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| issue date = 04/22/1988
| issue date = 04/22/1988
| title = Special Rept 2-SR-88-003:on 880324,radioactive Gaseous Effluent Monitor Inoperable for More than 72 H.Authorized Work Document Issued to Troubleshoot & Rework/Replace Components to Correct Low Flow Alarms
| title = Special Rept 2-SR-88-003:on 880324,radioactive Gaseous Effluent Monitor Inoperable for More than 72 H.Authorized Work Document Issued to Troubleshoot & Rework/Replace Components to Correct Low Flow Alarms
| author name = HAYNES J G
| author name = Haynes J
| author affiliation = ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
| author affiliation = ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
| addressee name =  
| addressee name =  
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:gC CZMRATZD DISrRIBUTION MMONSYRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:8805020149 DOC.DATE: 88/04/22 NOTARIZED:
{{#Wiki_filter:gC CZMRATZD         DISrRIBUTION       MMONSYRATION                     SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
NO DOCKET I FACIL:STN-50-529 Palo Verde Nuclear Station, Unit 2, Arizona Publi 05000529 AUTH.NAME AUTHOR AFFILIATION HAYNES,J.G.
ACCESSION NBR:8805020149     DOC.DATE: 88/04/22             NOTARIZED: NO       DOCKET I FACIL:STN-50-529 Palo Verde Nuclear Station,             Unit 2, Arizona Publi 05000529 AUTH. NAME         AUTHOR AFFILIATION HAYNES,J.G.       Arizona Nuclear Power Project (formerly Arizona Public Serv RECIP.NAME         RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
Arizona Nuclear Power Project (formerly Arizona Public Serv RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)


==SUBJECT:==
==SUBJECT:==
Special Rept 2-SR-88-003:on 880324,radioactive gaseous effluent monitor inoperable for more than 72 h.DISTRIBUTION CODE..IE22D COPIES RECEIVED..LTR l ENCL g SIZE.~TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.NOTES:Standardized plant.I 05000529 RECIPIENT ID CODE/NAME PD5 LA LICITRA,E INTERNAL: ACRS MICHELSON=AEOD/DOA AEOD/DSP/ROAB ARM/DCTS/DAB NRR/DEST/ADS 7E NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB 8D NRR/DEST/SGB 8D NRR/DLPQ/QAB 10 NRR/DREP/RAB 10 DE/EIB RGN5 FILE 01 EXTERNAL: EG&G GROH,M H ST LOBBY WARD NRC PDR NSIC MAYS,G NOTES: COPIES LTTR ENCL 1 1 1 1 1 1 1 1 2 2 1 1 1 0 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 4 4 1 1 1 1 1 1 1 1 RECIPIENT'D CODE/NAME'D5 PD DAVIS,M ACRS MOELLER AEOD/DS P/NAS AEOD/DSP/TPAB DEDRO NRR/DEST/CEB 8H NRR/DEST/ICSB 7 NRR/DEST/MTB 9H NRR/DEST/RSB 8E NRR/DLPQ/HFB 10 NRR/DOEA/EAB ll NRR/DREP/RPB 10 NRR/PMAS/ILRB12 RES TELFORD,J RES/DRPS DIR FORD BLDG HOY,A LPDR NSIC HARRIS,J COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 A TOTAL NUMBER OF COPIES REQUIRED: LTTR 47 ENCL 46  
Special Rept 2-SR-88-003:on 880324,radioactive gaseous effluent monitor inoperable for more than 72 h.
DISTRIBUTION CODE..IE22D COPIES RECEIVED..LTR l ENCL TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.
g SIZE. ~              I NOTES:Standardized   plant.                                                       05000529 RECIPIENT       COPIES          RECIPIENT          'D COPIES ID CODE/NAME     LTTR ENCL          CODE/NAME'D5 LTTR ENCL PD5 LA               1    1          PD                        1    1 LICITRA,E           1    1    DAVIS,M                        1    1 INTERNAL: ACRS MICHELSON   =
1    1    ACRS MOELLER                  2    2 AEOD/DOA             1    1    AEOD/DS P/NAS                  1    1 AEOD/DSP/ROAB       2    2    AEOD/DSP/TPAB                  1    1 ARM/DCTS/DAB         1    1    DEDRO                          1    1 NRR/DEST/ADS 7E     1    0    NRR/DEST/CEB 8H                1    1 NRR/DEST/ESB 8D     1    1    NRR/DEST/ICSB 7                1    1 NRR/DEST/MEB 9H       1    1    NRR/DEST/MTB 9H                1    1 NRR/DEST/PSB 8D       1    1    NRR/DEST/RSB 8E                1    1 NRR/DEST/SGB 8D NRR/DLPQ/QAB 10 NRR/DREP/RAB 10 1
1 1
1 1
1 NRR/DLPQ/HFB 10 NRR/DOEA/EAB NRR/DREP/RPB 10 ll  1 1
2 1
1 2
1   1     NRR/PMAS/ILRB12                1     1 1   1     RES TELFORD,J                  1     1 DE/EIB          1   1     RES/DRPS DIR                  1     1 RGN5    FILE  01    1   1 EXTERNAL: EG&G GROH,M            4    4    FORD BLDG HOY,A                1     1 H ST LOBBY WARD      1   1     LPDR                          1     1 NRC PDR              1   1     NSIC HARRIS,J                  1     1 NSIC MAYS,G          1   1 NOTES:                            1   1 A
TOTAL NUMBER OF COPIES REQUIRED: LTTR       47     ENCL         46


