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| {{#Wiki_filter:ACCELERATED UTION DEMONSATION SYSTEM'EGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:8912270188 DOC.DATE: 89/12/16 NOTARIZED: | | {{#Wiki_filter:ACCELERATED UTION DEMONSATION SYSTEM INFORMATION DISTRIBUTION SYSTEM (RIDS) |
| NO DOCKET 45 FACIL:STN-50-.528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH.NAME AUTHOR AFFILIATION | | 'EGULATORY ACCESSION NBR:8912270188 DOC.DATE: 89/12/16 NOTARIZED: NO DOCKET 45 FACIL:STN-50-.528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH. NAME AUTHOR AFFILIATION |
| 'EVINE,J.M. | | 'EVINE,J.M. Arizona Public Service Co. (formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk) |
| Arizona Public Service Co.(formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)SUBJECT': Special Rept 1-SR-89-005,Suppl 1:on 890505-08,radiation monitoring unit inoperable for greater than 72 h.DISTRIBUTION CODE: IE22D COPIES RECEIVED LTR+ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), incident Rpt, etc.NOTES: 05000528 RECIPIENT ID CODE/NAME PD5 LA CHAN,T COPIES RECIPIENT LTTR ENCL ID CODE/NAME 1 1-PD5 PD 1 1 DAVIS,M.COPIES LTTR ENCL 1 1 1 1 INTERNAL: ACRS MICHELSON ACRS WYLIE'EOD/DSP/TPAB DEDRO NRR/DET/EMEB9H3 NRR/DLPQ/LHFB11 NRR/DOEA/OEAB11 NRR/DST/SELB 8D NRR/DST/S PLB8 D1 NUDOCS-ABSTRACT RES/DSIR/EIB EXTERNAL: EG&G WILLIAMS,S LPDR NSIC MAYS,G NUDOCS FULL TXT NOTES 1 1 1 1.1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 4 4 1 1 1 1 1 1 1 1 ACRS MOELLER AEOD/DOA AEOD/ROAB/DSP NRR/DET/ECMB 9H NRR/DET/ESGB 8D NRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICB 7E GN5 FILE 01 L ST LOBBY WARD NRC PDR NSIC MURPHY,G.A 2 2 1 1 2'1 1-1.1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 NOTE TO ALL"RIDS" RECIPIENIS: | | SUBJECT': Special Rept 1-SR-89-005,Suppl 1:on 890505-08,radiation monitoring unit inoperable for greater than 72 h. |
| PLEASE HEL'P US TO REDUCE WASTE!CONTACf THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISIS FOR DOCUMENTS YOU DON'T NEEDl TOTAL NUMBER OF COPIES REQUIRED: LTTR 40 ENCL 40 J | | DISTRIBUTION CODE: IE22D COPIES RECEIVED LTR TITLE: 50.73/50.9 Licensee Event Report (LER), |
| JAMES M.LEVINE VICE PRESIDENT NUCLEAR PRODUCilDN Arizona Public Service Company PALO VERDE NUCLEAR GENERATING STATION P,O, BOX 52034~PHOENIX, ARIZONA 85072-2034 192-00606-JHL/TOS/SBJ December 16, 1989 U.S.Nuclear Regulatory Commission NRC Document C'ontrol Desk Washington, D.C.20555
| | +incident ENCL SIZE: |
| | Rpt, etc. |
| | NOTES: 05000528 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 1 - PD5 PD 1 1 CHAN,T 1 1 DAVIS,M. 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS 1 1 AEOD/DOA 1 1 WYLIE'EOD/DSP/TPAB |
| | .1 1 AEOD/ROAB/DSP 2 ' |
| | DEDRO 1 1 NRR/DET/ECMB 9H 1 1-NRR/DET/EMEB9H3 1 1 NRR/DET/ESGB 8D 1. 1 NRR/DLPQ/LHFB11 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB11 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1 NRR/DST/SICB 7E 1 1 NRR/DST/S PLB8 D1 1 1 1 1 NUDOCS-ABSTRACT 1 1 1 1 RES/DSIR/EIB 1 1 GN5 FILE 01 1 1 EXTERNAL: EG&G WILLIAMS,S 4 4 L ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 NUDOCS FULL TXT 1 1 NOTES 1 1 NOTE TO ALL "RIDS" RECIPIENIS: |
| | PLEASE HEL'P US TO REDUCE WASTE! CONTACf THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISIS FOR DOCUMENTS YOU DON'T NEEDl TOTAL NUMBER OF COPIES REQUIRED: LTTR 40 ENCL 40 |
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| ==Dear Sirs:== | | J Arizona Public Service Company PALO VERDE NUCLEAR GENERATING STATION P,O, BOX 52034 ~ PHOENIX, ARIZONA85072-2034 192-00606-JHL/TOS/SBJ JAMES M. LEVINE December 16, 1989 VICE PRESIDENT NUCLEAR PRODUCilDN U. S. Nuclear Regulatory Commission NRC Document C'ontrol Desk Washington, D.C. 20555 |
| | |
| | ==Dear Sirs:== |
|
| |
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| ==Subject:== | | ==Subject:== |
| Palo Verde Nuclear Generating Station (PVNGS)Unit 1 Docket No.STN 50-528 (License No.NPF-41)Supplement to Special Report 1-SR-89-005 File: 89-020-404 Attached please find Supplement Number 1 to Special Report 1-SR-89-005 prepared and submitted pursuant to Technical Specification 3.3.3.8 ACTION 42.This report'iscusses the, inoperability of a high range radiation effluent monitor., If you have any questions, please contact T.D.Shriver, Compliance Hanager, at (602)393-2521.Very truly yours, JHL/TDS/SBJ/kj Attachment cc: W..F.Conway J.B.Hartin T.J.Polich'.J.Davis A.C.Gehr (all w/a)8912270l88 85'1226 PDR ADOCK 05000528 PDC Il PALO VERDE NUCLEAR GENERATING STATION UNIT 1 Radiation Monitoring Unit Inoperable Greater'han 72 Hours License No.NPF-41 Docket No.50-528 Supplement to Special Report No.1-SR-89-005 DESCRIPTION OF WHAT OCCURRED:.A.Initial Conditions: | | Palo Verde Nuclear Generating Station (PVNGS) |
| During this event between Hay 5, 1989 and Hay 8, 1989, Unit 1 was.in Mode 5 (COLD SHUTDOWN). | | Unit 1 Docket No. STN 50-528 (License No. NPF-41) |
| B.Reportable Event Description (Including Dates and Approximate Times of Major Occurrences): | | Supplement to Special Report 1-SR-89-005 File: 89-020-404 Attached please find Supplement Number 1 to Special Report 1-SR-89-005 prepared and submitted pursuant to Technical Specification 3.3.3.8 ACTION 42. |
| Event Classification: | | This report'iscusses the, inoperability of a high range radiation effluent monitor., |
| Submitted in accordance with ACTION 42.b of Technical Specification 3.3.3.8.V At approximately 1805 HST on Hay 8, 1989, Plant Ventilation Radiation Effluent Honitor.(RU-144)was discovered with two of three particulate filter/iodine cartridge assemblies not tightly sealed, thereby, rendering the monitor inoperable. | | If you have any questions, please contact T. D. Shriver, Compliance Hanager, at (602) 393-2521. |
| Investigation determined that the assemblies had not been adequately restored during troubleshooting conducted May 6, 1989.RU-144 has three (3)channels, each with a particulate filter/iodine cartridge assembly.Each assembly consists of a particulate filter and iodine cartridge contained in a removeable cannister assembly.Each cannister assembly is installed in a fixed holder in the monitor.Sample flow is directed through one cannister assembly at a time.As radioactive particulates and iodine are collected in the filters, the radiation levels will.increase.At a predetermined radiation-level,'he sample flow is automatically redirected to the next standby filter/cartridge assembly.Prior to this event, on Hay 5, 1989 at approximately 0815 HST, the Low Range and High Range Plant Ventilation Radiation Effluent Monitors (RU-143 and RU-144 respectively) were declared inoperable for performance of Surveillance Test (ST)36ST-9S(04,"Radiation Monitoring quarterly Functional Test." This ST provides direction for functional verification of radiation monitor performance. | | Very truly yours, JHL/TDS/SBJ/kj Attachment cc: W.. F. Conway (all w/a) |
| During the source check portion of the ST on RU-144, one of the three detectors monitoring the filter/cartridge assemblies did not properly respond.The Instrumentation and Control (ISC)Technician (utility, non-licensed) performing the ST notified the Shift Supervisor and | | J. B. Hartin T. J. Polich J. Davis A. C. Gehr 8912270l88 85'1226 PDR ADOCK 05000528 PDC |
| | |
| | Il PALO VERDE NUCLEAR GENERATING STATION UNIT 1 Radiation Monitoring Unit Inoperable Greater'han 72 Hours License No. NPF-41 Docket No. 50-528 Supplement to Special Report No. 1-SR-89-005 DESCRIPTION OF WHAT OCCURRED: . |
| | A. Initial Conditions: |
| | During this event between Hay 5, 1989 and Hay 8, 1989, Unit 1 was . |
| | in Mode 5 (COLD SHUTDOWN). |
| | B. Reportable Event Description (Including Dates and Approximate Times of Major Occurrences): |
| | Event Classification: Submitted in accordance with ACTION 42.b of Technical Specification 3.3.3.8. |
| | V At approximately 1805 HST on Hay 8, 1989, Plant Ventilation Radiation Effluent Honitor .(RU-144) was discovered with two of three particulate filter/iodine cartridge assemblies not tightly sealed, thereby, rendering the monitor inoperable. Investigation determined that the assemblies had not been adequately restored during troubleshooting conducted May 6, 1989. |
| | RU-144 has three (3) channels, each with a particulate filter/iodine cartridge assembly. Each assembly consists of a particulate filter and iodine cartridge contained in a removeable cannister assembly. Each cannister assembly is installed in a fixed holder in the monitor. Sample flow is directed through one cannister assembly at a time. As radioactive particulates and iodine are collected in the filters, the radiation levels will . |
| | increase. At a predetermined radiation -level,'he sample flow is automatically redirected to the next standby filter/cartridge assembly. |
| | Prior to this event, on Hay 5, 1989 at approximately 0815 HST, the Low Range and High Range Plant Ventilation Radiation Effluent Monitors (RU-143 and RU-144 respectively) were declared inoperable for performance of Surveillance Test (ST) 36ST-9S(04, "Radiation Monitoring quarterly Functional Test." This ST provides direction for functional verification of radiation monitor performance. |
