ML18110A612: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
(One intermediate revision by the same user not shown)
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:U,S.NUCLEAR REGUI ATORY COMMISSION DOCKET NUMBER NRC FORM 195 I2 76)50-335 FILE NUMBER INCIDENT REPORT NRC DISTRIBUTION FQR PART 50 DOC KfT MATf RIAL TO: (N.C.Moseley FRoM;or ia ower 8 Light Co.Miami, Flordia A.D.Schmidt-DATE OF DOCUMENT 4-12-76 DATE RECEIVED 4-22-76 OLETTER t,ORIG INAI 0 COPY QNOTORIZEO g UNC LASS IF I E D PROP INPUT FORM NUMBER OF COPIES RECEIVED 30 DESCRIPTION Ltr.trans the following.......
{{#Wiki_filter:NRC FORM 195                                            U,S. NUCLEAR REGUI ATORY COMMISSION DOCKET NUMBER I2 76)                                                                                             50-335 FILE NUMBER NRC DISTRIBUTION FQR PART 50 DOC KfT MATfRIAL                                  INCIDENT REPORT TO:                                             FRoM;       or ia ower 8     Light Co.     DATE OF DOCUMENT
ENCLOSU RE Licensee Event Report (R.O b 76-9)on 3-31-76 Concerning dei'ective mechahical pipe restraints (30 Carbon Cys.Received).'DO NOT REMOVE A.CENO%LEDGED.
(                                      Miami, Flordia                           4-12-76 N.C. Moseley                                A.D. Schmidt-                       DATE RECEIVED 4-22-76 OLETTER                 QNOTORIZEO            PROP                    INPUT FORM          NUMBER OF COPIES RECEIVED t,ORIG INAI           g UNC LASS IF I E D 0 COPY                                                                                              30 DESCRIPTION                                                     ENCLOSU RE Ltr. trans the following.......                                   Licensee Event Report (R.O b 76-9) on 3-31-76 Concerning dei'ective mechahical pipe restraints (30 Carbon Cys. Received) .
PLANT NAME: St.Lucie 8 1 0 NOTE: IF PERSO~iL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J.COLLINS SAFETY BRANCH CHIEF.: W 3 CYS FOR ACTION LIC.ASST: W/CYS ACRS 16 CYS FOR ACTION/INFORMATION mann/SIENT TO LA ENVIRO SAB 4-2-E FILF NRC PDR&E 2 IN TE R NAL D RI BUTION IST SCHROEDER/IPPOLITO NOVAK CHECK R lfES S OWEN E TEDE CO MACCA BAER SHAO OLLMER BUNC KRE F.OL NS LPDR: Ft.Pierce FL TIC NSIC EXTERNAL DISTRIBUTION d a.CONTROL NUMBER 4014 NRC FORIVI IBS I2.76)
                                                                  'DO NOT REMOVE A.CENO%LEDGED.
E~i).'"3J b" 4 f'j,eafza":~.3.N C'p~I~~"f J ply~[,]g w qual'"f'>',fl"*"~<, 7>~'f,)V,X,')(,g+r)gq il>ll p~~"l k I c ll ll,,~~~~)<~A pjf Jh.')f."I~.s I I hl'll,j 1 V,'-.;-',i,.;
PLANT NAME:         St. Lucie   8 1                               NOTE:   IF PERSO~iL EXPOSURE IS INVOLVED 0
>J]r)-,,~g.,j.~;
SEND DIRECTLY TO KREGER/J. COLLINS SAFETY                               FOR ACTION/INFORMATION                  ENVIRO      SAB  4      BRANCH CHIEF.:                           mann W 3 CYS FOR ACTION LIC. ASST:
April 12, 1976 PRN-LI-76-77
W/     CYS ACRS     16 CYS             /SIENT TO LA IN TE R NAL D IST RI BUTION E   FILF NRC PDR
%e~tato~~i CU*~/DOC KITED ff/2 1876~P.O.8OX 013100, iIi1IAMI, FLORIDA'33101 F;~eb-;O t'saksCdha51 j FLORIOA POWER 8i LIGHT COi%1PAiNY Cb Mr.Norman C.Moseley, Director, egxon II Office of Inspection and Enforcement U.S.Nuclear Regulatory Commission 230 Peachtree Street, N.W.', Suite 818 Atlanta, Georgia.30303 P
        & E 2 SCHROEDER/IPPOLITO NOVAK CHECK R lfES S OWEN E TEDE CO MACCA BAER SHAO OLLMER BUNC KRE F.           OL NS EXTERNAL DISTRIBUTION                                        CONTROL NUMBER LPDR:     Ft. Pierce   FL   d a.
TIC NSIC                                                                                                4014 NRC FORIVI IBS I2.76)


