA-AA-726-620, Installation Instructions for 0-600 Volt EQ Related Splices, Revision 6
MA-OC-741-101, Diesel Generator Inspection (24 Month) - Electrical, Revision 15
NO-AA-300-1001, Nuclear Oversight Independent Inspection Plan, Revision 10
2400-GME-3780.52, Installation, Testing and Termination of Wire and Cable, Revision 6
2400-SME-3780.03, Electrical Termination Taping and Raychem Splicing, Revision 16
Maintenance Orders/Work Orders
R2239604
R2230340
R2229008
R2207589
R2191838
R2190504
R2151723
R2111307
R2032680
R2065956
R0808797
R0522916
R0504310
R0055415
R0041081
R0029109
4695984
4695269
4697086
4694906
Issue Reports
4060815
4089829
1436376
4061089
4073377
4060815
4060818
4061527
4061931
4066706
4061093
Miscellaneous
ES-023, Selection and Sizing of Power, Lighting and Control Cables, Revision 2
SP-9000-31-213, Class 1E, Electric Cable for Power, Control & Instrumentation, Revision 9
SP-9000-41-005, Cables & Raceways at Oyster Creek, Revision 3
71153: Follow-up of Events and Notices of Enforcement Discretion
Issue Reports
4091183
4091037
4091010
4090950
4090920
4090820
4090803
4091287
4091455
 
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION I
2100 RENAISSANCE BOULEVARD, SUITE 100
KING OF PRUSSIA, PA 19406-2713
May 8, 2018
EA-18-007
Mr. Bryan Hanson
Senior Vice President, Exelon Generation Co., LLC
President and Chief Nuclear Officer, Exelon Nuclear
4300 Winfield Road
Warrenville, IL 60555
SUBJECT: OYSTER CREEK NUCLEAR GENERATING STATION - INTEGRATED INSPECTION
REPORT 05000219/2018001 AND EXERCISE OF ENFORCEMENT DISCRETION
Dear Mr. Hanson:
On March 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection
at Oyster Creek Nuclear Generating Station. On April 4, 2018, the NRC inspectors discussed
the results of this inspection with Mr. Timothy Moore, Site Vice President, and other members of
your staff. The results of this inspection are documented in the enclosed report.
NRC inspectors documented one Severity Level IV violation with no associated finding. The
NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of
the Enforcement Policy.
In addition, the NRC reviewed Licensee Event Report 05000219/2017-005-00, which described
the circumstances associated with a failed electrical ring lug on the No. 2 emergency diesel
generator. It was recognized that the No. 2 emergency diesel generator was inoperable for a
period of time that exceeded the allowed outage time of seven days detailed in Technical
Specification 3.7.C.2.b, and therefore, is a violation of technical specifications. Regional staff
performed a risk evaluation and determined the issue was of low to moderate safety
significance (White).
Although this issue constitutes a violation of NRC requirements, the NRC determined that the
electrical ring lug failure which caused the No. 2 emergency diesel generator to be inoperable
was not within Exelons ability to reasonably foresee and correct. As a result, the NRC did not
identify a performance deficiency associated with this condition. The NRCs assessment
considered Exelons maintenance practices, industry operating experience, vendor and industry
maintenance and testing recommendations, and Exelons corrective actions to prevent
recurrence of the issue.
Based on the results of the NRCs inspection and assessment, I have been authorized, after
consultation with the Director, Office of Enforcement, to exercise enforcement discretion in
accordance with NRC Enforcement Policy Section 2.2.4, Exceptions to Using Only the
Operating Reactor Assessment Program, and Section 3.10, Reactor Violations with No
Performance Deficiency. The Region I Regional Administrator was also consulted regarding
enforcement discretion for this issue.
B. Hanson
 
If you contest the non-cited violation in this report, you should provide a response within 30 days
of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with
copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC
Resident Inspector at Oyster Creek Nuclear Generating Station.
This letter, its enclosure, and your response (if any) will be made available for public inspection
and copying at http://www.nrc.gov/reading-rm/adams.html and the NRCs Public Document
Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390,
Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
 
David
: [[contact::L. Pelton]], Director
Division of Reactor Projects
Docket Number: 50-219
License Number: DPR-16
Enclosure:
Inspection Report 05000219/2018001
cc w/encl:
Distribution via ListServ
 
ML18128A232
SUNSI Review
Non-Sensitive
Sensitive
 
Publicly Available
Non-Publicly Available
OFFICE
RI/DRP
RI/DRP
RI/DRP
RI/DRP
NAME
EAndrews
SShaffer
MYoung
DLPelton
DATE
04/26/18
04/26/18
05/08/18
05/07/18
 
U.S. NUCLEAR REGULATORY COMMISSION
Inspection Report
 
Docket Number:
50-219
 
License Number:
DPR-16
 
Report Number:
05000219/2018001
 
Enterprise Identifier:
I-2018-001-0078
 
Licensee:
Exelon Nuclear
 
Facility:
Oyster Creek Nuclear Generating Station
 
Location:
Forked River, New Jersey
 
Inspection Dates:
January 1, 2018 to March 31, 2018
 
Inspectors:
: [[contact::A. Patel]], Senior Resident Inspector
: [[contact::E. Andrews]], Resident Inspector
: [[contact::F. Arner]], Senior Reactor Analyst
: [[contact::J. Furia]], Senior Health Physicist
: [[contact::J. Kulp]], Senior Reactor Inspector
: [[contact::J. Schoppy]], Senior Reactor Inspector
 
Approved By:
David
: [[contact::L. Pelton]], Director
 
Division of Reactor Projects
 
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Exelons performance at
Oyster Creek Nuclear Generating Station by conducting the baseline inspections described in
this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process
is the NRCs program for overseeing the safe operation of commercial nuclear power reactors.
Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC
identified and self-revealing findings, violations, and additional items are summarized in the
table below.
List of Findings and Violations
Untimely Licensee Event Report for Reportable Conditions Associated with the No. 2
Emergency Diesel Generator
Cornerstone
Severity
Cross-Cutting
Aspect
Report
Section
Not Applicable
Severity Level IV, NCV
05000219/2018001-01
Closed
Not Applicable
71153
The inspectors identified a non-cited, Severity IV violation of 10 CFR 50.73(a)(1) for a failure to
submit a licensee event report (LER) within 60 days after the discovery of an event requiring a
report. Specifically, on October 9, 2017, Exelon determined that the No. 2 emergency diesel
generator was inoperable for longer than the allowed outage time, which is reportable as a
condition prohibited by technical specifications. Exelon did not submit an LER for this event
until January 3, 2018.
Additional Tracking Items
Type
Issue Number
Title
Report
Section
Status
LER
05000219/2017-005-00
No. 2 emergency diesel
generator inoperable
71153
Closed
 
PLANT STATUS
Oyster Creek began the inspection period at 100 percent power. On January 6, 2018, operators
lowered power to 70 percent due to low intake levels. Operators returned the unit to
100 percent on January 8, 2018. The unit remained at or near 100 percent power for the
remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with
their attached revision histories are located on the public website at
http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html.
Samples were declared complete when the IP requirements most appropriate to the inspection
activity were met consistent with Inspection Manual Chapter 2515, Light-Water Reactor
Inspection Program - Operations Phase.
 
The inspectors performed plant status activities described in IMC 2515 Appendix D,
Plant Status and conducted routine reviews using IP 71152, Problem Identification and
Resolution. The inspectors reviewed selected procedures and records, observed activities,
and interviewed personnel to assess licensees performance and compliance with Commission
rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Impending Severe Weather (2 Samples)
The inspectors evaluated readiness for impending adverse weather conditions for a blizzard
warning issued on January 4, 2018, and for low intake levels on January 6, 2018.
External Flooding (1 Sample)
The inspectors evaluated protection from external flooding prior to and during high winds
and heavy rain on March 2, 2018.
71111.04 - Equipment Alignment
Partial Walkdown (6 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following
systems/trains:
(1) No. 1 emergency diesel generator while No. 2 emergency diesel generator was
inoperable on January 3, 2018
(2) Emergency service water pumps during low intake level on January 6, 2018
(3) A isolation condenser during emergent unavailability of the B isolation condenser on
February 12, 2018
(4) Core spray system II during planned unavailability of core spray system I on
February 20, 2018
(5) B isolation condenser during shell side makeup on March 5, 2018
(6) B isolation condenser during emergent work on A isolation condenser on
March 12, 2018
Complete Walkdown (1 Sample)
The inspectors evaluated system configurations during a complete walkdown of the standby
liquid control system on February 15-16, 2018.
 
71111.05Q - Fire Protection Quarterly
Quarterly Inspection (9 Samples)
The inspectors evaluated fire protection program implementation in the following selected
areas:
(1) No. 1 emergency diesel generator room on January 24, 2018
(2) No. 2 emergency diesel generator room on January 24, 2018
(3) Reactor building 95 elevation on February 21, 2018
(4) Reactor building 75 elevation on February 21, 2018
(5) Reactor building 23 elevation on February 21, 2018
(6) C 125 VDC battery room on February 28, 2018
(7) A and B 4kV switchgear room on February 28, 2018
(8) New cable spreading room on March 1, 2018
(9) Recirculation pump motor generator set room on March 1, 2018
71111.06 - Flood Protection Measures
Internal Flooding (1 Sample)
The inspectors evaluated internal flooding mitigation protections in turbine building
switchgear area on February 22, 2018.
71111.07 - Heat Sink Performance
Heat Sink (1 Sample)
The inspectors evaluated Exelons monitoring and maintenance of B isolation condenser
performance on March 5, 2018.
71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance
Operator Requalification (2 Samples)
The inspectors observed and evaluated a crew of licensed operators in the plants simulator
during licensed operator requalification training on January 23, 2018, and March 13, 2018.
Operator Performance (1 Sample)
The inspectors observed licensed operator performance during the Notice of Unusual Event on
January 6, 2018.
71111.12 - Maintenance Effectiveness
Routine Maintenance Effectiveness (4 Samples)
The inspectors evaluated the effectiveness of routine maintenance activities associated with
the following equipment and/or safety significant functions:
(1) Periodic 10 CFR 50.65(a)(3) evaluation on January 17, 2018
(2) Service air system on January 22, 2018
(3) Start-up transformers on February 21, 2018
(4) Reactor recirculation system on March 5, 2018
 
71111.13 - Maintenance Risk Assessments and Emergent Work Control (6 Samples)
The inspectors evaluated the risk assessments for the following planned and emergent work
activities:
(1) Notice of Unusual Event declaration due to low intake levels on January 6, 2018
(2) Planned maintenance on the A isolation condenser on January 9, 2018
(3) Planned maintenance on the B isolation condenser on January 18, 2018
(4) Planned maintenance on core spray system I on February 20, 2018
(5) Planned maintenance on core spray system II on March 14, 2018
(6) Planned maintenance on the No. 2 emergency diesel generator on March 26, 2018
71111.15 - Operability Determinations and Functionality Assessments (7 Samples)
The inspectors evaluated the following operability determinations and functionality
assessments:
(1) Emergency service water pumps during low intake level on January 6, 2018
(2) Standby liquid control poison tank low level on January 29, 2018
(3) B isolation condenser elevated temperatures on February 16, 2018
(4) Control rod 34-43 slow five percent scram time on March 5, 2018
(5) B isolation condenser lowering shell side level on March 6, 2018
(6) A isolation condenser steam leak on March 12, 2018
(7) No. 2 emergency diesel generator elevated lead levels in oil sample on March 15, 2018
71111.18 - Plant Modifications (1 Sample)
The inspectors evaluated the following temporary or permanent modifications:
Engineering Change 620725, Refuel Bridge Software Modification to Allow Offloading Fuel
from a Cask
71111.19 - Post Maintenance Testing (8 Samples)
The inspectors evaluated post maintenance testing for the following maintenance/repair
activities:
(1) A recirculation pump relay replacement on January 22, 2018
(2) B isolation condenser valve, V-14-37, following valve repair on February 13, 2018
(3) A core spray pump relay replacement on February 20, 2018
(4) Average power range monitor 7 restoration to an operable condition on
February 22, 2018
(5) B isolation condenser remote shutdown panel level indication following emergent
inoperability on February 22, 2018
(6) Main generator exciter direct current (DC) brush inspection and replacement on
March 1, 2018
(7) 1-8 sump control logic following fuse replacement on March 27, 2018
(8) No. 2 emergency diesel generator following biannual overhaul on March 28, 2018
 
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Routine (6 Samples)
(1) 636.4.013, Diesel Generator 2 Load Test on January 3, 2018
(2) 609.3.003, Isolation Condenser Automatic Actuation Sensor Calibration and Test on
January 18, 2018
(3) 607.4.016, Containment Spray and Emergency Service Water System I Pump
Operability and Quarterly Inservice Test on January 23, 2018
(4) 604.3.001, Reactor Building to Torus Power Vacuum Breaker Test and Calibration on
February 8, 2018
(5) 602.3.004, Electromatic Relief Valve Pressure Sensor Test and Calibration on
March 6, 2018
(6) 651.4.003, Standby Gas Treatment System 15-minute Run - System 2 on
March 17, 2018
Inservice (2 Samples)
(1) 612.4.001, A Standby Liquid Control Pump and Valve Operability and In-service Test on
January 9, 2018
(2) 610.4.003, Core Spray Valve Operability and In-Service Test on March 12, 2018
71114.06 - Drill Evaluation
Emergency Planning Drill (1 Sample)
The inspectors evaluated the conduct of a routine Exelon emergency planning drill on
March 13, 2018.
Drill/Training Evolution (1 Sample)
The inspectors observed a simulator training evolution for licensed operators on
January 23, 2018.
RADIATION SAFETY
71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,
and Transportation
Radioactive Material Storage (1 Sample)
The inspectors observed radioactive waste container storage areas and verified the postings
and controls and that Exelon had established a process for monitoring the impact of long-
term storage of the waste.
 
