ML17252A246: Difference between revisions
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| number = ML17252A246 | | number = ML17252A246 | ||
| issue date = 11/04/1976 | | issue date = 11/04/1976 | ||
| title = | | title = Letter Submitting Reportable Occurrence Number 050-249/1976-23 in Accordance with Technical Specifications, Section 6.6.B | ||
| author name = Stephenson | | author name = Stephenson B | ||
| author affiliation = Commonwealth Edison Co | | author affiliation = Commonwealth Edison Co | ||
| addressee name = Keppler J | | addressee name = Keppler J | ||
| addressee affiliation = NRC/RGN-III | | addressee affiliation = NRC/RGN-III | ||
| docket = 05000237, 05000249 | | docket = 05000237, 05000249 | ||
Line 14: | Line 14: | ||
| page count = 3 | | page count = 3 | ||
}} | }} | ||
=Text= | =Text= | ||
{{#Wiki_filter:. | {{#Wiki_filter:.* . Comrnonv.h Edison | ||
. LICENSEE EVd\JT REPOR. *. -. . * .. ' CONTROL BLOCK: I ' I *.1 1. I I (PLEASE PRll'JT ALL REQUIRED INFORMATION) ' 1 6 | * Dresde,1 Nuclear Power Station R.R. #i Morris, Illinois 60450 Telephone 815/942-2920 BBS Ltr. #76-775 November 4, 1976 Mr. James G~ Keppler, Regional Director Directorate of R~gulatory Operations -.Region III U. S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, Illinois 60137 Enclosed please find Reportable Occurrence report number 50-249/1976-23. | ||
This report is being submitted to your office in accordance with the Dresden Nuclear Powe~ Station Techriical ~pecifications, Section 6.6.B. | |||
}} | A n n.: .*1Y).. _/) ~. * -I- . | ||
h un~ ~ | |||
. B. Stephensori | |||
* tation Superintendent. . | |||
Dresden Nuclear Power Station BBS :jo Enclosure cc: Director of Inspection & *Enforcement | |||
. Direct'or of Management Information & Program Control File/NRC | |||
~* . LICENSEE EVd\JT REPOR. *. -. . *.. | |||
' CONTROL BLOCK: I ' I *.1 1. I I (PLEASE PRll'JT ALL REQUIRED INFORMATION) | |||
' 1 6 LICENSEE LICENSE EVENT | |||
* < NAME LICENSE NUMBER TYPE TYPE | |||
.@El II I L. ID IR I s 13 I 10101-10101010101-10101 1!1111111111 10131 7 8 9 ' 14 15 25 26 ' 30 '31 ' 32' REPORT REPORT CATEGORY TYPE. SOURCE OOCl\ET NUM6ER | |||
* EVENT* DATE REPORT DATE lof1 IcoN1 I I I llJ LLl 101s101~101~1~191 11 IOIOl?l71(,l .*II II 1014171(, L 7 8 57 58' 59 60 61 68 69 74 75 80 EVENT DESCRIPTION . | |||
(filg].lD!JRtAJ.G- REFUELING- OUTAGE LDC.AL l.t:Ak-:-RATE TESTING; *LPC/ PRtrnARV I 7* 8' 9 . ' 80. | |||
7 lol31Ei' 9ltSO.L..ATION'. | |||
CA*IE:CI< | |||
VfU;V 3-!S-O/-J.5& | |||
£XHtBtT£.D A l...EAr<AC-£ RAT£.... U!J' | |||
' ' 80 I, | |||
7 | |||
~ IEXC£$$'0F /HT:; T£CH SP£.C. /_JM/{ OF .J.Cf.~f!/_. SC'l="H. TH OTH~g*. VAL.VE: | |||
8 9' ' ' '' ' 80 I | |||
