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| {{#Wiki_filter:i1 I/"p ACCELERATED DISTRIBUTION DEMONSTRATION SYSTEM REGULATORY IN FORMATION DISTRX BUTION SYSTEM (RI DS)ACCESSXON NBR:9008300181 DOC.DATE: 90/08/21 NOTARIZED: | | {{#Wiki_filter:ACCELERATED DISTRIBUTION DEMONSTRATION SYSTEM i1 I |
| NO DOCKET FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH.NAME AUTHOR AFFILIATION LEVINE,J.M. | | /"p REGULATORY IN FORMATION DISTRX BUTION SYSTEM (RI DS ) |
| Arizona Public Service Co.(formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk) | | ACCESSXON NBR:9008300181 DOC.DATE: 90/08/21 NOTARIZED: NO DOCKET FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH. NAME AUTHOR AFFILIATION LEVINE,J.M. Arizona Public Service Co. (formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk) |
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| ==SUBJECT:== | | ==SUBJECT:== |
| Special Rept 1-SR-90-005:on 900725,performance of loose parts detection sys might result in alarm condition. | | Special Rept 1-SR-90-005:on 900725,performance of loose parts detection sys might result in alarm condition. |
| DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR U ENCL L SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), incident Rpt, etc.NOTES'TANDARDIZED PLANT RECXPIENT ID CODE/NAME PD5 LA PETERSON,S. | | DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR ENCL L SIZE: |
| INTERNAL: ACNW AEOD/DOA AEOD/ROAB/DS P NRR/DET/EMEB9H3 NRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICB 7E NRR/DST/SRXB 8E RES/DSIR/EIB EXTERNAL EG&G BRYCE i J H LPDR NSIC MAYS,G NUDOCS FULL TXT NOTES: COPIES LTTR ENCL 1 1 1 1 2.2 1 1 2 2 1 1 1 1 2 2 1 1 1 1 1 1 3 3 1 1 1 1 1 1 1 1 RECIPIENT XD CODE/NAME PD5 PD TRAMMELL,C. | | Uincident TITLE: 50.73/50.9 Licensee Event Report (LER), Rpt, etc. |
| ACRS AEOD/DSP/TPAB NRR/DET/ECMB 9H NRR/DLPQ/LHFB1 1 NRR/DOEA/OEAB11 NRR/DST/SELB 8D D LB8D1 EG 02 FILE 01 L ST LOBBY WARD NRC PDR NSXC MURPHY i G~A COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1'.1 1 1 1 1 1 05000528/A D D NOTE TO ALL"RIDS" RECIPIENTS:
| | NOTES 'TANDARDIZED PLANT 05000528 / |
| D D PLEASE HELP US TO REDUCE iVASTE!CONTACT.THE DOCUb!ENT CONTROL DESK, ROOil PI-37 (EXT.2N79)TO ELIilINATE YOUR NAiiIE FROiil DISTRII)UTION LISTS FOR DOCUiIENTS YOU DON'T NEED!TOTAL NUMBER OF COPIES REQUIRED: LTTR 36 ENCL 36 t 1 Arizona Public Service Company PALO VERDE NUCLEAR GENERATING STATION P.O, BOX 52034~PHOENIX, ARIZONA 85072-2034 JAMES M, LEVINE VICE PAESIDEN7 NDCt.EAR PRDDUC7ION 192-00686-JML/TRB/SBJ August 21, 1990 U.S.Nuclear Regulatory Commission NRC Document Control Desk'Pl-37 Washington, D.C.,20555
| | RECXPIENT COPIES RECIPIENT COPIES A ID CODE/NAME LTTR ENCL XD CODE/NAME LTTR ENCL D |
| | PD5 LA 1 1 PD5 PD 1 1 PETERSON,S. 1 1 TRAMMELL,C. 1 1 INTERNAL: ACNW 2 .2 ACRS 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DS P 2 2 NRR/DET/ECMB 9H 1 1 NRR/DET/EMEB9H3 1 1 NRR/DLPQ/LHFB1 1 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB11 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1 EXTERNAL NRR/DST/SICB 7E NRR/DST/SRXB 8E RES/DSIR/EIB EG&G BRYCE i J H 1 |
| | 1 1 |
| | 3 1 |
| | 1 1 |
| | 3 EG D |
| | FILE LB8D1 L ST LOBBY WARD 02 01 1'. |
| | 1 1 |
| | 1 1 |
| | 1 1 |
| | LPDR 1 1 NRC PDR 1 1 NSIC MAYS,G 1 1 NSXC MURPHY i G ~ A 1 1 NUDOCS FULL TXT 1 1 NOTES: 1 1 D |
| | D D |
| | NOTE TO ALL "RIDS" RECIPIENTS: |
| | PLEASE HELP US TO REDUCE iVASTE! CONTACT. THE DOCUb!ENT CONTROL DESK, ROOil PI-37 (EXT. 2N79) TO ELIilINATEYOUR NAiiIE FROiil DISTRII)UTION LISTS FOR DOCUiIENTS YOU DON'T NEED! |
| | TOTAL NUMBER OF COPIES REQUIRED: LTTR 36 ENCL 36 |
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| ==Dear Sirs:== | | t 1 |