Arizona Nuclear Power Project P,O, BOX 52034~PHOENIX, ARIZONA 85072-2034 192-00370-JGH/TDS/JEM Apri 1 22, 1988 U.S.Nuclear Regulatory Commission NRC Document Control Desk Washington, D.C.20555  
Arizona Nuclear Power Project P,O, BOX 52034 ~ PHOENIX, ARIZONA85072-2034 192-00370-JGH/TDS/JEM Apri 1 22, 1988 U. S. Nuclear Regulatory Commission NRC Document Control Desk Washington, D.C. 20555


==Dear Sirs:==
==Dear Sirs:==


==Subject:==
==Subject:==
Palo Verde Nuclear Generating Station (PVNGS)Unit 2 Docket No.STN 50-529 (License No.NPF-51)Special Report 2-SR-88-003 File: 88-020-404 Attached please find Special Report 2-SR-88-003 prepared and submitted pursuant to Technical Specification 3.3.3.8 ACTION 42b and Technical Specification 6.9.2.This report discusses a radiation monitoring unit inoperable for greater than 72 hours.If you have any questio'ns, please contact T.D.Shriver, Compliance Manager at (602)393-2521, Very tru y yours, vA,'-~J.G.Ha es Vice President Nuclear Production JGH/TDS/JEM/kj Attachment cc: 0.H.DeHichele (all w/a)E.E.Van Brunt, Jr.J.B.Hartin T.J.Polich E.A.Licitra A.C.Gehr INPO Records Center SS05I)20149 SS0422 PDt", ADOCK 05000529 DCD'
Palo Verde Nuclear Generating Station (PVNGS)
Unit 2 Docket No. STN 50-529 (License No. NPF-51)
Special Report 2-SR-88-003 File: 88-020-404 Attached please find Special Report 2-SR-88-003 prepared and submitted pursuant to Technical Specification 3.3.3.8 ACTION 42b and Technical Specification 6.9.2. This report discusses a radiation monitoring unit inoperable for greater than 72 hours.
If you have any questio'ns,     please contact T. D. Shriver, Compliance Manager at (602) 393-2521, Very   tru y yours, vA,'-
J. G. Ha
                                                                            ~
es Vice President Nuclear Production JGH/TDS/JEM/kj Attachment cc:   0. H. DeHichele           (all   w/a)
E. E. Van Brunt,   Jr.
J. B. Hartin T. J. Polich E. A. Licitra A. C. Gehr INPO Records Center SS05I)20149 SS0422 PDt",   ADOCK 05000529 '
DCD