==Dear Mr.Moseley:==
                                                                        ~ i).
REPORTABLE OCCURRENCE 335-76-9 ST.LUCIE UNIT 1 DATE OF OCCURRENCE:
j,eafza":~.3.N E
MARCH 31, 1976 DEFECTIVE MECHANICAL PIPE RESTRAINTS The attached Licensee Event,.Report is being submitted in accordance with Technical Specification 6.9 to provide prompt notification of the subject occurrence..
                                                                        '"3J  b"  4 f'
Very truly yours, D.Schmidt, Vice President Power Resources I MAS/jn Attachment cc: Jack R.Newman, Esquire Director, Office of Inspection and Enforcement (40)Director, Of fice of Management Information and'rogram Control (3)%(
                                                                                  ~  I
A 1~&f+t lip~.44".~~i LIUl I AIVI L I V LI'O'I"" I ILI Vfl'I~'.X~CONTROL BLOCK: 1 UCENSEE a NAME m~~'''7 89 14 15 LCENSE NUMBER 0-0 0 0 0 0-0 0 25 I (P PAINT ALL REQUIRED INFORMATION)
                                                                                        ~  ~
%CENSE EVENT TYPE TYPE I 1 1 1 1~01 26 30 31 32 REPORT REPORT CATEGORY TYPE SOURCF~ac CONV~~I~Z..O 7 8 57 58 59 60 61'OCXET N 5'0 UMBER~EVENT OATE REPORT CATE 0 3 3 5 0 3 3 1 7 6 0 4 l 2 7 6 68 69 74 75 BO EVENT OESCRIPTIQN t002 Preo erational testing of piping restraints (snubbers) was being performed during 8 9~0 3 the heatuo for Post Core Hot Functional testing.At the 260 F heatup plateau, five 7 8 9 BO w found to be locked uo.The immediate action was to oromptly~o4 7 8 9 Qog of this t e.(335-76-9).
C 'p "f    J ply  ~[,]            g w qual'"f
7 8 9 BO[ODg re lace the defective snubbers with operable snubbers.This was the first occurrence 7 89 SYSTEM CAUSE CQOE COOE COMPONENT COOE~ZZ~B H A N H R'7 8 9 10 11 12 17 CAUSE OESCRIPTIQN
'>',fl"*"~<, 7>~'f,) V,X,'  )(,g+ r)gq il>ll p ~~"l k I c ll ll,,~~~  ~  )<~A pjf      Jh
'gQB The five defective snubbers were PAP4IE CCMPONENT COMPONENT'UPPUER MAhKlFACTURER
                                                                                                      .')f  .    "I    ~ .s I    I hl'll,j V,'
~A B 2 1 0 43'.44 47 Model MSVA-l snubbers.Two VCIVLTCN N 48 of the defective 80 7 8 9 80 Q<s snubbars were disassembled on site by a manufacturer's representative.
1
It was found;7 89~10 OTHER STATUS NA AMOUNT OF ACTIVITY NA PRQBABL CONSEQUENCES, 7 8 9 LOSS OR OAMAGE TO FACIUTY TYPE OESCRiPTIQN PUBLICITY'7, 89 FATTY STATUS'4 POWER co 7 8 9 10 12 13 FORM OF ACTIVITY COATENT RELEASEO OF RELEASE ia~~z'7 a e 10 11 PERSONNEL EXPOSURES NUMBER TYI E QESCRIPTIQN fit~]~oo o~z 7 8 9'1 12 13 PERSONNEL (N JURIES NUMBER CESCRIPTION
                                                                                            -.;-',i,.; >J    ]      r)-,, ~
~4~ol o o 7 89 11 12 METHOO QF OISCOVERY 44"45 NA NA NA NA OISCOVERY OESCRIPTIQN preo erational test procedure 46 LOCATION QF RELEASE NA 80 80 80 80 80 80" 7 89 ADOITIONAL FACTORS.+18 Bee pa e Iwo for continuation of Cause Description.
g .,j. ~;
.7 89 BO 7 89 M.A.Schoppman P ONE'05/552-3779 80 CF0 0 II~~CT Repor"able Occurrence 335-76-9 Licensee Event Report Page Two Cause Descri tion (continued) that moisture had caused oxidation of internal carbon steel parts which had then caused the snubbers to 1'ock.Followup action was to send the other;three snubbers to the manufacturer for laboratory testing and analysis.A'followup report will be prepared and submitted upon completion of the inves-tigation..The five defective snubbers were found in the following order: s/w Location Date 000377 000343 000525 000695 090632 RC-142 RC-142 RC-142'H-142 CH-142 3/31 (disassembled on site)3/31 4/1 4/1 (disassembled on site)4/2 Pa 4%iI 4 I}}
 