Radioactive Waste System Walkdown (1 Sample)
The inspectors walked down the following:
*
Accessible portions of liquid and solid radioactive waste processing systems to verify
current system alignment and material condition
*
Abandoned in place radioactive waste processing equipment to review the controls
in place to ensure protection of personnel
*
Changes made to the radioactive waste processing systems since the last inspection
*
Processes for mixing and transferring radioactive waste resin and/or sludge
discharges into shipping/disposal containers
*
Current methods and procedures for dewatering waste
Waste Characterization and Classification (1 Sample)
The inspectors identified radioactive waste streams and reviewed radiochemical sample
analysis results to support radioactive waste characterization. The inspectors reviewed
the use of scaling factors and calculations to account for difficult-to-measure
radionuclides.
Shipment Preparations (1 Sample)
The inspectors reviewed the records of shipment packaging, surveying, labeling,
marking, placarding, vehicle checks, emergency instructions, disposal manifest, shipping
papers provided to the driver, and Exelons verification of shipment readiness.
Shipment Records (1 Sample)
The inspectors reviewed selected non-excepted package shipment records.
OTHER ACTIVITIES - BASELINE
71152 - Problem Identification and Resolution
Annual Follow-up of Selected Issues (1 Sample)
The inspectors reviewed Exelons implementation of its corrective action program related
to the following issues:
No. 2 Emergency Diesel Generator Ring Lug Failure
71153 - Follow-up of Events and Notices of Enforcement Discretion
Events (1 Sample)
The inspectors evaluated response to the following events:
Notice of Usual Event due to low intake levels on January 6, 2018
 
Licensee Event Reports (1 Sample)
The inspectors evaluated the following LERs which can be accessed at
https://lersearch.inl.gov/LERSearchCriteria.aspx:
LER 05000219/2017-005-00 and -01, Failure of the Emergency Diesel Generator #2,
During Surveillance Testing due to a Broken Electrical Connector, on February 14, 2018
INSPECTION RESULTS
Enforcement
Discretion
Enforcement Action (EA)-18-007: No. 2 Emergency Diesel
Generator Ring Lug Failure
71152
Description: On October 9, 2017, during a routine surveillance load test, the No. 2 emergency
diesel generator failed approximately 5 minutes into the run due to a broken ring lug on a
current transformer. Laboratory analysis of the broken ring lug determined that the ring lug
failed due to fatigue cracking that was initiated due to stresses caused by bending and
twisting of the electrical lug. Exelon last conducted a load surveillance on the No. 2
emergency diesel generator on September 25, 2017.
Corrective Actions: Corrective actions included replacement on the broken ring lug on the
No. 2 emergency diesel generator, extent of condition inspections on the No. 1 and No. 2
emergency diesel generators for additional bent or twisted ring lug connectors, and revision to
the electrical ring lug installation and emergency diesel generator procedures to include
inspection for bent or twisted ring lugs.
Corrective Action Reference(s): Issue report 4060815
Enforcement:
Violation: Oyster Creek Technical Specification 3.7.C.2.b states, in part, that if one diesel
generator becomes inoperable during power operation, the reactor may remain in operation
for a period not to exceed 7 days.
Contrary to the above, on October 9, 2017, it was recognized that one diesel generator was
inoperable for greater than the technical specification allowed outage time of 7 days, and
Oyster Creek continued power operation. Specifically, on October 9, 2017, No. 2 emergency
diesel generator failed to run during a routine surveillance test due to a broken ring lug on a
current transformer, which resulted in a total inoperability time of 6.5 months.
Severity/Significance: For violations warranting enforcement discretion, Inspection Manual
Chapter 0612 does not require a detailed risk evaluation, however, safety significance
characterization is appropriate. A Region I Senior Reactor Analyst (SRA) performed a best
estimate analysis of the safety significance using the Oyster Creek Standardized Plant
Analysis Risk (SPAR) model, Version 8.50 and Systems Analysis Programs for Hands-On
Integrated Reliability Evaluations (SAPHIRE). The evaluation estimated the total (internal and
external events risk) increase in core damage frequency (CDF) to be in the mid to high
E-6/yr range, or a low to moderate safety significance. The SRA evaluated the internal events
risk contribution due to the inoperability of the No. 2 emergency diesel generator for an
approximate 6.5 month exposure time. The exposure time relative to when the No. 2
emergency diesel generator was no longer capable of meeting its 24 hour mission time is
uncertain due to the effect of vibration induced fatigue, and therefore the method prescribed
within the RASP handbook guidance was used.
 
The analyst used the guidance in Section 2.5 of the Handbook, Revision 2.0, to estimate the
exposure time of 6.5 months based on the cumulative 24 hour summation of the No. 2
emergency diesel generator surveillance test proven run time. This approach is appropriate
for periodically operated components that degrade during operation (i.e. vibration induced
fatigue only occurs while the emergency diesel generator is in-service/operating). Given this
approach, the dominant internal events, loss of offsite power were evaluated for the estimated
internal risk increase. This contribution was estimated at 2E-6/yr increase in CDF. The
dominant sequences involved loss of offsite power events with a concurrent failure of the
No. 1 emergency diesel generator, failure of the combustion turbines, and failure to recover
offsite power or recover an emergency diesel generator prior to core damage.
The SRA performed various modeling changes after a review of revised calculations for DC
battery life:
Analysis noted that Oyster Creek Generating Station recirculation pump seals are similar in
design to those tested in reports generated for Nine Mile Point Unit 1 with the use of CAN2A
seals. Therefore, the failure probability of the seals in the station blackout sequence was
adjusted from 0.1 to 5E-2 similar to Nine Mile Point Unit 1 SPAR model 8.50.
The failure to load shed action (DCP-XHE-XM-LSHED) in the model was calculated using the
SPAR-H method and revised to 1.2E-2 versus being assumed to always fail (TRUE).
*
Failure probabilities for 1, 2, or 3 stuck open electromatic relief valves were revised to
be consistent with the previous model version 8.22 because of the isolation condenser
design at Oyster Creek Generating Station which limits cycling and significantly
reduces the probability of a failed open electromatic relief valve due to isolation
condensers controlling pressure.
*
The depressurization function using electromatic relief valves, if required, was
calculated through SPAR-H to be 1E-2 for sequences where total seal failure is
assumed (DEPSEALFAIL) (conservatively assumed limited time available).
*
The diesel driven firewater pumps are both available and were set to calculated fault
tree failure probabilities instead of always failed in the previous model. These are
2,000 gallons per minute pumps with a large supply of water and relatively simple
operator actions to inject to the reactor pressure vessel. The firewater was assumed
to fail at 0.1 when a total recirculation seal failure occurs due to assumed time
constraints.
*
The offsite power and the emergency diesel generator required recovery time events
were increased to 24 hours for events where DC load shedding was successful,
without seal failures and isolation condenser success along with diesel driven firewater
success.
The SRA noted the No. 2 emergency diesel generator was recoverable. In fact, the diagnosis
of the failed condition was performed in a nominal 8-10 hours from the failure. Therefore, a
probability of failure to recover event for the conditional case was developed. The SRA used
SPAR-H as simple guidance, which conservatively supported a reasonable assumption of a
0.10 conditional probability of failure to recover the emergency diesel generator within
hours. The base case utilized a calculation within SPAR of 0.33 failure to recover
probability for 24 hour sequences.
To estimate the external risk contribution, the SRA identified that the most significant external
risk contribution was from fire events. Seismic, external flooding, and high wind events were
not significant contributors for the issue.
 
From discussions with Oyster Creek Fire probabilistic risk analysts and a review of this failure
condition, the increase in CDF due to the failed No. 2 emergency diesel generator for the
assumed 6.5 month exposure time was estimated at 4.5E-6/yr [(8.5E-5/yr-4.5E-5/yr) x (6.5/12
months) x 0.2].
The DC safety-related battery life would be at least a nominal 14 hours and longer if DC bus
stripping occurred, this allows for extended isolation condenser or electromatic relief valve
function, with injection from diesel driven firewater. Given the time considerations and
characteristics of the failure, an assumed recovery at a failure probability of 0.2 (slightly higher
than internal due to less time) was applied for the No. 2 emergency diesel generator, which
was a best estimate determined through SPAR-H insights. The dominant fire sequence was a
fire affecting the A and B 4kV switchgear rooms, where combustion turbine support would
be lost, with failure of the No. 1 emergency diesel generator breaker to close, and failure of
locally operating the isolation condenser due to eventual loss of power. The SRA noted that
FLEX credit was not quantified and would result in a lower risk estimation likely in the low
E-6/yr range. Combining internal and external risk contributions, the total increase in CDF
was 6.5E-6/yr, or low to moderate safety significance. The SRA determined that Exelon uses
a Large Early Release Frequency (LERF) factor value of 8E-2. This value takes into
consideration operator action for those relevant high pressure vessel breach scenarios
(fuel-coolant interaction, liner-melt-through, and direct containment heating). This also credits
procedure strategies where other mitigating actions are taken such as flooding the drywell.
The SRA review of the dominant sequences and time to core damage affirmed that LERF did
not increase the risk over that determined from the increase in CDF.
Basis for Discretion: The inspectors determined that the ring lug failure was not within
Exelons ability to foresee and prevent. As a result, no performance deficiency was identified.
The inspectors assessment considered:
1. Exelons review of emergency diesel maintenance performed in 2015 checked all
connections of the current transformer for tightness. The inspectors did not identify
any gaps or deficiencies in the 2015 inspections. Inspectors also reviewed completed
biennial inspections of the connection dating back to 1991 and did not identify any
gaps.
2. At the time of the failure, the current transformer connections did not have a time
directed replacement frequency recommended by the Emergency Diesel Generator
Owners Group. The inspectors did not identify any additional vendor or industry
recommendations specific to the failed component or considerations specific to the
failed component that existed prior to the failure.
3. Industry operating experience information available to Exelon did not identify the
potential for the fatigue cracking of the bent wire ring lug that was experienced.
4. The bent ring lug failure was not the result of a failure on the part of Exelon staff; no
standards existed on bending of the lug during installation and is considered skill of
the craft.
The NRC determined that it was not reasonable for Exelon to have been able to foresee and
prevent this violation of NRC requirements, and as such, no performance deficiency existed.
Therefore, the NRC has decided to exercise enforcement discretion in accordance with
Sections 2.2.4 and 3.10 of the NRC Enforcement Policy and refrain from issuing enforcement
action for the violation of technical specifications (EA-18-007). Further, because Exelons
actions did not contribute to this violation, it will not be considered in the assessment process
or the NRC Action Matrix.
 
Observation
71152
Exelons equipment corrective action program evaluation report (ECAPE) determined that the
ring lug failed on the No. 2 emergency diesel generator as a result of fatigue cracking, which
was initiated due to excessive stress caused by bending and twisting of the ring lug beyond
limits specified in industry guidelines. The inspectors noted that the ECAPE did not provide
supporting information regarding how the ring lug was bent and twisted beyond industry
guidelines. Specifically, industry guidance states that ring lugs can be bent up to 90 degrees.
The broken ring lug found in the No. 2 emergency diesel generator was bent at approximately
45-55 degrees per the ECAPE, which was within industry guidelines. Additionally, the ECAPE
did not include specific guidance on twisting allowances for ring lugs. Exelon documented the
inspectors observation in Issue Report 4089829. As a result of the inspectors observation,
Exelon revised the ECAPE to say the ring lug failed on the No. 2 emergency diesel generator
as a result of fatigue cracking, which was initiated due to excessive stress caused by bending
and twisting of the ring lug.
 