| | During the source check portion of the ST on RU-144, one of the three detectors monitoring the filter/cartridge assemblies did not properly respond. |
| | The Instrumentation and Control (ISC) Technician (utility, non-licensed) performing the ST notified the Shift Supervisor and |
| | |
| | Supplement to Special Report 1-SR-89-005 Page 2 appropriate troubleshooting work instructions were prepared. |
| | Troubleshooting commenced at approximately 0715 HST on Hay 6, 1989. Part of the troubleshooting required access to two of the particulate filter/iodine cartridge assemblies. The troubleshooting identified a deteriorated cable connection and the troubleshooting work document was amended to include instructions for reworking the connector. Upon completion of the work, the ISC Technician reinstalled the assembly into the holder. However, the holder was not properly locked down to prevent bypass flow. |
| | Following completion of the work, a Chemistry Technician (utility, non-licensed) performed a visual check of RU-144 but did not identify that the assembly holders were not properly locked down. |
| | The Chemistry Technician then performed Surveillance Test 75ST-9ZZ07, "Effluent Monitoring System .Daily Surveillance Testing" on RU-143 and verified the setpoints in accordance with 36ST-9S(04, "Radiation Monitor quarterly Functional Test" to declare the monitor operable. At approximately 1040 HST on Hay 7, 1989, RU-143 and RU-144 were declared operable. |
| | During a routine tour at approximately 1805 MST on Hay 8, 1989, a Chemistry Effluent Technician (utility, non-licensed) found two of the three particulate filter/iodine cartridge assembly holders not properly locked down. The Assistant Shift Supervisor (utility, licensed) was notified and RU-144 was declared inoperable. |
| | Technical Specification 3.3.3.8 requires RU-144 be operable at all times. ACTION 42 requires that when the monitor is inoperable greater than 72 hours, the following actions be taken: |
| | : a. Initiate the Preplanned Alternate Sampling Program to monitor the appropriate parameter(s) when it is needed. |
| | : b. Prepare and submit a Special Report to the Commission pursuant to Technical Specification 6.9.2 within 30 days..." |
| | These action requirements were met. The following action was taken to restore RU-144 to an operable status: |
| | : a. The assemblies were locked down. |
| | A filter check and leak rate test were performed in accordance with an approved procedure. |
| | c ~ The Effluent Monitor Daily =Surveillance Test, "75ST-9ZZ07," |
| | was performed satisfactorily. |
| | At approximately 2300 HST on Hay 8, 1989, RU-144 was declared OPERABLE. The total time of inoperability for RU-144 was approximately 81 hours and 50 minutes. |
| | |
| | f Supplement to Special Report I-SR-89-005 Page 3 C. Status of structures, systems, or components that were inoperable at the start of the event that contributed to .the event: |
| | 'ot applicable - no structures, systems, or components were inoperable which contributed to the event. |
| | D. Cause of each component or system failure, if known: |
| | Not applicable - no'omponent or system failures were involved. |
| | I E. Failure mode, mechanism, and effect of each failed component', if. |
| | known: |
| | Not applicable - no component failures were involved. |
| | F. For failures of components with multiple functions, list of systems or secondary functions that were also affected: |
| | Not applicable - no component failures were involved. |
| | G. For failures that rendered a train of a safety system inoperable, estimated time elapsed from the discovery of the failure until .the train was 'returned to service: |
| | Not applicable - no failures were involved. |
| | H. Hethod of discovery of each component or system failure or procedural error: |
| | Not applicable - there were no component or system failures or |
| | .procedural errors. |
| | I. Cause of Event: |
| | The cause of this event was a personnel error by the Chemistry Technician who did not adequately verify the configuration of the particulate filter/iodine cartridge filter assembly after work had been performed on the'onitor. An investigation of this event revealed the following were contributing factors to the event. |
| | : 1) Incomplete communications between the 18C Technician and the Chemistry Technician as to the .scope of the RU-144 work, especially'in regard to the sample holder.. |
| | : 2) The Work Order did not include a section requiring the Chemistry Technician to inspect the particulate filter/iodine cartridge filter holder and sample chamber for operability. |
| | : 3) The Chemistry Technician had not been qualified adequately in the high range monitors as evidenced by being unable to identify the proper position of the sample holder lock down mechanism. |
| | |
| | CI I |
| | |
| | Supplement to Special Report- 1-SR-89-005 Page 4 |
| | : 4) The Chemistry procedure for media change out in RU-142,- 144 and 146 did not verify,.the 'correct position of the sample chamber or require independent verification. |
| | J. Safety System Response: |
| | Not applicable - no safety system response was expected and none were received. |
| | K. Failed Component Information: |
| | Not applicable - no failed component was involved in this event. |
| | II. ASSESSMENT OF THE SAFETY CONSEQUENCES. AND IMPLICATIONS OF THIS EVENT: |
| | The radioactive gaseous effluent instrumentation is provided to monitor and control, as applicable, the releases of radioactive materials in gaseous effluents during actual or potential releases of gaseous effluents. The alarm/trip setpoints for these instruments are calculated and adjusted in accordance with the methodology and parameters in the Off-Site Dose=Calculation'anual (ODCM) to ensure that the alarm/trip will occur prior to exceeding the limits of 10 CFR Part 20. |
| | There are two separate radioactive gaseous effluent monitoring systems: |
| | the low range. effluent monitors for normal plant radioactive gaseous effluents and the high range effluent monitors for post-accident plant radioactive gaseous effluents. The low range monitors operate at all times until the concentration of radioactivity in the effluent becomes too high during post-accident conditions. The high range monitors only operate, when the concentration or radioactivity in the effluent is above the setpoint of the low range monitors. |
| | Throughout this event the Plant Ventilation Exhaust was monitored with the Low Range Monitor (RU-143) .or an alternate sample cart. Release activities did not approach a level requiring the high range monitor (RU-144). Thus, there is no impact on the health and safety of the public. |
| | I I I. CORRECTIVE ACTIONS: |
| | A. Immediate: |
| | Chemistry positioned the locking mechanism to obtain a seal on the particulate filter/iodine cartridge assembly. The Radiation Monitor was leak rate'ested in accordance with an approved procedure. Chemistry then performed the daily channel check Surveillance Test, "75ST-9ZZ07." |
| | l |
| | : 2. The responsible individual has received appropriate counseling/disciplinary action. |
| | |
| | I Supplement to Special Report 1-SR-89-005 Page 5 |
| | : 3. As an interim measure, all work order packages for high range effluent monitors have a signoff for Chemistry to perform a leak check on the sample chamber per 75RP-9ZZ64. This will be performed any time the chamber has been disturbed. |
| | 75RP-9ZZ64, "RMS Sample Collection", has been revised to include a section addressing verification of correct position of the sample chamber and operability of the monitors after work has been performed on the high range monitor. |
| | e 5, A qualification card has been implemented for the High Range Monitors and will be completed by Chemistry Effluent Technicians. Completion of this qualification card will ensure understanding of the de'vices utilized for securing the filters and actions to be taken when the devices are removed or missing. |
| | B. Action to Prevent Recurrence: |
| | : 1. Radiation Monitoring Calibration Tests, 36ST-9SQ09, 36ST-9SQ10 and 36ST-9SQll will be rev'ised to provide direction for Chemistry to perform a leak check per the leak check procedure. This will be completed by December 31, 1989. |
| | : 2. As a permanent corrective action, Chemistry Standards and Plant Standards will identify the appropriate retests for monitor operability and incorporate them into the retest procedure. This will be completed by December 31, 1989. |
| | I V. SIMILAR EVENTS A similar event was reported under LER 529/88.-17. As a result of this event, a complete revision to the Radiological Effluent Program procedures was initiated. Completion dates for this program upgrade were provided in a letter to the commission on March 27, 1989. The corrective action which could have prevented this event were in progress and therefore could not have prevented this event. |
|
| |
|
| Supplement to Special Report 1-SR-89-005 Page 2 appropriate troubleshooting work instructions were prepared.Troubleshooting commenced at approximately 0715 HST on Hay 6, 1989.Part of the troubleshooting required access to two of the particulate filter/iodine cartridge assemblies.