| Subj ect: Palo Verde Nuclear Generating Station (PVNGS)Unit 1 Docket No.STN 50-528 (License.No.NPF-41)Special Report 1-SR-90-005 File: 90-020-404 Attached please find Special Report 1-SR-90-005 which is being voluntarily submitted to describe the performance of the Unit 1 Loose Parts Detection System.If you have any questions on this matter, please contact T.R.Bradish, Compliance Manager, at (602)393-2521.Very truly yours, JML/TRB/SBJ/dmn Attachment (all w/attachment) cc: W.F.Conway J.B.Martin C.M.Tramell D.H.Coe A.C.Gehr A.H.Gutterman INPO Records Center (i I I h It'~1 I ( | | |
| PALO VERDE NUCLEAR GENERATING STATION UNIT 1 License No.NPF-41 Docket No.50-528 Special Report 1-SR-90-005 Initial Conditions: | | Arizona Public Service Company PALO VERDE NUCLEAR GENERATING STATION P.O, BOX 52034 ~ PHOENIX, ARIZONA 85072-2034 JAMES M, LEVINE 192-00686-JML/TRB/SBJ VICE PAESIDEN7 August 21, 1990 NDCt.EAR PRDDUC7ION U. S. Nuclear Regulatory Commission NRC Document Control Desk |
| On July 25, 1990 Palo Verde Unit 1 was in Mode 1 (POWER OPERATION) at one hundred percent power with the Reactor Coolant System (RCS)at normal operating temperature and pressure.Descri tion of Event: This Special Report is being voluntarily submitted to provide information on the performance of the Unit 1 Loose Part Detection System (LPDS).The Palo Verde Unit 1 Loose Parts Detection System, (LPDS)consists of eight (8)channels.Each channel consists of a piezoelectric crystal motion sensor and associated amplification, indication, and recording circuitry. | | ' |
| The sensors are positioned in the following locations: | | Pl-37 Washington, D.C. ,20555 |
| two (2)mounted on the Reactor Vessel upper head (channels 1 and 2), two (2)mounted on the Reactor Vessel lower incore nozzle (channels 3 and 4), and one (1)on each of the two (2)Steam Generators'nlet and outlet nozzles (channels 5, 6, 7 and 8).The piezoelectric sensors detect the loose parts using acoustic signals which are generated when loose parts impact a Reactor Coolant System component or structure. | | |
| Signals in excess of the alarm setpoint will result in an alarm condition. | | ==Dear Sirs:== |
| The alarms are the"latch-on" type, i.e., the alarms will remain on'when the system returns to normal and will not clear until the alarm is manually reset.There is one alarm indicator in the Control Room for the eight channels such that a"latch on" alarm effectively renders the Control Room alarm indication inoperable for the remaining channels upon receipt of an alarm condition. | | |
| In addition to the alarm in the Control Room, tape recorders will start when the system is in'Auto'.There are two tape recorders; each tape recorder can record four system channels at a time.Technical Specification 3.3.3.7 requires all eight channels of LPDS to be OPERABLE in Modes 1 and 2 (POWER OPERATIONS and STARTUP).Tech'nical Specification 4.3.3.7 requires each channel to be demonstrated OPERABLE by a)a channel check at least once per 24 hours, b)a Channel Functional Test at least once per 31 days, and c)a Channel Calibration at least once per 18 months' NRC Document Control Desk Page 2 Special Report 1-SR-90-005 During the previous fuel cycle (March 1988 to March 1989)channel 5, located on Hot Leg 1A, experienced numerous spurious alarms.An engineering evaluation completed in October 1988 determined the system was functioning properly.The channel 5 alarm setpoint was temporarily raised and additional manual monitoring of the LPDS was initiated during the remainder of the fuel cycle (Reference | | Subj ect: Palo Verde Nuclear Generating Station (PVNGS) |
| 'Special Report 1-SR-88-008). | | Unit 1 Docket No. STN 50-528 (License. No. NPF-41) |
| During the subsequent refueling outage, the channel 5 alarm setpoint was re'set, the required surveillance tests were performed, and the system placed in service The LPDS was not declared operable because of documentation that could not be closed until after full power was achieved.With the reactor at full power, the LPDS was monitored and Channel 5 was found to be spuriously activating. | | Special Report 1-SR-90-005 File: 90-020-404 Attached please find Special Report 1-SR-90-005 which is being voluntarily submitted to describe the performance of the Unit 1 Loose Parts Detection System. |
