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| issue date = 05/10/1993
| issue date = 05/10/1993
| title = LER 93-004-00:on 930409,typo Discovered in Rept Used to Determine RPS Low RCS Flow Trip Setpoint.Error Existed Since Aug 1988.Caused by Design Control Inadequacy.Engineering Package Developed to Correct calculations.W/930510 Ltr
| title = LER 93-004-00:on 930409,typo Discovered in Rept Used to Determine RPS Low RCS Flow Trip Setpoint.Error Existed Since Aug 1988.Caused by Design Control Inadequacy.Engineering Package Developed to Correct calculations.W/930510 Ltr
| author name = SAGER D A, YOUNG R J
| author name = Sager D, Young R
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:ACCELERANT DOCUMENTDISTRj:UTIONSYSTEMREGULATINFORMATION DISTRIBUTION STEM(RIDS)ACCESSION NBR:9305180328 DOC.DATE:
{{#Wiki_filter:ACCELERANT                 DOCUMENT DISTRj: UTION SYSTEM REGULAT        INFORMATION DISTRIBUTION         STEM (RIDS)
93/05/10NOTARIZED:
ACCESSION NBR:9305180328             DOC.DATE:     93/05/10  NOTARIZED: NO          DOCKET  ¹ FACIL:50-335 St. Lucie Plant, Unit 1, Florida Power                & Light  Co. 05000335 AUTH. NAME            AUTHOR AFFILIATION YOUNG,R.J.           Florida    Power & Light Co.
NOFACIL:50-335 St.LuciePlant,Unit1,FloridaPower&LightCo.AUTH.NAMEAUTHORAFFILIATION YOUNG,R.J.
SAGER,D.A.           Florida    Power & Light Co.
FloridaPower&LightCo.SAGER,D.A.
RECIP.NAME           RECIPIENT AFFILIATION
FloridaPower&LightCo.RECIP.NAME RECIPIENT AFFILIATION DOCKET¹05000335