P.O. 8OX 013100, iIi1IAMI, FLORIDA'33101
                              %e~tato~~
O F;~eb-;
i t'saksCdha51  j CU
                                                      ~
FLORIOA POWER 8i LIGHT COi%1PAiNY
                                  /      DOC KITED April 12,  1976                ff /
PRN-LI-76-77                                    2  1876  ~
Cb Mr. Norman C. Moseley,    Director,          egxon      II Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N.W.', Suite 818 Atlanta, Georgia 30303 P
 
==Dear Mr. Moseley:==
 
REPORTABLE OCCURRENCE           335-76-9 ST. LUCIE UNIT 1 DATE OF OCCURRENCE:           MARCH       31, 1976 DEFECTIVE MECHANICAL PIPE RESTRAINTS The attached   Licensee Event,.Report           is     being submitted in accordance with Technical Specification 6.9 to provide prompt notification of the subject occurrence..
Very truly yours, D. Schmidt, Vice President Power Resources I
MAS/jn Attachment cc:   Jack R. Newman, Esquire Director, Office of Inspection and Enforcement                       (40)
Director, Of fice of Management Information and
        'rogram Control     (3)
                                    % (
 
1 A
              ~&f+
t lip
~. 44".~~i
 
  ~  '.        X~      CONTROL BLOCK:
1 LIUl I AIVI L     I   V LI 'O'I "" I ILI               Vfl'I (P
I PAINT ALL REQUIRED INFORMATION)
UCENSEE     a                                                                                               %CENSE                EVENT NAME                                     LCENSE NUMBER                                                      TYPE                  TYPE m89 ~ ~                           '                 0   0       0   0     0 0     0                 0             I   1     1   1   1     ~01
                  ~
  '7                                    14    15                                                              25      26                     30     31     32 REPORT     REPORT
    ~ac CONV CATEGORY 57      58 TYPE
                                    ~I 59 SOURCF
                                              ~Z..       O
                                                                'OCXET 5 '0 N UMBER 0     3   3   5 68                  69 0
                                                                                                                        ~ EVENT 3 3 OATE 1   7   6 74 0
75 4   l REPORT CATE 2   7     6 7    8                                      60      61                                                                                                                      BO EVENT OESCRIPTIQN t002     Preo     erational testing of piping restraints (snubbers)                                                   was   being performed during 8 9
    ~0 3       the heatuo for Post Core Hot Functional testing.                                                     At the 260 F heatup plateau,                   five 7 8 9                                                                                                                                                                         BO
  ~o4                                            w       found to be locked uo.                             The immediate             action     was   to oromptly 7     8 9                                                                                                                                                                     BO
[ODg       re lace the defective snubbers with operable snubbers.                                                         This was the         first     occurrence 7   8 9 Qog          of this t e. (335-76-9).
7    89                                                                 PAP4IE                                                                                              80 SYSTEM     CAUSE                                           CCMPONENT                COMPONENT'UPPUER CQOE       COOE               COMPONENT COOE                                     MAhKlFACTURER                        VCIVLTCN
'7
          ~ZZ           ~B               H   A   N       H   R         ~A
                                                                                        '.44 B                2    1    0              N 8 9 10             11         12                       17         43                                              47          48 CAUSE OESCRIPTIQN
  'gQB         The   five defective             snubbers were Model MSVA-l snubbers.                                         Two     of the defective 7     8 9                                                                                                                                                                     80 Q<s         snubbars         were disassembled             on site   by a       manufacturer's representative.                                     It was found
;7     89                                                                                                                                                                     80
    ~10
'7,     89   FATTY                                                               METHOO QF 80 STATUS           '4 POWER                 OTHER STATUS            OISCOVERY                                        OISCOVERY OESCRIPTIQN co8                                                        NA                                                  preo erational            test procedure 7             9             10             12 13                                                 46                                                                        80 FORM OF ACTIVITY       COATENT
'7 ia a      e
                ~
RELEASEO     OF RELEASE
                                ~z 10       11 AMOUNT OF ACTIVITY NA 44      "45 LOCATION QF RELEASE NA 80
                '1 PERSONNEL EXPOSURES NUMBER           TYI E       QESCRIPTIQN fit~]   ~oo         o       ~z                                                   NA 7     8 9                     12       13                                                                                                                                   80 PERSONNEL (NJURIES NUMBER           CESCRIPTION
    ~4 ~ol         o   o 7     89             11   12 PRQBABL          CONSEQUENCES, NA 7      8 9 LOSS OR OAMAGE TO FACIUTY TYPE      OESCRiPTIQN NA 80" PUBLICITY NA 7   89 ADOITIONAL FACTORS
  .+18         Bee pa e Iwo             for continuation of           Cause       Description.
.7     89                                                                                                                                                                     BO 7     89                                                                                                                                                                     80 M. A. Schoppman                                                                         P   ONE'05/552-3779 CF0 0 II ~ ~ CT
 