| Therefore, the LPDS was not declared operable pending an evaluation of the actuations. | | If you have any questions on this matter, please contact T. R. Bradish, Compliance Manager, at (602) 393-2521. |
| The surveillance tests required by the Technical Specification 4.3.3.7 were performed and kept current during the time the evaluation was being performed. | | Very truly yours, JML/TRB/SBJ/dmn Attachment cc: W. F. Conway (all w/attachment) |
| On June 25, 1990 at approximately 1951 MST Unit 1 entered Mode 2 (STARTUP). | | J. B. Martin C. M. Tramell D. H. Coe A. C. Gehr A. H. Gutterman INPO Records Center |
| Technical Specifications permit entry into Mode 1 or Mode 2 with the LPDS inoperable. | | |
| Unit 1 subsequently entered Mode 1 on June 30, 1990 at approximately 0226 MST.An engineering evaluation determined that LPDS was operating properly.The spurious alarms were caused by the system sensitivity required to meet the requirements of Regulatory Guide 1.133, the same cause established in 1988.Following the engineering evaluation, an action plan for responding to and monitoring the LPDS after spurious alarms was developed. | | (i I |
| On July 25, 1990 at approximately 1910 MST, LPDS was declared operable.Cause of Event'he cause of the LPDS Spurious alarms is the sensitivity of the system, as discussed above.The LPDS Channel response is reflective of the excitative energy from the Reactor Coolant System (RCS).APS has observed that, at different power levels and during different plant transients, RCS excitative energies vary which affect the response of the LPDS.Also, other sources (e.g., flow vortexing, core barrel bypass flow, etc.)can produce energy waves which excite the accelerometers. | | I h |
| In many cases, it takes a significant length of time after a plant transient for the RCS to"stabilize" to the point where spurious LPVMS alarms do not occur.This sensitivity is required to meet the requirements of Regulatory Guide 1.133.Corrective Actions: An engineer'ing evaluation was performed and determined LPDS was operating properly.The LPDS was declared operable on July 25, 1990 prior to the 30 day Technical Specification Action expiring. | | It'~ |
| NRC Document Control Desk Page 3 Special Report 1-SR-90-005 The operating procedure for the LPDS has been revised to include a'high alarm rate condition'lassification for LPDS channels that alarm four or more times in one shift without any'correlation to plant events or conditions. | | 1 I |
| If a channel is determined to be in the'high alarm rate condition', the audio from the channel will be monitored once per shift instead of on each alarm occurrence, and a work authorization document initiated to have the channel evaluated every 72 hours.The'high alarm rate condition's cancelled if a channel does not alarm for 24.hours.APS is continuing to evaluate the LPDS to identify opportunities for improvements. | | ( |
| An Event Analysis Computer modification is under development which is intended to enhance the ability of the system todiscriminate false alarms.}} | | |
| | PALO VERDE NUCLEAR GENERATING STATION UNIT 1 License No. NPF-41 Docket No. 50-528 Special Report 1-SR-90-005 Initial Conditions: |
| | On July 25, 1990 Palo Verde Unit 1 was in Mode 1 (POWER OPERATION) at one hundred percent power with the Reactor Coolant System (RCS) at normal operating temperature and pressure. |
| | Descri tion of Event: |
| | This Special Report is being voluntarily submitted to provide information on the performance of the Unit 1 Loose Part Detection System (LPDS). |