Untimely Licensee Event Report for Reportable Conditions Associated with the No. 2
Emergency Diesel Generator
Cornerstone
Severity
Cross-Cutting
Aspect
Report
Section
Not Applicable
Severity Level IV, NCV
05000219/2018001-01
Opened/Closed
Not Applicable
71153
The inspectors identified a Severity IV non-cited violation of 10 CFR 50.73(a)(1) for a failure
to submit an LER within 60 days after the discovery of an event requiring a report.
Specifically, on October 9, 2017, Exelon determined that the No. 2 emergency diesel
generator was inoperable for longer than the allowed outage time, which is reportable as a
condition prohibited by technical specifications. Exelon did not submit an LER for this event
until January 3, 2018.
Description: On October 9, 2017, the No. 2 emergency diesel was operated for its bi-weekly
load surveillance. Approximately five minutes into the run, the main control room received
LKOUT RELAY TRIP and EDG 2 DISABLED alarms. Following an automatic shutdown of
the No. 2 emergency diesel generator, Exelon staff discovered a ring lug of a current
transformer had broken. The last time the No. 2 emergency diesel generator was operated
for its bi-weekly load surveillance was on September 25, 2017. Oyster Creek Technical
Specification 3.7.C.2 states, in part, that if one diesel generator becomes inoperable during
power operation, the reactor may remain in operation for a period not to exceed 7 days.
Details regarding the broken lug on the No. 2 emergency diesel generator can be found in
Section 71152.
On December 9, 2017, the inspectors identified that the No. 2 emergency diesel generator
was inoperable for longer than its technical specification allowed outage time of 7 days, which
is reportable to the NR
: [[contact::C. 10 CFR 50.73 states]], in part, that the licensee shall report any
operation or condition which was prohibited by the plants technical specifications. Exelon
had not submitted an LER within the 60 day requirement because they did not consider the
inoperable No. 2 emergency diesel generator as an event that required an LER as specified
in 10 CFR 50.73.
Corrective Action(s): Exelon submitted the required LER on January 3, 2018.
Corrective Action Reference: Issue Report 4092328
 
Performance Assessment:
__________________________________________________________________________
Performance Deficiency: The inspectors determined that the failure to report a condition
which is prohibited by technical specifications within the time frame required by 10 CFR
50.73(a)(1) was a performance deficiency.
Screening: Traditional enforcement applies because a failure to report an event in a timely
manner has the potential to impact the NRCs ability to perform its regulatory function.
 
Significance: The finding was determined to be a Severity Level IV violation consistent with
Section 6.9.d.9 of the NRC Enforcement Policy.
Cross-Cutting Aspect: No cross-cutting aspect was assigned to this finding because it was
screened under the traditional enforcement process.
Enforcement:
Severity: The ROPs significance determination process does not specifically consider the
regulatory process impact in its assessment of licensee performance. Therefore, it is
necessary to address this violation which impedes the NRCs ability to regulate using
traditional enforcement to adequately determine non-compliance.
The inspectors determined that the violation was a Severity Level IV, which is a more than
minor violation, which is a concern that resulted in no or relatively inappreciable potential
safety or security consequence. The untimely LER was not used to make an unacceptable
change to the facility nor did it impact a licensing or safety decision by the NRC.
Violation: 10 CFR 50.73(a)(1) requires, in part, that a licensee submit an LER for any event
of the type described in this paragraph within 60 days after the discovery of the event.
CFR 50.73(a)(2)(i)(B) requires, in part, that the licensee report any event or condition
prohibited by the plants technical specifications. Contrary to the above, on December 9,
2017, Exelon failed to submit an LER within 60 days after the discovery that the No. 2
emergency diesel generator was inoperable for longer than its technical specification allowed
outage time of 7 days. This event occurred on October 9, 2017, and Exelon submitted the
LER on January 3, 2018, which exceeded the 10 CFR 50.73(a)(11) 60 day requirement.
Exelon entered this issue into their corrective action program in issue report 4092328.
Enforcement Action(s): This Severity Level IV violation is being treated as a non-cited
violation, consistent with Section 2.3.2.a of the NRC Enforcement Policy.
 
EXIT MEETINGS AND DEBRIEFS
Inspectors verified no proprietary information was retained or documented in this report.
*
On February 9, 2018, the inspectors presented the radiation safety inspection results to
Mr. Michael Gillin, Plant Manager, and other members of the Oyster Creek staff.
*
On April 4, 2018, the inspectors presented the quarterly resident inspector inspection results
to Mr. Timothy Moore, Site Vice President, and other members of the Oyster Creek staff.
 
DOCUMENTS REVIEWED
71111.01: Adverse Weather Protection
Procedures
ABN 18, Service Water Failure Response, Revision 7
ABN-31, High Winds, Revision 21
ABN 32, Abnormal Intake Level, Revision 30
OP-AA-108-111-1001, Severe Weather and Natural Disaster Guidelines, Revision 16
OP-OC-108-109-1001, Severe Weather Preparation T&RM for Oyster Creek, Revision 38
Issue Reports
4110580
71111.04: Equipment Alignment
Drawings
GE 885D781 Sh.1, Core Spray System Flow Diagram, Revision 76
GE 148F262 Sh.1, Emergency Condenser Flow Diagram, Revision 56
Issue Reports
1619946
4102875
4108748
4108767
4109454
71111.05: Fire Protection
Procedures
101.2, Oyster Creek Site Fire Protection Program, Revision 73
ABN 29, Plant Fires, Revision 32
ER-AA-600-1069, High Risk Fire Area Identification, Revision 4
OP-OC-201-008, Oyster Creek Pre-fire Plans, Revision 26
OP-OC-201-012-1001, On-line Fire Risk Management, Revision 4
Issue Reports
3971381
4059012
71111.06: Flood Protection Measures
Miscellaneous
OP-PSA-012, Internal Flood Evaluation Summary Notebook, dated May 2014
OC-PSA-022, Internal Flood Walkdown Notebook, dated May 2014
71111.11: Licensed Operator Requalification Program
Procedures
EP-AA-1010, Addendum 3, Exelon Nuclear Emergency Action Levels for Oyster Creek Station,
Revision 2
71111.12: Maintenance Effectiveness
Procedures
ER-AA-310, Implementation of the Maintenance Rule, Revision 11
ER-AA-310-1004, Maintenance Rule - Performance Monitoring, Revision 14
ER-AA-310-1005, Maintenance Rule - Dispositioning Between (a)(1) and (a)(2), Revision 7
 
Issue Reports
0516160
0648480
0687240
1501306
1514742
2472912
23130
2536453
2537005
2572740
25933
29443
29982
2637292
2643485
2643486
2702946
2714199
2715226
2719824
3949214
3952496
4060818
4069654
4089360
4089390
4109343
Miscellaneous
Oyster Creek Generating Station Maintenance Rule Periodic (a)(3) Assessment from
July 1, 2015 - June 30, 2017, dated November 29, 2017
Maintenance Orders/Work Orders
4345665
4345669
4345671
4345673
71111.15: Operability Evaluations
Issue Reports
4111295
4111496
4111518
4111506
71111.18: Plant Modifications
Miscellaneous
EC 620725, Refuel Bridge PLC Software Modification to Allow Offloading Fuel from a Cask,
dated February 23, 2018
71111.19: Post-Maintenance Testing
Issue Reports
4070270
4103389
4104381
4106951
4107367
4110560
Maintenance Orders/Work Orders
4745244
4745324
4745979
4748691
71124.08: Radioactive Solid Waste Processing and Radioactive Material Handling,
Storage, and Transportation
Procedures
RW-AA-100, Process Control Program for Radioactive Wastes, Revision 12
RW-AA-605, 10 CFR 61 Program, Revision 8
RP-AA-600, Radioactive Material/Waste Shipments, Revision 16
RP-AA-600-1001, Exclusive Use and Emergency Response Information, Revision 9
RP-AA-600-1005, Radioactive Material and Non Disposal Site Waste Shipments, Revision 19
RP-AA-600-1006, Shipment of Category 1 Quantities of Radioactive Material or Waste
(Category 1 RAMQC), Revision 11
RP-AA-600-1009, Shipment of Category 2 Quantities of Radioactive Material or Waste
(Category 2 RAMQC), Revision 2
RP-AA-600-1010, Use and Operation of WMG Software for Creating Containers, Samples,
Waste Streams and Waste Types, Revision 2
RP-AA-600-1011, Use and Operation of WMG Software for Gross Gamma Characterization and
Generation of Shipping Paperwork, Revision 4
RP-AA-601, Surveying Radioactive Material Shipments, Revision 20
RP-AA-602, Packaging of Radioactive Material Shipments, Revision 20
RP-AA-602-1001, Packaging of Radioactive Material/Waste Shipments, Revision 17
RP-AA-603, Inspection and Loading of Radioactive Material Shipments, Revision 10
RP-AA-605, 10 CFR 61 Program, Revision 7
 
Quality Assurance
NOSA-OYS-16-04, Chemistry, Radwaste, Effluent and Environmental Monitoring Audit Report
NOSA-OYS-17-06, Radiation Protection Audit Report
Fleet Assessment T-18 Assessment Report, October 2016
Fleet Assessment T-6 Assessment Report, September 2017
Fleet Assessment Mid-Cycle Assessment Report, March 2017
CFR Part 61 Scaling Factors
Dry Active Waste, Bead Resin, Sludge, CLW Composite, Cartridge Filters
2016-2017 10 CFR 61 Waste Stream Analysis, December 2016
Assignment Reports
23501
20554
2608094
Training
HAZSEC, DOT Security Awareness and Transportation Security Plan, Revision 1
NRWSHP-1000, DOT/79-19 Training for Support of Radioactive and Asbestos Shipments,
Revision 4
Shipments
OC-3001-16 OC-4003-16 OC-3001-17 OC-3002-17 OC-3003-17
71152: Problem Identification and Resolution
Procedures
PI-AA-125, Corrective Action Program Procedure, Revision 6
PI-AA-125-1006, Investigation Techniques Manual, Revision 3
MA-AA-726-620, Installation Instructions for 0-600 Volt EQ Related Splices, Revision 6
MA-OC-741-101, Diesel Generator Inspection (24 Month) - Electrical, Revision 15
NO-AA-300-1001, Nuclear Oversight Independent Inspection Plan, Revision 10
2400-GME-3780.52, Installation, Testing and Termination of Wire and Cable, Revision 6
2400-SME-3780.03, Electrical Termination Taping and Raychem Splicing, Revision 16
Maintenance Orders/Work Orders
R2239604
R2230340
R2229008
R2207589
R2191838
R2190504
R2151723
R2111307
R2032680
R2065956
R0808797
R0522916
R0504310
R0055415
R0041081
R0029109
4695984
4695269
4697086
4694906
Issue Reports
4060815
4089829
1436376
4061089
4073377
4060815
4060818
4061527
4061931
4066706
4061093
Miscellaneous
ES-023, Selection and Sizing of Power, Lighting and Control Cables, Revision 2
SP-9000-31-213, Class 1E, Electric Cable for Power, Control & Instrumentation, Revision 9
SP-9000-41-005, Cables & Raceways at Oyster Creek, Revision 3
71153: Follow-up of Events and Notices of Enforcement Discretion
Issue Reports
4091183
4091037
4091010
4090950
4090920
4090820
4090803
4091287
4091455
}}
}}

Latest revision as of 22:27, 5 January 2025

Integrated Inspection Report 05000219-2018001 and Exercise of Enforcement Discretion
ML18128A232
Person / Time
Site: Oyster Creek
Issue date: 05/08/2018
From: David Pelton
Division Reactor Projects I
To: Bryan Hanson
Exelon Generation Co, Exelon Nuclear
Young M
References
EA-18-007 IR 2018001
Download: ML18128A232 (18)


Text

May 8, 2018

SUBJECT:

OYSTER CREEK NUCLEAR GENERATING STATION - INTEGRATED INSPECTION REPORT 05000219/2018001 AND EXERCISE OF ENFORCEMENT DISCRETION

Dear Mr. Hanson:

On March 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Oyster Creek Nuclear Generating Station. On April 4, 2018, the NRC inspectors discussed the results of this inspection with Mr. Timothy Moore, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented one Severity Level IV violation with no associated finding. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

In addition, the NRC reviewed Licensee Event Report 05000219/2017-005-00, which described the circumstances associated with a failed electrical ring lug on the No. 2 emergency diesel generator. It was recognized that the No. 2 emergency diesel generator was inoperable for a period of time that exceeded the allowed outage time of seven days detailed in Technical Specification 3.7.C.2.b, and therefore, is a violation of technical specifications. Regional staff performed a risk evaluation and determined the issue was of low to moderate safety significance (White).

Although this issue constitutes a violation of NRC requirements, the NRC determined that the electrical ring lug failure which caused the No. 2 emergency diesel generator to be inoperable was not within Exelons ability to reasonably foresee and correct. As a result, the NRC did not identify a performance deficiency associated with this condition. The NRCs assessment considered Exelons maintenance practices, industry operating experience, vendor and industry maintenance and testing recommendations, and Exelons corrective actions to prevent recurrence of the issue.

