ML19210C433: Difference between revisions

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[i li l l radiographed but tne results were unsuccessful due to the thickness of the valve body.                                                                            I i  2 The valve will be disassembled and repaired as determined necessary during the current l
[i li l l radiographed but tne results were unsuccessful due to the thickness of the valve body.                                                                            I i  2 The valve will be disassembled and repaired as determined necessary during the current l
     ,  3      l outage.                                                                                                                                                    l i  4        1                                                                                                                                                            1 7        8 9                                                                                                                                                            80 ST        5            % POWER                    OTHER STATUS                ISCOV RY                          DISCOVERY DESCRIPTION i  s      LtLj@ l 0101 nl@l                                  ra                        l  [L.j@l          onaratnr nhwrvatinn                                        l
     ,  3      l outage.                                                                                                                                                    l i  4        1                                                                                                                                                            1 7        8 9                                                                                                                                                            80 ST        5            % POWER                    OTHER STATUS                ISCOV RY                          DISCOVERY DESCRIPTION i  s      LtLj@ l 0101 nl@l                                  ra                        l  [L.j@l          onaratnr nhwrvatinn                                        l
'                                '                '      "                              "                '
           ' JTIVITY          CC TNT RELEASED OF RELEASE                                                                                                LOCATION OF RELEASE @
           ' JTIVITY          CC TNT RELEASED OF RELEASE                                                                                                LOCATION OF RELEASE @
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PERSCNNEL EXPCSURES
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                                            '
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                     ,ERSONNabu'R,ES                                                                                                  -
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a 8  9 1010101@l12          11 NA 80 l
a 8  9 1010101@l12          11 NA 80 l
LOSS TYPE OF OR OAMAGE TO FACILITY Q DESCRIPTION                  N/
LOSS TYPE OF OR OAMAGE TO FACILITY Q DESCRIPTION                  N/
[i    9 l Z l@l10                            NA                                                                                                                    l 7          8 9                                                                                                                                                            80
[i    9 l Z l@l10                            NA                                                                                                                    l 7          8 9                                                                                                                                                            80 iSSU            OESCR:    PTiON O                                                    7911140 g Q                                          NRC usE CNa 17 I o l [ Jds81                                    NA                                                                                    I 68 69 IIIIIi        III  iS0lI5 7        8 9                10 N A*.1E CF PPE P AP E R W. R. Cartwright                                        psoye.          701-894-5151
                              '''*
iSSU            OESCR:    PTiON O                                                    7911140 g Q                                          NRC usE CNa 17 I o l [ Jds81                                    NA                                                                                    I 68 69 IIIIIi        III  iS0lI5 7        8 9                10 N A*.1E CF PPE P AP E R W. R. Cartwright                                        psoye.          701-894-5151


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Virginia Electric and Pcwer Company fiorth Anna Power Station, Unit #1                   
Virginia Electric and Pcwer Company fiorth Anna Power Station, Unit #1                   



Latest revision as of 04:34, 2 February 2020

LER 79-140/03L-0:on 791013,after Condensate & Feedwater Pumps Secured for Refueling,Containment Isolation Check Valve 1-FW-111 Be Stuck Open.Cause Unknown.Valve Will Be Disassembled & Repaired During Current Outage
ML19210C433
Person / Time
Site: North Anna Dominion icon.png
Issue date: 11/12/1979
From: Cartwright W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19210C432 List:
References
LER-79-140-03L, LER-79-140-3L, NUDOCS 7911140243
Download: ML19210C433 (2)


Text

,

uCEisSdd Ev EN i nErOrii CONTROL BLOCK: l l l l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 7 o i 8 9 lVlA l N l A l S 14l1 l@l LICENSEE CODE 13 0l 0l -l 0 lLICEtJSE0 l 0NUMBEH l 0 l 0 l- l 0 l 025l@l4 26 l1LICENSE 1