| |
| The troubleshooting identified a deteriorated cable connection and the troubleshooting work document was amended to include instructions for reworking the connector.
| |
| Upon completion of the work, the ISC Technician reinstalled the assembly into the holder.However, the holder was not properly locked down to prevent bypass flow.Following completion of the work, a Chemistry Technician (utility, non-licensed) performed a visual check of RU-144 but did not identify that the assembly holders were not properly locked down.The Chemistry Technician then performed Surveillance Test 75ST-9ZZ07,"Effluent Monitoring System.Daily Surveillance Testing" on RU-143 and verified the setpoints in accordance with 36ST-9S(04,"Radiation Monitor quarterly Functional Test" to declare the monitor operable.At approximately 1040 HST on Hay 7, 1989, RU-143 and RU-144 were declared operable.During a routine tour at approximately 1805 MST on Hay 8, 1989, a Chemistry Effluent Technician (utility, non-licensed) found two of the three particulate filter/iodine cartridge assembly holders not properly locked down.The Assistant Shift Supervisor (utility, licensed)was notified and RU-144 was declared inoperable.
| |
| Technical Specification 3.3.3.8 requires RU-144 be operable at all times.ACTION 42 requires that when the monitor is inoperable greater than 72 hours, the following actions be taken: a.Initiate the Preplanned Alternate Sampling Program to monitor the appropriate parameter(s) when it is needed.b.Prepare and submit a Special Report to the Commission pursuant to Technical Specification 6.9.2 within 30 days..." These action requirements were met.The following action was taken to restore RU-144 to an operable status: a.The assemblies were locked down.c~A filter check and leak rate test were performed in accordance with an approved procedure.
| |
| The Effluent Monitor Daily=Surveillance Test,"75ST-9ZZ07," was performed satisfactorily.
| |
| At approximately 2300 HST on Hay 8, 1989, RU-144 was declared OPERABLE.The total time of inoperability for RU-144 was approximately 81 hours and 50 minutes.-
| |
| f Supplement to Special Report I-SR-89-005 Page 3 C.Status of structures, systems, or components that were inoperable at the start of the event that contributed to.the event: 'ot applicable
| |
| -no structures, systems, or components were inoperable which contributed to the event.D.Cause of each component or system failure, if known: Not applicable
| |
| -no'omponent or system failures were involved.I E.Failure mode, mechanism, and effect of each failed component', if.known: Not applicable
| |
| -no component failures were involved.F.For failures of components with multiple functions, list of systems or secondary functions that were also affected: Not applicable
| |
| -no component failures were involved.G.For failures that rendered a train of a safety system inoperable, estimated time elapsed from the discovery of the failure until.the train was'returned to service: Not applicable
| |
| -no failures were involved.H.Hethod of discovery of each component or system failure or procedural error: Not applicable
| |
| -there were no component or system failures or.procedural errors.I.Cause of Event: The cause of this event was a personnel error by the Chemistry Technician who did not adequately verify the configuration of the particulate filter/iodine cartridge filter assembly after work had been performed on the'onitor.
| |
| An investigation of this event revealed the following were contributing factors to the event.1)Incomplete communications between the 18C Technician and the Chemistry Technician as to the.scope of the RU-144 work, especially'in regard to the sample holder..2)The Work Order did not include a section requiring the Chemistry Technician to inspect the particulate filter/iodine cartridge filter holder and sample chamber for operability.
| |
| 3)The Chemistry Technician had not been qualified adequately in the high range monitors as evidenced by being unable to identify the proper position of the sample holder lock down mechanism.
| |
| CI I Supplement to Special Report-1-SR-89-005 Page 4 4)The Chemistry procedure for media change out in RU-142,-144 and 146 did not verify,.the
| |
| 'correct position of the sample chamber or require independent verification.
| |
| J.Safety System Response: Not applicable
| |
| -no safety system response was expected and none were received.K.Failed Component Information:
| |
| Not applicable
| |
| -no failed component was involved in this event.II.ASSESSMENT OF THE SAFETY CONSEQUENCES.
| |
| AND IMPLICATIONS OF THIS EVENT: The radioactive gaseous effluent instrumentation is provided to monitor and control, as applicable, the releases of radioactive materials in gaseous effluents during actual or potential releases of gaseous effluents.
| |
| -The alarm/trip setpoints for these instruments are calculated and adjusted in accordance with the methodology and parameters in the Off-Site Dose=Calculation'anual (ODCM)to ensure that the alarm/trip will occur prior to exceeding the limits of 10 CFR Part 20.There are two separate radioactive gaseous effluent monitoring systems: the low range.effluent monitors for normal plant radioactive gaseous effluents and the high range effluent monitors for post-accident plant radioactive gaseous effluents.
| |
| The low range monitors operate at all times until the concentration of radioactivity in the effluent becomes too high during post-accident conditions.
| |
| The high range monitors only operate, when the concentration or radioactivity in the effluent is above the setpoint of the low range monitors.Throughout this event the Plant Ventilation Exhaust was monitored with the Low Range Monitor (RU-143).or an alternate sample cart.Release activities did not approach a level requiring the high range monitor (RU-144).Thus, there is no impact on the health and safety of the public.I I I.CORRECTIVE ACTIONS: A.Immediate:
| |
| 2.Chemistry positioned the locking mechanism to obtain a seal on the particulate filter/iodine cartridge assembly.The Radiation Monitor was leak rate'ested in accordance with an approved procedure.
| |
| Chemistry then performed the daily channel check Surveillance Test,"75ST-9ZZ07." l The responsible individual has received appropriate counseling/disciplinary action.
| |
| I Supplement to Special Report 1-SR-89-005 Page 5 3.e 5, As an interim measure, all work order packages for high range effluent monitors have a signoff for Chemistry to perform a leak check on the sample chamber per 75RP-9ZZ64.
| |
| This will be performed any time the chamber has been disturbed.
| |
| 75RP-9ZZ64,"RMS Sample Collection", has been revised to include a section addressing verification of correct position of the sample chamber and operability of the monitors after work has been performed on the high range monitor.A qualification card has been implemented for the High Range Monitors and will be completed by Chemistry Effluent Technicians.
| |
| Completion of this qualification card will ensure understanding of the de'vices utilized for securing the filters and actions to be taken when the devices are removed or missing.B.Action to Prevent Recurrence:
| |
| 1.Radiation Monitoring Calibration Tests, 36ST-9SQ09, 36ST-9SQ10 and 36ST-9SQll will be rev'ised to provide direction for Chemistry to perform a leak check per the leak check procedure.
| |
| This will be completed by December 31, 1989.2.As a permanent corrective action, Chemistry Standards and Plant Standards will identify the appropriate retests for monitor operability and incorporate them into the retest procedure.
| |
| This will be completed by December 31, 1989.I V.SIMILAR EVENTS A similar event was reported under LER 529/88.-17.
| |
| As a result of this event, a complete revision to the Radiological Effluent Program procedures was initiated.