PALO VERDE NUCLEAR GENERATING STATION Radiation Monitoring Unit Inoperable for Greater Than 72 Hours License No.NPF-51 Docket No.-STN 50-529 Special Report No.2-SR-88-004 This Special Report is being submitted pursuant to Technical Specification (TS)3.3.3.8 ACTION 42b and Technical Specificati'on 6.9.2 to report an event in which the Radioactive Gaseous Effluent Monitor (Plant Vent High Range.Gaseous Activity Monitor RU-144)was inoperable for greater than 72 hours.The 72 hour limit for returning to operability was exceeded at approximately 1430 HST on March 27, 1988.Pursuant to Technical Specification 3.3.3.8 ACTION 42a the Preplanned Alternate Sampling Program was initiated to monitor the Plant Vent System.At approximately 1430 HST on March 24, 1988, Palo Verde Unit 2 was shutdown for refueling'with the core offloaded into the Spent Fuel Pool when the Plant Ven't System Radioactive Gaseous Effluent Monitors, low range RU-143 and high range RU-144, were declared inoperable for implementation of a Plant Change'ackage (PCP)to improve the reliability of the radiation monitoring system.Monitors RU-143 and RU-144 work as a pair with RU-143 being the low range monitor and RU-144 being the high range monitor.Normal configuration consists of RU-143 operating and RU-144 in standby.When RU-143 reaches a predetermined point, RU-144 starts and RU-143 goes to standby.RU-144 is provided for tracking of postulated accident releases.Since RU-143 and RU-144 work in tandem, both monitors must be declared inoperable if the other is out of service.An authorized work document was issued to implement the PCP for RU-143 and to change its default parameters.
PALO VERDE NUCLEAR GENERATING STATION Radiation Monitoring Unit Inoperable for Greater Than   72 Hours License No. NPF-51 Docket No.- STN 50-529 Special Report No. 2-SR-88-004 This Special Report is being submitted pursuant to Technical Specification (TS) 3.3.3.8 ACTION 42b and Technical Specificati'on 6.9.2 to report an event in which the Radioactive Gaseous Effluent Monitor (Plant Vent High Range .
In the event of a Loss of Power (LOP), the.default parameter provides conservative setpoints upon restoration of.power.The new default parameter will improve the reliability of RU-143 by assuring that the setpoints provide sufficient operating margin to minimize spurious alarms but are still conservative to ensure that the limits of TS 3.11.2.1 are not exceeded.After the new software was installed, which incorporate the new default values, the proper flow rates could not be achieved.An authorized work document was issued to troubleshoot, rework, replace components to correct the problem.It was identified that there were incorrect flow values in the software.The original software was reinstalled, appropriate surveillance testing performed satisfactorily, and RU-143 and RU-144 were returned to an operable status at 0330 on April 6, 1988.The moni,tors were inoperable for approximately 12 days and 13 hours.The new revision software is planned to be ready for installation by April 26, 1988.=After appropriate retesting and surveillance testing it is planned to have RU-143 and RU-144 operable with the new software by April 29, 1988.}}
Gaseous Activity Monitor RU-144) was inoperable for greater than 72 hours.
The 72 hour limit for returning to operability was exceeded at approximately 1430 HST on March 27, 1988. Pursuant to Technical Specification 3.3.3.8 ACTION 42a the Preplanned Alternate Sampling Program was initiated to monitor the Plant Vent System.
At approximately 1430 HST on March 24, 1988, Palo Verde Unit 2 was shutdown for refueling 'with the core offloaded into the Spent Fuel Pool when the Plant Ven't System Radioactive Gaseous Effluent Monitors, low range RU-143 and high range RU-144, were declared inoperable for implementation of a Plant Change (PCP) to improve the reliability of the radiation monitoring system.   'ackage Monitors RU-143 and RU-144 work as a pair with RU-143 being the low range monitor and RU-144 being the high range monitor. Normal configuration consists of RU-143 operating and RU-144 in standby. When RU-143 reaches a predetermined point, RU-144 starts and RU-143 goes to standby. RU-144 is provided for tracking of postulated accident releases. Since RU-143 and RU-144 work in tandem, both monitors must be declared inoperable is out of service.
if  the other An authorized work document was issued to implement the PCP for RU-143 and to change   its default parameters. In the event of a Loss of Power (LOP), the .
default parameter provides conservative setpoints upon restoration of. power.
The new default parameter will improve the reliability of RU-143 by assuring that the setpoints provide sufficient operating margin to minimize spurious alarms but are still conservative to ensure that the limits of TS 3. 11.2. 1 are not exceeded.
After the   new software was installed, which incorporate the new default values, the proper flow rates could not be achieved. An authorized work document was issued to troubleshoot, rework, replace components to correct the problem. It was identified that there were incorrect flow values in the software. The original software was reinstalled, appropriate surveillance testing performed satisfactorily, and RU-143 and RU-144 were returned to an operable status at 0330 on April 6, 1988. The moni,tors were inoperable for approximately 12 days and 13 hours.
The new   revision software is planned to be ready for installation by April 26, 1988. After appropriate retesting and surveillance testing
      =
it is planned to have RU-143 and RU-144 operable with the new software by April 29, 1988.}}