1TYPE l1JOl@lbl LAIl 58 l@

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o i 3

,"j]"y l L l@l 0 l 5 l0 l0 l0 l3 l3 l8 68l@l1 60 61 69 011 l3 l 71974l@l75 i i REPORT EVENT DATE li l9DATE 17 h 80l@

DOCKET NUMSER EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h

&LLJ l After the condensate and feedwater pumps were secured for refueling, containment i O 3 isolation check valve 1-FW-ill was observed to be partially stuck open as evidenced l 0 ., lby back leakage from "C" steam generator to the feedwater heaters. The health and I o 3  ; safety of the general public were not affected by this event. Reportable pursur.. to l O 3 ;T.S. 6.9.1.9.b. l 0 7 l l 0 8 l l 7 8 9 80 bE CC E S3 0 E COVPONE NT CODE SUSCODE SU E o 9 l c l H l@ lE l@ l R l@ IV l A lL IV IE lX l@ LC_j@ (Lj @

7 8 9 10 11 12 13 18 19 20

' SEQUE NTI AL OCCURRENCE REPORT REVISION LE R RO EVENT YEAR REPORT NO. CCCE TYPE NO.

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l217l229l 23 24 26 27 28 23 30 31 32 T K N A T ON O PL NT .t TH HOURS 22 S B IT D FOf 1 B. 5 PPLIE VAN FA TURER I33X l@lD 34 l@ l35 Z]@ l36Z l@ l 0 l 0 l 010 l 3/ 40 lY 41 l@ l42N ]@ [Al@

43 lC 2l5[5l@

44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i O l The cause for the check valve stit'<ing open is not known at this time. The valve was l

[i li l l radiographed but tne results were unsuccessful due to the thickness of the valve body. I i 2 The valve will be disassembled and repaired as determined necessary during the current l

, 3 l outage. l i 4 1 1 7 8 9 80 ST 5  % POWER OTHER STATUS ISCOV RY DISCOVERY DESCRIPTION i s LtLj@ l 0101 nl@l ra l [L.j@l onaratnr nhwrvatinn l

' JTIVITY CC TNT RELEASED OF RELEASE LOCATION OF RELEASE @

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e 8 9 LLl@ Lzl@l 10 11 rmWOUNTOhCTIVITY 44 I

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PERSCNNEL EXPCSURES NUVBER .YPE DE SCRIPTION i 2 1010 Ol@lzl@lNA 2 "

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i NUven oESCR,PTiON@

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a 8 9 1010101@l12 11 NA 80 l

LOSS TYPE OF OR OAMAGE TO FACILITY Q DESCRIPTION N/

[i 9 l Z l@l10 NA l 7 8 9 80 iSSU OESCR: PTiON O 7911140 g Q NRC usE CNa 17 I o l [ Jds81 NA I 68 69 IIIIIi III iS0lI5 7 8 9 10 N A*.1E CF PPE P AP E R W. R. Cartwright psoye. 701-894-5151

Virginia Electric and Pcwer Company fiorth Anna Power Station, Unit #1

Attachment:

Page 1 of 1 Docket tio. 50-338 Report flo. LER 79-140/03L-0 Description of Event On October 13, 1979, with the unit in refueling mode, containment isolation check valve 1-FN-lll was observed to be partially stuck open as evidenced by back leakaSe from "C" steam generator to the feedwater heaters when the condensate and feedwater pumps were secured. The inoperability of containment isolation valve 1-FW-lll is contrary to T.S. 3.6.3.1 and reportable pursuant to T.S. 6.9.1.9.b.

Probable Consequences of Occurrence The health and safety of the general public were not affected because the check valve was found inoperable while the unit was in a safe shutdown condition and will be restored to operable status prior to resuming operation.

There are no generic implications associated with this event.

Cause of Occurrence The exact cc.use for 1-FW-lli sticking open is not known at this time.

Immediate Corrective Action The valve was radiographed but the results of the examination were unsuccessful because of the thickness of the valve body.

Scheduled Corrective Action The check valve will be disassembled and repaired as necessary during the current refueling outage.

Actions Taken to Prevent Recurrence flo further actions are required.

'"9 280