| | The Palo Verde Unit 1 Loose Parts Detection System, (LPDS) consists of eight (8) channels. Each channel consists of a piezoelectric crystal motion sensor and associated amplification, indication, and recording circuitry. The sensors are positioned in the following locations: two (2) mounted on the Reactor Vessel upper head (channels 1 and 2), two (2) mounted on the Reactor Vessel lower incore nozzle (channels 3 and 4), |
| | and one (1) on each of the two (2) Steam Generators'nlet and outlet nozzles (channels 5, 6, 7 and 8). The piezoelectric sensors detect the loose parts using acoustic signals which are generated when loose parts impact a Reactor Coolant System component or structure. Signals in excess of the alarm setpoint will result in an alarm condition. The alarms are the "latch-on" type, i.e., the alarms will remain on'when the system returns to normal and will not clear until the alarm is manually reset. There is one alarm indicator in the Control Room for the eight channels such that a "latch on" alarm effectively renders the Control Room alarm indication inoperable for the remaining channels upon receipt of an alarm condition. In addition to the alarm in the Control Room, tape recorders will start when the system is in 'Auto'. There are two tape recorders; each tape recorder can record four system channels at a time. |
| | Technical Specification 3.3.3.7 requires all eight channels of LPDS to be OPERABLE in Modes 1 and 2 (POWER OPERATIONS and STARTUP). Tech'nical Specification 4.3.3.7 requires each channel to be demonstrated OPERABLE by a) a channel check at least once per 24 hours, b) a Channel Functional Test at least once per 31 days, and c) a Channel Calibration at least once per 18 months' |
| | |
| | NRC Document Control Desk Special Report 1-SR-90-005 Page 2 During the previous fuel cycle (March 1988 to March 1989) channel 5, located on Hot Leg 1A, experienced numerous spurious alarms. An engineering evaluation completed in October 1988 determined the system was functioning properly. The channel 5 alarm setpoint was temporarily raised and additional manual monitoring of the LPDS was initiated during the remainder of the fuel cycle (Reference 'Special Report 1-SR-88-008). |
| | During the subsequent refueling outage, the channel 5 alarm setpoint was re'set, the required surveillance tests were performed, and the system placed in service The LPDS was not declared operable because of documentation that could not be closed until after full power was achieved. With the reactor at full power, the LPDS was monitored and Channel 5 was found to be spuriously activating. Therefore, the LPDS was not declared operable pending an evaluation of the actuations. The surveillance tests required by the Technical Specification 4.3.3.7 were performed and kept current during the time the evaluation was being performed. On June 25, 1990 at approximately 1951 MST Unit 1 entered Mode 2 (STARTUP). Technical Specifications permit entry into Mode 1 or Mode 2 with the LPDS inoperable. Unit 1 subsequently entered Mode 1 on June 30, 1990 at approximately 0226 MST. |
| | An engineering evaluation determined that LPDS was operating properly. |
| | The spurious alarms were caused by the system sensitivity required to meet the requirements of Regulatory Guide 1.133, the same cause established in 1988. |
| | Following the engineering evaluation, an action plan for responding to and monitoring the LPDS after spurious alarms was developed. On July 25, 1990 at approximately 1910 MST, LPDS was declared operable. |
| | Cause of Event'he cause of the LPDS Spurious alarms is the sensitivity of the system, as discussed above. The LPDS Channel response is reflective of the excitative energy from the Reactor Coolant System (RCS). APS has observed that, at different power levels and during different plant transients, RCS excitative energies vary which affect the response of the LPDS. Also, other sources (e.g., flow vortexing, core barrel bypass flow, etc.) can produce energy waves which excite the accelerometers. |