| |
| Completion dates for this program upgrade were provided in a letter to the commission on March 27, 1989.The corrective action which could have prevented this event were in progress and therefore could not have prevented this event.
| |
| I}} | | I}} |
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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A1271997-11-26026 November 1997 Special Rept 2-SR-97-002:on 971103,loose-part Detection Sys Channel 2 Declared Inoperable.Caused by Malfunction of Coaxial Cable Connector to accelerometer.Loose-part Detection Sys Channel Will Be Reworked ML17312A6871996-04-0505 April 1996 Rev 1 to Special Rept 2-SR-96-001,on 960404,alert Declared Due to Fire in Voltage Regulator for CR & Remote Shutdown Panel Essential Lighting,Clarifying Status of Power to UPS 2EQDNN02.Further Investigations Into Event Being Performed ML17312A6611996-04-0404 April 1996 Special Rept 2-SR-96-001:on 960404,fault Occurred in Voltage Regulator for CR & Remote Shutdown Panel Essential Lighting, Resulting in Fire in 100 Ft Elevation of Cb B Battery Equipment Room & Requiring Declaration of Alert,Per EPIP-04 ML17312A5771996-03-0101 March 1996 Special Rept 1-SR-96-01 on:960225,unit 1 Turbine Tripped Followed by Reactor Power Cutback.Caused by Lightning Strike.Unit 1 Will Not Be Connected to Grid Until Repairs Can Be Made to C Neutral Bushing of Transformer ML17311A8971995-05-25025 May 1995 Special Rept:On 950416,loose-part Detection Sys Channel 1 Declared Inoperable.Caused by Malfunction of Coaxial Cable Connector to Transducer.Channel Will Be Reworked & Returned to Svc During First Available Outage of Sufficient Duration ML17310B3621994-06-0909 June 1994 Special Rept 1-SR-94-001:on 940511,plant Ventilation Sys High Range Effluent Monitors in Units 1 & 2 Inoperable for Periods Greater than 72 H.Caused by High Voltage Failure Alarm.Design Change Package Installed ML17310B3071994-05-20020 May 1994 Special Rept 2-SR-94-002:on 940518,NOUE Declared Due to Fire Which Burned in Excess of 10 Minutes within Protected Area. Fire Extinguished W/Portable Fire Extinguisher.Investigation Initiated to Determine Cause of Fire & Develop C/As ML17310A9951994-01-13013 January 1994 Suppl 2 to Special Rept 3-SR-92-006:on 921217,PASS Declared Inoperable for Greater than Seven Days Following Failure to Meet Pressurized Sample Portion of Acceptance Criteria for Monthly Functional Sr.Pass Declared Operable on 921226 ML17310A9941994-01-13013 January 1994 Suppl 2 to Special Rept 2-SR-92-004:on 921222,PASS Declared Inoperable for Greater than Seven Days Due to Failure of Containment Air Flow Indicator & Indication of Water Leakage at PASS RCS Sample Septum.Pass Declared Operable on 930105 ML17310A8951994-01-0303 January 1994 Special rept:1-SR-93-008:on 940103,fuel Bldg Ventilation Sys High Range Radiation Monitor Inoperable for Period Greater than 72 Hours.Caused by Difficulties in Installing Mod 1-FJ-SQ-060 ML17310A8701993-12-25025 December 1993 Special Rept 1-SR-93-006:on 931224,30 Day Period for Returning loose-part Detection Sys (Lpds) to Operable Status Exceeded.Inoperable Lpds Channel Scheduled to Be Reworked & Returned to Svc During Next Outage of Sufficient Duration ML17310A8671993-12-15015 December 1993 Special Rept 1-SR-93-007:on 931215,30 Day Period for Returning Accelerometer to Operable Condition Exceeded. Accelerometer Will Be Replaced During Next Outage of Sufficient Duration ML17310A7581993-10-30030 October 1993 Special Rept 1-SR-93-004:on 931008,high Range RM RU-146 Made Inoperable for Period of Greater than 72 H as Result of Scheduled Electrical Bus Outage.Maint on Associated Bus Completed on 931015 & RU-146 Returned to Service ML17310A7001993-10-0909 October 1993 Special Rept 2-SR-93-003:on 931002,thirty Day Period for Returning loose-part Detection Sys Channel 8 to Operable Status Exceeded.Subj Channel Scheduled to Be Reworked & Returned to Svc During Next Outage ML17310A6301993-09-13013 September 1993 Special Rept 3-SR-93-003:on 930806,loose-part Detection Sys (Lpds) Declared Inoperable & Exceeded 30 Day Period for Being Returned to Svc on 930905.LPDS Channel 5 Scheduled to Be Reworked & Returned to Svc During Next Outage ML17310A5401993-08-11011 August 1993 Special Rept 1-SR-93-003:on 930806,NOUE Declared When Unit 1 CR Received Verification That Meteorological Instrumentation Unavailable Due to Loss of Power to Meteorological Tower. Caused by Severe Weather.Instrumentation Repaired ML17310A4961993-08-0202 August 1993 Special Rept 2-SR-93-002:on 930722,Unit 2 in Mode 5,Cold Shutdown During Refueling Outage When ISI of Both SGs Completed.Insp Resulted in Plugging of 74 Tubes in SG 1 & 175 Tubes in SG 2 ML17310A4401993-07-12012 July 1993 Special Rept 1-SR-93-002:on 930526,period for Returning Min Number of Explosive Gas Monitoring Channels to Operable Condition Exceeded.After All Four Cells Rebuilt,Calibr Completed on 930602 & Subj Analyzer Returned to Svc ML17306B4231993-04-24024 April 1993 Suppl 1 to Special Repts 2-SR-92-004 & 3-SR-92-006:on 921222 Unit 2 PASS Declared Inoperable Due to Failure of Containment Air Flow Indicator.On 921217,Unit 3 PASS Declared Inoperable.Equipment Replaced & Sample Obtained ML17306B3371993-03-15015 March 1993 Special Rept 2-SR-93-001:on 930314,control Room Personnel Manually Tripped Reactor Due to Rapid Decrease in Pressurizer Heaters.Personnel Commenced Controlled Plant Cooldown.Unit Remains Shut Down for Further Investigation ML17306B2901993-02-22022 February 1993 Special Rept 1-SR-92-005,suppl 1,provided Per Emergency Plan Implementing Procedure EPIP-03, Notification of Unusual Event Implementing Actions, Occurring on 920822 Re Loss of Power at Meteorological Tower ML17306B2781993-02-0909 February 1993 Special Rept 3-SR-93-001:on 930204,reactor Trip Occurred & Main Feedwater Pump a Experienced Rapidly Decreasing Pump Speed.Valid Actuation of SI Actuation Sys & Containment Isolation Actuation Sys Also Occurred.Evaluation Underway ML17306B2721993-01-27027 January 1993 Special Rept 3-SR-004-03:on 920817,PASS Inoperable for More than 7 Days.On 920902,discovered That PASS Unable to Draw Vacuum on Gaseous Sample Bomb.Vent Line Reworked & Procedure Revised ML17306B2551993-01-24024 January 1993 Special Rept 2-SR-92-004:on 921222,PASS Declared Inoperable for Period Greater than 7 Days Due to Failure of Containment Air Flow Indicator & Indication of Water Leakage at PASS Rcs.Pass Returned to Operable Status on 930105 ML17306B2561993-01-24024 January 1993 Special Rept 1-SR-92-007:on 921227,CB Atmosphere RM Inoperable for Period Greater than 72 H Due to High Flow Conditions.Temporary Mod Installed on Subj RM to Remove Monitor from Dedicated Rms Grounding Sys ML17306B2541993-01-22022 January 1993 Special Rept 3-SR-92-006:on 921217,PASS Declared Inoperable Following Failure to Meet Pressurized Sample Portion of Acceptance Criteria for Monthly Functional Sr.Pass Returned to Operable Status Following Satisfactory Repairs & Testing ML17306B1911992-12-21021 December 1992 Special Rept 3-SR-92-004-01:on 920201 PASS Declared Inoperable for Period Greater than Seven Days.Caused by Tubing Being Rerouted.Pass Reworked & Operability Restored on 920905 ML17306B1841992-12-14014 December 1992 Special Rept:On 920810,PASS Declared Inoperable Due to Tubing Being Rerouted.Chemistry Sys Status Procedure 74DP-9ZZ04 Revised to Direct Chemistry Personnel to Ensure That Functional Test Is performed.W/921214 Ltr ML17306B1291992-11-17017 November 1992 Special Rept 2-SR-92-003:on 921113,reactor Trip Occurred While Motor Generator Set a Out of Svc for Scheduled Maint & Set B Inadvertently Deenergized,Resulting in Loss of Power. State & Local Agencies Notified & Sys Reset ML17306B0931992-10-30030 October 1992 Suppl 1 to Special Rept 3-SR-92-004:on 920817,seven-day Period for Returning PASS to Service exceeded.30DP-9WP04 Revised to Retest for PASS & Gaseous Radwaste to Be Completed by 921120 ML17306A9951992-09-18018 September 1992 Special Rept 3-SR-92-004:seven-day Period for Returning PASS to Svc Exceeded on 920817.On 920902,discovered That PASS Unable to Draw Vacuum on Gaseous Sample Bomb.Possibly Caused by Maint on 920810.PASS Reworked & Operability Restored ML17306A9651992-09-16016 September 1992 Special Rept 3-SR-92-003:on 920903,discovered That PASS Unable to Draw Vacuum on Gaseous Sample Bomb & Declared Inoperable for More than 7 Days.Cause Under Investigation. Sys Returned to Operable Status on 920905 ML17306A9401992-08-28028 August 1992 Special Rept 1-SR-92-005:on 920822,discovered That Info Could Not Be Dispatched from Meterological Tower During Routine Surveillance of Daily Midnight Logs.Tower Declared Operable on 920823 Following Power Restoration ML17306A8101992-06-27027 June 1992 Special Rept 1-SR-92-004:on 920620,loose Part Detection Sys Inoperable for More than 30 Days.Caused by Hardware Problems Associated W/Installation of Loose Part Detection Sys Mods.New Computer Processor Board Installed ML17306A7971992-06-18018 June 1992 Special Rept 3-SR-92-003:on 920520,RMs RU-145 & 146 Declared Inoperable & Removed from Svc.Caused by Personnel Errors in Documenting Clearance for Retest of RU-146.Shift Supervisor Disciplined & Technician Verified That Pumps Were Energized ML17306A7961992-06-18018 June 1992 Special Rept 1-SR-92-003:on 920514,unit 1 Entered Mode 3 & PASS Declare Inoperable & Failed Surveillance Test.Caused by Leaking Relief Valve & Malfunctioning Pressure Transducer. Relief Valve & Pressure Transducer Replaced ML17306A7101992-05-0606 May 1992 Special Rept:On 920504,Control Room Received Alarms on All Seven Control Boards.Plan Computer Returned to Svc & Was Declared operable.W/920506 Ltr ML17306A6811992-04-18018 April 1992 Special Rept SR-92-002:on 920411,insp of SGs Resulted in Plugging of 23 Tubes in SG 1 & 18 Tubes in SG 2.Complete Results of SG Tube ISI Will Be Submitted by 930411 ML17306A4521992-02-0707 February 1992 Special Rept:On 920101,PASS Declared Inoperable When Chemistry Personnel Could Not Obtain a Containment Air Sample.Caused by Malfunctioning Flow Sensor.Pass Expected to Be Returned to an Operable status.W/920207 Ltr ML17306A3901992-01-0707 January 1992 Special Rept 1-SR-92-001:on 920102,determined That Leak Existed in Pressurizer Steam Space Instrument Nozzle Mfg from Inconnel 600.Caused by Nonvisible Intergranular Crack.Addl Investigation Underway ML17306A2981991-12-0505 December 1991 Special Rept 2-SR-91-002:on 911107,fuel Bldg Ventilation Sys high-range Radioactive Gaseous Effluent Monitor Inoperable for More than 72 H.Caused by Power Supply Deenergized for Scheduled Maint.Monitor Returned to Svc on 911114 ML17306A2791991-11-20020 November 1991 Special Rept 3-SR-91-007:on 911115,mobile Crane Came in Contact W/Energized 13.8 Kv Power Line Resulting in Arcing of Crane Outrigger Pads to Ground & Burning of Asphalt Area in Contact W/Pads.Investigation Re Event Being Performed ML17306A2221991-10-10010 October 1991 Special Rept 1-SR-91-001-01:on 910111,fuel Bldg Ventilation Sys High Range Radioactive Gaseous Effluent Monitor Declared Inoperable for Period Greater than 72 H in Order to Perform Scheduled 18-month Surveillance Testing & Maint ML17306A2211991-10-10010 October 1991 Special Rept 2-SR-89-007-03:on 891002,fuel Bldg Ventilation Sys High Range Gaseous Effluent Monitor Declared Inoperable for More than 72 H.Caused by Low Flow Limit Switch Being Out of Adjustment.Microprocessor Operated Manual Mode ML17306A2201991-10-10010 October 1991 Special Rept 2-SR-90-005-01:on 900716,plant Vent Sys High Range Effluent Monitor Inoperable for More than 72 H.Caused by Requirement to Perform Scheduled 18-month Surveillance Testing.Monitor Returned to Svc on 900729 ML17306A2181991-10-10010 October 1991 Special Rept 2-SR-90-004-01:on 910613,fuel Bldg Ventilation Sys high-range Radioactive Gaseous Effluent Monitor Inoperable for More than 72 H.Caused by Need to Perform 18 Month Surveillance Testing.Monitor Returned to Svc ML17305B7441991-09-18018 September 1991 Special Rept 1-SR-91-002,on 910914:steam Generator Econimizer Valve SGN-FV-1112 Fully Opened Causing Level in Steam Generator 1 to Rapidly Increase.Caused by Malfunction of Lower Gripper High Voltage on Slipped Part Length CEA 1999-06-21
[Table view] Category:LER)
MONTHYEARML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A1271997-11-26026 November 1997 Special Rept 2-SR-97-002:on 971103,loose-part Detection Sys Channel 2 Declared Inoperable.Caused by Malfunction of Coaxial Cable Connector to accelerometer.Loose-part Detection Sys Channel Will Be Reworked ML17312A6871996-04-0505 April 1996 Rev 1 to Special Rept 2-SR-96-001,on 960404,alert Declared Due to Fire in Voltage Regulator for CR & Remote Shutdown Panel Essential Lighting,Clarifying Status of Power to UPS 2EQDNN02.Further Investigations Into Event Being Performed ML17312A6611996-04-0404 April 1996 Special Rept 2-SR-96-001:on 960404,fault Occurred in Voltage Regulator for CR & Remote Shutdown Panel Essential Lighting, Resulting in Fire in 100 Ft Elevation of Cb B Battery Equipment Room & Requiring Declaration of Alert,Per EPIP-04 ML17312A5771996-03-0101 March 1996 Special Rept 1-SR-96-01 on:960225,unit 1 Turbine Tripped Followed by Reactor Power Cutback.Caused by Lightning Strike.Unit 1 Will Not Be Connected to Grid Until Repairs Can Be Made to C Neutral Bushing of Transformer ML17311A8971995-05-25025 May 1995 Special Rept:On 950416,loose-part Detection Sys Channel 1 Declared Inoperable.Caused by Malfunction of Coaxial Cable Connector to Transducer.Channel Will Be Reworked & Returned to Svc During First Available Outage of Sufficient Duration ML17310B3621994-06-0909 June 1994 Special Rept 1-SR-94-001:on 940511,plant Ventilation Sys High Range Effluent Monitors in Units 1 & 2 Inoperable for Periods Greater than 72 H.Caused by High Voltage Failure Alarm.Design Change Package Installed ML17310B3071994-05-20020 May 1994 Special Rept 2-SR-94-002:on 940518,NOUE Declared Due to Fire Which Burned in Excess of 10 Minutes within Protected Area. Fire Extinguished W/Portable Fire Extinguisher.Investigation Initiated to Determine Cause of Fire & Develop C/As ML17310A9951994-01-13013 January 1994 Suppl 2 to Special Rept 3-SR-92-006:on 921217,PASS Declared Inoperable for Greater than Seven Days Following Failure to Meet Pressurized Sample Portion of Acceptance Criteria for Monthly Functional Sr.Pass Declared Operable on 921226 ML17310A9941994-01-13013 January 1994 Suppl 2 to Special Rept 2-SR-92-004:on 921222,PASS Declared Inoperable for Greater than Seven Days Due to Failure of Containment Air Flow Indicator & Indication of Water Leakage at PASS RCS Sample Septum.Pass Declared Operable on 930105 ML17310A8951994-01-0303 January 1994 Special rept:1-SR-93-008:on 940103,fuel Bldg Ventilation Sys High Range Radiation Monitor Inoperable for Period Greater than 72 Hours.Caused by Difficulties in Installing Mod 1-FJ-SQ-060 ML17310A8701993-12-25025 December 1993 Special Rept 1-SR-93-006:on 931224,30 Day Period for Returning loose-part Detection Sys (Lpds) to Operable Status Exceeded.Inoperable Lpds Channel Scheduled to Be Reworked & Returned to Svc During Next Outage of Sufficient Duration ML17310A8671993-12-15015 December 1993 Special Rept 1-SR-93-007:on 931215,30 Day Period for Returning Accelerometer to Operable Condition Exceeded. Accelerometer