==SUBJECT:==
==SUBJECT:==
LER93-004-00:on 930409,typo discovered inreptusedtodetermine RPSlowRCSflowtripsetpoint.Error existedsinceAug1988.Caused bydesigncontrolinadequacy.
LER    93-004-00:on 930409,typo discovered in rept used to determine RPS low RCS flow trip setpoint.Error existed since                        D Aug 1988.Caused by design control inadequacy. Engineering package developed to correct calculations.W/930510                 ltr.
Engineering packagedeveloped tocorrectcalculations.W/930510 ltr.DZSTRZSUTZON CODE:IE22TCOPIESRECEIVED:LTR IENCL/SIZE:TITIE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.NOTES:DRECIPIENT IDCODE/NAME PD2-2LANORRISgJINTERNAL:
DZSTRZSUTZON CODE:     IE22T      COPIES RECEIVED:LTR       I ENCL    / SIZE:
ACNWAEOD/DOAAEOD/ROAB/DSP NRR/DE/EMEB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRSS/PRPB NRR/DSSA/SRXB RES/DSIR/EIB EXTERNAL:
TITIE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
EG&GBRYCEPJ.H NRCPDRNSICPOOREPW.COPIESLTTRENCL1111221122111111221111221111RECIPIENT IDCODE/NAME PD2-2PDACRSAEOD/DSP/TPAB NRR/DE/EELB NRR/DORS/OEAB NRR/DRCH/HICB NRR/DRIL/RPEB NRR.DSSA/SPLB 02RGN2FILE01LSTLOBBYWARDNSICMURPHY,G.A NUDOCSFULLTXTCOPIESLTTRENCL11221111111,111111111111.111DDDDNOTETOALL"RIDS"RECIPIENTS:
NOTES:
PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.504-2065)
RECIPIENT              COPIES              RECIPIENT          COPIES ID CODE/NAME            LTTR ENCL        ID CODE/NAME       LTTR ENCL            D PD2-2 LA                    1      1      PD2-2 PD                1      1 NORRISgJ                    1      1                                                D INTERNAL: ACNW                        2      2      ACRS                    2      2 AEOD/DOA                    1      1      AEOD/DSP/TPAB          1      1 AEOD/ROAB/DSP               2      2      NRR/DE/EELB            1      1 NRR/DE/EMEB                 1      1      NRR/DORS/OEAB          1      1 NRR/DRCH/HHFB               1      1      NRR/DRCH/HICB          1,    1 NRR/DRCH/HOLB               1      1      NRR/DRIL/RPEB          1      1 NRR/DRSS/PRPB               2      2      NRR .DSSA/SPLB          1      1 NRR/DSSA/SRXB               1      1                    02      1      1 RES/DSIR/EIB                 1      1      RGN2    FILE  01      1      1 EXTERNAL: EG&G BRYCEPJ.H               2      2      L ST LOBBY WARD        1      1 NRC PDR                      1      1      NSIC MURPHY,G.A         1  . 1 NSIC POOREPW.               1      1      NUDOCS FULL TXT        1      1 D
TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!DFULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:
D D
LTTR32ENCL32 PP'fMay10,1993L-93-12910CFR50.73U.S.NuclearRegulatory Commission Attn:DocumentControlDeskWashington, D.C.20555Re:.St.LucieUnit1DocketNo.50-335Reportable Event:93-004DateofEvent:April9,1993Incorrect RCSLowFlowTripSetpointduetoaDesinErrorTheattachedLicenseeEventReportisbeingsubmitted pursuanttotherequirements of10CFR50.73toprovidenotification ofthesubjectevent.Verytrulyyours,4A8a~D.A.gerVicersidentSt.LuePlantDAS/JWH/kw Attachment cc:StewartD.Ebneter,RegionalAdministrator, USNRCRegionIISeniorResidentInspector, USNRC,St.LuciePlantDAS/PSL8917-931700339305i80328 9305i0PDRADOCK05000335SPDRanFPLGroupcompany PPPFPLFEOElmloolNRCFormK6(M9)L.S.tEUCLEARREGULATORY COMMISSION LICENSEEEVENTREPORT(LER)APPROYOTONENCk0110010IENNPEE'NHNT EETPIATE0NAaENPENINEPCNTETOCEPNCYWITHTI00NfOIEAATlON CCATECSTINTINCEEET.>>0 HTESONWNaCONNENTESNONEPNOTAfaENEETTwIE ToTHEINOCla0ANTPEPONTENANAKINNTEAANCHTPANIAIANIANAENIPEIANATCNY~WATPNarol.
NOTE TO ALL"RIDS" RECIPIENTS:
OCIPHENaToTHEPPENWITTN SEOOCTONPNOECTo'110010PA CfSCEOfNAMOEIENT PIEIOAXNT.WASPNeOTCPC OCITNELFACILITYNAME(1)St.LucieUnit1DOCKETNUMBER(2)PAGE3050003351 04(4)Incorrect ReactorCoolantSystemLowFlowTripSetpointresultsinacondition prohibited byTechnical Specifications duetoaDesignControlInadequacy.
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
EVENTDATE(5)LERNUMBER(6)REPORTDATE(7)OTHERFACILITIES INVOLVED(8)MOMlHDAY0409OPERATING MODE(9)YEARYEAR9393SIAL004MONTHDAYYEAR00051093FACILITYNAMESN/AN/A20.402(b) 20.405(c) 50.73(a)(2)(iv)
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR                32  ENCL    32
THISREPORTISSUBMITTED PURSUANTTOTHEREQUIREMENTS OF10CFR:Checkoneormoreofthefollowin(11)DOCKETNUMBER(S) 050000500073.71(b)POWERLEVEL(10)20.405(a)(1
)(i)20.405(a)(1
)(ii)20.405(a)(1)(iii) 20.405(a)(1)(iv) 20.405(a)(1)(v) 50.36(c)(1) 50.36(c)(2) 50.73(a)(2)(i) 50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(v) 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 50.73(a)(2)(x) 73.71(c)OTHER(SpecifyinAbstractbelowandinTextNRCForm366A)NAMELICENSEECONTACTFORTHISLER12RobertJ.Young,ShiftTechnical AdvisorTELEPONENUMBERAREACODE407465.3550COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT13CAUSESYSTEMCOMPONENT MANUFAG-REPORTABLE TURERTONPRDSCAUSESYSTEMCOMPONENT MANUFAC-REPORTABLE lURERTONPRDSSUPPLEMENTAL REPORTEXPECTED14IIIEXPECTEDMONIHDAYYEARSUBMISSION DATE(15)YES(Ifyes,completeEXPECTEDSUBMISSION DATE)ABSTRACT(Limitto1400spaces.ie.approximately fifteensingle-space typewritten lines)(16)OnApril9,1993,St.LucieUnit1wasinMode6whenatypographical errorwasdiscovered byFPLNuclearEngineering inareportusedtodetermine theReactorProtection System(RPS)lowReactorCoolantSystem(RCS)flowtripsetpoint.
Technical Specification 2.2.1,Table2.2-1statesthatthetripsetpointwillbegreaterthanorequalto95%ofdesignreactorcoolantflow.TheFPLNuclearEngineering report,whichdescribed theconversion ofpressuredropacrossthesteamgenerators totheRPSlowRCSflowtripsetpoint, contained anincorrect constant.
Thereportwassubsequently transmitted totheplantstaffandtheInstrument andControlDepartment adjustedtheRCSlowflowsetpoint.
ThiserrorcausedthesettingoftheRCSlowflowtripsetpointtoavalueapproximately 3%belowtheminimum95%ofdesignflow.ThissetpointerrorexistedsinceAugust1988.Therootcauseofthiseventwasadesigncontrolinadequacy.
Atypographical errorwasmadeinthereporttransmitted totheplantstaff.Theerrorwouldhavebeendiscovered ifthereviewprocessforthetransmitted reporthadundergone anindependent review.TheNuclearEngineering processcurrently inplacepreventsasimilareventfromoccurring byrequiring independent reviewoftransmitted setpoints.
Corrective actionsforthisevent:Anengineering evaluation wasperformed thatconcluded thattheoperation ofUnit1duringthistimeperiodwaswithintheboundsofthesafetyanalysis.
Areviewoftheprocedure usedtodetermine theUnit2lowRCSflowsetpointverifiedthatitdidnotcontainasimilarerror.Afterareviewofinternalrecords,NuclearEngineering verifiedthatnootherUnit1or2RPSsetpointchangesweretransmitted totheplantinerror.Anengineering packagewasdeveloped toprovidethecorrected calculations fordetermination oftheRPSreactorcoolantsystemlowflowtripsetpoint.
Instrumentation andControlpersonnel willreviseappropriate procedures andinstallthecorrecttripsetpointintheUnit1RPSpriortoenteringmode2.Priortodiscovery ofthisevent,Engineering adoptedaprocessrequiring independent reviewofsetpoints beforetransmittal totheplantstaff.FPLFacsimile ofNRGForm366(6-89)
FPLFsaslnilsof NRCFormSEI(&89)U.S.NUCLEARREGULATORY COMMISSION LICENSEEEVENTREPORT(LER)TEXTCONTINUATION Asswosf0oeIxsssssCIssfxssus'ass sfSTAIATf0OATCENsfilINSAONsfToCOINETWITHsissSfCWNATTCNCasEfCOONIfoUECTIsfsIsxsssxswNecoNNENTsIKOANowoEssesNfsoNATEToTIOINcsxsssNeISAONTSNANACEsfNTfssANCHTASTCEuaNXXENTIuauATEXTT
~wAEINeTON.OossssfNeToTIOSNEIIwowIsoucwoNTwofcsETIsseIsssasrscfosswNACEISNT NeTseofs.WANNesfsf ocssexsFACILITYNAME(1)St.LucieUnit1DOCKETNUMBER(2)YEARLERNUMBER(6)gEQUENTIAL NUMBERREVISIONNUMBERPAGE(3)0500033593TEXT(lfmorespaceisrequired, useadditional NRCForm366A's)(1/)004000204OnApril9,1993,withUnit1inMode6,FPLNuclearEngineering performed areviewofthecalculations thatarecontained intheSt.LucieUnit1LowFlowTripSetpointCalibration Guidelines.
Thereviewwasbeingperformed tosupportaproposedchangetothesteamgenerator tubepluggingcriteria.
Duringthisreview,atypographical errorinareportthatdescribed conversion ofpressuredropacrosstheSteamGenerators (EIIS:AB) totheReactorProtection System(RPS)(EIIS:JC)ReactorCoolantSystem(RCS)lowflowtripsetpointwasfound.Theerrorresultedinthecalculation ofanon-conservative setpointwithwhichtheRPScreatesanautomatic reactortriptoprotectagainstalossofRCSflow.ThiserrorcausedtheRPSlowRCSflowtripsetpointtobeapproximately 3percentbelowtheTechnical Specification minimumof95percentofdesignflow.In1987thereportcontaining theincorrect information wassenttotheplantstafftosupportamodification totheRPS.InAugust1988,thereportwasreferenced whenthemodification totheRPSwasimplemented andwasusedtomodifyplantprocedures fortheinitialsettingandsubsequent monthlychecksofthisRPSlowflowtripsetpoint.
Thiscondition wasdiscovered inAprilof1993.Therootcauseofthiseventwasadesigncontrolinadequacy.
Atypographical errorwasmadebyFPLNuclearEngineering inthetransmittal ofacalculated setpointtotheplantstaff.Duringatransferofinformation fromanindependently verifiedengineering calculation toareport,atranscription errorcausedaconstantthatconvertspressuredropacrosstheSteamGenerators tothelowRCSflowtripsetpointtobenon-conservative.
Theincorrect reportwouldhavebeendiscovered andcorrected hadthetransmitted reporttotheplantstaffreceivedthesameindependent reviewthattheoriginalcalculation hadreceived.
Priortothediscovery ofthisevent,FPLNuclearEngineering adoptedtheprocessforrequiring independent reviewofallsetpoints beforetransmittal totheplantstaff.Thiseventisreportable under10CFR50.73(a)(2)(i)(B),
as"Anyoperation orcondition prohibited bytheplant'sTechnical Specifications."
Technical Specification 2.2.1requiresthattheRPStripsetpointforRCSlowflowbesetatorabove95percentofdesignflow(370,000gpm).Forcycles9,10and11ofUnit1operation, theRCSlowflowtripwaserroneously setatslightlyhigherthan92percentofdesignflow.TheRCSlowflowtripsetpointensuresthatforadegradation ofRCSflowresulting fromanalyzedtransients, areactortripoccurstopreventdeparture fromnucleateboilingratio(DNBR)safetylimits.Theprocesssignalforthisfunctionisdeveloped fromfourindependent differential pressurechannelswhichmeasurethepressuredropacrosstheprimarysideofbothSteamGenerators.
ThetotalSteamGenerator pressuredropiscomparedwiththelowRCSflowtripsetpoint.
Iftwochannelsindicateaflowwhichislessthanthetripsetpoint, anRPStripsignalisinitiated.
FPLFacsimile ofNRCForm366(6-89)
FPLFacstmloolNRCFormS66($89)U.S.NUCLEARREGULATORY COMMrSSIONUCENSEEEVENTREPORT(LER)TEXTCONTINUATION
,AAINorrocooNI$
$$$oerorcofrfoarrfoeooeTAIATToofvcrNITNIoefcfocToccoe$vTATNoooofrfvAACON couococNIacracTl$04IeoafoNwrfoccrrrNTofccfrlooro IAATIENoeoNATcToTtoIocofoowo$fafomoNANACT$CNTONANCNreeTCAuaNOCITANIN$$AATONv~wANNIOTCN, oc$0$$aANITollofATNAwrovr IacucocNffvoacI$$$Ioeror$cffICEofIIANAccoaNT Afo$$$$ccr,wANNrcrcfo ocToooaFACILITYNAME(1)St.LucieUnit1DOCKETNUMBER(2)YEARLERNUMBER(6)EQUENTIAL
-rREVISIONNUMBER4NUMBERPAGE(3)0500033593 TEXT(Ifmorespaceisrequired, useadditional NRCForm366A's)(17)004000304Anevaluation (JPN-PSL1-SEFJ-93-006) wasperformed byFPLEngineering todetermine theavailable safetyanalysismarginforthemostlimitingtransients (lossofoffsitepowerandlossofRCSflow)forwhichprotection isprovidedbytheRCSlowflowtrip.Theresultsshowthattheapproximate 3percentsetpointerrorissufficiently offsetbyavailable flowmargin.Thus,violation oftheDNBRlimitforalossofoffsitepoweroralossofRCSfloweventwouldnothaveoccurrediftherehadbeenadegradation ofRCSfloweventduringthetimeperiodthatthesetpointerrorwasinplace.(AreviewofUnit1reactortripsshowedthattheRCSlowflowtripfunctionwasnotchallenged duringcycles9,10and11.Anadditional reviewofactualoperating conditions duringcycles9,10,and11wasperformed toensurethatnoothercondition existedthatwouldfurtheraggravate thecondition described inthisLER).TheReactorCoolantPump(RCP)(EIIS:P) seizedrotoreventhasbeenreanalyzed bythefuelvendorfora4percentreduction indesignflowandthecorresponding 4percentreduction intheRCSlowflowtripsetpoint.
Theanalysisshowsthattheacceptance criteriaforthepostulated RCPseizedrotoreventwasnotviolated.
Therefore, thehealthandsafetyofthepublicwasnotaffectedbythiscondition.
1.Priortothediscovery ofthisevent,NuclearEngineering proceduralized areviewprocesstoensuretheaccuracyofsetpoints andplantchanges.Thisprocessrequiresanindependent verification ofsetpoints andplantchangesbeforetransmittal totheplantstaff,andwouldhavedetectedtheerrordescribed inthisreport.2.NuclearEngineering preparedanengineering evaluation anddetermined thatoperation ofUnit1wasboundedbythesafetyanalysesforCycles9,10,and11.3.NuclearEngineering reviewedinternalrecordsandverifiedthatnootherUnit1or2RPSsetpointchangesweretransmitted totheplantstaffinerror.4.NuclearEngineering reviewedtheUnit2RCSLowFlowTripSetpointDetermination procedure andverifiedthatitdidnotuseerroneous data.5.AFPLengineering packagewasdeveloped todocumentandtransmitthecorrected calculation fortheUnit1RPSIowRCSflowtripsetpoint.
6.TheI&CDepartment willreviseprocedures 1-0120050 and1-1400050
~toreflectthecorrectRCSlowflowtripsetpoints priortoUnit1enteringMode2.7.TheI&CDepartment willmaketheRPSlowRCSflowtripsetpointchangespriortoUnit1enteringMode2.FPLFacsimile ofNRCForm366(6-89)