Repor"able Occurrence 335-76-9 Licensee Event Report Page Two Cause Descri tion (continued) that moisture had caused oxidation of internal carbon steel parts which had then caused the snubbers to 1'ock. Followup action was to send the other
; three snubbers to the manufacturer for laboratory testing and analysis. A
'followup report will be prepared and submitted upon completion of the inves-tigation.
.The five defective snubbers were found   in the following order:
s/w       Location     Date 000377       RC-142     3/31 (disassembled   on site) 000343      RC-142      3/31 000525      RC-142      4/1 000695      'H-142      4/1   (disassembled on site) 090632      CH-142      4/2
 
Pa 4%iI 4
I}}

Latest revision as of 03:31, 3 February 2020

LER 1976-009-00 for St. Lucie Unit 1, Defective Mechanical Pipe Restraints
ML18110A612
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 04/12/1976
From: Schmidt A
Florida Power & Light Co
To: Moseley N
NRC/IE, NRC/RGN-II
References
PRN-LI-76-77 LER 1976-009-00
Download: ML18110A612 (7)


Text

NRC FORM 195 U,S. NUCLEAR REGUI ATORY COMMISSION DOCKET NUMBER I2 76) 50-335 FILE NUMBER NRC DISTRIBUTION FQR PART 50 DOC KfT MATfRIAL INCIDENT REPORT TO: FRoM; or ia ower 8 Light Co. DATE OF DOCUMENT

( Miami, Flordia 4-12-76 N.C. Moseley A.D. Schmidt- DATE RECEIVED 4-22-76 OLETTER QNOTORIZEO PROP INPUT FORM NUMBER OF COPIES RECEIVED t,ORIG INAI g UNC LASS IF I E D 0 COPY 30 DESCRIPTION ENCLOSU RE Ltr. trans the following....... Licensee Event Report (R.O b 76-9) on 3-31-76 Concerning dei'ective mechahical pipe restraints (30 Carbon Cys. Received) .

'DO NOT REMOVE A.CENO%LEDGED.

PLANT NAME: St. Lucie 8 1 NOTE: IF PERSO~iL EXPOSURE IS INVOLVED 0

SEND DIRECTLY TO KREGER/J. COLLINS SAFETY FOR ACTION/INFORMATION ENVIRO SAB 4 BRANCH CHIEF.: mann W 3 CYS FOR ACTION LIC. ASST:

W/ CYS ACRS 16 CYS /SIENT TO LA IN TE R NAL D IST RI BUTION E FILF NRC PDR

& E 2 SCHROEDER/IPPOLITO NOVAK CHECK R lfES S OWEN E TEDE CO MACCA BAER SHAO OLLMER BUNC KRE F. OL NS EXTERNAL DISTRIBUTION CONTROL NUMBER LPDR: Ft. Pierce FL d a.

TIC NSIC 4014 NRC FORIVI IBS I2.76)

~ i).

j,eafza":~.3.N E

'"3J b" 4 f'

~ I

~ ~

C 'p "f J ply ~[,] g w qual'"f

'>',fl"*"~<, 7>~'f,) V,X,' )(,g+ r)gq il>ll p ~~"l k I c ll ll,,~~~ ~ )<~A pjf Jh

.')f . "I ~ .s I I hl'll,j V,'

1

-.;-',i,.; >J ] r)-,, ~

g .,j. ~;

P.O. 8OX 013100, iIi1IAMI, FLORIDA'33101

%e~tato~~

O F;~eb-;

i t'saksCdha51 j CU

~

FLORIOA POWER 8i LIGHT COi%1PAiNY

/ DOC KITED April 12, 1976 ff /

PRN-LI-76-77 2 1876 ~

Cb Mr. Norman C. Moseley, Director, egxon II Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N.W.', Suite 818 Atlanta, Georgia 30303 P

Dear Mr. Moseley:

REPORTABLE OCCURRENCE 335-76-9 ST. LUCIE UNIT 1 DATE OF OCCURRENCE: MARCH 31, 1976 DEFECTIVE MECHANICAL PIPE RESTRAINTS The attached Licensee Event,.Report is being submitted in accordance with Technical Specification 6.9 to provide prompt notification of the subject occurrence..