Based on the results of the NRCs inspection and assessment, I have been authorized, after consultation with the Director, Office of Enforcement, to exercise enforcement discretion in accordance with NRC Enforcement Policy Section 2.2.4, Exceptions to Using Only the Operating Reactor Assessment Program, and Section 3.10, Reactor Violations with No Performance Deficiency. The Region I Regional Administrator was also consulted regarding enforcement discretion for this issue. If you contest the non-cited violation in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at Oyster Creek Nuclear Generating Station.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRCs Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

David L. Pelton, Director Division of Reactor Projects

Docket Number: 50-219 License Number: DPR-16

Enclosure:

Inspection Report 05000219/2018001

Inspection Report

Docket Number:

50-219

License Number:

DPR-16

Report Number:

05000219/2018001

Enterprise Identifier:

I-2018-001-0078

Licensee:

Exelon Nuclear

Facility:

Oyster Creek Nuclear Generating Station

Location:

Forked River, New Jersey

Inspection Dates:

January 1, 2018 to March 31, 2018

Inspectors:

A. Patel, Senior Resident Inspector

E. Andrews, Resident Inspector

F. Arner, Senior Reactor Analyst

J. Furia, Senior Health Physicist

J. Kulp, Senior Reactor Inspector

J. Schoppy, Senior Reactor Inspector

Approved By:

David L. Pelton, Director

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Exelons performance at

Oyster Creek Nuclear Generating Station by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors.

Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC identified and self-revealing findings, violations, and additional items are summarized in the table below.

List of Findings and Violations

Untimely Licensee Event Report for Reportable Conditions Associated with the No. 2 Emergency Diesel Generator Cornerstone Severity Cross-Cutting Aspect Report Section Not Applicable Severity Level IV, NCV 05000219/2018001-01 Closed Not Applicable 71153 The inspectors identified a non-cited, Severity IV violation of 10 CFR 50.73(a)(1) for a failure to submit a licensee event report (LER) within 60 days after the discovery of an event requiring a report. Specifically, on October 9, 2017, Exelon determined that the No. 2 emergency diesel generator was inoperable for longer than the allowed outage time, which is reportable as a condition prohibited by technical specifications. Exelon did not submit an LER for this event until January 3, 2018.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000219/2017-005-00 No. 2 emergency diesel generator inoperable 71153 Closed

PLANT STATUS

Oyster Creek began the inspection period at 100 percent power. On January 6, 2018, operators lowered power to 70 percent due to low intake levels. Operators returned the unit to 100 percent on January 8, 2018. The unit remained at or near 100 percent power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html.

Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter 2515, Light-Water Reactor Inspection Program - Operations Phase.

The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensees performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather (2 Samples)

The inspectors evaluated readiness for impending adverse weather conditions for a blizzard warning issued on January 4, 2018, and for low intake levels on January 6, 2018.

External Flooding (1 Sample)

The inspectors evaluated protection from external flooding prior to and during high winds and heavy rain on March 2, 2018.

71111.04 - Equipment Alignment

Partial Walkdown (6 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) No. 1 emergency diesel generator while No. 2 emergency diesel generator was inoperable on January 3, 2018
(2) Emergency service water pumps during low intake level on January 6, 2018
(3) A isolation condenser during emergent unavailability of the B isolation condenser on February 12, 2018
(4) Core spray system II during planned unavailability of core spray system I on February 20, 2018
(5) B isolation condenser during shell side makeup on March 5, 2018
(6) B isolation condenser during emergent work on A isolation condenser on March 12, 2018

Complete Walkdown (1 Sample)

The inspectors evaluated system configurations during a complete walkdown of the standby liquid control system on February 15-16, 2018.

71111.05Q - Fire Protection Quarterly

Quarterly Inspection (9 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) No. 1 emergency diesel generator room on January 24, 2018
(2) No. 2 emergency diesel generator room on January 24, 2018
(3) Reactor building 95 elevation on February 21, 2018
(4) Reactor building 75 elevation on February 21, 2018
(5) Reactor building 23 elevation on February 21, 2018
(6) C 125 VDC battery room on February 28, 2018
(7) A and B 4kV switchgear room on February 28, 2018
(8) New cable spreading room on March 1, 2018
(9) Recirculation pump motor generator set room on March 1, 2018

71111.06 - Flood Protection Measures

Internal Flooding (1 Sample)

The inspectors evaluated internal flooding mitigation protections in turbine building switchgear area on February 22, 2018.

71111.07 - Heat Sink Performance

Heat Sink (1 Sample)

The inspectors evaluated Exelons monitoring and maintenance of B isolation condenser performance on March 5, 2018.

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance

Operator Requalification (2 Samples)

The inspectors observed and evaluated a crew of licensed operators in the plants simulator during licensed operator requalification training on January 23, 2018, and March 13, 2018.

Operator Performance (1 Sample)

The inspectors observed licensed operator performance during the Notice of Unusual Event on January 6, 2018.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness (4 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Periodic 10 CFR 50.65(a)(3) evaluation on January 17, 2018
(2) Service air system on January 22, 2018
(3) Start-up transformers on February 21, 2018
(4) Reactor recirculation system on March 5, 2018

71111.13 - Maintenance Risk Assessments and Emergent Work Control

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Notice of Unusual Event declaration due to low intake levels on January 6, 2018
(2) Planned maintenance on the A isolation condenser on January 9, 2018
(3) Planned maintenance on the B isolation condenser on January 18, 2018
(4) Planned maintenance on core spray system I on February 20, 2018
(5) Planned maintenance on core spray system II on March 14, 2018
(6) Planned maintenance on the No. 2 emergency diesel generator on March 26, 2018

71111.15 - Operability Determinations and Functionality Assessments

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Emergency service water pumps during low intake level on January 6, 2018
(2) Standby liquid control poison tank low level on January 29, 2018
(3) B isolation condenser elevated temperatures on February 16, 2018
(4) Control rod 34-43 slow five percent scram time on March 5, 2018
(5) B isolation condenser lowering shell side level on March 6, 2018
(6) A isolation condenser steam leak on March 12, 2018
(7) No. 2 emergency diesel generator elevated lead levels in oil sample on March 15, 2018

71111.18 - Plant Modifications

The inspectors evaluated the following temporary or permanent modifications:

Engineering Change 620725, Refuel Bridge Software Modification to Allow Offloading Fuel from a Cask

71111.19 - Post Maintenance Testing

The inspectors evaluated post maintenance testing for the following maintenance/repair activities:

(1) A recirculation pump relay replacement on January 22, 2018
(2) B isolation condenser valve, V-14-37, following valve repair on February 13, 2018
(3) A core spray pump relay replacement on February 20, 2018
(4) Average power range monitor 7 restoration to an operable condition on February 22, 2018
(5) B isolation condenser remote shutdown panel level indication following emergent inoperability on February 22, 2018
(6) Main generator exciter direct current (DC) brush inspection and replacement on March 1, 2018
(7) 1-8 sump control logic following fuse replacement on March 27, 2018
(8) No. 2 emergency diesel generator following biannual overhaul on March 28, 2018

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Routine

(1) 636.4.013, Diesel Generator 2 Load Test on January 3, 2018
(2) 609.3.003, Isolation Condenser Automatic Actuation Sensor Calibration and Test on January 18, 2018
(3) 607.4.016, Containment Spray and Emergency Service Water System I Pump Operability and Quarterly Inservice Test on January 23, 2018
(4) 604.3.001, Reactor Building to Torus Power Vacuum Breaker Test and Calibration on February 8, 2018
(5) 602.3.004, Electromatic Relief Valve Pressure Sensor Test and Calibration on March 6, 2018
(6) 651.4.003, Standby Gas Treatment System 15-minute Run - System 2 on March 17, 2018

Inservice (2 Samples)

(1) 612.4.001, A Standby Liquid Control Pump and Valve Operability and In-service Test on January 9, 2018
(2) 610.4.003, Core Spray Valve Operability and In-Service Test on March 12, 2018

71114.06 - Drill Evaluation

Emergency Planning Drill (1 Sample)

The inspectors evaluated the conduct of a routine Exelon emergency planning drill on March 13, 2018.

Drill/Training Evolution (1 Sample)

The inspectors observed a simulator training evolution for licensed operators on January 23,

RADIATION SAFETY

71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,

and Transportation

Radioactive Material Storage

The inspectors observed radioactive waste container storage areas and verified the postings and controls and that Exelon had established a process for monitoring the impact of long-term storage of the waste.

Radioactive Waste System Walkdown (1 Sample)

The inspectors walked down the following:

  • Accessible portions of liquid and solid radioactive waste processing systems to verify current system alignment and material condition
  • Abandoned in place radioactive waste processing equipment to review the controls in place to ensure protection of personnel
  • Changes made to the radioactive waste processing systems since the last inspection
  • Processes for mixing and transferring radioactive waste resin and/or sludge discharges into shipping/disposal containers
  • Current methods and procedures for dewatering waste

Waste Characterization and Classification (1 Sample)

The inspectors identified radioactive waste streams and reviewed radiochemical sample analysis results to support radioactive waste characterization. The inspectors reviewed the use of scaling factors and calculations to account for difficult-to-measure radionuclides.

Shipment Preparations (1 Sample)

The inspectors reviewed the records of shipment packaging, surveying, labeling, marking, placarding, vehicle checks, emergency instructions, disposal manifest, shipping papers provided to the driver, and Exelons verification of shipment readiness.

Shipment Records (1 Sample)

The inspectors reviewed selected non-excepted package shipment records.

OTHER ACTIVITIES - BASELINE

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (1 Sample)

The inspectors reviewed Exelons implementation of its corrective action program related to the following issues:

No. 2 Emergency Diesel Generator Ring Lug Failure

===71153 - Follow-up of Events and Notices of Enforcement Discretion

Events===

The inspectors evaluated response to the following events:

Notice of Usual Event due to low intake levels on January 6, 2018

Licensee Event Reports (1 Sample)

The inspectors evaluated the following LERs which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:

LER 05000219/2017-005-00 and -01, Failure of the Emergency Diesel Generator #2, During Surveillance Testing due to a Broken Electrical Connector, on February 14,

INSPECTION RESULTS

Enforcement Discretion Enforcement Action (EA)-18-007: No. 2 Emergency Diesel Generator Ring Lug Failure 71152

Description:

On October 9, 2017, during a routine surveillance load test, the No. 2 emergency diesel generator failed approximately 5 minutes into the run due to a broken ring lug on a current transformer. Laboratory analysis of the broken ring lug determined that the ring lug failed due to fatigue cracking that was initiated due to stresses caused by bending and twisting of the electrical lug. Exelon last conducted a load surveillance on the No. 2 emergency diesel generator on September 25, 2017.

Corrective Actions: Corrective actions included replacement on the broken ring lug on the No. 2 emergency diesel generator, extent of condition inspections on the No. 1 and No. 2 emergency diesel generators for additional bent or twisted ring lug connectors, and revision to the electrical ring lug installation and emergency diesel generator procedures to include inspection for bent or twisted ring lugs.

Corrective Action Reference(s): Issue report 4060815

Enforcement:

Violation: Oyster Creek Technical Specification 3.7.C.2.b states, in part, that if one diesel generator becomes inoperable during power operation, the reactor may remain in operation for a period not to exceed 7 days.

Contrary to the above, on October 9, 2017, it was recognized that one diesel generator was inoperable for greater than the technical specification allowed outage time of 7 days, and Oyster Creek continued power operation. Specifically, on October 9, 2017, No. 2 emergency diesel generator failed to run during a routine surveillance test due to a broken ring lug on a current transformer, which resulted in a total inoperability time of 6.5 months.

Severity/Significance: For violations warranting enforcement discretion, Inspection Manual Chapter 0612 does not require a detailed risk evaluation, however, safety significance characterization is appropriate. A Region I Senior Reactor Analyst (SRA) performed a best estimate analysis of the safety significance using the Oyster Creek Standardized Plant Analysis Risk (SPAR) model, Version 8.50 and Systems Analysis Programs for Hands-On Integrated Reliability Evaluations (SAPHIRE). The evaluation estimated the total (internal and external events risk) increase in core damage frequency (CDF) to be in the mid to high E-6/yr range, or a low to moderate safety significance. The SRA evaluated the internal events risk contribution due to the inoperability of the No. 2 emergency diesel generator for an approximate 6.5 month exposure time. The exposure time relative to when the No. 2 emergency diesel generator was no longer capable of meeting its 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> mission time is uncertain due to the effect of vibration induced fatigue, and therefore the method prescribed within the RASP handbook guidance was used.

The analyst used the guidance in Section 2.5 of the Handbook, Revision 2.0, to estimate the exposure time of 6.5 months based on the cumulative 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> summation of the No. 2 emergency diesel generator surveillance test proven run time. This approach is appropriate for periodically operated components that degrade during operation (i.e. vibration induced fatigue only occurs while the emergency diesel generator is in-service/operating). Given this approach, the dominant internal events, loss of offsite power were evaluated for the estimated internal risk increase. This contribution was estimated at 2E-6/yr increase in CDF. The dominant sequences involved loss of offsite power events with a concurrent failure of the No. 1 emergency diesel generator, failure of the combustion turbines, and failure to recover offsite power or recover an emergency diesel generator prior to core damage.

