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{{#Wiki_filter:EOP: AP-RCP.1 TITLE: RCP SEAL MALFUNCTION REV 11 PAGE 1 of 10 ROCHESTER GAS AND ELECTRIC CORPORATION GINNA STATION CONTROLLED COPY NUMBER RESPONSIBLE AGER EFFECTIVE DATE CATEGORY 1.0 REVIEWED BY: 9708i30125 970805 PDR ADOCK 05000244 PDR EOP: AP-RCP.1 RCP SEAL MALFUNCTION REV 11 PAGE 2 of 10 A.PURPOSE-This procedure provides the instructions necessary to diagnose and to respond to a reactor coolant pump seal malfunction.
{{#Wiki_filter:EOP:           TITLE:
B.ENTRY CONDITIONS/SYMPTOMS 1.ENTRY CONDITIONS
REV  11 AP-RCP.1                   RCP SEAL MALFUNCTION PAGE 1 of 10 ROCHESTER GAS AND ELECTRIC CORPORATION GINNA STATION CONTROLLED COPY NUMBER RESPONSIBLE   AGER EFFECTIVE DATE CATEGORY 1.0 REVIEWED BY:
-This procedure is entered from: a.E-3, STEAM GENERATOR TUBE RUPTURE, or b.ES-l.l, SI TERMINATION, or c.ES-1.2, POST LOCA COOLDOWN AND DEPRESSURIZATION, or d.ECA-0.1, LOSS OF ALL AC POWER RECOVERY WITHOUT SI REQUIRED, or e.ECA-2.1, UNCONTROLLED DEPRESSURIZATION OF BOTH STEAM GENERATORS, or f.ECA-3.1, SGTR WITH LOSS OF REACTOR COOLANT-SUBCOOLED RECOVERY DESIRED, or g.ECA-3.2, SGTR WITH LOSS OF REACTOR COOLANT-SATURATED RECOVERY DESIRED,.or h.ECA-3.3, SGTR WITHOUT PRESSURIZER PRESSURE CONTROL, or i.FR-I.1, RESPONSE TO HIGH PRESSURIZER LEVEL, when RCP seal malfunction is indicated.
9708i30125 970805 PDR ADOCK   05000244 PDR
2.SYMPTOMS-The symptoms of RCP SEAL MALFUNCTION are;a.Annunciator B-17(18), RCP A(B)No.1 SEAL HI-LO FLOW 5.0 GPM 1.0 , lit, or b.Annunciator B-9(10), RCP A(B)LABYR SEAL LO DIFF PRESS 15" H20, lit, or c.Annunciator B-3(4), RCP A(B)STAND PIPE HI LEVEL+1 FT, lit, or Continued on next page AP-RCP.1 RCP SEAL MALFUNCTION REV: 11 PAGE 3 of 10 2.SYMPTOMS (cont)d.Annunciator B-ll(12), RCP A(B)STAND PIPE LO LEVEL-4 FT, lit, or e.Annunciator B-25(26), RCP A(B)No.1 SEAL LO DIFF PRESS 220 PSID, lit, or f.Annunciator B-l(2), RCP A(B)No.1 SEAL OUT HI TEMP 200'F, lit, or, g.Annunciator A-7(15), RCP A(B)CCW RETURN HIGH TEMP OR LOW FLOW, lit.
EOP: AP-RCP.1 TITLE: RCP SEAL MALFUNCTION REV 11 PAGE 4 of 10 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED CAUTION o IF, AT ANY TIME DURING THIS PROCEDURE, A'EACTOR TRIP OR SI OCCURS, E-O, REACTOR TRIP OR SAFETY INJECTION, SHALL BE PERFORMED.
o IF ANY RCP IS TRIPPED, THEN SHUTDOWN MARGIN REQUIREMENTS SHOULD BE VERIFIED (REFER TO 0-3.1, BORON CONCENTRATION FOR XENON FREE ALL RODS IN MOST REACTIVE ROD STUCK OUT SHUTDOWN MARGIN).o IF A RCP IS SECURED BECAUSE OF A SEAL MALFUNCTION, IT SHOULD NOT BE RESTARTED UNTIL THE CAUSE OF THE MALFUNCTION HAS BEEN DETERMINED AND CORRECTED.
NOTE;o If a Reactor trip is iTIitiated while performing Step 1, transition to E-0 should occur while completing subsequent actions of the step.o Total¹1 Seal Flow is defined as the sum of indicated¹1 Seal Leakoff Flow and RCDT leak rate (PPCS Point ID L1003, 3.2 gal/8 in the normal operating range).1 Check Total$1 Seal Leakaff Flows-LESS THAN 8.0 GPM IF a¹1 Seal Failure is verified by a decrease in Labyr Seal Diff Pressure OR increasing Seal Inlet/Outlet temps, THEN perform the following:
a.IF reactor trip breakers closed, THEN trip the reactor.b.Trip the affected RCP(s).c.Allow 4 minutes for pump coast down, THEN close affected RCP(s)seal disch valve.~RCP A, AOV-270A~RCP B, AOV-270B d.IF reactor trip was NOT required, THEN go to Step 4.
EOP: AP-RCP.1 RCP SEAL MALFUNCTION REV 11 PAGE 5 of 10 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 2 Check RCP Seal Return Valve Alignment:
a.RCP seal return isolation valve, MOV-313-OPEN a.Perform the following:
1)Ensure CI reset.2)Ensure both trains of XY relays for RCP seal return isolation valve, MOV-313, reset.3)Open RCP seal return isolation valve, MOV-313.IF MOV-313 can NOT be opened, THEN dispatch AO to AUX BLDG with RWST area key to check valve and breaker locally (breaker MCC C position 13J).b.Verify RCP seal disch valves OPEN~RCP A, AOV-270A~RCP B, AOV-270B b.Manually open valves.IF valves can NOT be opened, THEN verify IA aligned to CNMT and go to Step 3.
I 0 f EOP: AP-RCP.1 TITLE: RCP SEAL MALFUNCTXON REV 11 PAGE 6 of 10 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED V NOTE: o If a reactor trip is initiated while performing Step 3, transition to E-0 should occur while completing subsequent actions of the step.o The 0.8 GPM limit for¹1 seal flow applies when the RCS is at normal operating pressure.Refer to Figure RCP SEAL LEAKOFF and consult plant staff for guidance if the RCS is at reduced pressure.3 Check Total gl Seal Flow-BETWEEN 0.8 GPM AND 6.0 GPM IF¹1 Seal Inlet and Outlet temperatures are increasing, THEN perform the following:
a.IF reactor trip breakers closed, THEN trip the reactor.b.Trip the affected RCP(s).c.Allow 4 minutes for pump coast down, THEN close affected RCP(s)seal disch valve.~RCP A)AOV-270A~RCP B)AOV-270B IF¹1 Seal Inlet and Outlet temperatures are stable, THEN perform the following while continuing with this procedure.
o IF total¹1 Seal Flow greater than 6.0 gpm, THEN maintain seal injection flow rate of 9.0 GPM or greater to the affected RCP.o IF total¹1 Seal flow exceeds 8.0 GPM OR Seal Inlet/Outlet temperatures begin to increase, THEN return to Step 1.o Prepare for orderly pump shutdown by placing the plant in Hot Shutdown using 0-2.1, NORMAL SHUTDOWN TO HOT SHUTDOWN.o Secure the affected RCP with 8 hours.


EOP: AP-RCP.1 RCP SEAL MALFUNCTION REV 11 PAGE 7 of 10 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: Attachment RCP DIAGNOSTICS may be used to aid in diagnosis.
EOP:
4 Check RCP Cooling: o Annunciator A-7, RCP A CCW RETURN HIGH TEMP OR LOW FLOW-EXTINGUISHED o Annunciator A-15, RCP B CCW RETURN HIGH TEMP OR LOW FLOW-EXTINGUISHED Perform the following:
REV    11 AP-RCP.1                     RCP SEAL MALFUNCTION PAGE 2    of   10 A. PURPOSE  This  procedure provides the instructions necessary to diagnose  and  to respond to a reactor coolant pump seal malfunction.
a.Verify RCP CCW supply and return valves open.~RCP A, MOV-749A and MOV-759A~RCP B, MOV-749B and MOV>>759B b.En'sure open CCW outlet valves from RCP thermal barriers.~RCP A, AOV-754A~RCP B, AOV-754B 5 Check RCP g2 Seal Indications:
B. ENTRY CONDITIONS/SYMPTOMS
o Annunciator B-3, RCP A STANDPIPE HI LEVEL+1 FT-EXTINGUISHED' Annunciator B-4, RCP B STANDPIPE HI LEVEL+1 FT-EXTINGUISHED IF affected RCP¹1 seal leakoff flow decreasing, THEN failure of¹2 seal may be indicated.
: 1. ENTRY CONDITIONS  This    procedure  is entered from:
Continue plant operation while closely monitoring RCP seal indications.
: a. E-3, STEAM GENERATOR TUBE RUPTURE,    or
: b. ES-l.l,  SI TERMINATION, or
: c. ES-1.2,  POST LOCA COOLDOWN AND DEPRESSURIZATION,       or
: d. ECA-0.1,  LOSS OF ALL AC POWER RECOVERY WITHOUT      SI REQUIRED,  or
: e. ECA-2.1,  UNCONTROLLED DEPRESSURIZATION OF BOTH STEAM GENERATORS, or
: f. ECA-3.1, SGTR WITH LOSS OF REACTOR COOLANT-SUBCOOLED RECOVERY DESIRED, or
: g. ECA-3.2, SGTR WITH LOSS OF REACTOR COOLANT-SATURATED RECOVERY DESIRED, .or
: h. ECA-3.3,  SGTR WITHOUT PRESSURIZER PRESSURE    CONTROL,     or
: i. FR-I.1, RESPONSE TO HIGH PRESSURIZER      LEVEL, when RCP seal malfunction is indicated.
: 2. SYMPTOMS  - The symptoms  of  RCP SEAL MALFUNCTION  are;
: a. Annunciator B-17(18),     RCP A(B) No.1 SEAL HI-LO  FLOW 5.0 GPM 1.0 ,  lit,  or
: b. Annunciator B-9(10),    RCP  A(B) LABYR SEAL LO  DIFF PRESS 15" H20,  lit, or
: c. Annunciator B-3(4),   RCP   A(B) STAND PIPE HI LEVEL +     1 FT, lit, or Continued on next page