10'581 lusED VO f6R<YYI THE. 4'?'-Psf(:; PRESSUfV~ DECAY 7EST BouJVDl1R..Y .. fYlANuALf 7 9 i ' ' '' ' ' ' " 80 lolsl I VAt..VE'.' 3- 15°0! -:Y,,B J 1-lfJD A $ IGNI FICA NT WATER HC/IJ) PR£s£NTj CONSEQLJOJT1..y,, I 7 8 9. * .. . PRIME * . (5,£ /IT!FICHEV -<;;ft£GT) 80 | |||
. | |||
* SYSTEM CAUSE COMPONENT COMPON!:NT - . | |||
. CODE CODE | |||
* COMPONENT CODE SUPPLIER MANUFACTURER VIOLATION | |||
@0 ISIFLlsJ 1v1AIL1v1£1x1 lt!J 1A1s1*~1s1 L'Ll 7 8 9 10 ' 11 12 17 ' 43 44 47 48 | |||
. CAUSE DES.CA!PTION | |||
~ l::TJ1£ VA/..-1/E f:fll L-UR.6 'WA~ CAUSED Bi EXCESS I 116 ])15C-To -SEAi 1-£AKAG-~. J 7 8 9 ' 80 lo'91 l1r1cs J.£AK-fK-G: i,.JA~ A77R.t8UIED, ..To TH£ PREsEl'JCG.* OE DtRTA*No | |||
* SIYIAL-t~ I 7 8 9 ' ', ' ' ' 80. ' | |||
,.~.: (iE1 .I S:CRATc.HC:S OtJ THE Vf/LV~ $£fl'0 APPARENTLY IHE REs()t,..T oF.Jv'ORWl,fiL .W£AR. J | |||
' '' 7 ;*, 8 9 ,: FACILllY '' '' ' METHOD OF ' 'Js:t:E-:/rrjA~/t;F,.P ~}:/.!) . co | |||
' STATUS * %.. POWER OTHER STATUS - OISCOVEAY | |||
* DISCOVERY DESC.RIPTION EE] , 9*lHJ | |||
* lO 16 l *6112 *1..__"'""-'.AJ'--A_ ___,I44 .** lBJ ,__,,..-.N-.;,..11'-'--.---~..,.-.-'-._-_ ___,! | |||
. 7. | |||
* 0** * .10 | |||
* 13 45 **. 46 so FORM OF ACTIVITY CONTENT rn .lZJ 7 8 | |||
*RELEASED 9 | |||
OF RELEASE | |||
* l~J 10 11 AMOUNT OF ACTIVITY | |||
*I.__*--~N_ll_ _______. | |||
44 I | |||
45 ' | |||
LOCATION OF RELEASE 80 PERSONNEL EXPOSURES NUMBER * | |||
* TYPE DESCRIPTION | |||
~ lo Io JO11I : *~ . ~-.....::.JtJ_tt~--,---.,.---------~-------~-~-"-'-'-'-:-'-'------__.___, | |||
7 * *a s 12.. 13 ea. | |||
'. PERS'ONNEL INJURIES NUMBER . OESCRIPTION v. | |||
[EJ*1n10.l.ol L - -. | |||
; ._ * * - | |||
* _A_f1_._*- - - - - - - - - - - - - - - - - - - - J 7 8 ~ 11 12 80 OFFSITE CONSEQUENCES | |||
.Elfil I A/A 7 8 9 80 | |||
. LOSS ~F;l DAMAGE . TO FACILITY TYPE .DESCRIPTION * | |||
~ .~ A)ff' 7 8 9 10 80 PUBLICITY l:illl8 7 81..;_---L.~L-----------------,-------------'-----.,---~--'-----"------.---::-2~J ADDITIONAL FACTOfiS (1JUJ /v*>0' 7 89 80 EEi89 7 BC NAME: _ _ R;._A_/i_V_])_o_'-_**_?_1:...... 1 _c_.*_w_c._:-_r_D_M_'E----'R"-.---~ PHONE: £xT. d...G 5 | |||
EVENT DESCRIPTION (Continued) the as-found leakage of 61.0 SCFH was attributed entirely to leakage through check valve 1501-25B. A second leak test using valves 1501-26B, i501-22B, and 1001-SB as boundaries yielded a leakage rate of 4.2 SCFH: Since .the second test volume included the volume of the previous test, total through-leakage for the penetration was well under the Tech Spec limit. A similar valve on Unit-2 failed 16cal leak~rate testing in early 1975. (50-249/1976-23) | |||
CAUSE DESCRIPTION. (Continued) | |||
The valve was disassembled, the seat was lapped, and the packing and _Flexitallic gasket were replaced. Leak-rate testing of the reassembled valve was satisfactory. | |||