Will Be Replaced During Next Outage of Sufficient Duration ML17310A7581993-10-30030 October 1993 Special Rept 1-SR-93-004:on 931008,high Range RM RU-146 Made Inoperable for Period of Greater than 72 H as Result of Scheduled Electrical Bus Outage.Maint on Associated Bus Completed on 931015 & RU-146 Returned to Service ML17310A7001993-10-0909 October 1993 Special Rept 2-SR-93-003:on 931002,thirty Day Period for Returning loose-part Detection Sys Channel 8 to Operable Status Exceeded.Subj Channel Scheduled to Be Reworked & Returned to Svc During Next Outage ML17310A6301993-09-13013 September 1993 Special Rept 3-SR-93-003:on 930806,loose-part Detection Sys (Lpds) Declared Inoperable & Exceeded 30 Day Period for Being Returned to Svc on 930905.LPDS Channel 5 Scheduled to Be Reworked & Returned to Svc During Next Outage ML17310A5401993-08-11011 August 1993 Special Rept 1-SR-93-003:on 930806,NOUE Declared When Unit 1 CR Received Verification That Meteorological Instrumentation Unavailable Due to Loss of Power to Meteorological Tower. Caused by Severe Weather.Instrumentation Repaired ML17310A4961993-08-0202 August 1993 Special Rept 2-SR-93-002:on 930722,Unit 2 in Mode 5,Cold Shutdown During Refueling Outage When ISI of Both SGs Completed.Insp Resulted in Plugging of 74 Tubes in SG 1 & 175 Tubes in SG 2 ML17310A4401993-07-12012 July 1993 Special Rept 1-SR-93-002:on 930526,period for Returning Min Number of Explosive Gas Monitoring Channels to Operable Condition Exceeded.After All Four Cells Rebuilt,Calibr Completed on 930602 & Subj Analyzer Returned to Svc ML17306B4231993-04-24024 April 1993 Suppl 1 to Special Repts 2-SR-92-004 & 3-SR-92-006:on 921222 Unit 2 PASS Declared Inoperable Due to Failure of Containment Air Flow Indicator.On 921217,Unit 3 PASS Declared Inoperable.Equipment Replaced & Sample Obtained ML17306B3371993-03-15015 March 1993 Special Rept 2-SR-93-001:on 930314,control Room Personnel Manually Tripped Reactor Due to Rapid Decrease in Pressurizer Heaters.Personnel Commenced Controlled Plant Cooldown.Unit Remains Shut Down for Further Investigation ML17306B2901993-02-22022 February 1993 Special Rept 1-SR-92-005,suppl 1,provided Per Emergency Plan Implementing Procedure EPIP-03, Notification of Unusual Event Implementing Actions, Occurring on 920822 Re Loss of Power at Meteorological Tower ML17306B2781993-02-0909 February 1993 Special Rept 3-SR-93-001:on 930204,reactor Trip Occurred & Main Feedwater Pump a Experienced Rapidly Decreasing Pump Speed.Valid Actuation of SI Actuation Sys & Containment Isolation Actuation Sys Also Occurred.Evaluation Underway ML17306B2721993-01-27027 January 1993 Special Rept 3-SR-004-03:on 920817,PASS Inoperable for More than 7 Days.On 920902,discovered That PASS Unable to Draw Vacuum on Gaseous Sample Bomb.Vent Line Reworked & Procedure Revised ML17306B2551993-01-24024 January 1993 Special Rept 2-SR-92-004:on 921222,PASS Declared Inoperable for Period Greater than 7 Days Due to Failure of Containment Air Flow Indicator & Indication of Water Leakage at PASS Rcs.Pass Returned to Operable Status on 930105 ML17306B2561993-01-24024 January 1993 Special Rept 1-SR-92-007:on 921227,CB Atmosphere RM Inoperable for Period Greater than 72 H Due to High Flow Conditions.Temporary Mod Installed on Subj RM to Remove Monitor from Dedicated Rms Grounding Sys ML17306B2541993-01-22022 January 1993 Special Rept 3-SR-92-006:on 921217,PASS Declared Inoperable Following Failure to Meet Pressurized Sample Portion of Acceptance Criteria for Monthly Functional Sr.Pass Returned to Operable Status Following Satisfactory Repairs & Testing ML17306B1911992-12-21021 December 1992 Special Rept 3-SR-92-004-01:on 920201 PASS Declared Inoperable for Period Greater than Seven Days.Caused by Tubing Being Rerouted.Pass Reworked & Operability Restored on 920905 ML17306B1841992-12-14014 December 1992 Special Rept:On 920810,PASS Declared Inoperable Due to Tubing Being Rerouted.Chemistry Sys Status Procedure 74DP-9ZZ04 Revised to Direct Chemistry Personnel to Ensure That Functional Test Is performed.W/921214 Ltr ML17306B1291992-11-17017 November 1992 Special Rept 2-SR-92-003:on 921113,reactor Trip Occurred While Motor Generator Set a Out of Svc for Scheduled Maint & Set B Inadvertently Deenergized,Resulting in Loss of Power. State & Local Agencies Notified & Sys Reset ML17306B0931992-10-30030 October 1992 Suppl 1 to Special Rept 3-SR-92-004:on 920817,seven-day Period for Returning PASS to Service exceeded.30DP-9WP04 Revised to Retest for PASS & Gaseous Radwaste to Be Completed by 921120 ML17306A9951992-09-18018 September 1992 Special Rept 3-SR-92-004:seven-day Period for Returning PASS to Svc Exceeded on 920817.On 920902,discovered That PASS Unable to Draw Vacuum on Gaseous Sample Bomb.Possibly Caused by Maint on 920810.PASS Reworked & Operability Restored ML17306A9651992-09-16016 September 1992 Special Rept 3-SR-92-003:on 920903,discovered That PASS Unable to Draw Vacuum on Gaseous Sample Bomb & Declared Inoperable for More than 7 Days.Cause Under Investigation. Sys Returned to Operable Status on 920905 ML17306A9401992-08-28028 August 1992 Special Rept 1-SR-92-005:on 920822,discovered That Info Could Not Be Dispatched from Meterological Tower During Routine Surveillance of Daily Midnight Logs.Tower Declared Operable on 920823 Following Power Restoration ML17306A8101992-06-27027 June 1992 Special Rept 1-SR-92-004:on 920620,loose Part Detection Sys Inoperable for More than 30 Days.Caused by Hardware Problems Associated W/Installation of Loose Part Detection Sys Mods.New Computer Processor Board Installed ML17306A7971992-06-18018 June 1992 Special Rept 3-SR-92-003:on 920520,RMs RU-145 & 146 Declared Inoperable & Removed from Svc.Caused by Personnel Errors in Documenting Clearance for Retest of RU-146.Shift Supervisor Disciplined & Technician Verified That Pumps Were Energized ML17306A7961992-06-18018 June 1992 Special Rept 1-SR-92-003:on 920514,unit 1 Entered Mode 3 & PASS Declare Inoperable & Failed Surveillance Test.Caused by Leaking Relief Valve & Malfunctioning Pressure Transducer. Relief Valve & Pressure Transducer Replaced ML17306A7101992-05-0606 May 1992 Special Rept:On 920504,Control Room Received Alarms on All Seven Control Boards.Plan Computer Returned to Svc & Was Declared operable.W/920506 Ltr ML17306A6811992-04-18018 April 1992 Special Rept SR-92-002:on 920411,insp of SGs Resulted in Plugging of 23 Tubes in SG 1 & 18 Tubes in SG 2.Complete Results of SG Tube ISI Will Be Submitted by 930411 ML17306A4521992-02-0707 February 1992 Special Rept:On 920101,PASS Declared Inoperable When Chemistry Personnel Could Not Obtain a Containment Air Sample.Caused by Malfunctioning Flow Sensor.Pass Expected to Be Returned to an Operable status.W/920207 Ltr ML17306A3901992-01-0707 January 1992 Special Rept 1-SR-92-001:on 920102,determined That Leak Existed in Pressurizer Steam Space Instrument Nozzle Mfg from Inconnel 600.Caused by Nonvisible Intergranular Crack.Addl Investigation Underway ML17306A2981991-12-0505 December 1991 Special Rept 2-SR-91-002:on 911107,fuel Bldg Ventilation Sys high-range Radioactive Gaseous Effluent Monitor Inoperable for More than 72 H.Caused by Power Supply Deenergized for Scheduled Maint.Monitor Returned to Svc on 911114 ML17306A2791991-11-20020 November 1991 Special Rept 3-SR-91-007:on 911115,mobile Crane Came in Contact W/Energized 13.8 Kv Power Line Resulting in Arcing of Crane Outrigger Pads to Ground & Burning of Asphalt Area in Contact W/Pads.Investigation Re Event Being Performed ML17306A2221991-10-10010 October 1991 Special Rept 1-SR-91-001-01:on 910111,fuel Bldg Ventilation Sys High Range Radioactive Gaseous