EOP.AP-RCP.1 TITLE: RCP SEAL MALFUNCTION REV: 11 PAGE 8 of 10 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED CAUTION REDUCING CHARGING FLOW'WILL RESULT IN INCREASING REGEN HX OUTLET TEMPERATURE.
REV: 11 AP-RCP. 1                   RCP SEAL MALFUNCTION PAGE of 10
6 Check RCP Labyrinth Seal D/Ps-GREATER THAN 15 INCHES OF MATER Perform the following:
: 2. SYMPTOMS  (cont)
a.Ensure open CCW outlet valves from RCP thermal barriers.~RCP A, AOV-754A~RCP B, AOV-754B b.Verify seal injection flow greater than 5 GPM for affected RCP.c.Adjust HCV-142 as necessary.
: d. Annunciator B-ll(12),  RCP A(B) STAND PIPE  LO LEVEL  -4 FT, lit, or
d.Dispatch AO to check seal injection filter D/P.e.Check CCW surge tank level stable.IF level increasing, THEN go to AP-CCW.l, LEAKAGE INTO THE COMPONENT COOLING LOOP.7 Check RCP g3 Seal Indications:
: e. Annunciator B-25(26), RCP A(B) No. 1 SEAL LO  DIFF PRESS 220 PSID, lit, or
o Annunciator B-ll, RCP A STAND PIPE LO LEVEL-4FT-EXTINGUISHED o Annunciator B-12, RCP B STAND PIPE LO LEVEL-4FT-EXTINGUISHED Check CNMT radiation monitors normal.~R-11~R-12 IF RCP standpipe level low and CNMT radiation'increasing, THEN¹3 seal leakage increase is probable.Continue plant operation while closely monitoring RCP seal indications.
: f. Annunciator B-l(2), RCP A(B) No. 1  SEAL OUT HI TEMP  200'F, lit, or,
1'l F.OP: AP-RCP.1 LITLE: RCP SEAL MALFUNCTION REV 11 PAGE 9 of 10 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: In the absence of other seal failure indications, an elevated¹1 seal outlet temperature may indicate pump bearing damage.*8 Monitor Plant Conditions:
: g. Annunciator A-7(15),  RCP  A(B) CCW RETURN  HIGH TEMP OR FLOW, lit.
a.RCP¹1 seal flow o Total¹1 seal leakoff flow-LESS THAN 6.0 GPM o Total¹1 seal flow-GREATER THAN 0.8 GPM a.IF affected RCP running, THEN return to Step 1.IF NOT, THEN perform the follow'ing:
LOW
1)Monitor affected RCP (Refer to Attachment RCP DIAGNOSTICS).
 
b.RCP¹1 Seal Flow-WITHIN THE NORMAL OPERATING RANGE OF FIGURE RCP SEAL LEAKOFF 2)Consult Plant Staff to determine if cooldown required.b.Perform the following:
EOP:            TITLE:
o Ensure seal injection flow exceeds¹1 seal leakoff flow.o Refer to S-2.1, Reactor Coolant Pump Operation.
REV    11 AP-RCP. 1                        RCP SEAL MALFUNCTION PAGE 4    of 10 STEP    ACTION/EXPECTED RESPONSE              RESPONSE NOT OBTAINED CAUTION  o    IF, AT ANY TIME DURING THIS PROCEDURE, A'EACTOR TRIP OR      SI OCCURS, E-O, REACTOR TRIP OR SAFETY INJECTION, SHALL BE PERFORMED.
o Consult plant staff for further instructions.
o   IF ANY RCP IS TRIPPED,  THEN SHUTDOWN MARGIN REQUIREMENTS SHOULD BE VERIFIED (REFER TO  0-3.1, BORON CONCENTRATION FOR XENON FREE ALL RODS IN MOST REACTIVE ROD STUCK OUT SHUTDOWN MARGIN).
c.RCP¹1 seal outlet temperatures LESS THAN 215'ND STABLE d.RCS leakage-NORMAL (Refer to leakage surveillance sheet)c.IF pump bearing damage is suspected, THEN notify plant staff and expedite shutdown of the affected RCP.IF NOT, THEN return tc Step 1.d.Perform the following:
o    IF A RCP IS SECURED BECAUSE OF A SEAL MALFUNCTION, IT SHOULD NOT BE RESTARTED UNTIL THE CAUSE OF THE MALFUNCTION HAS BEEN DETERMINED AND CORRECTED.
1)Calculate RCS leakrate.2)Refer to ITS section 3.4e13.
NOTE;    o If a  Reactor trip is iTIitiated while performing Step 1, transition to E-0 should occur while completing subsequent actions of the step.
AP-RCP.1 T RCP SEAL MALFUNCTION REV: 11 PAGE 10 of 10 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: Refer to 0-9.3, NRC IMMEDIATE NOTIFICATION, for reporting requirements.
o Total ¹1 Seal Flow is defined as the sum of indicated ¹1 Seal Leakoff Flow and RCDT leak rate (PPCS Point ID L1003, 3.2 gal/8 in the normal operating range).
9 Notify Higher Supervision-END-EOP: AP-RCP.1 TITLE: RCP SEAL MALFUNCTION REV: 11 PAGE 1 of 1 AP-RCP.1 APPENDIX LIST TITLE r 1)FIGURE RCP SEAL LEAKOFF 2)ATTACHMENT RCP DIAGNOSTICS PAGES EOP: AP-RCP.1 T!ZLE: RCP SEAL MALFUNCTION REV: 11 PAGE 1 of 1 FIGURE RGP SEAL LEAKOFF O'I SEAL LEAK RATE (GPM)6 LEAK RATE INCREMENTS 0.2 GPH NORMAL OPERATING RANGE DP INCREMENTS 50 PSI 250 500 750 1000 1250 1500 1750 2000 2250 2500 81 SEAL DP (RCS PRESS-VCT PRESS)PSI EOP: ,P-TURB.5'f ITLE: RAPID LOAD REDUCTION REV'PAGE 1 of 11 ROCHESTER GAS AND ELECTRIC CORPORATION GINNA STATION CONTROLLED COPY NUMBER TECHNICAL REVIEW RES 0 SIBLE MANAGER EFFECTIVE DATE CATEGORY 1.0 REVIEWED BY:
1 Check  Total    $ 1 Seal Leakaff          IF a ¹1 Seal Failure is verified by Flows  LESS THAN 8.0 GPM                a decrease in Labyr Seal Diff Pressure  OR  increasing Seal Inlet/Outlet  temps,  THEN perform the following:
0 EOP: 'P-TURB.5 RAPID LOAD REDUCTION REV: 1 PAGE 2 of 11 A.PURPOSE B.ENTRY CONDITIONS/SYMPTOMS 1.ENTRY CONDITIONS
: a. IF reactor  trip breakers closed, THEN  trip  the reactor.
-This procedure is entered from a.The SS has determined that a rapid load reduction is required.
: b. Trip the affected RCP(s).
EOP: P-TURB.5[ITl.E: RAPID LOAD REDUCTION REV: 1 PAGE 3 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED*************
: c. Allow 4 minutes for pump coast down, THEN close affected RCP(s) seal disch valve.
x*x*x*x**x*x x***************
                                                      ~ RCP A, AOV-270A
CAUTION o IF AT ANY TIME DURING THIS PROCEDURE, A REACTOR TRIP OR SI OCCURS, THEN E-O, REACTOR TRIP OR SAFETY INJECTION, SHALL BE PERFORMED.
                                                      ~ RCP B, AOV-270B
o IF MAIN FEEDWATER FLOW SHOULD DECREASE TO 25%OF FULL POWER VALUE (.825 E+6 LBM/HR)PRIOR TO THE AMSAC SYSTEM AUTOMATICALLY BLOCKING, THEN A TURBINE TRIP AND AUX FEED PUMPS START COULD RESULT.********x*******x x x x*x x x x x*x x**x*x****x**
: d. IF reactor  trip was  NOT required,  THEN go  to Step 4.
NOTE: o This procedure is intended for use when the required load reduction rate is)1%/min.o A maximum continuous load reduction rate of)5%/min would not normally be used unless otherwise directed by the Shift Supervisor.
 