In 1975, a test/drain line was installed on this penetration which permitted leak-rate testing of check valve 3-1501-25B for the first time since unit oper-ation began. Since this valve has performed* satisfactorily over a period of . | |||
several years, testing of this vaLve on an approximately annual basis should permit timely identification of a recurring problem. | |||
* Valve 3-15.0l-25B is a 16-inch tilting disc check valve, manufactured by.Atwood and Morrill Company, Inc. | |||
~ .. | |||
;; .}} |
Latest revision as of 08:07, 24 February 2020
ML17252A246 | |
Person / Time | |
---|---|
Site: | Dresden |
Issue date: | 11/04/1976 |
From: | Stephenson B Commonwealth Edison Co |
To: | James Keppler NRC/RGN-III |
References | |
BBS Ltr. #76-775 | |
Download: ML17252A246 (3) | |
Text
.* . Comrnonv.h Edison
- Dresde,1 Nuclear Power Station R.R. #i Morris, Illinois 60450 Telephone 815/942-2920 BBS Ltr. #76-775 November 4, 1976 Mr. James G~ Keppler, Regional Director Directorate of R~gulatory Operations -.Region III U. S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, Illinois 60137 Enclosed please find Reportable Occurrence report number 50-249/1976-23.
This report is being submitted to your office in accordance with the Dresden Nuclear Powe~ Station Techriical ~pecifications, Section 6.6.B.
A n n.: .*1Y).. _/) ~. * -I- .
h un~ ~
. B. Stephensori
- tation Superintendent. .
Dresden Nuclear Power Station BBS :jo Enclosure cc: Director of Inspection & *Enforcement
. Direct'or of Management Information & Program Control File/NRC
~* . LICENSEE EVd\JT REPOR. *. -. . *..
' CONTROL BLOCK: I ' I *.1 1. I I (PLEASE PRll'JT ALL REQUIRED INFORMATION)
' 1 6 LICENSEE LICENSE EVENT
- < NAME LICENSE NUMBER TYPE TYPE
.@El II I L. ID IR I s 13 I 10101-10101010101-10101 1!1111111111 10131 7 8 9 ' 14 15 25 26 ' 30 '31 ' 32' REPORT REPORT CATEGORY TYPE. SOURCE OOCl\ET NUM6ER
- EVENT* DATE REPORT DATE lof1 IcoN1 I I I llJ LLl 101s101~101~1~191 11 IOIOl?l71(,l .*II II 1014171(, L 7 8 57 58' 59 60 61 68 69 74 75 80 EVENT DESCRIPTION .
(filg].lD!JRtAJ.G- REFUELING- OUTAGE LDC.AL l.t:Ak-:-RATE TESTING; *LPC/ PRtrnARV I 7* 8' 9 . ' 80.
7 lol31Ei' 9ltSO.L..ATION'.
CA*IE:CI<
VfU;V 3-!S-O/-J.5&
£XHtBtT£.D A l...EAr<AC-£ RAT£.... U!J'
' ' 80 I,
7
~ IEXC£$$'0F /HT:; T£CH SP£.C. /_JM/{ OF .J.Cf.~f!/_. SC'l="H. TH OTH~g*. VAL.VE:
8 9' ' ' ' 80 I
10'581 lusED VO f6R<YYI THE. 4'?'-Psf(:; PRESSUfV~ DECAY 7EST BouJVDl1R..Y .. fYlANuALf 7 9 i ' ' ' ' ' " 80 lolsl I VAt..VE'.' 3- 15°0! -:Y,,B J 1-lfJD A $ IGNI FICA NT WATER HC/IJ) PR£s£NTj CONSEQLJOJT1..y,, I 7 8 9. * .. . PRIME * . (5,£ /IT!FICHEV -<;;ft£GT) 80
.
- SYSTEM CAUSE COMPONENT COMPON!:NT - .