| | In many cases, it takes a significant length of time after a plant transient for the RCS to "stabilize" to the point where spurious LPVMS alarms do not occur. This sensitivity is required to meet the requirements of Regulatory Guide 1.133. |
| | Corrective Actions: |
| | An engineer'ing evaluation was performed and determined LPDS was operating properly. The LPDS was declared operable on July 25, 1990 prior to the 30 day Technical Specification Action expiring. |
| | |
| | NRC Document Control Desk Special Report 1-SR-90-005 Page 3 The operating procedure for the LPDS has been revised to include a 'high alarm rate condition'lassification for LPDS channels that alarm four or more times in one shift without any 'correlation to plant events or conditions. If a channel is determined to be in the 'high alarm rate condition', the audio from the channel will be monitored once per shift instead of on each alarm occurrence, and a work authorization document initiated to have the channel evaluated every 72 hours. The 'high alarm rate condition's cancelled if a channel does not alarm for 24 .hours. |
| | APS is continuing to evaluate the LPDS to identify opportunities for improvements. An Event Analysis Computer modification is under development which is intended to enhance the ability of the system to discriminate false alarms.}} |
|
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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A1271997-11-26026 November 1997 Special Rept 2-SR-97-002:on 971103,loose-part Detection Sys Channel 2 Declared Inoperable.Caused by Malfunction of Coaxial Cable Connector to accelerometer.Loose-part Detection Sys Channel Will Be Reworked ML17312A6871996-04-0505 April 1996 Rev 1 to Special Rept 2-SR-96-001,on 960404,alert Declared Due to Fire in Voltage Regulator for CR & Remote Shutdown Panel Essential Lighting,Clarifying Status of Power to UPS 2EQDNN02.Further Investigations Into Event Being Performed ML17312A6611996-04-0404 April 1996 Special Rept 2-SR-96-001:on 960404,fault Occurred in Voltage Regulator for CR & Remote Shutdown Panel Essential Lighting, Resulting in Fire in 100 Ft Elevation of Cb B Battery Equipment Room & Requiring Declaration of Alert,Per EPIP-04 ML17312A5771996-03-0101 March 1996 Special Rept 1-SR-96-01 on:960225,unit 1 Turbine Tripped Followed by Reactor Power Cutback.Caused by Lightning Strike.Unit 1 Will Not Be Connected to Grid Until Repairs Can Be Made to C Neutral Bushing of Transformer ML17311A8971995-05-25025 May 1995 Special Rept:On 950416,loose-part Detection Sys Channel 1 Declared Inoperable.Caused by Malfunction of Coaxial Cable Connector to Transducer.Channel Will Be Reworked & Returned to Svc During First Available Outage of Sufficient Duration ML17310B3621994-06-0909 June 1994 Special Rept 1-SR-94-001:on 940511,plant Ventilation Sys High Range Effluent Monitors in Units 1 & 2 Inoperable for Periods Greater than 72 H.Caused by High Voltage Failure Alarm.Design Change Package Installed ML17310B3071994-05-20020 May 1994 Special Rept 2-SR-94-002:on 940518,NOUE Declared Due to Fire Which Burned in Excess of 10 Minutes within Protected Area. Fire Extinguished W/Portable Fire Extinguisher.Investigation Initiated to Determine Cause of Fire & Develop C/As ML17310A9951994-01-13013 January 1994 Suppl 2 to Special Rept 3-SR-92-006:on 921217,PASS Declared Inoperable for Greater than Seven Days Following Failure to Meet Pressurized Sample Portion of Acceptance Criteria for Monthly Functional Sr.Pass Declared Operable on 921226 ML17310A9941994-01-13013 January 1994 Suppl 2 to Special Rept 2-SR-92-004:on 921222,PASS Declared Inoperable for Greater than Seven Days Due to Failure of Containment Air Flow Indicator & Indication of Water Leakage at PASS RCS Sample Septum.Pass Declared Operable on 930105 ML17310A8951994-01-0303 January 1994 Special