*1 Initiate Load Reduction a.Verify ROD CONTROL BANK SELECTOR SWITCH is in AUTOMATIC a.IF Auto Rod Control is inoperable OR Manual Control is desired, THEN perform the following:
EOP:
1)Place ROD CONTROL BANK SELECTOR SWITCH to MANUAL.b.Reduce turbine load using Auto Turbine EH Control if desired 1)Select desired rate on thumbwheel 2)Insert Rods as necessary to match Tavg and Tref.b.IF Auto Control is inoperable OR Manual Control, is desired, THEN reduce turbine load in manual as desired.2)Reduce the setter to the desired load 3)Depress the GO button c.Verify Steam Dump operating in auto, as required c.Place Steam Dump in manual and operate as necessary.
REV    11 AP-RCP.1                         RCP SEAL MALFUNCTION PAGE 5    of 10 STEP      ACTION/EXPECTED RESPONSE          RESPONSE NOT OBTAINED 2 Check RCP Seal Return Valve Alignment:
EOP: P-TURB.5 TITLE: RAPID LOAD REDUCTION REV 1 PAGE 4 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED***********x x x x*x**x***x**x x x x x x x*x x*x*x x CAUTION EXTREME AND RAPID ROD MOTION TO MITIGATE TAVG SWINGS MAY RESULT IN LARGE POWER EXCURSIONS AND SHOULD BE AVOIDED.**************x x x x x****x*x x*x x x x x*x x x*x*x 2 Monitor RCS Tavg o Tavg-GREATER THAN 545'F o Tavg-LESS THAN 578'F Verify AUTO control rod motion as required.IF NOT, THEN place rod control bank selector switch to MANUAL and adjust control rods as necessary.
: a. RCP  seal return isolation valve, a. Perform the following:
IF Tavg is outside limits AND CANNOT be controlled, THEN trip the reactor and go to E-O, REACTOR TRIP OR SAFETY INJECTION.
MOV-313 - OPEN
NOTE: A thumb rule for initial boron addition is-2 gal/0 load reduction.
: 1) Ensure CI    reset.
3 Add Boric Acid As Necessary To: o Maintain or return a Flux to the target band o Maintain control rods above insertion limits o Match Tavg and Tref o Compensate for xenon EOP: P-TURB.5 TlTLE: RAPID LOAD REDUCTION REV: l PAGE 5 of ll STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: It is permissible to operate RCPs for limited periods without seal injection, provided CCW is being supplied to the thermal barriers.4 Check IA Available To CNMT o IA pressure->60 psig o Instr Air to CN>lT Isol Valve, AOV-5392-OPEN Control PRZR level and pressure and follows: I o Adjust load reduction rate o Ensure control rods are moving to control Tavg o Secure charging pumps if necessary o Operate proportional and backup heaters as required 5 Monitor Plant Parameters-CONTROLLING AT OR TRENDING TO PROGRAM VALUES~PRZR Pressure~PRZR Level~S/G Level IF any parameter is approaching a trip setpoint AND CANNOT be controlled, THEN trip the reactor and go to E-O, REACTOR TRIP OR SAFETY INJECTION.
: 2) Ensure both    trains of  XY relays for RCP seal return isolation valve, MOV-313, reset.
NOTE: The load reduction should not be delayed to perform the remaining steps.6 Check If Condensate Booster Pumps Should Be Secured a.Power<65%OR Trim Valve V-9508G indicates>80%open a.Go to Step 13.b.Place the auto condensate booster pump to the trip position c.Stop one condensate booster pump d.WHEN the condensate system stabilizes, THEN stop the remaining condensate booster pump EOP: 'P-TURB.5 I'I TLE: RAPID LOAD REDUCTION REV: 1 PAGE 6 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 7 Check If One MFW Pump Should Be Secured a.Power<50%a.Go to Step 13.b.Verify at least one MFWP Seal Booster pump in service b.Notify AO to start one MFWP Seal Booster pump c.Two MFW Pumps running c.Go to Step 8.d.Close discharge valve for the pump to be secured~MFW Pump A-MOV-3977~MFW Pump B-MOV-3976 e.Stop the desired MFW Pump f.Close the secured MFW pump recirc valve by placing the control switch in pull stop g.Close the service water block valve to the secured MFW pump oil cooler~MFW Pump A-V-4701~MFW Pump B-V-4702 8 Verify Trim Valves Controlling Condensate System Pressure in Auto (300-375 PSIG)Place controller in manual and adjust pressure as necessary EOP: P-TURB.5 T,I TLE: RAPID LOAD REDUCTION REV: 1 PAGE 7 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 9 Check ANSAC System Status a.Power<35%(-150 psig first stage pressure)b.Verify AMSAC Auto Block Status Light is ON a.Go to Step 13.b.Place AMSAC Manual Block switch to the BLOCK position 10 Check Heater Drain Tank Pump Status a.Generator load<175 MWe b.Stop one Heater Drain Tank Pump c.WHEN Heater Drain Tank level control is stable, THEN stop the second Heater Drain Tank Pump a.Go to Step 13.11 Check FW Flow Bypass Vlv Status a.Power<30%b.FW Flow Bypass Vlvs in AUTO~HCV-480~HCV-481 a.Go to Step 13.b.Perform the following:
: 3) Open  RCP  seal return isolation valve,    MOV-313.
1)Slowly open the FW Flow Bypass Vlvs while verifying the associated FW Reg Vlv compensates by closing slightly 2)Place FW Flow Bypass Vlvs in AUTO EOP: P-TURB.5 RAPID LOAD REDUCTION REV 1 PAGE 8 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 12 Align Systems For Low Power Operation a.Power<30%a.Go to Step 13.b.Place AOU-3959, CNDST Bypass Ulv to CLOSE c.Place LC-107, Hotwell Level Control, to MANUAL d.Generator load<100 MWe e.Open turbine drain valves d.Go to Step 13.13 Evaluate Plant Status a.Power stable at desired level a.IF power)20%and further reduction is required, THEN continue load reduction and return to Step 6.IF power<20%and further reduction is required, THEN refer to procedure 0-2.1, NORMAL SHUTDOWN TO HOT SHUTDOWN.
IF MOV-313 can NOT be opened, THEN dispatch  AO to AUX BLDG with  RWST  area key to check valve and breaker locally (breaker MCC C position 13J).
EOP: P-TURB.5 jITLE: RAPID LOAD REDUCTION REV: 1 PAGE 9 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 14 Establish Stable Plant Conditions:
: b. Verify  RCP seal disch valves      b. Manually open valves.        IF valves OPEN                                  can  NOT be opened,   THEN verify IA aligned to    CNMT  and go to
a.Tavg-TRENDING TO TREF a.Perform the following:
          ~ RCP  A, AOV-270A                    Step 3.
1)Verify AUTO control rod motion as, required.IF NOT, THEN place rod control bank selector switch to MANUAL and adjust control rods as necessary.
          ~ RCP B, AOV-270B
2)Borate if required for power reduction.
 
b.PRZR pressure-TRENDING TO 2235 PSIG b.Verify proper operation of PRZR heaters and spray OR take manual control of PRZR pressure controller 431K.IF PRZR pressure can NOT be controlled, THEN refer to AP-PRZR.1, ABNORMAL PRESSURIZER PRESSURE.c.PRZR level-TRENDING TO PROGRAM c.Verify proper operation of charging pump speed controllers OR take manual control of speed controllers to control PRZR level.d.Rod insertion limit alarms EXTINGUISHED d.Borate as necessary and withdraw control rods to clear insertion limit alarms (refer to affected rod bank alarm response procedures if necessary).
I 0
e.Narrow range S/G levels TRENDING TO PROGRAM LEVEL e.Ensure MFW regulating valves controlling in AUTO, OR control feedwater in MANUAL.
f
EOP: P-TURB.5 TITLE: RAPID LOAD REDUCTION REV'PAGE 10 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 15 Establish Normal Plant Conditions:
 