FPLF55cslrrllo olNRCFormS6BU.S.NUCLEARREGULATORY COMMrSSION
May 10, 1993 PP'f L-93-129 10 CFR 50.73 U. S. Nuclear Regulatory Commission Attn:      Document Control Desk Washington, D. C. 20555 Re:  .St. Lucie Unit 1 Docket No. 50-335 Reportable Event: 93-004 Date of Event: April 9, 1993 Incorrect RCS      Low Flow Trip Setpoint due    to a Desi  n Error The  attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.
~LICENSEEEVENTREPORT(LER)TEXTCONTINUATION APAN5TITO CAONCI$1500505fAASNS:IO00550TWATToTAANNN05IIINSAONICTOGTANAYWoilTIIS005$0AAOONCOTITCOONISISNST:500ITISICAINNoOONNANT0NTOAIIONO TAAoCNTSTYAATSloTININGTAYISAIAIINICNTSNANAGSISNTSNANCHTNINa IASIANATAIIINGAAATGNY
Very  truly      yours, 4A8a ~
~WANNNTTGN.OG505$
D. A.        ger Vice r sident St. Lu e Plant DAS/JWH/kw Attachment cc: Stewart D. Ebneter, Regional Administrator, USNRC Region Senior Resident Inspector, USNRC, St. Lucie Plant II DAS/PSL 8917-93 170033 9305i80328 9305i0 PDR  ADOCK    05000335 S                      PDR an FPL Group company
5N05TOONAAIYNWCa<ISTACTTGNTNOXGTTITIOSTINTTYNCS TNINNAGSINNT AI05TAOGCT,WAONKITTYA OO5050$.FACILITYNAME(1)DOCKETNUMBER(2)LERNUMBER(6)PAGE(3)St.LucieUnit1YEAR':0500033593EQUENTIAL NUMBER004.REVISIONUMBER000404TEXT(Ifmorespaceisrequired, useadditional NRCForm366A's)(1/)NoneAprevioussimilarLERatSt.Lucieinvolving adesignerrorfortheRPSwas:LER335-79-30 SteamGenerator LowLevelRPStripsetpoints lessthanTechnical Specifications duetoadesignermr.FPLFacsimile ofNRCForm366(6-89)}}
 