The SRA performed various modeling changes after a review of revised calculations for DC battery life:

Analysis noted that Oyster Creek Generating Station recirculation pump seals are similar in design to those tested in reports generated for Nine Mile Point Unit 1 with the use of CAN2A seals. Therefore, the failure probability of the seals in the station blackout sequence was adjusted from 0.1 to 5E-2 similar to Nine Mile Point Unit 1 SPAR model 8.50.

The failure to load shed action (DCP-XHE-XM-LSHED) in the model was calculated using the SPAR-H method and revised to 1.2E-2 versus being assumed to always fail (TRUE).

  • Failure probabilities for 1, 2, or 3 stuck open electromatic relief valves were revised to be consistent with the previous model version 8.22 because of the isolation condenser design at Oyster Creek Generating Station which limits cycling and significantly reduces the probability of a failed open electromatic relief valve due to isolation condensers controlling pressure.
  • The depressurization function using electromatic relief valves, if required, was calculated through SPAR-H to be 1E-2 for sequences where total seal failure is assumed (DEPSEALFAIL) (conservatively assumed limited time available).
  • The diesel driven firewater pumps are both available and were set to calculated fault tree failure probabilities instead of always failed in the previous model. These are 2,000 gallons per minute pumps with a large supply of water and relatively simple operator actions to inject to the reactor pressure vessel. The firewater was assumed to fail at 0.1 when a total recirculation seal failure occurs due to assumed time constraints.
  • The offsite power and the emergency diesel generator required recovery time events were increased to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> for events where DC load shedding was successful, without seal failures and isolation condenser success along with diesel driven firewater success.

The SRA noted the No. 2 emergency diesel generator was recoverable. In fact, the diagnosis of the failed condition was performed in a nominal 8-10 hours from the failure. Therefore, a probability of failure to recover event for the conditional case was developed. The SRA used SPAR-H as simple guidance, which conservatively supported a reasonable assumption of a 0.10 conditional probability of failure to recover the emergency diesel generator within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The base case utilized a calculation within SPAR of 0.33 failure to recover probability for 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> sequences.

To estimate the external risk contribution, the SRA identified that the most significant external risk contribution was from fire events. Seismic, external flooding, and high wind events were not significant contributors for the issue.

From discussions with Oyster Creek Fire probabilistic risk analysts and a review of this failure condition, the increase in CDF due to the failed No. 2 emergency diesel generator for the assumed 6.5 month exposure time was estimated at 4.5E-6/yr [(8.5E-5/yr-4.5E-5/yr) x (6.5/12 months) x 0.2].

The DC safety-related battery life would be at least a nominal 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br /> and longer if DC bus stripping occurred, this allows for extended isolation condenser or electromatic relief valve function, with injection from diesel driven firewater. Given the time considerations and characteristics of the failure, an assumed recovery at a failure probability of 0.2 (slightly higher than internal due to less time) was applied for the No. 2 emergency diesel generator, which was a best estimate determined through SPAR-H insights. The dominant fire sequence was a fire affecting the A and B 4kV switchgear rooms, where combustion turbine support would be lost, with failure of the No. 1 emergency diesel generator breaker to close, and failure of locally operating the isolation condenser due to eventual loss of power. The SRA noted that FLEX credit was not quantified and would result in a lower risk estimation likely in the low E-6/yr range. Combining internal and external risk contributions, the total increase in CDF was 6.5E-6/yr, or low to moderate safety significance. The SRA determined that Exelon uses a Large Early Release Frequency (LERF) factor value of 8E-2. This value takes into consideration operator action for those relevant high pressure vessel breach scenarios (fuel-coolant interaction, liner-melt-through, and direct containment heating). This also credits procedure strategies where other mitigating actions are taken such as flooding the drywell.

The SRA review of the dominant sequences and time to core damage affirmed that LERF did not increase the risk over that determined from the increase in CDF.

Basis for Discretion: The inspectors determined that the ring lug failure was not within Exelons ability to foresee and prevent. As a result, no performance deficiency was identified.

The inspectors assessment considered:

1. Exelons review of emergency diesel maintenance performed in 2015 checked all

connections of the current transformer for tightness. The inspectors did not identify any gaps or deficiencies in the 2015 inspections. Inspectors also reviewed completed biennial inspections of the connection dating back to 1991 and did not identify any gaps.

2. At the time of the failure, the current transformer connections did not have a time

directed replacement frequency recommended by the Emergency Diesel Generator Owners Group. The inspectors did not identify any additional vendor or industry recommendations specific to the failed component or considerations specific to the failed component that existed prior to the failure.

3. Industry operating experience information available to Exelon did not identify the

potential for the fatigue cracking of the bent wire ring lug that was experienced.

4. The bent ring lug failure was not the result of a failure on the part of Exelon staff; no

standards existed on bending of the lug during installation and is considered skill of the craft.

The NRC determined that it was not reasonable for Exelon to have been able to foresee and prevent this violation of NRC requirements, and as such, no performance deficiency existed.

Therefore, the NRC has decided to exercise enforcement discretion in accordance with Sections 2.2.4 and 3.10 of the NRC Enforcement Policy and refrain from issuing enforcement action for the violation of technical specifications (EA-18-007). Further, because Exelons actions did not contribute to this violation, it will not be considered in the assessment process or the NRC Action Matrix.

Observation 71152 Exelons equipment corrective action program evaluation report (ECAPE) determined that the ring lug failed on the No. 2 emergency diesel generator as a result of fatigue cracking, which was initiated due to excessive stress caused by bending and twisting of the ring lug beyond limits specified in industry guidelines. The inspectors noted that the ECAPE did not provide supporting information regarding how the ring lug was bent and twisted beyond industry guidelines. Specifically, industry guidance states that ring lugs can be bent up to 90 degrees.

The broken ring lug found in the No. 2 emergency diesel generator was bent at approximately 45-55 degrees per the ECAPE, which was within industry guidelines. Additionally, the ECAPE did not include specific guidance on twisting allowances for ring lugs. Exelon documented the inspectors observation in Issue Report 4089829. As a result of the inspectors observation, Exelon revised the ECAPE to say the ring lug failed on the No. 2 emergency diesel generator as a result of fatigue cracking, which was initiated due to excessive stress caused by bending and twisting of the ring lug.

Untimely Licensee Event Report for Reportable Conditions Associated with the No. 2 Emergency Diesel Generator Cornerstone Severity Cross-Cutting Aspect Report Section Not Applicable Severity Level IV, NCV 05000219/2018001-01 Opened/Closed Not Applicable 71153 The inspectors identified a Severity IV non-cited violation of 10 CFR 50.73(a)(1) for a failure to submit an LER within 60 days after the discovery of an event requiring a report.

Specifically, on October 9, 2017, Exelon determined that the No. 2 emergency diesel generator was inoperable for longer than the allowed outage time, which is reportable as a condition prohibited by technical specifications. Exelon did not submit an LER for this event until January 3, 2018.

Description:

On October 9, 2017, the No. 2 emergency diesel was operated for its bi-weekly load surveillance. Approximately five minutes into the run, the main control room received LKOUT RELAY TRIP and EDG 2 DISABLED alarms. Following an automatic shutdown of the No. 2 emergency diesel generator, Exelon staff discovered a ring lug of a current transformer had broken. The last time the No. 2 emergency diesel generator was operated for its bi-weekly load surveillance was on September 25, 2017. Oyster Creek Technical Specification 3.7.C.2 states, in part, that if one diesel generator becomes inoperable during power operation, the reactor may remain in operation for a period not to exceed 7 days.

Details regarding the broken lug on the No. 2 emergency diesel generator can be found in Section 71152.

On December 9, 2017, the inspectors identified that the No. 2 emergency diesel generator was inoperable for longer than its technical specification allowed outage time of 7 days, which is reportable to the NRC. 10 CFR 50.73 states, in part, that the licensee shall report any operation or condition which was prohibited by the plants technical specifications. Exelon had not submitted an LER within the 60 day requirement because they did not consider the inoperable No. 2 emergency diesel generator as an event that required an LER as specified in 10 CFR 50.73.

Corrective Action(s): Exelon submitted the required LER on January 3, 2018.

Corrective Action Reference: Issue Report 4092328

Performance Assessment:

__________________________________________________________________________

Performance Deficiency: The inspectors determined that the failure to report a condition which is prohibited by technical specifications within the time frame required by 10 CFR 50.73(a)(1) was a performance deficiency.

Screening: Traditional enforcement applies because a failure to report an event in a timely manner has the potential to impact the NRCs ability to perform its regulatory function.

Significance: The finding was determined to be a Severity Level IV violation consistent with Section 6.9.d.9 of the NRC Enforcement Policy.

Cross-Cutting Aspect: No cross-cutting aspect was assigned to this finding because it was screened under the traditional enforcement process.

Enforcement:

Severity: The ROPs significance determination process does not specifically consider the regulatory process impact in its assessment of licensee performance. Therefore, it is necessary to address this violation which impedes the NRCs ability to regulate using traditional enforcement to adequately determine non-compliance.

The inspectors determined that the violation was a Severity Level IV, which is a more than minor violation, which is a concern that resulted in no or relatively inappreciable potential safety or security consequence. The untimely LER was not used to make an unacceptable change to the facility nor did it impact a licensing or safety decision by the NRC.

Violation: 10 CFR 50.73(a)(1) requires, in part, that a licensee submit an LER for any event of the type described in this paragraph within 60 days after the discovery of the event.

10 CFR 50.73(a)(2)(i)(B) requires, in part, that the licensee report any event or condition prohibited by the plants technical specifications. Contrary to the above, on December 9, 2017, Exelon failed to submit an LER within 60 days after the discovery that the No. 2 emergency diesel generator was inoperable for longer than its technical specification allowed outage time of 7 days. This event occurred on October 9, 2017, and Exelon submitted the LER on January 3, 2018, which exceeded the 10 CFR 50.73(a)(11) 60 day requirement.

Exelon entered this issue into their corrective action program in issue report 4092328.

Enforcement Action(s): This Severity Level IV violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the NRC Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

Inspectors verified no proprietary information was retained or documented in this report.

  • On February 9, 2018, the inspectors presented the radiation safety inspection results to Mr. Michael Gillin, Plant Manager, and other members of the Oyster Creek staff.
  • On April 4, 2018, the inspectors presented the quarterly resident inspector inspection results to Mr. Timothy Moore, Site Vice President, and other members of the Oyster Creek staff.

DOCUMENTS REVIEWED

71111.01: Adverse Weather Protection

Procedures

ABN 18, Service Water Failure Response, Revision 7

ABN-31, High Winds, Revision 21

ABN 32, Abnormal Intake Level, Revision 30

OP-AA-108-111-1001, Severe Weather and Natural Disaster Guidelines, Revision 16

OP-OC-108-109-1001, Severe Weather Preparation T&RM for Oyster Creek, Revision 38

Issue Reports

4110580

71111.04: Equipment Alignment

Drawings

GE 885D781 Sh.1, Core Spray System Flow Diagram, Revision 76

GE 148F262 Sh.1, Emergency Condenser Flow Diagram, Revision 56

Issue Reports

1619946

4102875

4108748

4108767

4109454

71111.05: Fire Protection

Procedures

101.2, Oyster Creek Site Fire Protection Program, Revision 73

ABN 29, Plant Fires, Revision 32

ER-AA-600-1069, High Risk Fire Area Identification, Revision 4

OP-OC-201-008, Oyster Creek Pre-fire Plans, Revision 26

OP-OC-201-012-1001, On-line Fire Risk Management, Revision 4

Issue Reports

3971381

4059012

71111.06: Flood Protection Measures

Miscellaneous

OP-PSA-012, Internal Flood Evaluation Summary Notebook, dated May 2014

OC-PSA-022, Internal Flood Walkdown Notebook, dated May 2014

71111.11: Licensed Operator Requalification Program

Procedures

EP-AA-1010, Addendum 3, Exelon Nuclear Emergency Action Levels for Oyster Creek Station,

Revision 2

71111.12: Maintenance Effectiveness

Procedures

ER-AA-310, Implementation of the Maintenance Rule, Revision 11

ER-AA-310-1004, Maintenance Rule - Performance Monitoring, Revision 14

ER-AA-310-1005, Maintenance Rule - Dispositioning Between (a)(1) and (a)(2), Revision 7