a.Verify EH control in OPER PAN and IMP IN b.Verify steam dump controller, HC-484, in AUTO at 1005 psig c.Verify annunciator G-15, STEAM DUMP ARMED-EXTINGUISHED a.IF conditions requiring manual operation have cleared, THEN place EH in OPER PAN and IMP IN.c.IF Tavg within 6'F of Tref, THEN perform the following:
EOP:          TITLE:
1)Ensure steam dump valves closed.d.Verify PRZR presssure control in AUTO 2)Reset steam dump.d.Place PRZR pressure control in AUTO as desired.~431K master controller
REV    11 AP-RCP. 1                       RCP SEAL MALFUNCTXON PAGE 6    of 10 STEP     ACTION/EXPECTED RESPONSE             RESPONSE NOT OBTAINED NOTE: o  If E-0 a reactor  trip is initiated while  performing Step 3, transition V
~PRZR spray valve controllers
to      should occur while completing subsequent actions of the step.
~PRZR heater controllers e.Verify PRZR level control in AUTO)e.Place one charging pump speed controller in AUTO if desired.f.Verify Rod Control Selector Switch in AUTO f.Place Rod Control Selector Switch in AUTO if desired.NOTE: Refer to 0-9.3, NRC IMMEDIATE NOTIFICATION, for reporting requirements.
o  The 0.8  GPM limit for &#xb9;1 seal flow applies when the    RCS  is at normal operating pressure. Refer to Figure  RCP SEAL LEAKOFF     and consult plant staff for guidance  if  the RCS  is at reduced pressure.
16 Notify Higher Supervision FOP: P-TURB.5%1TLE: RAPID LOAD REDUCTION REV 1 PAGE 11 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 17 Refer to 0-5.1, LOAD REDUCTIONS, for additional"guidance 18 Return To Procedure Or Guidance In Effect-END-
3 Check    Total gl Seal Flow              IF &#xb9;1 Seal    Inlet  and  Outlet BETWEEN  0.8  GPM AND  6.0 GPM        temperatures are increasing,      THEN perform the following:
''I~P EOIa: ATT-9.0 TITLE: ATTACHMENT LETDOWN REV: 5 PAGE 1 of 1 Superintendent
: a. IF reactor    trip breakers closed, THEN  trip  the reactor.
.Y~.I nate 7 A'i A)The following conditions must be met to place either normal or excess letdown in service: o IA to CNMT-ESTABLISHED Q CCW-IN SERVICE o PRZR level-GREATER THAN 13%B)Establish Normal Letdown: 1.Establish charging line flow to REGEN Hx-GREATER THAN 20 gpm.2.Place the following switches to CLOSE: o Letdown orifice valves (AOV-200A, AOV-200B, and AOV-202)o AOV-427, loop B cold leg to REGEN Hx 3.Place letdown controllers in MANUAL at 40%open: o Temperature control valve, TCV-130 o Pressure control valve, PCV-135 4.Verify AOV-371, letdown isolation valve-OPEN.5.Open loop B cold leg to REGEN Hx, AOV-427.6.Open one 40 gpm letdown orifice valve (AOV-200A or AOV-200B).
: b. Trip the affected RCP(s).
7.Place TCV-130 in AUTO at 105'F.8.Place PCV-135 in AUTO at 250 psig.9.Adjust charging pump speed and HCV-142 as necessary to stablizie PRZR level and maintain RCP labyrinth seal D/P.C)IF normal letdown can NOT be established, THEN establish excess letdown: 1.Place AOV-312 to NORMAL.2.Ensure CCW from excess letdown Hx, (AOV-745)-OPEN.3.Open excess letdown isolation valve AOV-310.4.Slowly open HCV-123 to maintain excess letdown temperature less than 195'F and pressure less than 100 psig.1 5.Adjust charging pump speed as necessary to stabilize PRZR level and maintain RCP labyrinth.seal D/P.
: c. Allow 4 minutes for pump coast down, THEN close affected RCP(s) seal disch valve.
Distribution Sheet Distri-.txt~Hi$PP>/~a~~Priority: Normal From: E-RIDS1 Action Recipients:
                                                    ~ RCP  A) AOV-270A
RidsNrrPMGVissing Copies: 0 OK Internal Recipients:
                                                    ~ RCP  B) AOV-270B IF &#xb9;1 Seal Inlet and Outlet temperatures are stable, THEN perform the following while continuing with this procedure.
RidsRgn1 MailCenter RidsNrrDipmEphp Rids Mana ger IRO DHa an Fl E CENTER Ol Dennis Hagan External Recipients:
o  IF total &#xb9;1 Seal Flow greater than 6.0 gpm, THEN maintain seal injection flow rate of 9.0 GPM or greater to the affected RCP.
0 1 1 0 0 0 OK OK OK Paper Copy Paper Copy OK Total Copies: Item: ADAMS Document Library: ML ADAMS" HQNTAD01 ID'03719331:1
o  IF total &#xb9;1 Seal flow exceeds 8.0 GPM OR Seal Inlet/Outlet temperatures begin to increase, THEN  return to Step 1.
o  Prepare for orderly pump shutdown by placing the plant in Hot Shutdown using 0-2.1, NORMAL SHUTDOWN TO HOT SHUTDOWN.
o  Secure the  affected  RCP with  8 hours.
 
EOP:
REV  11 AP-RCP. 1                      RCP SEAL MALFUNCTION PAGE 7  of 10 STEP    ACTION/EXPECTED RESPONSE            RESPONSE  NOT OBTAINED NOTE:  Attachment RCP DIAGNOSTICS may  be used  to aid in diagnosis.
4 Check RCP Cooling:                      Perform the following:
o Annunciator A-7,  RCP A CCW          a. Verify RCP  CCW supply and return RETURN HIGH TEMP OR LOW FLOW-            valves open.
EXTINGUISHED
                                                    ~  RCP A, MOV-749A and MOV-759A o Annunciator A-15,  RCP B CCW              ~ RCP  B, MOV-749B and MOV>>759B RETURN HIGH TEMP OR LOW FLOW-EXTINGUISHED                          b. En'sure open CCW outlet valves from RCP thermal barriers.
                                                    ~  RCP A, AOV-754A
                                                    ~ RCP  B, AOV-754B 5 Check RCP g2 Seal    Indications:      IF affected RCP &#xb9;1 seal leakoff flow decreasing, THEN failure of &#xb9;2 o Annunciator B-3,  RCP A STANDPIPE    seal may be indicated. Continue HI LEVEL +1 FT - EXTINGUISHED'        plant operation while closely monitoring RCP seal indications.
Annunciator B-4,  RCP B STANDPIPE HI LEVEL +1 FT - EXTINGUISHED
 
EOP.           TITLE:
REV: 11 AP-RCP.1                         RCP SEAL MALFUNCTION PAGE 8  of 10 STEP      ACTION/EXPECTED RESPONSE            RESPONSE    NOT OBTAINED CAUTION  REDUCING CHARGING FLOW'WILL RESULT  IN INCREASING    REGEN HX OUTLET TEMPERATURE.
6 Check RCP    Labyrinth Seal D/Ps        Perform the following:
      -  GREATER THAN 15 INCHES OF MATER                                    a. Ensure open CCW outlet valves from RCP thermal barriers.
                                                    ~ RCP A, AOV-754A
                                                    ~ RCP  B, AOV-754B
: b. Verify seal injection flow greater than 5 GPM for affected RCP.
: c. Adjust HCV-142 as necessary.
: d. Dispatch    AO to check seal injection  filter D/P.
: e. Check  CCW  surge tank level stable. IF level increasing, THEN go  to AP-CCW.l, LEAKAGE INTO THE COMPONENT COOLING LOOP.
7 Check RCP g3 Seal    Indications:      Check  CNMT  radiation monitors normal.
o  Annunciator B-ll, RCP A STAND PIPE LO LEVEL -4FT - EXTINGUISHED    ~  R-11
                                                ~  R-12 o  Annunciator B-12, RCP B STAND PIPE LO LEVEL -4FT - EXTINGUISHED    IF  RCP standpipe level low and CNMT radiation'increasing, THEN &#xb9; 3 seal leakage increase is probable.
Continue plant operation while closely monitoring RCP seal indications.
 
1'l F.OP:            LITLE:
REV  11 AP-RCP.1                          RCP SEAL MALFUNCTION PAGE 9  of 10 STEP      ACTION/EXPECTED RESPONSE            RESPONSE NOT OBTAINED NOTE:    In the absence of other seal failure indications, an elevated &#xb9;1 seal outlet temperature  may indicate pump bearing damage.
* 8 Monitor Plant Conditions:
: a. RCP  &#xb9;1 seal flow                      a. IF affected RCP running, THEN return to Step 1. IF NOT, THEN o   Total &#xb9;1 seal leakoff  flow-          perform the follow'ing:
LESS THAN  6.0 GPM
: 1) Monitor  affected  RCP (Refer o  Total &#xb9;1 seal flow  - GREATER              to Attachment  RCP THAN  0.8 GPM                            DIAGNOSTICS).
: 2) Consult Plant    Staff determine  if cooldownto required.
: b. RCP &#xb9;1  Seal Flow - WITHIN THE        b. Perform the following:
NORMAL    OPERATING RANGE OF FIGURE RCP SEAL LEAKOFF                    o Ensure seal injection flow exceeds &#xb9;1 seal leakoff flow.
o Refer to S-2.1, Reactor Coolant Pump Operation.
o Consult plant    staff for further instructions.
: c. RCP  &#xb9;1 seal outlet temperatures      c. IF pump bearing damage is LESS THAN  215'ND    STABLE            suspected, THEN notify plant staff and expedite shutdown of the affected RCP. IF NOT, THEN return tc Step 1.
: d. RCS  leakage - NORMAL (Refer to       d. Perform the following:
leakage surveillance sheet)
: 1) Calculate    RCS  leakrate.
: 2) Refer to ITS section 3.4e13.
 
T REV: 11 AP-RCP.1                    RCP SEAL MALFUNCTION PAGE 10 of 10 STEP    ACTION/EXPECTED RESPONSE          RESPONSE NOT OBTAINED NOTE: Refer to 0-9.3, NRC IMMEDIATE NOTIFICATION, for reporting requirements.
9 Notify Higher Supervision
                                      -END-
 
EOP:       TITLE:
REV: 11 AP-RCP.1                 RCP SEAL MALFUNCTION PAGE of 1 AP-RCP.1 APPENDIX LIST TITLE                        PAGES r
: 1)  FIGURE RCP SEAL LEAKOFF
: 2)  ATTACHMENT RCP DIAGNOSTICS
 
EOP:            T!ZLE:
REV: 11 AP-RCP. 1                        RCP SEAL MALFUNCTION PAGE 1    of  1 FIGURE RGP SEAL LEAKOFF O'I SEAL LEAK RATE (GPM) 6 LEAK RATE INCREMENTS 0.2  GPH NORMAL OPERATING RANGE DP INCREMENTS 50  PSI 250      500  750    1000    1250    1500    1750    2000    2250    2500 81 SEAL DP (RCS PRESS  - VCT PRESS)  PSI
 
EOP:          'f ITLE:
REV'
,P-TURB.5                    RAPID LOAD REDUCTION PAGE 1 of 11 ROCHESTER GAS AND ELECTRIC CORPORATION GINNA STATION CONTROLLED COPY NUMBER TECHNICAL REVIEW RES  0 SIBLE MANAGER EFFECTIVE DATE CATEGORY 1.0 REVIEWED BY:
 
0 EOP:
REV: 1
'P-TURB.5                  RAPID LOAD REDUCTION PAGE 2 of 11 A. PURPOSE B. ENTRY CONDITIONS/SYMPTOMS
: 1. ENTRY CONDITIONS  This  procedure  is entered from
: a. The SS has determined  that  a rapid load reduction is required.
 