. CODE CODE
- COMPONENT CODE SUPPLIER MANUFACTURER VIOLATION
@0 ISIFLlsJ 1v1AIL1v1£1x1 lt!J 1A1s1*~1s1 L'Ll 7 8 9 10 ' 11 12 17 ' 43 44 47 48
. CAUSE DES.CA!PTION
~ l::TJ1£ VA/..-1/E f:fll L-UR.6 'WA~ CAUSED Bi EXCESS I 116 ])15C-To -SEAi 1-£AKAG-~. J 7 8 9 ' 80 lo'91 l1r1cs J.£AK-fK-G: i,.JA~ A77R.t8UIED, ..To TH£ PREsEl'JCG.* OE DtRTA*No
- SIYIAL-t~ I 7 8 9 ' ', ' ' ' 80. '
,.~.: (iE1 .I S:CRATc.HC:S OtJ THE Vf/LV~ $£fl'0 APPARENTLY IHE REs()t,..T oF.Jv'ORWl,fiL .W£AR. J
' 7 ;*, 8 9 ,: FACILllY ' METHOD OF ' 'Js:t:E-:/rrjA~/t;F,.P ~}:/.!) . co
' STATUS * %.. POWER OTHER STATUS - OISCOVEAY
- DISCOVERY DESC.RIPTION EE] , 9*lHJ
- lO 16 l *6112 *1..__"'""-'.AJ'--A_ ___,I44 .** lBJ ,__,,..-.N-.;,..11'-'--.---~..,.-.-'-._-_ ___,!
. 7.
- 0** * .10
- 13 45 **. 46 so FORM OF ACTIVITY CONTENT rn .lZJ 7 8
- RELEASED 9
OF RELEASE
- l~J 10 11 AMOUNT OF ACTIVITY
- I.__*--~N_ll_ _______.
44 I
45 '
LOCATION OF RELEASE 80 PERSONNEL EXPOSURES NUMBER *
- TYPE DESCRIPTION
~ lo Io JO11I : *~ . ~-.....::.JtJ_tt~--,---.,.---------~-------~-~-"-'-'-'-:-'-'------__.___,
7 * *a s 12.. 13 ea.
'. PERS'ONNEL INJURIES NUMBER . OESCRIPTION v.
[EJ*1n10.l.ol L - -.
- ._ * * -
- _A_f1_._*- - - - - - - - - - - - - - - - - - - - J 7 8 ~ 11 12 80 OFFSITE CONSEQUENCES
.Elfil I A/A 7 8 9 80
. LOSS ~F;l DAMAGE . TO FACILITY TYPE .DESCRIPTION *
~ .~ A)ff' 7 8 9 10 80 PUBLICITY l:illl8 7 81..;_---L.~L-----------------,-------------'-----.,---~--'-----"------.---::-2~J ADDITIONAL FACTOfiS (1JUJ /v*>0' 7 89 80 EEi89 7 BC NAME: _ _ R;._A_/i_V_])_o_'-_**_?_1:...... 1 _c_.*_w_c._:-_r_D_M_'E----'R"-.---~ PHONE: £xT. d...G 5
EVENT DESCRIPTION (Continued) the as-found leakage of 61.0 SCFH was attributed entirely to leakage through check valve 1501-25B. A second leak test using valves 1501-26B, i501-22B, and 1001-SB as boundaries yielded a leakage rate of 4.2 SCFH: Since .the second test volume included the volume of the previous test, total through-leakage for the penetration was well under the Tech Spec limit. A similar valve on Unit-2 failed 16cal leak~rate testing in early 1975. (50-249/1976-23)
CAUSE DESCRIPTION. (Continued)
The valve was disassembled, the seat was lapped, and the packing and _Flexitallic gasket were replaced. Leak-rate testing of the reassembled valve was satisfactory.
In 1975, a test/drain line was installed on this penetration which permitted leak-rate testing of check valve 3-1501-25B for the first time since unit oper-ation began. Since this valve has performed* satisfactorily over a period of .
several years, testing of this vaLve on an approximately annual basis should permit timely identification of a recurring problem.
- Valve 3-15.0l-25B is a 16-inch tilting disc check valve, manufactured by.Atwood and Morrill Company, Inc.
~ ..
- .