Effluent Monitor Declared Inoperable for Period Greater than 72 H in Order to Perform Scheduled 18-month Surveillance Testing & Maint ML17306A2211991-10-10010 October 1991 Special Rept 2-SR-89-007-03:on 891002,fuel Bldg Ventilation Sys High Range Gaseous Effluent Monitor Declared Inoperable for More than 72 H.Caused by Low Flow Limit Switch Being Out of Adjustment.Microprocessor Operated Manual Mode ML17306A2201991-10-10010 October 1991 Special Rept 2-SR-90-005-01:on 900716,plant Vent Sys High Range Effluent Monitor Inoperable for More than 72 H.Caused by Requirement to Perform Scheduled 18-month Surveillance Testing.Monitor Returned to Svc on 900729 ML17306A2181991-10-10010 October 1991 Special Rept 2-SR-90-004-01:on 910613,fuel Bldg Ventilation Sys high-range Radioactive Gaseous Effluent Monitor Inoperable for More than 72 H.Caused by Need to Perform 18 Month Surveillance Testing.Monitor Returned to Svc ML17305B7441991-09-18018 September 1991 Special Rept 1-SR-91-002,on 910914:steam Generator Econimizer Valve SGN-FV-1112 Fully Opened Causing Level in Steam Generator 1 to Rapidly Increase.Caused by Malfunction of Lower Gripper High Voltage on Slipped Part Length CEA 1999-06-21
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17300B3811999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pvngs,Units 1,2 & 3.With 991007 Ltr ML17300B3271999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pvngs,Units 1,2 & 3 ML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0611999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pvngs,Units 1,2 & 3.With 990810 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17300B3151999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pvngs,Units 1,2 & 3.With 990714 Ltr ML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A9731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pvngs,Units 1,2 & 3.With 990608 Ltr ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A9201999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pvngs,Units 1,2 & 3.With 990512 Ltr ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17300B3071999-03-31031 March 1999 Seismic Portion of Submittal-Only Screening Review of Palo Verde Nuclear Generating Station Units Ipeee. ML17313A8801999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pvngs,Units 1,2 & 3.With 990412 Ltr ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207H7471999-03-10010 March 1999 1999 Emergency Preparedness Exercise 99-E-AEV-03003 ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A8501999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Palo Verde Nuclear Generating Station.With 990311 Ltr ML17313A7791999-02-0505 February 1999 Safety Evaluation Accepting Licensee Rev to Emergency Plan That Would Result in Two Less Radiation Protection Positions Immediatelu Available During Emergencies ML17313A8061999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Pvngs,Units 1,2 & 3.With 990218 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A7381998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.With 990113 Ltr ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML17313A7031998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pvngs,Unit 1,2 & 3. with 981209 Ltr ML17313A6701998-11-0404 November 1998 Rev 2 to PVNGS Unit 2 Colr. ML17313A6741998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pvngs,Units 1,2 & 3.With 981109 Ltr ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A6561998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for PVNGS Units 1,2 & 3.With 981007 Ltr ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML20151S0941998-08-21021 August 1998 Rev 6 to COLR for PVNGS Unit 3 ML20151S0861998-08-21021 August 1998 Rev 4 to COLR for PVNGS Unit 1 ML20151S0901998-08-21021 August 1998 Rev 1 to COLR for PVNGS Unit 2 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A5301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pvgns,Units 1,2 & 3.W/980812 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A5791998-07-0707 July 1998 to PVNGS SG Tube ISI Results for Seventh Refueling Outage Mar & Apr 1998. ML17313A5001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.W/980710 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4521998-06-19019 June 1998 Rev 5 to COLR for Pvngs,Unit 3. ML17313A4501998-06-19019 June 1998 Rev 4 to COLR for Pvngs,Unit 3. ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A4211998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pvngs,Units 1,2 & 3.W/980609 Ltr ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3691998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for PVNGS.W/980412 Ltr ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 1999-09-30
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ACCELERATED UTION DEMONSATION SYSTEM INFORMATION DISTRIBUTION SYSTEM (RIDS)
'EGULATORY ACCESSION NBR:8912270188 DOC.DATE: 89/12/16 NOTARIZED: NO DOCKET 45 FACIL:STN-50-.528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH. NAME AUTHOR AFFILIATION
'EVINE,J.M. Arizona Public Service Co. (formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SUBJECT': Special Rept 1-SR-89-005,Suppl 1:on 890505-08,radiation monitoring unit inoperable for greater than 72 h.
DISTRIBUTION CODE: IE22D COPIES RECEIVED LTR TITLE: 50.73/50.9 Licensee Event Report (LER),
+incident ENCL SIZE:
Rpt, etc.
NOTES: 05000528 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 1 - PD5 PD 1 1 CHAN,T 1 1 DAVIS,M. 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS 1 1 AEOD/DOA 1 1 WYLIE'EOD/DSP/TPAB
.1 1 AEOD/ROAB/DSP 2 '
DEDRO 1 1 NRR/DET/ECMB 9H 1 1-NRR/DET/EMEB9H3 1 1 NRR/DET/ESGB 8D 1. 1 NRR/DLPQ/LHFB11 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB11 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1 NRR/DST/SICB 7E 1 1 NRR/DST/S PLB8 D1 1 1 1 1 NUDOCS-ABSTRACT 1 1 1 1 RES/DSIR/EIB 1 1 GN5 FILE 01 1 1 EXTERNAL: EG&G WILLIAMS,S 4 4 L ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 NUDOCS FULL TXT 1 1 NOTES 1 1 NOTE TO ALL "RIDS" RECIPIENIS:
PLEASE HEL'P US TO REDUCE WASTE! CONTACf THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISIS FOR DOCUMENTS YOU DON'T NEEDl TOTAL NUMBER OF COPIES REQUIRED: LTTR 40 ENCL 40
J Arizona Public Service Company PALO VERDE NUCLEAR GENERATING STATION P,O, BOX 52034 ~ PHOENIX, ARIZONA85072-2034 192-00606-JHL/TOS/SBJ JAMES M. LEVINE December 16, 1989 VICE PRESIDENT NUCLEAR PRODUCilDN U. S. Nuclear Regulatory Commission NRC Document C'ontrol Desk Washington, D.C. 20555
Dear Sirs:
Subject:
Palo Verde Nuclear Generating Station (PVNGS)
Unit 1 Docket No. STN 50-528 (License No. NPF-41)
Supplement to Special Report 1-SR-89-005 File: 89-020-404 Attached please find Supplement Number 1 to Special Report 1-SR-89-005 prepared and submitted pursuant to Technical Specification 3.3.3.8 ACTION 42.
This report'iscusses the, inoperability of a high range radiation effluent monitor.,
If you have any questions, please contact T. D. Shriver, Compliance Hanager, at (602) 393-2521.
Very truly yours, JHL/TDS/SBJ/kj Attachment cc: W.. F. Conway (all w/a)
J. B. Hartin T. J. Polich J. Davis A. C. Gehr 8912270l88 85'1226 PDR ADOCK 05000528 PDC
Il PALO VERDE NUCLEAR GENERATING STATION UNIT 1 Radiation Monitoring Unit Inoperable Greater'han 72 Hours License No. NPF-41 Docket No. 50-528 Supplement to Special Report No. 1-SR-89-005 DESCRIPTION OF WHAT OCCURRED: .
A. Initial Conditions:
During this event between Hay 5, 1989 and Hay 8, 1989, Unit 1 was .
in Mode 5 (COLD SHUTDOWN).
B. Reportable Event Description (Including Dates and Approximate Times of Major Occurrences):
Event Classification: Submitted in accordance with ACTION 42.b of Technical Specification 3.3.3.8.