EOP:              [ITl.E:
REV: 1 P-TURB.5                               RAPID LOAD REDUCTION PAGE of 11 STEP       ACTION/EXPECTED RESPONSE                   RESPONSE   NOT OBTAINED
  *************                    x  *
* x    x
* x **x*x x **************
CAUTION o  IF AT ANY TIME DURING THIS PROCEDURE, A REACTOR TRIP OR SI OCCURS, THEN E-O, REACTOR TRIP OR SAFETY INJECTION, SHALL BE PERFORMED.
o  IF  MAIN FEEDWATER FLOW SHOULD DECREASE TO 25% OF FULL POWER VALUE
(.825  E+6 LBM/HR) PRIOR TO THE AMSAC SYSTEM AUTOMATICALLYBLOCKING, THEN A TURBINE TRIP AND AUX FEED PUMPS START COULD RESULT.
  ********x              *******x            x  x x
* x x x x  x*x x **x*x****x**
NOTE:    o  This procedure is intended for use when the required load reduction rate is      ) 1%/min.
o  A maximum    continuous load reduction rate of ) 5%/min would not normally be used unless otherwise directed by the Shift Supervisor.
* 1 Initiate        Load Reduction
: a. Verify ROD CONTROL BANK SELECTOR            a. IF Auto Rod Control is SWITCH is in AUTOMATIC                          inoperable OR Manual Control  is desired, THEN perform the following:
: 1) Place   ROD CONTROL BANK SELECTOR SWITCH to MANUAL.
: 2)  Insert  Rods as necessary to match Tavg and  Tref.
: b. Reduce turbine load using Auto                b. IF Auto Control is inoperable OR Turbine EH Control      if  desired              Manual Control, is desired, THEN reduce turbine load in manual as
: 1) Select desired      rate  on                  desired.
thumbwheel
: 2) Reduce the    setter to the desired load
: 3) Depress    the  GO button
: c. Verify Steam Dump operating in                c. Place Steam Dump in manual and auto, as required                               operate as necessary.
 
EOP:           TITLE:
REV    1 P-TURB.5                           RAPID LOAD REDUCTION PAGE 4    of 11 STEP     ACTION/EXPECTED RESPONSE                 RESPONSE NOT OBTAINED
  ***********xx*x**x***x**x  x x CAUTION x x x x x x*x x*x*xx EXTREME AND RAPID ROD MOTION TO MITIGATE TAVG SWINGS MAY RESULT      IN LARGE POWER EXCURSIONS AND SHOULD BE AVOIDED.
  **************xx****x*xx*x        x x x                          x x x x*x x x*x*x 2  Monitor  RCS  Tavg                        Verify AUTO control rod motion    as required. IF NOT, THEN place rod o  Tavg - GREATER THAN 545'F                control bank selector switch to MANUAL and adjust control rods as o  Tavg - LESS THAN 578'F                    necessary.
IF Tavg is outside limits  AND CANNOT  be controlled, THEN trip the reactor and go to E-O, REACTOR TRIP OR SAFETY INJECTION.
NOTE:    A thumb  rule for  initial boron  addition is -2 gal/0 load reduction.
3 Add  Boric Acid    As Necessary To:
o  Maintain or return    a Flux to the target  band o  Maintain control rods above insertion limits o  Match Tavg and  Tref o  Compensate  for xenon
 
EOP:
P-TURB.5 TlTLE:
RAPID LOAD REDUCTION REV:    l PAGE 5   of ll STEP       ACTION/EXPECTED RESPONSE                 RESPONSE NOT OBTAINED NOTE:   It is  permissible to operate RCPs for limited periods without seal injection, provided      CCW is being supplied to the thermal barriers.
4 Check IA      Available      To CNMT            Control  PRZR level and pressure  and follows:
o  IA pressure    - > 60  psig             I o  Adjust load reduction rate o  Instr Air to    CN>lT Isol Valve, AOV-5392    - OPEN                        o  Ensure  control rods are moving to control Tavg o  Secure charging pumps  if necessary o  Operate proportional and backup heaters as required 5 Monitor Plant Parameters                        IF any parameter is approaching a CONTROLLING AT OR TRENDING TO                    trip setpoint AND CANNOT be PROGRAM VALUES                                  controlled, THEN trip the reactor and go to E-O, REACTOR TRIP OR
        ~ PRZR  Pressure                              SAFETY INJECTION.
        ~ PRZR Level
        ~ S/G Level NOTE:    The  load reduction should not be delayed to perform the remaining steps.
6 Check Pumps If  Condensate Booster Should Be Secured
: a. Power <    65%    OR Trim Valve              a. Go to Step 13.
V-9508G  indicates    >  80%  open
: b. Place the auto condensate booster pump to the trip position
: c. Stop one condensate        booster  pump
: d. WHEN  the condensate    system stabilizes,     THEN  stop the remaining condensate booster        pump
 
EOP:            I'ITLE:
REV: 1
'P-TURB.5                         RAPID LOAD REDUCTION PAGE of 11 STEP     ACTION/EXPECTED RESPONSE             RESPONSE NOT OBTAINED 7  Check Be If One Secured MFW Pump    Should
: a. Power <  50%                        a. Go to Step 13.
: b. Verify at least one MFWP Seal        b. Notify AO to  start one  MFWP Seal Booster pump in service                  Booster pump
: c. Two MFW Pumps    running              c. Go to Step 8.
: d. Close discharge valve    for the pump to be secured
          ~ MFW  Pump A - MOV-3977
          ~ MFW  Pump B - MOV-3976
: e. Stop the desired    MFW Pump
: f. Close the secured MFW pump recirc valve by placing the control switch in pull stop
: g. Close the service water block valve to the secured MFW pump oil cooler
          ~ MFW  Pump A -  V-4701
          ~ MFW  Pump B - V-4702 8 Verify Trim Valves                        Place  controller in  manual and Controlling Condensate          System    adjust pressure  as necessary Pressure in Auto (300-375 PSIG)
 
EOP:            T,I TLE:
REV: 1 P-TURB.5                          RAPID LOAD REDUCTION PAGE 7  of 11 STEP      ACTION/EXPECTED RESPONSE            RESPONSE  NOT OBTAINED 9  Check ANSAC System Status
: a. Power < 35% (-150 psig   first      a. Go to Step 13.
stage pressure)
: b. Verify AMSAC Auto Block Status        b. Place AMSAC Manual Block switch Light is      ON                        to the BLOCK position 10  Check Heater Drain Tank Pump Status
: a. Generator load < 175    MWe          a. Go to Step 13.
: b. Stop one Heater Drain Tank    Pump
: c. WHEN  Heater Drain Tank level control is stable,    THEN stop the second Heater Drain Tank Pump 11  Check    FW    Flow Bypass Vlv Status
: a. Power <    30%                      a. Go to Step 13.
: b. FW  Flow Bypass Vlvs  in AUTO        b. Perform the following:
          ~ HCV-480                                1) Slowly open the FW Flow
          ~ HCV-481                                    Bypass Vlvs while verifying the associated FW Reg Vlv compensates  by closing slightly
: 2) Place  FW Flow Bypass Vlvs in AUTO
 
EOP:
REV  1 P-TURB.5                        RAPID LOAD REDUCTION PAGE 8  of 11 STEP      ACTION/EXPECTED RESPONSE          RESPONSE  NOT OBTAINED 12  Align Systems For      Low Power Operation
: a. Power <  30%                        a. Go to Step 13.
: b. Place AOU-3959, CNDST  Bypass Ulv to CLOSE
: c. Place LC-107, Hotwell Level Control, to MANUAL
: d. Generator load < 100  MWe          d. Go to Step 13.
: e. Open turbine drain valves 13  Evaluate Plant Status
: a. Power stable at desired level      a. IF power  ) 20% and further reduction is required, THEN continue load reduction and return to Step 6.
IF power < 20% and further reduction is required, THEN refer to procedure 0-2.1, NORMAL SHUTDOWN TO HOT SHUTDOWN.
 
EOP:            jITLE:
REV: 1 P-TURB.5                          RAPID LOAD REDUCTION PAGE 9  of 11 STEP      ACTION/EXPECTED RESPONSE          RESPONSE  NOT OBTAINED 14  Establish Stable Plant Conditions:
: a. Tavg - TRENDING  TO TREF            a. Perform the following:
: 1) Verify AUTO control rod motion as, required. IF NOT, THEN place rod control bank selector switch to MANUAL and adjust control rods as necessary.
: 2) Borate  if required reduction.
for power
: b. PRZR  pressure  - TRENDING TO        b. Verify proper operation of PRZR 2235 PSIG                                heaters and spray OR take manual control of PRZR pressure controller  431K. IF  PRZR pressure can    NOT be controlled, THEN  refer  to  AP-PRZR.1, ABNORMAL PRESSURIZER PRESSURE.
: c. PRZR  level  - TRENDING TO PROGRAM  c. Verify proper operation of charging pump speed controllers OR take manual control of speed controllers to control PRZR level.
: d. Rod  insertion limit alarms          d. Borate as necessary and withdraw EXTINGUISHED                            control rods to clear insertion limit alarms (refer to affected rod bank alarm response procedures  if  necessary).
: e. Narrow range S/G levels              e. Ensure  MFW  regulating valves TRENDING TO PROGRAM LEVEL                controlling in AUTO,    OR control feedwater in MANUAL.
 