Issue Reports

0516160

0648480

0687240

1501306

1514742

2472912

23130

2536453

2537005

2572740

25933

29443

29982

2637292

2643485

2643486

2702946

2714199

2715226

2719824

3949214

3952496

4060818

4069654

4089360

4089390

4109343

Miscellaneous

Oyster Creek Generating Station Maintenance Rule Periodic (a)(3) Assessment from

July 1, 2015 - June 30, 2017, dated November 29, 2017

Maintenance Orders/Work Orders

4345665

4345669

4345671

4345673

71111.15: Operability Evaluations

Issue Reports

4111295

4111496

4111518

4111506

71111.18: Plant Modifications

Miscellaneous

EC 620725, Refuel Bridge PLC Software Modification to Allow Offloading Fuel from a Cask,

dated February 23, 2018

71111.19: Post-Maintenance Testing

Issue Reports

4070270

4103389

4104381

4106951

4107367

4110560

Maintenance Orders/Work Orders

4745244

4745324

4745979

4748691

71124.08: Radioactive Solid Waste Processing and Radioactive Material Handling,

Storage, and Transportation

Procedures

RW-AA-100, Process Control Program for Radioactive Wastes, Revision 12

RW-AA-605, 10 CFR 61 Program, Revision 8

RP-AA-600, Radioactive Material/Waste Shipments, Revision 16

RP-AA-600-1001, Exclusive Use and Emergency Response Information, Revision 9

RP-AA-600-1005, Radioactive Material and Non Disposal Site Waste Shipments, Revision 19

RP-AA-600-1006, Shipment of Category 1 Quantities of Radioactive Material or Waste

(Category 1 RAMQC), Revision 11

RP-AA-600-1009, Shipment of Category 2 Quantities of Radioactive Material or Waste

(Category 2 RAMQC), Revision 2

RP-AA-600-1010, Use and Operation of WMG Software for Creating Containers, Samples,

Waste Streams and Waste Types, Revision 2

RP-AA-600-1011, Use and Operation of WMG Software for Gross Gamma Characterization and

Generation of Shipping Paperwork, Revision 4

RP-AA-601, Surveying Radioactive Material Shipments, Revision 20

RP-AA-602, Packaging of Radioactive Material Shipments, Revision 20

RP-AA-602-1001, Packaging of Radioactive Material/Waste Shipments, Revision 17

RP-AA-603, Inspection and Loading of Radioactive Material Shipments, Revision 10

RP-AA-605, 10 CFR 61 Program, Revision 7

Quality Assurance

NOSA-OYS-16-04, Chemistry, Radwaste, Effluent and Environmental Monitoring Audit Report

NOSA-OYS-17-06, Radiation Protection Audit Report

Fleet Assessment T-18 Assessment Report, October 2016

Fleet Assessment T-6 Assessment Report, September 2017

Fleet Assessment Mid-Cycle Assessment Report, March 2017

CFR Part 61 Scaling Factors

Dry Active Waste, Bead Resin, Sludge, CLW Composite, Cartridge Filters

2016-2017 10 CFR 61 Waste Stream Analysis, December 2016

Assignment Reports

23501

20554

2608094

Training

HAZSEC, DOT Security Awareness and Transportation Security Plan, Revision 1

NRWSHP-1000, DOT/79-19 Training for Support of Radioactive and Asbestos Shipments,

Revision 4

Shipments

OC-3001-16 OC-4003-16 OC-3001-17 OC-3002-17 OC-3003-17

71152: Problem Identification and Resolution

Procedures

PI-AA-125, Corrective Action Program Procedure, Revision 6

PI-AA-125-1006, Investigation Techniques Manual, Revision 3

MA-AA-726-620, Installation Instructions for 0-600 Volt EQ Related Splices, Revision 6

MA-OC-741-101, Diesel Generator Inspection (24 Month) - Electrical, Revision 15

NO-AA-300-1001, Nuclear Oversight Independent Inspection Plan, Revision 10

2400-GME-3780.52, Installation, Testing and Termination of Wire and Cable, Revision 6

2400-SME-3780.03, Electrical Termination Taping and Raychem Splicing, Revision 16

Maintenance Orders/Work Orders

R2239604

R2230340

R2229008

R2207589

R2191838

R2190504

R2151723

R2111307

R2032680

R2065956

R0808797

R0522916

R0504310

R0055415

R0041081

R0029109

4695984

4695269

4697086

4694906

Issue Reports

4060815

4089829

1436376

4061089

4073377

4060815

4060818

4061527

4061931

4066706

4061093

Miscellaneous

ES-023, Selection and Sizing of Power, Lighting and Control Cables, Revision 2

SP-9000-31-213, Class 1E, Electric Cable for Power, Control & Instrumentation, Revision 9

SP-9000-41-005, Cables & Raceways at Oyster Creek, Revision 3

71153: Follow-up of Events and Notices of Enforcement Discretion

Issue Reports

4091183

4091037

4091010

4090950

4090920

4090820

4090803

4091287

4091455

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

2100 RENAISSANCE BOULEVARD, SUITE 100

KING OF PRUSSIA, PA 19406-2713

May 8, 2018

EA-18-007

Mr. Bryan Hanson

Senior Vice President, Exelon Generation Co., LLC

President and Chief Nuclear Officer, Exelon Nuclear

4300 Winfield Road

Warrenville, IL 60555

SUBJECT: OYSTER CREEK NUCLEAR GENERATING STATION - INTEGRATED INSPECTION

REPORT 05000219/2018001 AND EXERCISE OF ENFORCEMENT DISCRETION

Dear Mr. Hanson:

On March 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at Oyster Creek Nuclear Generating Station. On April 4, 2018, the NRC inspectors discussed

the results of this inspection with Mr. Timothy Moore, Site Vice President, and other members of

your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented one Severity Level IV violation with no associated finding. The

NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of

the Enforcement Policy.

In addition, the NRC reviewed Licensee Event Report 05000219/2017-005-00, which described

the circumstances associated with a failed electrical ring lug on the No. 2 emergency diesel

generator. It was recognized that the No. 2 emergency diesel generator was inoperable for a

period of time that exceeded the allowed outage time of seven days detailed in Technical Specification 3.7.C.2.b, and therefore, is a violation of technical specifications. Regional staff

performed a risk evaluation and determined the issue was of low to moderate safety

significance (White).

Although this issue constitutes a violation of NRC requirements, the NRC determined that the

electrical ring lug failure which caused the No. 2 emergency diesel generator to be inoperable

was not within Exelons ability to reasonably foresee and correct. As a result, the NRC did not

identify a performance deficiency associated with this condition. The NRCs assessment

considered Exelons maintenance practices, industry operating experience, vendor and industry

maintenance and testing recommendations, and Exelons corrective actions to prevent

recurrence of the issue.

Based on the results of the NRCs inspection and assessment, I have been authorized, after

consultation with the Director, Office of Enforcement, to exercise enforcement discretion in

accordance with NRC Enforcement Policy Section 2.2.4, Exceptions to Using Only the

Operating Reactor Assessment Program, and Section 3.10, Reactor Violations with No

Performance Deficiency. The Region I Regional Administrator was also consulted regarding

enforcement discretion for this issue.

B. Hanson

If you contest the non-cited violation in this report, you should provide a response within 30 days

of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with

copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC

Resident Inspector at Oyster Creek Nuclear Generating Station.

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and the NRCs Public Document

Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390,

Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

David

L. Pelton, Director

Division of Reactor Projects

Docket Number: 50-219

License Number: DPR-16

Enclosure:

Inspection Report 05000219/2018001

cc w/encl:

Distribution via ListServ

ML18128A232

SUNSI Review

Non-Sensitive

Sensitive

Publicly Available

Non-Publicly Available

OFFICE

RI/DRP

RI/DRP

RI/DRP

RI/DRP

NAME

EAndrews

SShaffer

MYoung

DLPelton

DATE

04/26/18

04/26/18

05/08/18

05/07/18

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Number:

50-219

License Number:

DPR-16

Report Number:

05000219/2018001

Enterprise Identifier:

I-2018-001-0078

Licensee:

Exelon Nuclear

Facility:

Oyster Creek Nuclear Generating Station

Location:

Forked River, New Jersey

Inspection Dates:

January 1, 2018 to March 31, 2018

Inspectors:

A. Patel, Senior Resident Inspector
E. Andrews, Resident Inspector
F. Arner, Senior Reactor Analyst
J. Furia, Senior Health Physicist
J. Kulp, Senior Reactor Inspector
J. Schoppy, Senior Reactor Inspector

Approved By:

David

L. Pelton, Director

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Exelons performance at

Oyster Creek Nuclear Generating Station by conducting the baseline inspections described in

this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process

is the NRCs program for overseeing the safe operation of commercial nuclear power reactors.

Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC

identified and self-revealing findings, violations, and additional items are summarized in the

table below.

List of Findings and Violations

Untimely Licensee Event Report for Reportable Conditions Associated with the No. 2

Emergency Diesel Generator

Cornerstone

Severity

Cross-Cutting

Aspect

Report

Section

Not Applicable

Severity Level IV, NCV 05000219/2018001-01

Closed

Not Applicable

71153

The inspectors identified a non-cited, Severity IV violation of 10 CFR 50.73(a)(1) for a failure to

submit a licensee event report (LER) within 60 days after the discovery of an event requiring a

report. Specifically, on October 9, 2017, Exelon determined that the No. 2 emergency diesel

generator was inoperable for longer than the allowed outage time, which is reportable as a

condition prohibited by technical specifications. Exelon did not submit an LER for this event

until January 3, 2018.

Additional Tracking Items

Type

Issue Number

Title

Report

Section

Status

LER 05000219/2017-005-00

No. 2 emergency diesel

generator inoperable

71153

Closed

PLANT STATUS

Oyster Creek began the inspection period at 100 percent power. On January 6, 2018, operators

lowered power to 70 percent due to low intake levels. Operators returned the unit to

100 percent on January 8, 2018. The unit remained at or near 100 percent power for the

remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at

http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html.

Samples were declared complete when the IP requirements most appropriate to the inspection

activity were met consistent with Inspection Manual Chapter 2515, Light-Water Reactor

Inspection Program - Operations Phase.

The inspectors performed plant status activities described in IMC 2515 Appendix D,

Plant Status and conducted routine reviews using IP 71152, Problem Identification and

Resolution. The inspectors reviewed selected procedures and records, observed activities,

and interviewed personnel to assess licensees performance and compliance with Commission

rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather (2 Samples)

The inspectors evaluated readiness for impending adverse weather conditions for a blizzard

warning issued on January 4, 2018, and for low intake levels on January 6, 2018.

External Flooding (1 Sample)

The inspectors evaluated protection from external flooding prior to and during high winds

and heavy rain on March 2, 2018.

71111.04 - Equipment Alignment

Partial Walkdown (6 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1) No. 1 emergency diesel generator while No. 2 emergency diesel generator was

inoperable on January 3, 2018

(2) Emergency service water pumps during low intake level on January 6, 2018

(3) A isolation condenser during emergent unavailability of the B isolation condenser on

February 12, 2018

(4) Core spray system II during planned unavailability of core spray system I on

February 20, 2018

(5) B isolation condenser during shell side makeup on March 5, 2018

(6) B isolation condenser during emergent work on A isolation condenser on

March 12, 2018

Complete Walkdown (1 Sample)

The inspectors evaluated system configurations during a complete walkdown of the standby

liquid control system on February 15-16, 2018.

71111.05Q - Fire Protection Quarterly

Quarterly Inspection (9 Samples)

The inspectors evaluated fire protection program implementation in the following selected

areas:

(1) No. 1 emergency diesel generator room on January 24, 2018

(2) No. 2 emergency diesel generator room on January 24, 2018

(3) Reactor building 95 elevation on February 21, 2018

(4) Reactor building 75 elevation on February 21, 2018

(5) Reactor building 23 elevation on February 21, 2018

(6) C 125 VDC battery room on February 28, 2018

(7) A and B 4kV switchgear room on February 28, 2018

(8) New cable spreading room on March 1, 2018

(9) Recirculation pump motor generator set room on March 1, 2018

71111.06 - Flood Protection Measures

Internal Flooding (1 Sample)

The inspectors evaluated internal flooding mitigation protections in turbine building

switchgear area on February 22, 2018.

71111.07 - Heat Sink Performance

Heat Sink (1 Sample)

The inspectors evaluated Exelons monitoring and maintenance of B isolation condenser

performance on March 5, 2018.

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance

Operator Requalification (2 Samples)

The inspectors observed and evaluated a crew of licensed operators in the plants simulator

during licensed operator requalification training on January 23, 2018, and March 13, 2018.