rept:1-SR-93-008:on 940103,fuel Bldg Ventilation Sys High Range Radiation Monitor Inoperable for Period Greater than 72 Hours.Caused by Difficulties in Installing Mod 1-FJ-SQ-060 ML17310A8701993-12-25025 December 1993 Special Rept 1-SR-93-006:on 931224,30 Day Period for Returning loose-part Detection Sys (Lpds) to Operable Status Exceeded.Inoperable Lpds Channel Scheduled to Be Reworked & Returned to Svc During Next Outage of Sufficient Duration ML17310A8671993-12-15015 December 1993 Special Rept 1-SR-93-007:on 931215,30 Day Period for Returning Accelerometer to Operable Condition Exceeded. Accelerometer Will Be Replaced During Next Outage of Sufficient Duration ML17310A7581993-10-30030 October 1993 Special Rept 1-SR-93-004:on 931008,high Range RM RU-146 Made Inoperable for Period of Greater than 72 H as Result of Scheduled Electrical Bus Outage.Maint on Associated Bus Completed on 931015 & RU-146 Returned to Service ML17310A7001993-10-0909 October 1993 Special Rept 2-SR-93-003:on 931002,thirty Day Period for Returning loose-part Detection Sys Channel 8 to Operable Status Exceeded.Subj Channel Scheduled to Be Reworked & Returned to Svc During Next Outage ML17310A6301993-09-13013 September 1993 Special Rept 3-SR-93-003:on 930806,loose-part Detection Sys (Lpds) Declared Inoperable & Exceeded 30 Day Period for Being Returned to Svc on 930905.LPDS Channel 5 Scheduled to Be Reworked & Returned to Svc During Next Outage ML17310A5401993-08-11011 August 1993 Special Rept 1-SR-93-003:on 930806,NOUE Declared When Unit 1 CR Received Verification That Meteorological Instrumentation Unavailable Due to Loss of Power to Meteorological Tower. Caused by Severe Weather.Instrumentation Repaired ML17310A4961993-08-0202 August 1993 Special Rept 2-SR-93-002:on 930722,Unit 2 in Mode 5,Cold Shutdown During Refueling Outage When ISI of Both SGs Completed.Insp Resulted in Plugging of 74 Tubes in SG 1 & 175 Tubes in SG 2 ML17310A4401993-07-12012 July 1993 Special Rept 1-SR-93-002:on 930526,period for Returning Min Number of Explosive Gas Monitoring Channels to Operable Condition Exceeded.After All Four Cells Rebuilt,Calibr Completed on 930602 & Subj Analyzer Returned to Svc ML17306B4231993-04-24024 April 1993 Suppl 1 to Special Repts 2-SR-92-004 & 3-SR-92-006:on 921222 Unit 2 PASS Declared Inoperable Due to Failure of Containment Air Flow Indicator.On 921217,Unit 3 PASS Declared Inoperable.Equipment Replaced & Sample Obtained ML17306B3371993-03-15015 March 1993 Special Rept 2-SR-93-001:on 930314,control Room Personnel Manually Tripped Reactor Due to Rapid Decrease in Pressurizer Heaters.Personnel Commenced Controlled Plant Cooldown.Unit Remains Shut Down for Further Investigation ML17306B2901993-02-22022 February 1993 Special Rept 1-SR-92-005,suppl 1,provided Per Emergency Plan Implementing Procedure EPIP-03, Notification of Unusual Event Implementing Actions, Occurring on 920822 Re Loss of Power at Meteorological Tower ML17306B2781993-02-0909 February 1993 Special Rept 3-SR-93-001:on 930204,reactor Trip Occurred & Main Feedwater Pump a Experienced Rapidly Decreasing Pump Speed.Valid Actuation of SI Actuation Sys & Containment Isolation Actuation Sys Also Occurred.Evaluation Underway ML17306B2721993-01-27027 January 1993 Special Rept 3-SR-004-03:on 920817,PASS Inoperable for More than 7 Days.On 920902,discovered That PASS Unable to Draw Vacuum on Gaseous Sample Bomb.Vent Line Reworked & Procedure Revised ML17306B2551993-01-24024 January 1993 Special Rept 2-SR-92-004:on 921222,PASS Declared Inoperable for Period Greater than 7 Days Due to Failure of Containment Air Flow Indicator & Indication of Water Leakage at PASS Rcs.Pass Returned to Operable Status on 930105 ML17306B2561993-01-24024 January 1993 Special Rept 1-SR-92-007:on 921227,CB Atmosphere RM Inoperable for Period Greater than 72 H Due to High Flow Conditions.Temporary Mod Installed on Subj RM to Remove Monitor