                                                                                                      ~
PPP  FPL FEOElmlo ol                                        L.S. tEUCLEAR REGULATORY COMMISSION                                APPROYOT ONE NCk 01 10 010I ENNPEE'NHNT NRC Form K6 EET PIATE 0 NAaE N PEN INEPCNTE TO CEPNCY WITH TI00 NfOIEAATlONCCATEC STINT (M9)
LICENSEE EVENT REPORT (LER)                                          INCEEET.>>0 HTE SONWNa CONNENTE SNONEPNO TAfaENEETTwIE To THE INOCla0 ANT PE PONTE NANAKINNT EAANCHTPANIAIANIANAENIPE IANATCNY WATPNarol. OC IPHE    Na To THE PPENWITTN SEOOC TON PNOECT o'110010PA Cf SCE Of NAMOEIENTPIEI OAXNT.WASPNeOTCPC OC ITNEL FACILITYNAME (1)                                                                                                DOCKET NUMBER (2)                      PAGE 3 St. Lucie Unit    1 050003351                                        0 4 (4)    Incorrect Reactor Coolant System Low Flow Trip Setpoint results in a condition prohibited by Technical Specifications due to a Design Control Inadequacy.
EVENT DATE (5)                LER NUMBER (6)                    REPORT DATE (7)                  OTHER FACILITIES INVOLVED(8)
MOMlH DAY YEAR YEAR S                         IAL                MONTH DAY        YEAR        FACILITYNAMES                          DOCKET NUMBER(S)
N/A                      05 000 0    4    09    9 3    9 3      0    0    4    00051093 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR:
N/A                      05000 OPERATING                  Check one or more of the followin      (11)
MODE (9) 20.402(b)                      20.405(c)                    50.73(a)(2)(iv)                            73.71(b)
POWER 20.405(a)(1 )(i)              50.36(c)(1)                  50.73(a)(2)(v)                              73.71(c)
LEVEL (10)                        20.405(a)(1 )(ii)              50.36(c)(2)                50.73(a)(2)(vii)                            OTHER (Specify in Abstract 20.405(a)(1)(iii)              50.73(a)(2)(i)              50.73(a)(2)(viii)(A)                          below and in Text 20.405(a)(1)(iv)                                            50.73(a)(2)(viii)(B)                          NRC Form 366A) 50.73(a)(2)(ii) 20.405(a)(1)(v)                50.73(a)(2)(iii)            50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER 12 NAME                                                                                                                      TELEP ONE NUMBER AREA CODE Robert J. Young, Shift Technical Advisor 4      0 7          465.3550 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13 MANUFAG- REPORTABLE                                                                    MANUFAC- REPORTABLE CAUSE SYSTEM COMPONENT                  TURER        TO NPRDS                CAUSE SYSTEM COMPONENT                              lURER                TO NPRDS I    I      I SUPPLEMENTAL REPORT EXPECTED 14                                                        EXPECTED                    MONIH              DAY YEAR SUBMISSION YES (Ifyes, complete EXPECTED SUBMISSION DATE)                                                        DATE (15)
ABSTRACT (Limit to 1400 spaces. i e. approximately fifteen single-space typewritten lines)          (1 6)
On April 9, 1993, St. Lucie Unit 1 was in Mode 6 when a typographical error was discovered by FPL Nuclear Engineering in a report used to determine the Reactor Protection System (RPS) low Reactor Coolant System (RCS) flow trip setpoint. Technical Specification 2.2.1, Table 2.2-1 states that the trip setpoint will be greater than or equal to 95% of design reactor coolant flow. The FPL Nuclear Engineering report, which described the conversion of pressure drop across the steam generators to the RPS low RCS flow trip setpoint, contained an incorrect constant. The report was subsequently transmitted to the plant staff and the Instrument and Control Department adjusted the RCS low flow setpoint. This error caused the setting of the RCS low flow trip setpoint to a value approximately 3% below the minimum 95% of design flow. This setpoint error existed since August 1988.
The root cause of this event was a design control inadequacy. A typographical error was made in the report transmitted to the plant staff. The error would have been discovered if the review process for the transmitted report had undergone an independent review. The Nuclear Engineering process currently in place prevents a similar event from occurring by requiring independent review of transmitted setpoints.
Corrective actions for this event: An engineering evaluation was performed that concluded that the operation of Unit 1 during this time period was within the bounds of the safety analysis. A review of the procedure used to determine the Unit 2 low RCS flow setpoint verified that it did not contain a similar error. After a review of internal records, Nuclear Engineering verified that no other Unit 1 or 2 RPS setpoint changes were transmitted to the plant in error. An engineering package was developed to provide the corrected calculations for determination of the RPS reactor coolant system low flow trip setpoint. Instrumentation and Control personnel will revise appropriate procedures and install the correct trip setpoint in the Unit 1 RPS prior to entering mode 2. Prior to discovery of this event, Engineering adopted a process requiring independent review of setpoints before transmittal to the plant staff.
FPL Facsimile of NRG Form 366 (6-89)
 