Latest revision as of 10:00, 29 October 2019

Special Rept 2-SR-88-003:on 880324,radioactive Gaseous Effluent Monitor Inoperable for More than 72 H.Authorized Work Document Issued to Troubleshoot & Rework/Replace Components to Correct Low Flow Alarms
ML17303B078
Person / Time
Site: Palo Verde Arizona Public Service icon.png
Issue date: 04/22/1988
From: Haynes J
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
192-00370-JGH-J, 192-370-JGH-J, 2-SR-88-003, 2-SR-88-3, NUDOCS 8805020149
Download: ML17303B078 (6)


Text

gC CZMRATZD DISrRIBUTION MMONSYRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:8805020149 DOC.DATE: 88/04/22 NOTARIZED: NO DOCKET I FACIL:STN-50-529 Palo Verde Nuclear Station, Unit 2, Arizona Publi 05000529 AUTH. NAME AUTHOR AFFILIATION HAYNES,J.G. Arizona Nuclear Power Project (formerly Arizona Public Serv RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Special Rept 2-SR-88-003:on 880324,radioactive gaseous effluent monitor inoperable for more than 72 h.

DISTRIBUTION CODE..IE22D COPIES RECEIVED..LTR l ENCL TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.

g SIZE. ~ I NOTES:Standardized plant. 05000529 RECIPIENT COPIES RECIPIENT 'D COPIES ID CODE/NAME LTTR ENCL CODE/NAME'D5 LTTR ENCL PD5 LA 1 1 PD 1 1 LICITRA,E 1 1 DAVIS,M 1 1 INTERNAL: ACRS MICHELSON =

1 1 ACRS MOELLER 2 2 AEOD/DOA 1 1 AEOD/DS P/NAS 1 1 AEOD/DSP/ROAB 2 2 AEOD/DSP/TPAB 1 1 ARM/DCTS/DAB 1 1 DEDRO 1 1 NRR/DEST/ADS 7E 1 0 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB 8D 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D NRR/DLPQ/QAB 10 NRR/DREP/RAB 10 1

1 1

1 1

1 NRR/DLPQ/HFB 10 NRR/DOEA/EAB NRR/DREP/RPB 10 ll 1 1

2 1

1 2

1 1 NRR/PMAS/ILRB12 1 1 1 1 RES TELFORD,J 1 1 DE/EIB 1 1 RES/DRPS DIR 1 1 RGN5 FILE 01 1 1 EXTERNAL: EG&G GROH,M 4 4 FORD BLDG HOY,A 1 1 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC HARRIS,J 1 1 NSIC MAYS,G 1 1 NOTES: 1 1 A