from Dedicated Rms Grounding Sys ML17306B2541993-01-22022 January 1993 Special Rept 3-SR-92-006:on 921217,PASS Declared Inoperable Following Failure to Meet Pressurized Sample Portion of Acceptance Criteria for Monthly Functional Sr.Pass Returned to Operable Status Following Satisfactory Repairs & Testing ML17306B1911992-12-21021 December 1992 Special Rept 3-SR-92-004-01:on 920201 PASS Declared Inoperable for Period Greater than Seven Days.Caused by Tubing Being Rerouted.Pass Reworked & Operability Restored on 920905 ML17306B1841992-12-14014 December 1992 Special Rept:On 920810,PASS Declared Inoperable Due to Tubing Being Rerouted.Chemistry Sys Status Procedure 74DP-9ZZ04 Revised to Direct Chemistry Personnel to Ensure That Functional Test Is performed.W/921214 Ltr ML17306B1291992-11-17017 November 1992 Special Rept 2-SR-92-003:on 921113,reactor Trip Occurred While Motor Generator Set a Out of Svc for Scheduled Maint & Set B Inadvertently Deenergized,Resulting in Loss of Power. State & Local Agencies Notified & Sys Reset ML17306B0931992-10-30030 October 1992 Suppl 1 to Special Rept 3-SR-92-004:on 920817,seven-day Period for Returning PASS to Service exceeded.30DP-9WP04 Revised to Retest for PASS & Gaseous Radwaste to Be Completed by 921120 ML17306A9951992-09-18018 September 1992 Special Rept 3-SR-92-004:seven-day Period for Returning PASS to Svc Exceeded on 920817.On 920902,discovered That PASS Unable to Draw Vacuum on Gaseous Sample Bomb.Possibly Caused by Maint on 920810.PASS Reworked & Operability Restored ML17306A9651992-09-16016 September 1992 Special Rept 3-SR-92-003:on 920903,discovered That PASS Unable to Draw Vacuum on Gaseous Sample Bomb & Declared Inoperable for More than 7 Days.Cause Under Investigation. Sys Returned to Operable Status on 920905 ML17306A9401992-08-28028 August 1992 Special Rept 1-SR-92-005:on 920822,discovered That Info Could Not Be Dispatched from Meterological Tower During Routine Surveillance of Daily Midnight Logs.Tower Declared Operable on 920823 Following Power Restoration ML17306A8101992-06-27027 June 1992 Special Rept 1-SR-92-004:on 920620,loose Part Detection Sys Inoperable for More than 30 Days.Caused by Hardware Problems Associated W/Installation of Loose Part Detection Sys Mods.New Computer Processor Board Installed ML17306A7971992-06-18018 June 1992 Special Rept 3-SR-92-003:on 920520,RMs RU-145 & 146 Declared Inoperable & Removed from Svc.Caused by Personnel Errors in Documenting Clearance for Retest of RU-146.Shift Supervisor Disciplined & Technician Verified That Pumps Were Energized ML17306A7961992-06-18018 June 1992 Special Rept 1-SR-92-003:on 920514,unit 1 Entered Mode 3 & PASS Declare Inoperable & Failed Surveillance Test.Caused by Leaking Relief Valve & Malfunctioning Pressure Transducer. Relief Valve & Pressure Transducer Replaced ML17306A7101992-05-0606 May 1992 Special Rept:On 920504,Control Room Received Alarms on All Seven Control Boards.Plan Computer Returned to Svc & Was Declared operable.W/920506 Ltr ML17306A6811992-04-18018 April 1992 Special Rept SR-92-002:on 920411,insp of SGs Resulted in Plugging of 23 Tubes in SG 1 & 18 Tubes in SG 2.Complete Results of SG Tube ISI Will Be Submitted by 930411 ML17306A4521992-02-0707 February 1992 Special Rept:On 920101,PASS Declared Inoperable When Chemistry Personnel Could Not Obtain a Containment Air Sample.Caused by Malfunctioning Flow Sensor.Pass Expected to Be Returned to an Operable status.W/920207 Ltr ML17306A3901992-01-0707 January 1992 Special Rept 1-SR-92-001:on 920102,determined That Leak Existed in Pressurizer Steam Space Instrument Nozzle Mfg from Inconnel 600.Caused by Nonvisible Intergranular Crack.Addl Investigation Underway ML17306A2981991-12-0505 December 1991 Special Rept 2-SR-91-002:on 911107,fuel Bldg Ventilation Sys high-range Radioactive Gaseous Effluent Monitor Inoperable for More than 72 H.Caused by Power Supply