Very truly yours, D. Schmidt, Vice President Power Resources I

MAS/jn Attachment cc: Jack R. Newman, Esquire Director, Office of Inspection and Enforcement (40)

Director, Of fice of Management Information and

'rogram Control (3)

% (

1 A

~&f+

t lip

~. 44".~~i

~ '. X~ CONTROL BLOCK:

1 LIUl I AIVI L I V LI 'O'I "" I ILI Vfl'I (P

I PAINT ALL REQUIRED INFORMATION)

UCENSEE a %CENSE EVENT NAME LCENSE NUMBER TYPE TYPE m89 ~ ~ ' 0 0 0 0 0 0 0 0 I 1 1 1 1 ~01

~

'7 14 15 25 26 30 31 32 REPORT REPORT

~ac CONV CATEGORY 57 58 TYPE

~I 59 SOURCF

~Z.. O

'OCXET 5 '0 N UMBER 0 3 3 5 68 69 0

~ EVENT 3 3 OATE 1 7 6 74 0

75 4 l REPORT CATE 2 7 6 7 8 60 61 BO EVENT OESCRIPTIQN t002 Preo erational testing of piping restraints (snubbers) was being performed during 8 9

~0 3 the heatuo for Post Core Hot Functional testing. At the 260 F heatup plateau, five 7 8 9 BO

~o4 w found to be locked uo. The immediate action was to oromptly 7 8 9 BO

[ODg re lace the defective snubbers with operable snubbers. This was the first occurrence 7 8 9 Qog of this t e. (335-76-9).

7 89 PAP4IE 80 SYSTEM CAUSE CCMPONENT COMPONENT'UPPUER CQOE COOE COMPONENT COOE MAhKlFACTURER VCIVLTCN

'7

~ZZ ~B H A N H R ~A

'.44 B 2 1 0 N 8 9 10 11 12 17 43 47 48 CAUSE OESCRIPTIQN

'gQB The five defective snubbers were Model MSVA-l snubbers. Two of the defective 7 8 9 80 Q<s snubbars were disassembled on site by a manufacturer's representative. It was found

7 89 80

~10

'7, 89 FATTY METHOO QF 80 STATUS '4 POWER OTHER STATUS OISCOVERY OISCOVERY OESCRIPTIQN co8 NA preo erational test procedure 7 9 10 12 13 46 80 FORM OF ACTIVITY COATENT

'7 ia a e

~

RELEASEO OF RELEASE

~z 10 11 AMOUNT OF ACTIVITY NA 44 "45 LOCATION QF RELEASE NA 80

'1 PERSONNEL EXPOSURES NUMBER TYI E QESCRIPTIQN fit~] ~oo o ~z NA 7 8 9 12 13 80 PERSONNEL (NJURIES NUMBER CESCRIPTION

~4 ~ol o o 7 89 11 12 PRQBABL CONSEQUENCES, NA 7 8 9 LOSS OR OAMAGE TO FACIUTY TYPE OESCRiPTIQN NA 80" PUBLICITY NA 7 89 ADOITIONAL FACTORS

.+18 Bee pa e Iwo for continuation of Cause Description.

.7 89 BO 7 89 80 M. A. Schoppman P ONE'05/552-3779 CF0 0 II ~ ~ CT

Repor"able Occurrence 335-76-9 Licensee Event Report Page Two Cause Descri tion (continued) that moisture had caused oxidation of internal carbon steel parts which had then caused the snubbers to 1'ock. Followup action was to send the other

three snubbers to the manufacturer for laboratory testing and analysis. A

'followup report will be prepared and submitted upon completion of the inves-tigation.

.The five defective snubbers were found in the following order:

s/w Location Date 000377 RC-142 3/31 (disassembled on site) 000343 RC-142 3/31 000525 RC-142 4/1 000695 'H-142 4/1 (disassembled on site) 090632 CH-142 4/2

Pa 4%iI 4

I