EOP:            TITLE:
REV' P-TURB.5                            RAPID LOAD REDUCTION PAGE 10  of 11 STEP      ACTION/EXPECTED RESPONSE                RESPONSE  NOT OBTAINED 15  Establish Normal Plant Conditions:
: a. Verify EH control in    OPER PAN        a. IF conditions requiring manual and IMP IN                                    operation have cleared, THEN place EH in OPER PAN and IMP IN.
: b. Verify steam  dump  controller, HC-484,  in  AUTO  at  1005 psig
: c. Verify annunciator G-15,    STEAM        c. IF Tavg within 6'F of Tref,      THEN DUMP ARMED - EXTINGUISHED                    perform the following:
: 1) Ensure steam dump valves closed.
: 2) Reset steam dump.
: d. Verify  PRZR  presssure  control in      d. Place    PRZR pressure  control in AUTO                                          AUTO as desired.
                                                        ~ 431K master  controller
                                                        ~  PRZR  spray valve controllers
                                                        ~ PRZR  heater controllers
: e. Verify  PRZR  level control in    AUTO)  e. Place one charging pump speed controller in  AUTO  if desired.
: f. Verify Rod  Control Selector            f. Place Rod Control Selector Switch in  AUTO                              Switch in AUTO    if  desired.
NOTE:    Refer to 0-9.3,    NRC IMMEDIATE  NOTIFICATION,  for reporting requirements.
16  Notify Higher Supervision
 
FOP:          %1TLE:
REV  1 P-TURB.5                      RAPID LOAD REDUCTION PAGE 11 of 11 STEP    ACTION/EXPECTED RESPONSE          RESPONSE NOT OBTAINED 17  Refer to 0-5.1,    LOAD REDUCTIONS,    for additional "guidance 18  Return To Procedure Or Guidance In    Effect
                                        -END-
 
  'I
~
P
 
I EOIa:            TITLE:
REV:  5 ATT-9.0                              ATTACHMENT LETDOWN PAGE 1  of 1 Superintendent              . Y~.                  nate  7  A 'i A)  The  following conditions must be met to place either normal or excess letdown in service:
o IA to CNMT  ESTABLISHED Q  CCW      IN SERVICE o  PRZR    level  GREATER THAN 13%
B)  Establish Normal Letdown:
: 1. Establish charging line flow to                  REGEN Hx  GREATER THAN 20 gpm.
: 2. Place the following switches to                CLOSE:
o    Letdown orifice valves (AOV-200A, AOV-200B, and AOV-202) o    AOV-427, loop B cold leg to REGEN Hx
: 3. Place letdown controllers in MANUAL at                  40% open:
o    Temperature control valve, TCV-130 o    Pressure control valve, PCV-135
: 4. Verify      AOV-371, letdown        isolation valve      OPEN.
: 5. Open    loop  B    cold leg to    REGEN  Hx, AOV-427.
: 6. Open one 40 gpm          letdown    orifice valve    (AOV-200A  or AOV-200B).
: 7. Place TCV-130 in          AUTO  at 105'F.
: 8. Place PCV-135 in          AUTO  at 250 psig.
: 9. Adjust charging          pump speed    and HCV-142 as necessary      to stablizie      PRZR    level  and  maintain    RCP  labyrinth seal  D/P.
C)  IF normal letdown can              NOT  be  established, THEN establish excess letdown:
: 1. Place AOV-312 to          NORMAL.
: 2. Ensure      CCW  from excess      letdown Hx, (AOV-745)      OPEN.
: 3. Open excess          letdown  isolation valve      AOV-310.
: 4. Slowly open HCV-123 to maintain excess letdown temperature less than 195'F and pressure less than 100 psig.
1
: 5. Adjust charging          pump speed    as necessary    to stabilize PRZR    level  and    maintain    RCP  labyrinth .seal D/P.
 
                                                                      ~Hi $ PP
                                                                          >/~a~~
Distri- .txt Distribution Sheet Priority: Normal From: E-RIDS1 Action Recipients:              Copies:
RidsNrrPMGVissing                    0    OK Internal Recipients:
RidsRgn1 MailCenter                    0    OK RidsNrrDipmEphp                      0      OK Rids Mana ger                    0      OK IRO DHa an                      1        Paper Copy Fl E CENTER Ol                  1      Paper Copy Dennis Hagan                      0      OK External Recipients:
Total Copies:
Item: ADAMS Document Library: ML ADAMS"HQNTAD01 ID'03719331:1


==Subject:==
==Subject:==
Revision 22 to Ginna Station Emergency Plan Implementing Procedure 5-2.Body: ADAMS DISTRIBUTION NOTIFICATION.
 
Electronic Recipients can RIGHT CLICK and OPEN fhe first Attachment to View the Document in ADAMS.The Document may also be viewed by searching for Accession Number ML003719331
Revision 22 to Ginna Station Emergency Plan Implementing Procedure 5-2.
~A045-OR Submittal:
Body:
Emergency Preparedness Plans, Implementing Procedures, Corre Page 1 spondence Distri>>2.txt Docket: 05000244 Page 2}}
ADAMS DISTRIBUTION NOTIFICATION.
Electronic Recipients can RIGHT CLICK and OPEN fhe first Attachment to View the Document in ADAMS. The Document may also be viewed by searching for Accession Number ML003719331         ~
A045 - OR Submittal: Emergency Preparedness       Plans, Implementing Procedures, Corre Page   1
 
Distri>>2.txt spondence Docket: 05000244 Page 2}}

Latest revision as of 10:19, 4 February 2020

Rev 11 to AP-RCP.1, RCP Seal Malfunction.
ML17264A977
Person / Time
Site: Ginna Constellation icon.png
Issue date: 08/05/1997
From:
ROCHESTER GAS & ELECTRIC CORP.
To:
Shared Package
ML17264A976 List:
References
AP-RCP.1, NUDOCS 9708130125
Download: ML17264A977 (32)


Text

EOP: TITLE:

REV 11 AP-RCP.1 RCP SEAL MALFUNCTION PAGE 1 of 10 ROCHESTER GAS AND ELECTRIC CORPORATION GINNA STATION CONTROLLED COPY NUMBER RESPONSIBLE AGER EFFECTIVE DATE CATEGORY 1.0 REVIEWED BY:

9708i30125 970805 PDR ADOCK 05000244 PDR

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REV 11 AP-RCP.1 RCP SEAL MALFUNCTION PAGE 2 of 10 A. PURPOSE This procedure provides the instructions necessary to diagnose and to respond to a reactor coolant pump seal malfunction.

B. ENTRY CONDITIONS/SYMPTOMS

1. ENTRY CONDITIONS This procedure is entered from:
a. E-3, STEAM GENERATOR TUBE RUPTURE, or
b. ES-l.l, SI TERMINATION, or
c. ES-1.2, POST LOCA COOLDOWN AND DEPRESSURIZATION, or
d. ECA-0.1, LOSS OF ALL AC POWER RECOVERY WITHOUT SI REQUIRED, or
e. ECA-2.1, UNCONTROLLED DEPRESSURIZATION OF BOTH STEAM GENERATORS, or
f. ECA-3.1, SGTR WITH LOSS OF REACTOR COOLANT-SUBCOOLED RECOVERY DESIRED, or
g. ECA-3.2, SGTR WITH LOSS OF REACTOR COOLANT-SATURATED RECOVERY DESIRED, .or
h. ECA-3.3, SGTR WITHOUT PRESSURIZER PRESSURE CONTROL, or
i. FR-I.1, RESPONSE TO HIGH PRESSURIZER LEVEL, when RCP seal malfunction is indicated.
2. SYMPTOMS - The symptoms of RCP SEAL MALFUNCTION are;
a. Annunciator B-17(18), RCP A(B) No.1 SEAL HI-LO FLOW 5.0 GPM 1.0 , lit, or
b. Annunciator B-9(10), RCP A(B) LABYR SEAL LO DIFF PRESS 15" H20, lit, or
c. Annunciator B-3(4), RCP A(B) STAND PIPE HI LEVEL + 1 FT, lit, or Continued on next page

REV: 11 AP-RCP. 1 RCP SEAL MALFUNCTION PAGE 3 of 10

2. SYMPTOMS (cont)
d. Annunciator B-ll(12), RCP A(B) STAND PIPE LO LEVEL -4 FT, lit, or
e. Annunciator B-25(26), RCP A(B) No. 1 SEAL LO DIFF PRESS 220 PSID, lit, or
f. Annunciator B-l(2), RCP A(B) No. 1 SEAL OUT HI TEMP 200'F, lit, or,
g. Annunciator A-7(15), RCP A(B) CCW RETURN HIGH TEMP OR FLOW, lit.

LOW

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REV 11 AP-RCP. 1 RCP SEAL MALFUNCTION PAGE 4 of 10 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED CAUTION o IF, AT ANY TIME DURING THIS PROCEDURE, A'EACTOR TRIP OR SI OCCURS, E-O, REACTOR TRIP OR SAFETY INJECTION, SHALL BE PERFORMED.

o IF ANY RCP IS TRIPPED, THEN SHUTDOWN MARGIN REQUIREMENTS SHOULD BE VERIFIED (REFER TO 0-3.1, BORON CONCENTRATION FOR XENON FREE ALL RODS IN MOST REACTIVE ROD STUCK OUT SHUTDOWN MARGIN).

o IF A RCP IS SECURED BECAUSE OF A SEAL MALFUNCTION, IT SHOULD NOT BE RESTARTED UNTIL THE CAUSE OF THE MALFUNCTION HAS BEEN DETERMINED AND CORRECTED.

NOTE; o If a Reactor trip is iTIitiated while performing Step 1, transition to E-0 should occur while completing subsequent actions of the step.

o Total ¹1 Seal Flow is defined as the sum of indicated ¹1 Seal Leakoff Flow and RCDT leak rate (PPCS Point ID L1003, 3.2 gal/8 in the normal operating range).

1 Check Total $ 1 Seal Leakaff IF a ¹1 Seal Failure is verified by Flows LESS THAN 8.0 GPM a decrease in Labyr Seal Diff Pressure OR increasing Seal Inlet/Outlet temps, THEN perform the following:

a. IF reactor trip breakers closed, THEN trip the reactor.
b. Trip the affected RCP(s).
c. Allow 4 minutes for pump coast down, THEN close affected RCP(s) seal disch valve.