                                                                                                                                                        ~
FPL Fsaslnilsof                                    U.S. NUCLEAR REGULATORY COMMISSION                              Asswosf 0 oe Ixs ss ss C I ss NRC Form SEI
(&89)                                                                                                                      fxssus'ass  s LICENSEE EVENT REPORT (LER)                                      fSTAIATf0 OATCE N sf ilINSAONsf To COINET WITH siss SfCWNATTCN Cas EfCOON IfoUECTIsfs Isxs ssxswNe coNNENTs IKOANowoEsses N fsoNATE To TIO INcsxsss TEXT CONTINUATION                                          Ne ISAONTS NANACEsf NT fssANCH TASTCE ua NXXENTIuauATEXTT wAEINeTON. Oo ssssf Ne To TIO SNEIIwow IsoucwoN Twofcs ETI sseIsss asrscf os swNACEISNT Ne Tseofs. WANNesfsf oc ssexs FACILITYNAME (1)                                              DOCKET NUMBER (2)                LER NUMBER (6)                                            PAGE (3)
YEAR g EQUENTIAL                          REVISION St. Lucie Unit1                                                                      NUMBER                    NUMBER 0  500 0335              9 3            0        0      4            0            0  0 2            0 4 TEXT (lfmore spaceis required, use additional NRC Form 366A's) (1/)
On April 9, 1993, with Unit 1 in Mode 6, FPL Nuclear Engineering performed a review of the calculations that are contained in the St. Lucie Unit 1 Low Flow Trip Setpoint Calibration Guidelines.
The review was being performed to support a proposed change to the steam generator tube plugging criteria. During this review, a typographical error in a report that described conversion of pressure drop across the Steam Generators (EIIS:AB) to the Reactor Protection System (RPS) (EIIS:
JC) Reactor Coolant System (RCS) low flow trip setpoint was found. The error resulted in the calculation of a non-conservative setpoint with which the RPS creates an automatic reactor trip to protect against a loss of RCS flow. This error caused the RPS low RCS flow trip setpoint to be approximately 3 percent below the Technical Specification minimum of 95 percent of design flow.
In 1987 the report containing the incorrect information was sent to the plant staff to support a modification to the RPS. In August 1988, the report was referenced when the modification to the RPS was implemented and was used to modify plant procedures for the initial setting and subsequent monthly checks of this RPS low flow trip setpoint. This condition was discovered in April of 1993.
The root cause of this event was a design control inadequacy. A typographical error was made by FPL Nuclear Engineering in the transmittal of a calculated setpoint to the plant staff. During a transfer of information from an independently verified engineering calculation to a report, a transcription error caused a constant that converts pressure drop across the Steam Generators to the low RCS flow trip setpoint to be non-conservative. The incorrect report would have been discovered and corrected had the transmitted report to the plant staff received the same independent review that the original calculation had received. Prior to the discovery of this event, FPL Nuclear Engineering adopted the process for requiring independent review of all setpoints before transmittal to the plant staff.
This event is reportable under 10CFR50.73(a)(2)(i)(B), as "Any operation or condition prohibited by the plant's Technical Specifications." Technical Specification 2.2.1 requires that the RPS trip setpoint for RCS low flow be set at or above 95 percent of design flow (370,000 gpm). For cycles 9, 10 and 11 of Unit 1 operation, the RCS low flow trip was erroneously set at slightly higher than 92 percent of design flow.
The RCS low flow trip setpoint ensures that for a degradation of RCS flow resulting from analyzed transients, a reactor trip occurs to prevent departure from nucleate boiling ratio (DNBR) safety limits.
The process signal for this function is developed from four independent differential pressure channels which measure the pressure drop across the primary side of both Steam Generators. The total Steam Generator pressure drop is compared with the low RCS flow trip setpoint. If two channels indicate a flow which is less than the trip setpoint, an RPS trip signal is initiated.
FPL Facsimile of NRC Form 366 (6-89)
 