Operator Performance (1 Sample)

The inspectors observed licensed operator performance during the Notice of Unusual Event on

January 6, 2018.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness (4 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with

the following equipment and/or safety significant functions:

(1) Periodic 10 CFR 50.65(a)(3) evaluation on January 17, 2018

(2) Service air system on January 22, 2018

(3) Start-up transformers on February 21, 2018

(4) Reactor recirculation system on March 5, 2018

71111.13 - Maintenance Risk Assessments and Emergent Work Control (6 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work

activities:

(1) Notice of Unusual Event declaration due to low intake levels on January 6, 2018

(2) Planned maintenance on the A isolation condenser on January 9, 2018

(3) Planned maintenance on the B isolation condenser on January 18, 2018

(4) Planned maintenance on core spray system I on February 20, 2018

(5) Planned maintenance on core spray system II on March 14, 2018

(6) Planned maintenance on the No. 2 emergency diesel generator on March 26, 2018

71111.15 - Operability Determinations and Functionality Assessments (7 Samples)

The inspectors evaluated the following operability determinations and functionality

assessments:

(1) Emergency service water pumps during low intake level on January 6, 2018

(2) Standby liquid control poison tank low level on January 29, 2018

(3) B isolation condenser elevated temperatures on February 16, 2018

(4) Control rod 34-43 slow five percent scram time on March 5, 2018

(5) B isolation condenser lowering shell side level on March 6, 2018

(6) A isolation condenser steam leak on March 12, 2018

(7) No. 2 emergency diesel generator elevated lead levels in oil sample on March 15, 2018

71111.18 - Plant Modifications (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

Engineering Change 620725, Refuel Bridge Software Modification to Allow Offloading Fuel

from a Cask

71111.19 - Post Maintenance Testing (8 Samples)

The inspectors evaluated post maintenance testing for the following maintenance/repair

activities:

(1) A recirculation pump relay replacement on January 22, 2018

(2) B isolation condenser valve, V-14-37, following valve repair on February 13, 2018

(3) A core spray pump relay replacement on February 20, 2018

(4) Average power range monitor 7 restoration to an operable condition on

February 22, 2018

(5) B isolation condenser remote shutdown panel level indication following emergent

inoperability on February 22, 2018

(6) Main generator exciter direct current (DC) brush inspection and replacement on

March 1, 2018

(7) 1-8 sump control logic following fuse replacement on March 27, 2018

(8) No. 2 emergency diesel generator following biannual overhaul on March 28, 2018

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Routine (6 Samples)

(1) 636.4.013, Diesel Generator 2 Load Test on January 3, 2018

(2) 609.3.003, Isolation Condenser Automatic Actuation Sensor Calibration and Test on

January 18, 2018

(3) 607.4.016, Containment Spray and Emergency Service Water System I Pump

Operability and Quarterly Inservice Test on January 23, 2018

(4) 604.3.001, Reactor Building to Torus Power Vacuum Breaker Test and Calibration on

February 8, 2018

(5) 602.3.004, Electromatic Relief Valve Pressure Sensor Test and Calibration on

March 6, 2018

(6) 651.4.003, Standby Gas Treatment System 15-minute Run - System 2 on

March 17, 2018

Inservice (2 Samples)

(1) 612.4.001, A Standby Liquid Control Pump and Valve Operability and In-service Test on

January 9, 2018

(2) 610.4.003, Core Spray Valve Operability and In-Service Test on March 12, 2018

71114.06 - Drill Evaluation

Emergency Planning Drill (1 Sample)

The inspectors evaluated the conduct of a routine Exelon emergency planning drill on

March 13, 2018.

Drill/Training Evolution (1 Sample)

The inspectors observed a simulator training evolution for licensed operators on

January 23, 2018.

RADIATION SAFETY

71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,

and Transportation

Radioactive Material Storage (1 Sample)

The inspectors observed radioactive waste container storage areas and verified the postings

and controls and that Exelon had established a process for monitoring the impact of long-

term storage of the waste.

Radioactive Waste System Walkdown (1 Sample)

The inspectors walked down the following:

Accessible portions of liquid and solid radioactive waste processing systems to verify

current system alignment and material condition

Abandoned in place radioactive waste processing equipment to review the controls

in place to ensure protection of personnel

Changes made to the radioactive waste processing systems since the last inspection

Processes for mixing and transferring radioactive waste resin and/or sludge

discharges into shipping/disposal containers

Current methods and procedures for dewatering waste

Waste Characterization and Classification (1 Sample)

The inspectors identified radioactive waste streams and reviewed radiochemical sample

analysis results to support radioactive waste characterization. The inspectors reviewed

the use of scaling factors and calculations to account for difficult-to-measure

radionuclides.

Shipment Preparations (1 Sample)

The inspectors reviewed the records of shipment packaging, surveying, labeling,

marking, placarding, vehicle checks, emergency instructions, disposal manifest, shipping

papers provided to the driver, and Exelons verification of shipment readiness.

Shipment Records (1 Sample)

The inspectors reviewed selected non-excepted package shipment records.

OTHER ACTIVITIES - BASELINE

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (1 Sample)

The inspectors reviewed Exelons implementation of its corrective action program related

to the following issues:

No. 2 Emergency Diesel Generator Ring Lug Failure

71153 - Follow-up of Events and Notices of Enforcement Discretion

Events (1 Sample)

The inspectors evaluated response to the following events:

Notice of Usual Event due to low intake levels on January 6, 2018

Licensee Event Reports (1 Sample)

The inspectors evaluated the following LERs which can be accessed at

https://lersearch.inl.gov/LERSearchCriteria.aspx:

LER 05000219/2017-005-00 and -01, Failure of the Emergency Diesel Generator #2,

During Surveillance Testing due to a Broken Electrical Connector, on February 14, 2018

INSPECTION RESULTS

Enforcement

Discretion

Enforcement Action (EA)-18-007: No. 2 Emergency Diesel

Generator Ring Lug Failure

71152

Description: On October 9, 2017, during a routine surveillance load test, the No. 2 emergency

diesel generator failed approximately 5 minutes into the run due to a broken ring lug on a

current transformer. Laboratory analysis of the broken ring lug determined that the ring lug

failed due to fatigue cracking that was initiated due to stresses caused by bending and

twisting of the electrical lug. Exelon last conducted a load surveillance on the No. 2

emergency diesel generator on September 25, 2017.

Corrective Actions: Corrective actions included replacement on the broken ring lug on the

No. 2 emergency diesel generator, extent of condition inspections on the No. 1 and No. 2

emergency diesel generators for additional bent or twisted ring lug connectors, and revision to

the electrical ring lug installation and emergency diesel generator procedures to include

inspection for bent or twisted ring lugs.

Corrective Action Reference(s): Issue report 4060815

Enforcement:

Violation: Oyster Creek Technical Specification 3.7.C.2.b states, in part, that if one diesel

generator becomes inoperable during power operation, the reactor may remain in operation

for a period not to exceed 7 days.

Contrary to the above, on October 9, 2017, it was recognized that one diesel generator was

inoperable for greater than the technical specification allowed outage time of 7 days, and

Oyster Creek continued power operation. Specifically, on October 9, 2017, No. 2 emergency

diesel generator failed to run during a routine surveillance test due to a broken ring lug on a

current transformer, which resulted in a total inoperability time of 6.5 months.

Severity/Significance: For violations warranting enforcement discretion, Inspection Manual

Chapter 0612 does not require a detailed risk evaluation, however, safety significance

characterization is appropriate. A Region I Senior Reactor Analyst (SRA) performed a best

estimate analysis of the safety significance using the Oyster Creek Standardized Plant

Analysis Risk (SPAR) model, Version 8.50 and Systems Analysis Programs for Hands-On

Integrated Reliability Evaluations (SAPHIRE). The evaluation estimated the total (internal and

external events risk) increase in core damage frequency (CDF) to be in the mid to high

E-6/yr range, or a low to moderate safety significance. The SRA evaluated the internal events

risk contribution due to the inoperability of the No. 2 emergency diesel generator for an

approximate 6.5 month exposure time. The exposure time relative to when the No. 2

emergency diesel generator was no longer capable of meeting its 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> mission time is

uncertain due to the effect of vibration induced fatigue, and therefore the method prescribed

within the RASP handbook guidance was used.

The analyst used the guidance in Section 2.5 of the Handbook, Revision 2.0, to estimate the

exposure time of 6.5 months based on the cumulative 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> summation of the No. 2

emergency diesel generator surveillance test proven run time. This approach is appropriate

for periodically operated components that degrade during operation (i.e. vibration induced

fatigue only occurs while the emergency diesel generator is in-service/operating). Given this

approach, the dominant internal events, loss of offsite power were evaluated for the estimated

internal risk increase. This contribution was estimated at 2E-6/yr increase in CDF. The

dominant sequences involved loss of offsite power events with a concurrent failure of the

No. 1 emergency diesel generator, failure of the combustion turbines, and failure to recover

offsite power or recover an emergency diesel generator prior to core damage.

The SRA performed various modeling changes after a review of revised calculations for DC

battery life:

Analysis noted that Oyster Creek Generating Station recirculation pump seals are similar in

design to those tested in reports generated for Nine Mile Point Unit 1 with the use of CAN2A

seals. Therefore, the failure probability of the seals in the station blackout sequence was

adjusted from 0.1 to 5E-2 similar to Nine Mile Point Unit 1 SPAR model 8.50.

The failure to load shed action (DCP-XHE-XM-LSHED) in the model was calculated using the

SPAR-H method and revised to 1.2E-2 versus being assumed to always fail (TRUE).

Failure probabilities for 1, 2, or 3 stuck open electromatic relief valves were revised to

be consistent with the previous model version 8.22 because of the isolation condenser

design at Oyster Creek Generating Station which limits cycling and significantly

reduces the probability of a failed open electromatic relief valve due to isolation

condensers controlling pressure.

The depressurization function using electromatic relief valves, if required, was

calculated through SPAR-H to be 1E-2 for sequences where total seal failure is

assumed (DEPSEALFAIL) (conservatively assumed limited time available).

The diesel driven firewater pumps are both available and were set to calculated fault

tree failure probabilities instead of always failed in the previous model. These are

2,000 gallons per minute pumps with a large supply of water and relatively simple

operator actions to inject to the reactor pressure vessel. The firewater was assumed

to fail at 0.1 when a total recirculation seal failure occurs due to assumed time

constraints.

The offsite power and the emergency diesel generator required recovery time events

were increased to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> for events where DC load shedding was successful,

without seal failures and isolation condenser success along with diesel driven firewater

success.

The SRA noted the No. 2 emergency diesel generator was recoverable. In fact, the diagnosis

of the failed condition was performed in a nominal 8-10 hours from the failure. Therefore, a

probability of failure to recover event for the conditional case was developed. The SRA used

SPAR-H as simple guidance, which conservatively supported a reasonable assumption of a

0.10 conditional probability of failure to recover the emergency diesel generator within

hours. The base case utilized a calculation within SPAR of 0.33 failure to recover

probability for 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> sequences.

To estimate the external risk contribution, the SRA identified that the most significant external

risk contribution was from fire events. Seismic, external flooding, and high wind events were

not significant contributors for the issue.

From discussions with Oyster Creek Fire probabilistic risk analysts and a review of this failure

condition, the increase in CDF due to the failed No. 2 emergency diesel generator for the

assumed 6.5 month exposure time was estimated at 4.5E-6/yr [(8.5E-5/yr-4.5E-5/yr) x (6.5/12

months) x 0.2].

The DC safety-related battery life would be at least a nominal 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br /> and longer if DC bus

stripping occurred, this allows for extended isolation condenser or electromatic relief valve

function, with injection from diesel driven firewater. Given the time considerations and

characteristics of the failure, an assumed recovery at a failure probability of 0.2 (slightly higher

than internal due to less time) was applied for the No. 2 emergency diesel generator, which

was a best estimate determined through SPAR-H insights. The dominant fire sequence was a

fire affecting the A and B 4kV switchgear rooms, where combustion turbine support would

be lost, with failure of the No. 1 emergency diesel generator breaker to close, and failure of

locally operating the isolation condenser due to eventual loss of power. The SRA noted that

FLEX credit was not quantified and would result in a lower risk estimation likely in the low

E-6/yr range. Combining internal and external risk contributions, the total increase in CDF

was 6.5E-6/yr, or low to moderate safety significance. The SRA determined that Exelon uses

a Large Early Release Frequency (LERF) factor value of 8E-2. This value takes into

consideration operator action for those relevant high pressure vessel breach scenarios

(fuel-coolant interaction, liner-melt-through, and direct containment heating). This also credits

procedure strategies where other mitigating actions are taken such as flooding the drywell.

The SRA review of the dominant sequences and time to core damage affirmed that LERF did

not increase the risk over that determined from the increase in CDF.

Basis for Discretion: The inspectors determined that the ring lug failure was not within

Exelons ability to foresee and prevent. As a result, no performance deficiency was identified.

The inspectors assessment considered:

1. Exelons review of emergency diesel maintenance performed in 2015 checked all

connections of the current transformer for tightness. The inspectors did not identify

any gaps or deficiencies in the 2015 inspections. Inspectors also reviewed completed

biennial inspections of the connection dating back to 1991 and did not identify any

gaps.

2. At the time of the failure, the current transformer connections did not have a time

directed replacement frequency recommended by the Emergency Diesel Generator

Owners Group. The inspectors did not identify any additional vendor or industry

recommendations specific to the failed component or considerations specific to the

failed component that existed prior to the failure.