TOTAL NUMBER OF COPIES REQUIRED: LTTR 47 ENCL 46

Arizona Nuclear Power Project P,O, BOX 52034 ~ PHOENIX, ARIZONA85072-2034 192-00370-JGH/TDS/JEM Apri 1 22, 1988 U. S. Nuclear Regulatory Commission NRC Document Control Desk Washington, D.C. 20555

Dear Sirs:

Subject:

Palo Verde Nuclear Generating Station (PVNGS)

Unit 2 Docket No. STN 50-529 (License No. NPF-51)

Special Report 2-SR-88-003 File: 88-020-404 Attached please find Special Report 2-SR-88-003 prepared and submitted pursuant to Technical Specification 3.3.3.8 ACTION 42b and Technical Specification 6.9.2. This report discusses a radiation monitoring unit inoperable for greater than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

If you have any questio'ns, please contact T. D. Shriver, Compliance Manager at (602) 393-2521, Very tru y yours, vA,'-

J. G. Ha

~

es Vice President Nuclear Production JGH/TDS/JEM/kj Attachment cc: 0. H. DeHichele (all w/a)

E. E. Van Brunt, Jr.

J. B. Hartin T. J. Polich E. A. Licitra A. C. Gehr INPO Records Center SS05I)20149 SS0422 PDt", ADOCK 05000529 '

DCD

PALO VERDE NUCLEAR GENERATING STATION Radiation Monitoring Unit Inoperable for Greater Than 72 Hours License No. NPF-51 Docket No.- STN 50-529 Special Report No. 2-SR-88-004 This Special Report is being submitted pursuant to Technical Specification (TS) 3.3.3.8 ACTION 42b and Technical Specificati'on 6.9.2 to report an event in which the Radioactive Gaseous Effluent Monitor (Plant Vent High Range .

Gaseous Activity Monitor RU-144) was inoperable for greater than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

The 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> limit for returning to operability was exceeded at approximately 1430 HST on March 27, 1988. Pursuant to Technical Specification 3.3.3.8 ACTION 42a the Preplanned Alternate Sampling Program was initiated to monitor the Plant Vent System.

At approximately 1430 HST on March 24, 1988, Palo Verde Unit 2 was shutdown for refueling 'with the core offloaded into the Spent Fuel Pool when the Plant Ven't System Radioactive Gaseous Effluent Monitors, low range RU-143 and high range RU-144, were declared inoperable for implementation of a Plant Change (PCP) to improve the reliability of the radiation monitoring system. 'ackage Monitors RU-143 and RU-144 work as a pair with RU-143 being the low range monitor and RU-144 being the high range monitor. Normal configuration consists of RU-143 operating and RU-144 in standby. When RU-143 reaches a predetermined point, RU-144 starts and RU-143 goes to standby. RU-144 is provided for tracking of postulated accident releases. Since RU-143 and RU-144 work in tandem, both monitors must be declared inoperable is out of service.

if the other An authorized work document was issued to implement the PCP for RU-143 and to change its default parameters. In the event of a Loss of Power (LOP), the .

default parameter provides conservative setpoints upon restoration of. power.

The new default parameter will improve the reliability of RU-143 by assuring that the setpoints provide sufficient operating margin to minimize spurious alarms but are still conservative to ensure that the limits of TS 3. 11.2. 1 are not exceeded.

After the new software was installed, which incorporate the new default values, the proper flow rates could not be achieved. An authorized work document was issued to troubleshoot, rework, replace components to correct the problem. It was identified that there were incorrect flow values in the software. The original software was reinstalled, appropriate surveillance testing performed satisfactorily, and RU-143 and RU-144 were returned to an operable status at 0330 on April 6, 1988. The moni,tors were inoperable for approximately 12 days and 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br />.

The new revision software is planned to be ready for installation by April 26, 1988. After appropriate retesting and surveillance testing

=

it is planned to have RU-143 and RU-144 operable with the new software by April 29, 1988.