                                                                                                                                                                ~
FPL Facstmlo ol                                    U.S. NUCLEAR REGULATORY COMMrSS ION                                  , AAINorrocooNI$ $ $ $ oeror NRC Form S66                                                                                                                      cofrfoa rrfoeo
($ 89)                                                                                  oe TAIATTo ofvcrN ITN Ioefcfoc To ccoe$ v TATNooo ofrfvAACONcouococN UCENSEE EVENT REPORT (LER)                                        Iacra cTl $ 0 4 Ieoa foNwrfoccrrrNT o fccfrlooro IAATIENoeoNATc To Tto Iocofoo wo$ fafomo NANACT$C NT ONANCN reeTCA          ua  NOCIT AN IN$$ AATONv TEXT CONTINUATION                                          wANNIOTCN,oc $ 0$ $ a ANITo        llo f                          I ATNAwrovrIacucocN ffvoac $ $ $ Ioe ror$ cffICE of IIANAccoaNTAfo      $ $$ $ ccr,wANNrcrcfo oc Toooa FACILITYNAME (1)                                              DOCKET NUMBER (2)                  LER NUMBER (6)                                                  PAGE (3)
YEAR              EQUENTIAL -r REVISION St. Lucie Unit      1 NUMBER                  4 NUMBER 0500033593                                  0        0          4            0        0      0 3              0 4 TEXT (Ifmore spaceis required, use additional NRC Form 366A's) (17)
An evaluation (JPN-PSL1-SEFJ-93-006) was performed by FPL Engineering to determine the available safety analysis margin for the most limiting transients (loss of offsite power and loss of RCS flow) for which protection is provided by the RCS low flow trip. The results show that the approximate 3 percent setpoint error is sufficiently offset by available flow margin. Thus, violation of the DNBR limit for a loss of offsite power or a loss of RCS flow event would not have occurred if there hadbeen a degradation of RCS flow event during the time period that the setpoint error was in place. (A review of Unit 1 reactor trips showed that the RCS low flow trip function was not challenged during cycles 9,10 and 11. An additional review of actual operating conditions during cycles 9, 10, and 11 was performed to ensure that no other condition existed that would further aggravate the condition described in this LER).
The Reactor Coolant Pump (RCP)(EIIS:P) seized rotor event has been reanalyzed by the fuel vendor for a 4 percent reduction in design flow and the corresponding 4 percent reduction in the RCS low flow trip setpoint. The analysis shows that the acceptance criteria for the postulated RCP seized rotor event was not violated. Therefore, the health and safety of the public was not affected by this condition.
: 1. Prior to the discovery of this event, Nuclear Engineering proceduralized a review process to ensure the accuracy of setpoints and plant changes. This process requires an independent verification of setpoints and plant changes before transmittal to the plant staff, and would have detected the error described in this report.
: 2. Nuclear Engineering prepared an engineering evaluation and determined that operation of Unit 1 was bounded by the safety analyses for Cycles 9, 10, and 11.
: 3. Nuclear Engineering reviewed internal records and verified that no other Unit                            1  or 2 RPS setpoint changes were transmitted to the plant staff in error.
: 4. Nuclear Engineering reviewed the Unit 2 RCS Low Flow Trip Setpoint Determination procedure and verified that it did not use erroneous data.
: 5. A FPL engineering package was developed to document and transmit the corrected calculation for the Unit 1 RPS Iow RCS flow trip setpoint.
: 6. The I&C Department will revise procedures          1-0120050
                ~                                      and 1-1400050 to reflect the correct RCS low flow trip setpoints prior to Unit 1 entering Mode 2.
: 7. The I&C Department will make the RPS low RCS flow trip setpoint changes prior to Unit                                        1    entering Mode 2.
FPL Facsimile of NRC Form 366 (6-89)
 
                                                                                                                                                            ~
FPL F55cslrrllo ol                                  U.S. NUCLEAR REGULATORY COMMrSSION                                APAN5TITOCAO NCI $ 1 50 0505 NRC Form S6B                                                                                                                  fAASNS: IO005 LICENSEE EVENT REPORT (LER)                                      5 0TWAT To TAANNN05  II INSAONIC TO GTANAYW oil TIIS 005$ 0AAOON COTITCOON ISISN ST: 500 ITIS ICAINNo OONNANT0 NTOAIIONOTAAoCNTSTYAATS lo TIN INGTAYIS
                        ~
AIAIINICNTSNANAGSISNTSNANCHTNINaIAS IANATAIIINGAAATGNY TEXT CONTINUATION                                          WANNNTTGN.OG505$5 N05TOON AAIYNWCa<ISTACTTGNTNOXGTTITIOSTINTTYNCS TN INNAGSINNTAI05 TAOGCT, WAONKITTYAOO 5050$ .
FACILITYNAME (1)                                               DOCKET NUMBER (2)                 LER NUMBER (6)                                             PAGE (3)
YEAR ': EQUENTIAL NUMBER
                                                                                                                                . REVISIO NUMBER St. Lucie Unit  1 0  500 0335              9 3              0      0      4            0          0    0 4          0 4 TEXT (Ifmore spaceis required, use additional NRC Form 366A's) (1/)
None A previous similar LER at St. Lucie involving a design error for the RPS was:
LER 335-79-30     Steam Generator Low Level RPS trip setpoints less than Technical Specifications due to a design ermr.
FPL Facsimile of NRC Form 366 (6-89)}}

Latest revision as of 21:16, 29 October 2019

LER 93-004-00:on 930409,typo Discovered in Rept Used to Determine RPS Low RCS Flow Trip Setpoint.Error Existed Since Aug 1988.Caused by Design Control Inadequacy.Engineering Package Developed to Correct calculations.W/930510 Ltr
ML17228A158
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 05/10/1993
From: Sager D, Young R
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-93-129, LER-93-004-02, LER-93-4-2, NUDOCS 9305180328
Download: ML17228A158 (7)


Text

ACCELERANT DOCUMENT DISTRj: UTION SYSTEM REGULAT INFORMATION DISTRIBUTION STEM (RIDS)

ACCESSION NBR:9305180328 DOC.DATE: 93/05/10 NOTARIZED: NO DOCKET ¹ FACIL:50-335 St. Lucie Plant, Unit 1, Florida Power & Light Co. 05000335 AUTH. NAME AUTHOR AFFILIATION YOUNG,R.J. Florida Power & Light Co.

SAGER,D.A. Florida Power & Light Co.

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 93-004-00:on 930409,typo discovered in rept used to determine RPS low RCS flow trip setpoint.Error existed since D Aug 1988.Caused by design control inadequacy. Engineering package developed to correct calculations.W/930510 ltr.

DZSTRZSUTZON CODE: IE22T COPIES RECEIVED:LTR I ENCL / SIZE:

TITIE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL D PD2-2 LA 1 1 PD2-2 PD 1 1 NORRISgJ 1 1 D INTERNAL: ACNW 2 2 ACRS 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1, 1 NRR/DRCH/HOLB 1 1 NRR/DRIL/RPEB 1 1 NRR/DRSS/PRPB 2 2 NRR .DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 02 1 1 RES/DSIR/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: EG&G BRYCEPJ.H 2 2 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHY,G.A 1 . 1 NSIC POOREPW. 1 1 NUDOCS FULL TXT 1 1 D

D D

NOTE TO ALL"RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 32 ENCL 32

May 10, 1993 PP'f L-93-129 10 CFR 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Re: .St. Lucie Unit 1 Docket No. 50-335 Reportable Event: 93-004 Date of Event: April 9, 1993 Incorrect RCS Low Flow Trip Setpoint due to a Desi n Error The attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.