~ RCP A, AOV-270A

~ RCP B, AOV-270B

d. IF reactor trip was NOT required, THEN go to Step 4.

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REV 11 AP-RCP.1 RCP SEAL MALFUNCTION PAGE 5 of 10 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 2 Check RCP Seal Return Valve Alignment:

a. RCP seal return isolation valve, a. Perform the following:

MOV-313 - OPEN

1) Ensure CI reset.
2) Ensure both trains of XY relays for RCP seal return isolation valve, MOV-313, reset.
3) Open RCP seal return isolation valve, MOV-313.

IF MOV-313 can NOT be opened, THEN dispatch AO to AUX BLDG with RWST area key to check valve and breaker locally (breaker MCC C position 13J).

b. Verify RCP seal disch valves b. Manually open valves. IF valves OPEN can NOT be opened, THEN verify IA aligned to CNMT and go to

~ RCP A, AOV-270A Step 3.

~ RCP B, AOV-270B

I 0

f

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REV 11 AP-RCP. 1 RCP SEAL MALFUNCTXON PAGE 6 of 10 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: o If E-0 a reactor trip is initiated while performing Step 3, transition V

to should occur while completing subsequent actions of the step.

o The 0.8 GPM limit for ¹1 seal flow applies when the RCS is at normal operating pressure. Refer to Figure RCP SEAL LEAKOFF and consult plant staff for guidance if the RCS is at reduced pressure.

3 Check Total gl Seal Flow IF ¹1 Seal Inlet and Outlet BETWEEN 0.8 GPM AND 6.0 GPM temperatures are increasing, THEN perform the following:

a. IF reactor trip breakers closed, THEN trip the reactor.
b. Trip the affected RCP(s).
c. Allow 4 minutes for pump coast down, THEN close affected RCP(s) seal disch valve.

~ RCP A) AOV-270A

~ RCP B) AOV-270B IF ¹1 Seal Inlet and Outlet temperatures are stable, THEN perform the following while continuing with this procedure.

o IF total ¹1 Seal Flow greater than 6.0 gpm, THEN maintain seal injection flow rate of 9.0 GPM or greater to the affected RCP.

o IF total ¹1 Seal flow exceeds 8.0 GPM OR Seal Inlet/Outlet temperatures begin to increase, THEN return to Step 1.

o Prepare for orderly pump shutdown by placing the plant in Hot Shutdown using 0-2.1, NORMAL SHUTDOWN TO HOT SHUTDOWN.

o Secure the affected RCP with 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.

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REV 11 AP-RCP. 1 RCP SEAL MALFUNCTION PAGE 7 of 10 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: Attachment RCP DIAGNOSTICS may be used to aid in diagnosis.

4 Check RCP Cooling: Perform the following:

o Annunciator A-7, RCP A CCW a. Verify RCP CCW supply and return RETURN HIGH TEMP OR LOW FLOW- valves open.

EXTINGUISHED

~ RCP A, MOV-749A and MOV-759A o Annunciator A-15, RCP B CCW ~ RCP B, MOV-749B and MOV>>759B RETURN HIGH TEMP OR LOW FLOW-EXTINGUISHED b. En'sure open CCW outlet valves from RCP thermal barriers.

~ RCP A, AOV-754A

~ RCP B, AOV-754B 5 Check RCP g2 Seal Indications: IF affected RCP ¹1 seal leakoff flow decreasing, THEN failure of ¹2 o Annunciator B-3, RCP A STANDPIPE seal may be indicated. Continue HI LEVEL +1 FT - EXTINGUISHED' plant operation while closely monitoring RCP seal indications.

Annunciator B-4, RCP B STANDPIPE HI LEVEL +1 FT - EXTINGUISHED

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REV: 11 AP-RCP.1 RCP SEAL MALFUNCTION PAGE 8 of 10 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED CAUTION REDUCING CHARGING FLOW'WILL RESULT IN INCREASING REGEN HX OUTLET TEMPERATURE.

6 Check RCP Labyrinth Seal D/Ps Perform the following:

- GREATER THAN 15 INCHES OF MATER a. Ensure open CCW outlet valves from RCP thermal barriers.

~ RCP A, AOV-754A

~ RCP B, AOV-754B

b. Verify seal injection flow greater than 5 GPM for affected RCP.
c. Adjust HCV-142 as necessary.
d. Dispatch AO to check seal injection filter D/P.
e. Check CCW surge tank level stable. IF level increasing, THEN go to AP-CCW.l, LEAKAGE INTO THE COMPONENT COOLING LOOP.

7 Check RCP g3 Seal Indications: Check CNMT radiation monitors normal.

o Annunciator B-ll, RCP A STAND PIPE LO LEVEL -4FT - EXTINGUISHED ~ R-11

~ R-12 o Annunciator B-12, RCP B STAND PIPE LO LEVEL -4FT - EXTINGUISHED IF RCP standpipe level low and CNMT radiation'increasing, THEN ¹ 3 seal leakage increase is probable.

Continue plant operation while closely monitoring RCP seal indications.

1'l F.OP: LITLE:

REV 11 AP-RCP.1 RCP SEAL MALFUNCTION PAGE 9 of 10 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: In the absence of other seal failure indications, an elevated ¹1 seal outlet temperature may indicate pump bearing damage.

  • 8 Monitor Plant Conditions:
a. RCP ¹1 seal flow a. IF affected RCP running, THEN return to Step 1. IF NOT, THEN o Total ¹1 seal leakoff flow- perform the follow'ing:

LESS THAN 6.0 GPM

1) Monitor affected RCP (Refer o Total ¹1 seal flow - GREATER to Attachment RCP THAN 0.8 GPM DIAGNOSTICS).
2) Consult Plant Staff determine if cooldownto required.
b. RCP ¹1 Seal Flow - WITHIN THE b. Perform the following:

NORMAL OPERATING RANGE OF FIGURE RCP SEAL LEAKOFF o Ensure seal injection flow exceeds ¹1 seal leakoff flow.

o Refer to S-2.1, Reactor Coolant Pump Operation.

o Consult plant staff for further instructions.

c. RCP ¹1 seal outlet temperatures c. IF pump bearing damage is LESS THAN 215'ND STABLE suspected, THEN notify plant staff and expedite shutdown of the affected RCP. IF NOT, THEN return tc Step 1.
d. RCS leakage - NORMAL (Refer to d. Perform the following:

leakage surveillance sheet)

1) Calculate RCS leakrate.
2) Refer to ITS section 3.4e13.

T REV: 11 AP-RCP.1 RCP SEAL MALFUNCTION PAGE 10 of 10 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: Refer to 0-9.3, NRC IMMEDIATE NOTIFICATION, for reporting requirements.

9 Notify Higher Supervision

-END-

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REV: 11 AP-RCP.1 RCP SEAL MALFUNCTION PAGE 1 of 1 AP-RCP.1 APPENDIX LIST TITLE PAGES r

1) FIGURE RCP SEAL LEAKOFF
2) ATTACHMENT RCP DIAGNOSTICS

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REV: 11 AP-RCP. 1 RCP SEAL MALFUNCTION PAGE 1 of 1 FIGURE RGP SEAL LEAKOFF O'I SEAL LEAK RATE (GPM) 6 LEAK RATE INCREMENTS 0.2 GPH NORMAL OPERATING RANGE DP INCREMENTS 50 PSI 250 500 750 1000 1250 1500 1750 2000 2250 2500 81 SEAL DP (RCS PRESS - VCT PRESS) PSI

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REV'

,P-TURB.5 RAPID LOAD REDUCTION PAGE 1 of 11 ROCHESTER GAS AND ELECTRIC CORPORATION GINNA STATION CONTROLLED COPY NUMBER TECHNICAL REVIEW RES 0 SIBLE MANAGER EFFECTIVE DATE CATEGORY 1.0 REVIEWED BY:

0 EOP:

REV: 1

'P-TURB.5 RAPID LOAD REDUCTION PAGE 2 of 11 A. PURPOSE B. ENTRY CONDITIONS/SYMPTOMS

1. ENTRY CONDITIONS This procedure is entered from
a. The SS has determined that a rapid load reduction is required.

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REV: 1 P-TURB.5 RAPID LOAD REDUCTION PAGE 3 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED

                          • x *
  • x x
  • x **x*x x **************

CAUTION o IF AT ANY TIME DURING THIS PROCEDURE, A REACTOR TRIP OR SI OCCURS, THEN E-O, REACTOR TRIP OR SAFETY INJECTION, SHALL BE PERFORMED.

o IF MAIN FEEDWATER FLOW SHOULD DECREASE TO 25% OF FULL POWER VALUE

(.825 E+6 LBM/HR) PRIOR TO THE AMSAC SYSTEM AUTOMATICALLYBLOCKING, THEN A TURBINE TRIP AND AUX FEED PUMPS START COULD RESULT.

                • x *******x x x x
  • x x x x x*x x **x*x****x**

NOTE: o This procedure is intended for use when the required load reduction rate is ) 1%/min.

o A maximum continuous load reduction rate of ) 5%/min would not normally be used unless otherwise directed by the Shift Supervisor.

  • 1 Initiate Load Reduction
a. Verify ROD CONTROL BANK SELECTOR a. IF Auto Rod Control is SWITCH is in AUTOMATIC inoperable OR Manual Control is desired, THEN perform the following:
1) Place ROD CONTROL BANK SELECTOR SWITCH to MANUAL.
2) Insert Rods as necessary to match Tavg and Tref.
b. Reduce turbine load using Auto b. IF Auto Control is inoperable OR Turbine EH Control if desired Manual Control, is desired, THEN reduce turbine load in manual as
1) Select desired rate on desired.

thumbwheel

2) Reduce the setter to the desired load
3) Depress the GO button
c. Verify Steam Dump operating in c. Place Steam Dump in manual and auto, as required operate as necessary.