V At approximately 1805 HST on Hay 8, 1989, Plant Ventilation Radiation Effluent Honitor .(RU-144) was discovered with two of three particulate filter/iodine cartridge assemblies not tightly sealed, thereby, rendering the monitor inoperable. Investigation determined that the assemblies had not been adequately restored during troubleshooting conducted May 6, 1989.
RU-144 has three (3) channels, each with a particulate filter/iodine cartridge assembly. Each assembly consists of a particulate filter and iodine cartridge contained in a removeable cannister assembly. Each cannister assembly is installed in a fixed holder in the monitor. Sample flow is directed through one cannister assembly at a time. As radioactive particulates and iodine are collected in the filters, the radiation levels will .
increase. At a predetermined radiation -level,'he sample flow is automatically redirected to the next standby filter/cartridge assembly.
Prior to this event, on Hay 5, 1989 at approximately 0815 HST, the Low Range and High Range Plant Ventilation Radiation Effluent Monitors (RU-143 and RU-144 respectively) were declared inoperable for performance of Surveillance Test (ST) 36ST-9S(04, "Radiation Monitoring quarterly Functional Test." This ST provides direction for functional verification of radiation monitor performance.
During the source check portion of the ST on RU-144, one of the three detectors monitoring the filter/cartridge assemblies did not properly respond.
The Instrumentation and Control (ISC) Technician (utility, non-licensed) performing the ST notified the Shift Supervisor and
Supplement to Special Report 1-SR-89-005 Page 2 appropriate troubleshooting work instructions were prepared.
Troubleshooting commenced at approximately 0715 HST on Hay 6, 1989. Part of the troubleshooting required access to two of the particulate filter/iodine cartridge assemblies. The troubleshooting identified a deteriorated cable connection and the troubleshooting work document was amended to include instructions for reworking the connector. Upon completion of the work, the ISC Technician reinstalled the assembly into the holder. However, the holder was not properly locked down to prevent bypass flow.
Following completion of the work, a Chemistry Technician (utility, non-licensed) performed a visual check of RU-144 but did not identify that the assembly holders were not properly locked down.
The Chemistry Technician then performed Surveillance Test 75ST-9ZZ07, "Effluent Monitoring System .Daily Surveillance Testing" on RU-143 and verified the setpoints in accordance with 36ST-9S(04, "Radiation Monitor quarterly Functional Test" to declare the monitor operable. At approximately 1040 HST on Hay 7, 1989, RU-143 and RU-144 were declared operable.
During a routine tour at approximately 1805 MST on Hay 8, 1989, a Chemistry Effluent Technician (utility, non-licensed) found two of the three particulate filter/iodine cartridge assembly holders not properly locked down. The Assistant Shift Supervisor (utility, licensed) was notified and RU-144 was declared inoperable.
Technical Specification 3.3.3.8 requires RU-144 be operable at all times. ACTION 42 requires that when the monitor is inoperable greater than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />, the following actions be taken:
- a. Initiate the Preplanned Alternate Sampling Program to monitor the appropriate parameter(s) when it is needed.
- b. Prepare and submit a Special Report to the Commission pursuant to Technical Specification 6.9.2 within 30 days..."
These action requirements were met. The following action was taken to restore RU-144 to an operable status:
- a. The assemblies were locked down.
A filter check and leak rate test were performed in accordance with an approved procedure.
c ~ The Effluent Monitor Daily =Surveillance Test, "75ST-9ZZ07,"
was performed satisfactorily.
At approximately 2300 HST on Hay 8, 1989, RU-144 was declared OPERABLE. The total time of inoperability for RU-144 was approximately 81 hours9.375e-4 days <br />0.0225 hours <br />1.339286e-4 weeks <br />3.08205e-5 months <br /> and 50 minutes.
f Supplement to Special Report I-SR-89-005 Page 3 C. Status of structures, systems, or components that were inoperable at the start of the event that contributed to .the event:
'ot applicable - no structures, systems, or components were inoperable which contributed to the event.
D. Cause of each component or system failure, if known:
Not applicable - no'omponent or system failures were involved.
I E. Failure mode, mechanism, and effect of each failed component', if.
known:
Not applicable - no component failures were involved.
F. For failures of components with multiple functions, list of systems or secondary functions that were also affected:
Not applicable - no component failures were involved.
G. For failures that rendered a train of a safety system inoperable, estimated time elapsed from the discovery of the failure until .the train was 'returned to service:
Not applicable - no failures were involved.
H. Hethod of discovery of each component or system failure or procedural error:
Not applicable - there were no component or system failures or
.procedural errors.
I. Cause of Event:
The cause of this event was a personnel error by the Chemistry Technician who did not adequately verify the configuration of the particulate filter/iodine cartridge filter assembly after work had been performed on the'onitor. An investigation of this event revealed the following were contributing factors to the event.
- 1) Incomplete communications between the 18C Technician and the Chemistry Technician as to the .scope of the RU-144 work, especially'in regard to the sample holder..
- 2) The Work Order did not include a section requiring the Chemistry Technician to inspect the particulate filter/iodine cartridge filter holder and sample chamber for operability.
- 3) The Chemistry Technician had not been qualified adequately in the high range monitors as evidenced by being unable to identify the proper position of the sample holder lock down mechanism.
CI I
Supplement to Special Report- 1-SR-89-005 Page 4
- 4) The Chemistry procedure for media change out in RU-142,- 144 and 146 did not verify,.the 'correct position of the sample chamber or require independent verification.
J. Safety System Response:
Not applicable - no safety system response was expected and none were received.
K. Failed Component Information:
Not applicable - no failed component was involved in this event.
II. ASSESSMENT OF THE SAFETY CONSEQUENCES. AND IMPLICATIONS OF THIS EVENT:
The radioactive gaseous effluent instrumentation is provided to monitor and control, as applicable, the releases of radioactive materials in gaseous effluents during actual or potential releases of gaseous effluents. The alarm/trip setpoints for these instruments are calculated and adjusted in accordance with the methodology and parameters in the Off-Site Dose=Calculation'anual (ODCM) to ensure that the alarm/trip will occur prior to exceeding the limits of 10 CFR Part 20.
There are two separate radioactive gaseous effluent monitoring systems:
the low range. effluent monitors for normal plant radioactive gaseous effluents and the high range effluent monitors for post-accident plant radioactive gaseous effluents. The low range monitors operate at all times until the concentration of radioactivity in the effluent becomes too high during post-accident conditions. The high range monitors only operate, when the concentration or radioactivity in the effluent is above the setpoint of the low range monitors.
Throughout this event the Plant Ventilation Exhaust was monitored with the Low Range Monitor (RU-143) .or an alternate sample cart. Release activities did not approach a level requiring the high range monitor (RU-144). Thus, there is no impact on the health and safety of the public.
I I I. CORRECTIVE ACTIONS:
A. Immediate:
Chemistry positioned the locking mechanism to obtain a seal on the particulate filter/iodine cartridge assembly. The Radiation Monitor was leak rate'ested in accordance with an approved procedure. Chemistry then performed the daily channel check Surveillance Test, "75ST-9ZZ07."
l
- 2. The responsible individual has received appropriate counseling/disciplinary action.
I Supplement to Special Report 1-SR-89-005 Page 5
- 3. As an interim measure, all work order packages for high range effluent monitors have a signoff for Chemistry to perform a leak check on the sample chamber per 75RP-9ZZ64. This will be performed any time the chamber has been disturbed.
75RP-9ZZ64, "RMS Sample Collection", has been revised to include a section addressing verification of correct position of the sample chamber and operability of the monitors after work has been performed on the high range monitor.
e 5, A qualification card has been implemented for the High Range Monitors and will be completed by Chemistry Effluent Technicians. Completion of this qualification card will ensure understanding of the de'vices utilized for securing the filters and actions to be taken when the devices are removed or missing.
B. Action to Prevent Recurrence:
- 1. Radiation Monitoring Calibration Tests, 36ST-9SQ09, 36ST-9SQ10 and 36ST-9SQll will be rev'ised to provide direction for Chemistry to perform a leak check per the leak check procedure. This will be completed by December 31, 1989.
- 2. As a permanent corrective action, Chemistry Standards and Plant Standards will identify the appropriate retests for monitor operability and incorporate them into the retest procedure. This will be completed by December 31, 1989.
I V. SIMILAR EVENTS A similar event was reported under LER 529/88.-17. As a result of this event, a complete revision to the Radiological Effluent Program procedures was initiated. Completion dates for this program upgrade were provided in a letter to the commission on March 27, 1989. The corrective action which could have prevented this event were in progress and therefore could not have prevented this event.
I