Very truly yours, 4A8a ~

D. A. ger Vice r sident St. Lu e Plant DAS/JWH/kw Attachment cc: Stewart D. Ebneter, Regional Administrator, USNRC Region Senior Resident Inspector, USNRC, St. Lucie Plant II DAS/PSL 8917-93 170033 9305i80328 9305i0 PDR ADOCK 05000335 S PDR an FPL Group company

~

PPP FPL FEOElmlo ol L.S. tEUCLEAR REGULATORY COMMISSION APPROYOT ONE NCk 01 10 010I ENNPEE'NHNT NRC Form K6 EET PIATE 0 NAaE N PEN INEPCNTE TO CEPNCY WITH TI00 NfOIEAATlONCCATEC STINT (M9)

LICENSEE EVENT REPORT (LER) INCEEET.>>0 HTE SONWNa CONNENTE SNONEPNO TAfaENEETTwIE To THE INOCla0 ANT PE PONTE NANAKINNT EAANCHTPANIAIANIANAENIPE IANATCNY WATPNarol. OC IPHE Na To THE PPENWITTN SEOOC TON PNOECT o'110010PA Cf SCE Of NAMOEIENTPIEI OAXNT.WASPNeOTCPC OC ITNEL FACILITYNAME (1) DOCKET NUMBER (2) PAGE 3 St. Lucie Unit 1 050003351 0 4 (4) Incorrect Reactor Coolant System Low Flow Trip Setpoint results in a condition prohibited by Technical Specifications due to a Design Control Inadequacy.

EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED(8)

MOMlH DAY YEAR YEAR S IAL MONTH DAY YEAR FACILITYNAMES DOCKET NUMBER(S)

N/A 05 000 0 4 09 9 3 9 3 0 0 4 00051093 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR:

N/A 05000 OPERATING Check one or more of the followin (11)

MODE (9) 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b)

POWER 20.405(a)(1 )(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c)

LEVEL (10) 20.405(a)(1 )(ii) 50.36(c)(2) 50.73(a)(2)(vii) OTHER (Specify in Abstract 20.405(a)(1)(iii) 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) below and in Text 20.405(a)(1)(iv) 50.73(a)(2)(viii)(B) NRC Form 366A) 50.73(a)(2)(ii) 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)

LICENSEE CONTACT FOR THIS LER 12 NAME TELEP ONE NUMBER AREA CODE Robert J. Young, Shift Technical Advisor 4 0 7 465.3550 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13 MANUFAG- REPORTABLE MANUFAC- REPORTABLE CAUSE SYSTEM COMPONENT TURER TO NPRDS CAUSE SYSTEM COMPONENT lURER TO NPRDS I I I SUPPLEMENTAL REPORT EXPECTED 14 EXPECTED MONIH DAY YEAR SUBMISSION YES (Ifyes, complete EXPECTED SUBMISSION DATE) DATE (15)

ABSTRACT (Limit to 1400 spaces. i e. approximately fifteen single-space typewritten lines) (1 6)

On April 9, 1993, St. Lucie Unit 1 was in Mode 6 when a typographical error was discovered by FPL Nuclear Engineering in a report used to determine the Reactor Protection System (RPS) low Reactor Coolant System (RCS) flow trip setpoint. Technical Specification 2.2.1, Table 2.2-1 states that the trip setpoint will be greater than or equal to 95% of design reactor coolant flow. The FPL Nuclear Engineering report, which described the conversion of pressure drop across the steam generators to the RPS low RCS flow trip setpoint, contained an incorrect constant. The report was subsequently transmitted to the plant staff and the Instrument and Control Department adjusted the RCS low flow setpoint. This error caused the setting of the RCS low flow trip setpoint to a value approximately 3% below the minimum 95% of design flow. This setpoint error existed since August 1988.

The root cause of this event was a design control inadequacy. A typographical error was made in the report transmitted to the plant staff. The error would have been discovered if the review process for the transmitted report had undergone an independent review. The Nuclear Engineering process currently in place prevents a similar event from occurring by requiring independent review of transmitted setpoints.

Corrective actions for this event: An engineering evaluation was performed that concluded that the operation of Unit 1 during this time period was within the bounds of the safety analysis. A review of the procedure used to determine the Unit 2 low RCS flow setpoint verified that it did not contain a similar error. After a review of internal records, Nuclear Engineering verified that no other Unit 1 or 2 RPS setpoint changes were transmitted to the plant in error. An engineering package was developed to provide the corrected calculations for determination of the RPS reactor coolant system low flow trip setpoint. Instrumentation and Control personnel will revise appropriate procedures and install the correct trip setpoint in the Unit 1 RPS prior to entering mode 2. Prior to discovery of this event, Engineering adopted a process requiring independent review of setpoints before transmittal to the plant staff.

FPL Facsimile of NRG Form 366 (6-89)

~

FPL Fsaslnilsof U.S. NUCLEAR REGULATORY COMMISSION Asswosf 0 oe Ixs ss ss C I ss NRC Form SEI

(&89) fxssus'ass s LICENSEE EVENT REPORT (LER) fSTAIATf0 OATCE N sf ilINSAONsf To COINET WITH siss SfCWNATTCN Cas EfCOON IfoUECTIsfs Isxs ssxswNe coNNENTs IKOANowoEsses N fsoNATE To TIO INcsxsss TEXT CONTINUATION Ne ISAONTS NANACEsf NT fssANCH TASTCE ua NXXENTIuauATEXTT wAEINeTON. Oo ssssf Ne To TIO SNEIIwow IsoucwoN Twofcs ETI sseIsss asrscf os swNACEISNT Ne Tseofs. WANNesfsf oc ssexs FACILITYNAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

YEAR g EQUENTIAL REVISION St. Lucie Unit1 NUMBER NUMBER 0 500 0335 9 3 0 0 4 0 0 0 2 0 4 TEXT (lfmore spaceis required, use additional NRC Form 366A's) (1/)

On April 9, 1993, with Unit 1 in Mode 6, FPL Nuclear Engineering performed a review of the calculations that are contained in the St. Lucie Unit 1 Low Flow Trip Setpoint Calibration Guidelines.

The review was being performed to support a proposed change to the steam generator tube plugging criteria. During this review, a typographical error in a report that described conversion of pressure drop across the Steam Generators (EIIS:AB) to the Reactor Protection System (RPS) (EIIS:

JC) Reactor Coolant System (RCS) low flow trip setpoint was found. The error resulted in the calculation of a non-conservative setpoint with which the RPS creates an automatic reactor trip to protect against a loss of RCS flow. This error caused the RPS low RCS flow trip setpoint to be approximately 3 percent below the Technical Specification minimum of 95 percent of design flow.