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REV 1 P-TURB.5 RAPID LOAD REDUCTION PAGE 4 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED

                      • xx*x**x***x**x x x CAUTION x x x x x x*x x*x*xx EXTREME AND RAPID ROD MOTION TO MITIGATE TAVG SWINGS MAY RESULT IN LARGE POWER EXCURSIONS AND SHOULD BE AVOIDED.
                            • xx****x*xx*x x x x x x x x*x x x*x*x 2 Monitor RCS Tavg Verify AUTO control rod motion as required. IF NOT, THEN place rod o Tavg - GREATER THAN 545'F control bank selector switch to MANUAL and adjust control rods as o Tavg - LESS THAN 578'F necessary.

IF Tavg is outside limits AND CANNOT be controlled, THEN trip the reactor and go to E-O, REACTOR TRIP OR SAFETY INJECTION.

NOTE: A thumb rule for initial boron addition is -2 gal/0 load reduction.

3 Add Boric Acid As Necessary To:

o Maintain or return a Flux to the target band o Maintain control rods above insertion limits o Match Tavg and Tref o Compensate for xenon

EOP:

P-TURB.5 TlTLE:

RAPID LOAD REDUCTION REV: l PAGE 5 of ll STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: It is permissible to operate RCPs for limited periods without seal injection, provided CCW is being supplied to the thermal barriers.

4 Check IA Available To CNMT Control PRZR level and pressure and follows:

o IA pressure - > 60 psig I o Adjust load reduction rate o Instr Air to CN>lT Isol Valve, AOV-5392 - OPEN o Ensure control rods are moving to control Tavg o Secure charging pumps if necessary o Operate proportional and backup heaters as required 5 Monitor Plant Parameters IF any parameter is approaching a CONTROLLING AT OR TRENDING TO trip setpoint AND CANNOT be PROGRAM VALUES controlled, THEN trip the reactor and go to E-O, REACTOR TRIP OR

~ PRZR Pressure SAFETY INJECTION.

~ PRZR Level

~ S/G Level NOTE: The load reduction should not be delayed to perform the remaining steps.

6 Check Pumps If Condensate Booster Should Be Secured

a. Power < 65% OR Trim Valve a. Go to Step 13.

V-9508G indicates > 80% open

b. Place the auto condensate booster pump to the trip position
c. Stop one condensate booster pump
d. WHEN the condensate system stabilizes, THEN stop the remaining condensate booster pump

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REV: 1

'P-TURB.5 RAPID LOAD REDUCTION PAGE 6 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 7 Check Be If One Secured MFW Pump Should

a. Power < 50% a. Go to Step 13.
b. Verify at least one MFWP Seal b. Notify AO to start one MFWP Seal Booster pump in service Booster pump
c. Two MFW Pumps running c. Go to Step 8.
d. Close discharge valve for the pump to be secured

~ MFW Pump A - MOV-3977

~ MFW Pump B - MOV-3976

e. Stop the desired MFW Pump
f. Close the secured MFW pump recirc valve by placing the control switch in pull stop
g. Close the service water block valve to the secured MFW pump oil cooler

~ MFW Pump A - V-4701

~ MFW Pump B - V-4702 8 Verify Trim Valves Place controller in manual and Controlling Condensate System adjust pressure as necessary Pressure in Auto (300-375 PSIG)

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REV: 1 P-TURB.5 RAPID LOAD REDUCTION PAGE 7 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 9 Check ANSAC System Status

a. Power < 35% (-150 psig first a. Go to Step 13.

stage pressure)

b. Verify AMSAC Auto Block Status b. Place AMSAC Manual Block switch Light is ON to the BLOCK position 10 Check Heater Drain Tank Pump Status
a. Generator load < 175 MWe a. Go to Step 13.
b. Stop one Heater Drain Tank Pump
c. WHEN Heater Drain Tank level control is stable, THEN stop the second Heater Drain Tank Pump 11 Check FW Flow Bypass Vlv Status
a. Power < 30% a. Go to Step 13.
b. FW Flow Bypass Vlvs in AUTO b. Perform the following:

~ HCV-480 1) Slowly open the FW Flow

~ HCV-481 Bypass Vlvs while verifying the associated FW Reg Vlv compensates by closing slightly

2) Place FW Flow Bypass Vlvs in AUTO

EOP:

REV 1 P-TURB.5 RAPID LOAD REDUCTION PAGE 8 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 12 Align Systems For Low Power Operation

a. Power < 30% a. Go to Step 13.
b. Place AOU-3959, CNDST Bypass Ulv to CLOSE
c. Place LC-107, Hotwell Level Control, to MANUAL
d. Generator load < 100 MWe d. Go to Step 13.
e. Open turbine drain valves 13 Evaluate Plant Status
a. Power stable at desired level a. IF power ) 20% and further reduction is required, THEN continue load reduction and return to Step 6.

IF power < 20% and further reduction is required, THEN refer to procedure 0-2.1, NORMAL SHUTDOWN TO HOT SHUTDOWN.

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REV: 1 P-TURB.5 RAPID LOAD REDUCTION PAGE 9 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 14 Establish Stable Plant Conditions:

a. Tavg - TRENDING TO TREF a. Perform the following:
1) Verify AUTO control rod motion as, required. IF NOT, THEN place rod control bank selector switch to MANUAL and adjust control rods as necessary.
2) Borate if required reduction.

for power

b. PRZR pressure - TRENDING TO b. Verify proper operation of PRZR 2235 PSIG heaters and spray OR take manual control of PRZR pressure controller 431K. IF PRZR pressure can NOT be controlled, THEN refer to AP-PRZR.1, ABNORMAL PRESSURIZER PRESSURE.
c. PRZR level - TRENDING TO PROGRAM c. Verify proper operation of charging pump speed controllers OR take manual control of speed controllers to control PRZR level.
d. Rod insertion limit alarms d. Borate as necessary and withdraw EXTINGUISHED control rods to clear insertion limit alarms (refer to affected rod bank alarm response procedures if necessary).
e. Narrow range S/G levels e. Ensure MFW regulating valves TRENDING TO PROGRAM LEVEL controlling in AUTO, OR control feedwater in MANUAL.

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REV' P-TURB.5 RAPID LOAD REDUCTION PAGE 10 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 15 Establish Normal Plant Conditions:

a. Verify EH control in OPER PAN a. IF conditions requiring manual and IMP IN operation have cleared, THEN place EH in OPER PAN and IMP IN.
b. Verify steam dump controller, HC-484, in AUTO at 1005 psig
c. Verify annunciator G-15, STEAM c. IF Tavg within 6'F of Tref, THEN DUMP ARMED - EXTINGUISHED perform the following:
1) Ensure steam dump valves closed.
2) Reset steam dump.
d. Verify PRZR presssure control in d. Place PRZR pressure control in AUTO AUTO as desired.

~ 431K master controller

~ PRZR spray valve controllers

~ PRZR heater controllers

e. Verify PRZR level control in AUTO) e. Place one charging pump speed controller in AUTO if desired.
f. Verify Rod Control Selector f. Place Rod Control Selector Switch in AUTO Switch in AUTO if desired.

NOTE: Refer to 0-9.3, NRC IMMEDIATE NOTIFICATION, for reporting requirements.

16 Notify Higher Supervision

FOP: %1TLE:

REV 1 P-TURB.5 RAPID LOAD REDUCTION PAGE 11 of 11 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 17 Refer to 0-5.1, LOAD REDUCTIONS, for additional "guidance 18 Return To Procedure Or Guidance In Effect

-END-

'I

~

P

I EOIa: TITLE:

REV: 5 ATT-9.0 ATTACHMENT LETDOWN PAGE 1 of 1 Superintendent . Y~. nate 7 A 'i A) The following conditions must be met to place either normal or excess letdown in service:

o IA to CNMT ESTABLISHED Q CCW IN SERVICE o PRZR level GREATER THAN 13%

B) Establish Normal Letdown:

1. Establish charging line flow to REGEN Hx GREATER THAN 20 gpm.
2. Place the following switches to CLOSE:

o Letdown orifice valves (AOV-200A, AOV-200B, and AOV-202) o AOV-427, loop B cold leg to REGEN Hx

3. Place letdown controllers in MANUAL at 40% open:

o Temperature control valve, TCV-130 o Pressure control valve, PCV-135

4. Verify AOV-371, letdown isolation valve OPEN.
5. Open loop B cold leg to REGEN Hx, AOV-427.
6. Open one 40 gpm letdown orifice valve (AOV-200A or AOV-200B).
7. Place TCV-130 in AUTO at 105'F.
8. Place PCV-135 in AUTO at 250 psig.
9. Adjust charging pump speed and HCV-142 as necessary to stablizie PRZR level and maintain RCP labyrinth seal D/P.

C) IF normal letdown can NOT be established, THEN establish excess letdown:

1. Place AOV-312 to NORMAL.
2. Ensure CCW from excess letdown Hx, (AOV-745) OPEN.
3. Open excess letdown isolation valve AOV-310.
4. Slowly open HCV-123 to maintain excess letdown temperature less than 195'F and pressure less than 100 psig.

1

5. Adjust charging pump speed as necessary to stabilize PRZR level and maintain RCP labyrinth .seal D/P.

~Hi $ PP

>/~a~~

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Subject:

Revision 22 to Ginna Station Emergency Plan Implementing Procedure 5-2.

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