3. Industry operating experience information available to Exelon did not identify the

potential for the fatigue cracking of the bent wire ring lug that was experienced.

4. The bent ring lug failure was not the result of a failure on the part of Exelon staff; no

standards existed on bending of the lug during installation and is considered skill of

the craft.

The NRC determined that it was not reasonable for Exelon to have been able to foresee and

prevent this violation of NRC requirements, and as such, no performance deficiency existed.

Therefore, the NRC has decided to exercise enforcement discretion in accordance with

Sections 2.2.4 and 3.10 of the NRC Enforcement Policy and refrain from issuing enforcement

action for the violation of technical specifications (EA-18-007). Further, because Exelons

actions did not contribute to this violation, it will not be considered in the assessment process

or the NRC Action Matrix.

Observation

71152

Exelons equipment corrective action program evaluation report (ECAPE) determined that the

ring lug failed on the No. 2 emergency diesel generator as a result of fatigue cracking, which

was initiated due to excessive stress caused by bending and twisting of the ring lug beyond

limits specified in industry guidelines. The inspectors noted that the ECAPE did not provide

supporting information regarding how the ring lug was bent and twisted beyond industry

guidelines. Specifically, industry guidance states that ring lugs can be bent up to 90 degrees.

The broken ring lug found in the No. 2 emergency diesel generator was bent at approximately

45-55 degrees per the ECAPE, which was within industry guidelines. Additionally, the ECAPE

did not include specific guidance on twisting allowances for ring lugs. Exelon documented the

inspectors observation in Issue Report 4089829. As a result of the inspectors observation,

Exelon revised the ECAPE to say the ring lug failed on the No. 2 emergency diesel generator

as a result of fatigue cracking, which was initiated due to excessive stress caused by bending

and twisting of the ring lug.

Untimely Licensee Event Report for Reportable Conditions Associated with the No. 2

Emergency Diesel Generator

Cornerstone

Severity

Cross-Cutting

Aspect

Report

Section

Not Applicable

Severity Level IV, NCV 05000219/2018001-01

Opened/Closed

Not Applicable

71153

The inspectors identified a Severity IV non-cited violation of 10 CFR 50.73(a)(1) for a failure

to submit an LER within 60 days after the discovery of an event requiring a report.

Specifically, on October 9, 2017, Exelon determined that the No. 2 emergency diesel

generator was inoperable for longer than the allowed outage time, which is reportable as a

condition prohibited by technical specifications. Exelon did not submit an LER for this event

until January 3, 2018.

Description: On October 9, 2017, the No. 2 emergency diesel was operated for its bi-weekly

load surveillance. Approximately five minutes into the run, the main control room received

LKOUT RELAY TRIP and EDG 2 DISABLED alarms. Following an automatic shutdown of

the No. 2 emergency diesel generator, Exelon staff discovered a ring lug of a current

transformer had broken. The last time the No. 2 emergency diesel generator was operated

for its bi-weekly load surveillance was on September 25, 2017. Oyster Creek Technical Specification 3.7.C.2 states, in part, that if one diesel generator becomes inoperable during

power operation, the reactor may remain in operation for a period not to exceed 7 days.

Details regarding the broken lug on the No. 2 emergency diesel generator can be found in

Section 71152.

On December 9, 2017, the inspectors identified that the No. 2 emergency diesel generator

was inoperable for longer than its technical specification allowed outage time of 7 days, which

is reportable to the NR

C. 10 CFR 50.73 states, in part, that the licensee shall report any

operation or condition which was prohibited by the plants technical specifications. Exelon

had not submitted an LER within the 60 day requirement because they did not consider the

inoperable No. 2 emergency diesel generator as an event that required an LER as specified

in 10 CFR 50.73.

Corrective Action(s): Exelon submitted the required LER on January 3, 2018.

Corrective Action Reference: Issue Report 4092328

Performance Assessment:

__________________________________________________________________________

Performance Deficiency: The inspectors determined that the failure to report a condition

which is prohibited by technical specifications within the time frame required by 10 CFR 50.73(a)(1) was a performance deficiency.

Screening: Traditional enforcement applies because a failure to report an event in a timely

manner has the potential to impact the NRCs ability to perform its regulatory function.

Significance: The finding was determined to be a Severity Level IV violation consistent with

Section 6.9.d.9 of the NRC Enforcement Policy.

Cross-Cutting Aspect: No cross-cutting aspect was assigned to this finding because it was

screened under the traditional enforcement process.

Enforcement:

Severity: The ROPs significance determination process does not specifically consider the

regulatory process impact in its assessment of licensee performance. Therefore, it is

necessary to address this violation which impedes the NRCs ability to regulate using

traditional enforcement to adequately determine non-compliance.

The inspectors determined that the violation was a Severity Level IV, which is a more than

minor violation, which is a concern that resulted in no or relatively inappreciable potential

safety or security consequence. The untimely LER was not used to make an unacceptable

change to the facility nor did it impact a licensing or safety decision by the NRC.

Violation: 10 CFR 50.73(a)(1) requires, in part, that a licensee submit an LER for any event

of the type described in this paragraph within 60 days after the discovery of the event.

CFR 50.73(a)(2)(i)(B) requires, in part, that the licensee report any event or condition

prohibited by the plants technical specifications. Contrary to the above, on December 9,

2017, Exelon failed to submit an LER within 60 days after the discovery that the No. 2

emergency diesel generator was inoperable for longer than its technical specification allowed

outage time of 7 days. This event occurred on October 9, 2017, and Exelon submitted the

LER on January 3, 2018, which exceeded the 10 CFR 50.73(a)(11) 60 day requirement.

Exelon entered this issue into their corrective action program in issue report 4092328.

Enforcement Action(s): This Severity Level IV violation is being treated as a non-cited

violation, consistent with Section 2.3.2.a of the NRC Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

Inspectors verified no proprietary information was retained or documented in this report.

On February 9, 2018, the inspectors presented the radiation safety inspection results to

Mr. Michael Gillin, Plant Manager, and other members of the Oyster Creek staff.

On April 4, 2018, the inspectors presented the quarterly resident inspector inspection results

to Mr. Timothy Moore, Site Vice President, and other members of the Oyster Creek staff.

DOCUMENTS REVIEWED

71111.01: Adverse Weather Protection

Procedures

ABN 18, Service Water Failure Response, Revision 7

ABN-31, High Winds, Revision 21

ABN 32, Abnormal Intake Level, Revision 30

OP-AA-108-111-1001, Severe Weather and Natural Disaster Guidelines, Revision 16

OP-OC-108-109-1001, Severe Weather Preparation T&RM for Oyster Creek, Revision 38

Issue Reports

4110580

71111.04: Equipment Alignment

Drawings

GE 885D781 Sh.1, Core Spray System Flow Diagram, Revision 76

GE 148F262 Sh.1, Emergency Condenser Flow Diagram, Revision 56

Issue Reports

1619946

4102875

4108748

4108767

4109454

71111.05: Fire Protection

Procedures

101.2, Oyster Creek Site Fire Protection Program, Revision 73

ABN 29, Plant Fires, Revision 32

ER-AA-600-1069, High Risk Fire Area Identification, Revision 4

OP-OC-201-008, Oyster Creek Pre-fire Plans, Revision 26

OP-OC-201-012-1001, On-line Fire Risk Management, Revision 4

Issue Reports

3971381

4059012

71111.06: Flood Protection Measures

Miscellaneous

OP-PSA-012, Internal Flood Evaluation Summary Notebook, dated May 2014

OC-PSA-022, Internal Flood Walkdown Notebook, dated May 2014

71111.11: Licensed Operator Requalification Program

Procedures

EP-AA-1010, Addendum 3, Exelon Nuclear Emergency Action Levels for Oyster Creek Station,

Revision 2

71111.12: Maintenance Effectiveness

Procedures

ER-AA-310, Implementation of the Maintenance Rule, Revision 11

ER-AA-310-1004, Maintenance Rule - Performance Monitoring, Revision 14

ER-AA-310-1005, Maintenance Rule - Dispositioning Between (a)(1) and (a)(2), Revision 7

Issue Reports

0516160

0648480

0687240

1501306

1514742

2472912

23130

2536453

2537005

2572740

25933

29443

29982

2637292

2643485

2643486

2702946

2714199

2715226

2719824

3949214

3952496

4060818

4069654

4089360

4089390

4109343

Miscellaneous

Oyster Creek Generating Station Maintenance Rule Periodic (a)(3) Assessment from

July 1, 2015 - June 30, 2017, dated November 29, 2017

Maintenance Orders/Work Orders

4345665

4345669

4345671

4345673

71111.15: Operability Evaluations

Issue Reports

4111295

4111496

4111518

4111506

71111.18: Plant Modifications

Miscellaneous

EC 620725, Refuel Bridge PLC Software Modification to Allow Offloading Fuel from a Cask,

dated February 23, 2018

71111.19: Post-Maintenance Testing

Issue Reports

4070270

4103389

4104381

4106951

4107367

4110560

Maintenance Orders/Work Orders

4745244

4745324

4745979

4748691

71124.08: Radioactive Solid Waste Processing and Radioactive Material Handling,

Storage, and Transportation

Procedures

RW-AA-100, Process Control Program for Radioactive Wastes, Revision 12

RW-AA-605, 10 CFR 61 Program, Revision 8

RP-AA-600, Radioactive Material/Waste Shipments, Revision 16

RP-AA-600-1001, Exclusive Use and Emergency Response Information, Revision 9

RP-AA-600-1005, Radioactive Material and Non Disposal Site Waste Shipments, Revision 19

RP-AA-600-1006, Shipment of Category 1 Quantities of Radioactive Material or Waste

(Category 1 RAMQC), Revision 11

RP-AA-600-1009, Shipment of Category 2 Quantities of Radioactive Material or Waste

(Category 2 RAMQC), Revision 2

RP-AA-600-1010, Use and Operation of WMG Software for Creating Containers, Samples,

Waste Streams and Waste Types, Revision 2

RP-AA-600-1011, Use and Operation of WMG Software for Gross Gamma Characterization and

Generation of Shipping Paperwork, Revision 4

RP-AA-601, Surveying Radioactive Material Shipments, Revision 20

RP-AA-602, Packaging of Radioactive Material Shipments, Revision 20

RP-AA-602-1001, Packaging of Radioactive Material/Waste Shipments, Revision 17

RP-AA-603, Inspection and Loading of Radioactive Material Shipments, Revision 10

RP-AA-605, 10 CFR 61 Program, Revision 7

Quality Assurance

NOSA-OYS-16-04, Chemistry, Radwaste, Effluent and Environmental Monitoring Audit Report

NOSA-OYS-17-06, Radiation Protection Audit Report

Fleet Assessment T-18 Assessment Report, October 2016

Fleet Assessment T-6 Assessment Report, September 2017

Fleet Assessment Mid-Cycle Assessment Report, March 2017

CFR Part 61 Scaling Factors

Dry Active Waste, Bead Resin, Sludge, CLW Composite, Cartridge Filters

2016-2017 10 CFR 61 Waste Stream Analysis, December 2016

Assignment Reports

23501

20554

2608094

Training

HAZSEC, DOT Security Awareness and Transportation Security Plan, Revision 1

NRWSHP-1000, DOT/79-19 Training for Support of Radioactive and Asbestos Shipments,

Revision 4

Shipments

OC-3001-16 OC-4003-16 OC-3001-17 OC-3002-17 OC-3003-17

71152: Problem Identification and Resolution

Procedures

PI-AA-125, Corrective Action Program Procedure, Revision 6

PI-AA-125-1006, Investigation Techniques Manual, Revision 3

MA-AA-726-620, Installation Instructions for 0-600 Volt EQ Related Splices, Revision 6

MA-OC-741-101, Diesel Generator Inspection (24 Month) - Electrical, Revision 15

NO-AA-300-1001, Nuclear Oversight Independent Inspection Plan, Revision 10

2400-GME-3780.52, Installation, Testing and Termination of Wire and Cable, Revision 6

2400-SME-3780.03, Electrical Termination Taping and Raychem Splicing, Revision 16

Maintenance Orders/Work Orders

R2239604

R2230340

R2229008

R2207589

R2191838

R2190504

R2151723

R2111307

R2032680

R2065956

R0808797

R0522916

R0504310

R0055415

R0041081

R0029109

4695984

4695269

4697086

4694906

Issue Reports

4060815

4089829

1436376

4061089

4073377

4060815

4060818

4061527

4061931

4066706

4061093

Miscellaneous

ES-023, Selection and Sizing of Power, Lighting and Control Cables, Revision 2

SP-9000-31-213, Class 1E, Electric Cable for Power, Control & Instrumentation, Revision 9

SP-9000-41-005, Cables & Raceways at Oyster Creek, Revision 3

71153: Follow-up of Events and Notices of Enforcement Discretion

Issue Reports

4091183

4091037

4091010

4090950

4090920

4090820

4090803

4091287

4091455