In 1987 the report containing the incorrect information was sent to the plant staff to support a modification to the RPS. In August 1988, the report was referenced when the modification to the RPS was implemented and was used to modify plant procedures for the initial setting and subsequent monthly checks of this RPS low flow trip setpoint. This condition was discovered in April of 1993.

The root cause of this event was a design control inadequacy. A typographical error was made by FPL Nuclear Engineering in the transmittal of a calculated setpoint to the plant staff. During a transfer of information from an independently verified engineering calculation to a report, a transcription error caused a constant that converts pressure drop across the Steam Generators to the low RCS flow trip setpoint to be non-conservative. The incorrect report would have been discovered and corrected had the transmitted report to the plant staff received the same independent review that the original calculation had received. Prior to the discovery of this event, FPL Nuclear Engineering adopted the process for requiring independent review of all setpoints before transmittal to the plant staff.

This event is reportable under 10CFR50.73(a)(2)(i)(B), as "Any operation or condition prohibited by the plant's Technical Specifications." Technical Specification 2.2.1 requires that the RPS trip setpoint for RCS low flow be set at or above 95 percent of design flow (370,000 gpm). For cycles 9, 10 and 11 of Unit 1 operation, the RCS low flow trip was erroneously set at slightly higher than 92 percent of design flow.

The RCS low flow trip setpoint ensures that for a degradation of RCS flow resulting from analyzed transients, a reactor trip occurs to prevent departure from nucleate boiling ratio (DNBR) safety limits.

The process signal for this function is developed from four independent differential pressure channels which measure the pressure drop across the primary side of both Steam Generators. The total Steam Generator pressure drop is compared with the low RCS flow trip setpoint. If two channels indicate a flow which is less than the trip setpoint, an RPS trip signal is initiated.

FPL Facsimile of NRC Form 366 (6-89)

~

FPL Facstmlo ol U.S. NUCLEAR REGULATORY COMMrSS ION , AAINorrocooNI$ $ $ $ oeror NRC Form S66 cofrfoa rrfoeo

($ 89) oe TAIATTo ofvcrN ITN Ioefcfoc To ccoe$ v TATNooo ofrfvAACONcouococN UCENSEE EVENT REPORT (LER) Iacra cTl $ 0 4 Ieoa foNwrfoccrrrNT o fccfrlooro IAATIENoeoNATc To Tto Iocofoo wo$ fafomo NANACT$C NT ONANCN reeTCA ua NOCIT AN IN$$ AATONv TEXT CONTINUATION wANNIOTCN,oc $ 0$ $ a ANITo llo f I ATNAwrovrIacucocN ffvoac $ $ $ Ioe ror$ cffICE of IIANAccoaNTAfo $ $$ $ ccr,wANNrcrcfo oc Toooa FACILITYNAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

YEAR EQUENTIAL -r REVISION St. Lucie Unit 1 NUMBER 4 NUMBER 0500033593 0 0 4 0 0 0 3 0 4 TEXT (Ifmore spaceis required, use additional NRC Form 366A's) (17)

An evaluation (JPN-PSL1-SEFJ-93-006) was performed by FPL Engineering to determine the available safety analysis margin for the most limiting transients (loss of offsite power and loss of RCS flow) for which protection is provided by the RCS low flow trip. The results show that the approximate 3 percent setpoint error is sufficiently offset by available flow margin. Thus, violation of the DNBR limit for a loss of offsite power or a loss of RCS flow event would not have occurred if there hadbeen a degradation of RCS flow event during the time period that the setpoint error was in place. (A review of Unit 1 reactor trips showed that the RCS low flow trip function was not challenged during cycles 9,10 and 11. An additional review of actual operating conditions during cycles 9, 10, and 11 was performed to ensure that no other condition existed that would further aggravate the condition described in this LER).

The Reactor Coolant Pump (RCP)(EIIS:P) seized rotor event has been reanalyzed by the fuel vendor for a 4 percent reduction in design flow and the corresponding 4 percent reduction in the RCS low flow trip setpoint. The analysis shows that the acceptance criteria for the postulated RCP seized rotor event was not violated. Therefore, the health and safety of the public was not affected by this condition.

1. Prior to the discovery of this event, Nuclear Engineering proceduralized a review process to ensure the accuracy of setpoints and plant changes. This process requires an independent verification of setpoints and plant changes before transmittal to the plant staff, and would have detected the error described in this report.
2. Nuclear Engineering prepared an engineering evaluation and determined that operation of Unit 1 was bounded by the safety analyses for Cycles 9, 10, and 11.
3. Nuclear Engineering reviewed internal records and verified that no other Unit 1 or 2 RPS setpoint changes were transmitted to the plant staff in error.
4. Nuclear Engineering reviewed the Unit 2 RCS Low Flow Trip Setpoint Determination procedure and verified that it did not use erroneous data.
5. A FPL engineering package was developed to document and transmit the corrected calculation for the Unit 1 RPS Iow RCS flow trip setpoint.
6. The I&C Department will revise procedures 1-0120050

~ and 1-1400050 to reflect the correct RCS low flow trip setpoints prior to Unit 1 entering Mode 2.

7. The I&C Department will make the RPS low RCS flow trip setpoint changes prior to Unit 1 entering Mode 2.

FPL Facsimile of NRC Form 366 (6-89)

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AIAIINICNTSNANAGSISNTSNANCHTNINaIAS IANATAIIINGAAATGNY TEXT CONTINUATION WANNNTTGN.OG505$5 N05TOON AAIYNWCa<ISTACTTGNTNOXGTTITIOSTINTTYNCS TN INNAGSINNTAI05 TAOGCT, WAONKITTYAOO 5050$ .

FACILITYNAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

YEAR ': EQUENTIAL NUMBER

. REVISIO NUMBER St. Lucie Unit 1 0 500 0335 9 3 0 0 4 0 0 0 4 0 4 TEXT (Ifmore spaceis required, use additional NRC Form 366A's) (1/)

None A previous similar LER at St. Lucie involving a design error for the RPS was:

LER 335-79-30 Steam Generator Low Level RPS trip setpoints less than Technical Specifications due to a design ermr.

FPL Facsimile of NRC Form 366 (6-89)