Deenergized for Scheduled Maint.Monitor Returned to Svc on 911114 ML17306A2791991-11-20020 November 1991 Special Rept 3-SR-91-007:on 911115,mobile Crane Came in Contact W/Energized 13.8 Kv Power Line Resulting in Arcing of Crane Outrigger Pads to Ground & Burning of Asphalt Area in Contact W/Pads.Investigation Re Event Being Performed ML17306A2221991-10-10010 October 1991 Special Rept 1-SR-91-001-01:on 910111,fuel Bldg Ventilation Sys High Range Radioactive Gaseous Effluent Monitor Declared Inoperable for Period Greater than 72 H in Order to Perform Scheduled 18-month Surveillance Testing & Maint ML17306A2211991-10-10010 October 1991 Special Rept 2-SR-89-007-03:on 891002,fuel Bldg Ventilation Sys High Range Gaseous Effluent Monitor Declared Inoperable for More than 72 H.Caused by Low Flow Limit Switch Being Out of Adjustment.Microprocessor Operated Manual Mode ML17306A2201991-10-10010 October 1991 Special Rept 2-SR-90-005-01:on 900716,plant Vent Sys High Range Effluent Monitor Inoperable for More than 72 H.Caused by Requirement to Perform Scheduled 18-month Surveillance Testing.Monitor Returned to Svc on 900729 ML17306A2181991-10-10010 October 1991 Special Rept 2-SR-90-004-01:on 910613,fuel Bldg Ventilation Sys high-range Radioactive Gaseous Effluent Monitor Inoperable for More than 72 H.Caused by Need to Perform 18 Month Surveillance Testing.Monitor Returned to Svc ML17305B7441991-09-18018 September 1991 Special Rept 1-SR-91-002,on 910914:steam Generator Econimizer Valve SGN-FV-1112 Fully Opened Causing Level in Steam Generator 1 to Rapidly Increase.Caused by Malfunction of Lower Gripper High Voltage on Slipped Part Length CEA 1999-06-21
[Table view] Category:LER)
MONTHYEARML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A1271997-11-26026 November 1997 Special Rept 2-SR-97-002:on 971103,loose-part Detection Sys Channel 2 Declared Inoperable.Caused by Malfunction of Coaxial Cable Connector to accelerometer.Loose-part Detection Sys Channel Will Be Reworked ML17312A6871996-04-0505 April 1996 Rev 1 to Special Rept 2-SR-96-001,on 960404,alert Declared Due to Fire in Voltage Regulator for CR & Remote Shutdown Panel Essential Lighting,Clarifying Status of Power to UPS 2EQDNN02.Further Investigations Into Event Being Performed ML17312A6611996-04-0404 April 1996 Special Rept 2-SR-96-001:on 960404,fault Occurred in Voltage Regulator for CR & Remote Shutdown Panel Essential Lighting, Resulting in Fire in 100 Ft Elevation of Cb B Battery Equipment Room & Requiring Declaration of Alert,Per EPIP-04 ML17312A5771996-03-0101 March 1996 Special Rept 1-SR-96-01 on:960225,unit 1 Turbine Tripped Followed by Reactor Power Cutback.Caused by Lightning Strike.Unit 1 Will Not Be Connected to Grid Until Repairs Can Be Made to C Neutral Bushing of Transformer ML17311A8971995-05-25025 May 1995 Special Rept:On 950416,loose-part Detection Sys Channel 1 Declared Inoperable.Caused by Malfunction of Coaxial Cable Connector to Transducer.Channel Will Be Reworked & Returned to Svc During First Available Outage of Sufficient Duration ML17310B3621994-06-0909 June 1994 Special Rept 1-SR-94-001:on 940511,plant Ventilation Sys High Range Effluent Monitors in Units 1 & 2 Inoperable for Periods Greater than 72 H.Caused by High Voltage Failure Alarm.Design Change Package Installed ML17310B3071994-05-20020 May 1994 Special Rept 2-SR-94-002:on 940518,NOUE Declared Due to Fire Which Burned in Excess of 10 Minutes within Protected Area. Fire Extinguished W/Portable Fire Extinguisher.Investigation Initiated to Determine Cause of Fire & Develop C/As ML17310A9951994-01-13013 January 1994 Suppl 2 to Special Rept 3-SR-92-006:on 921217,PASS Declared Inoperable for Greater than Seven Days Following Failure to Meet Pressurized Sample Portion of Acceptance Criteria for Monthly Functional Sr.Pass Declared Operable on 921226 ML17310A9941994-01-13013 January 1994 Suppl 2 to Special Rept 2-SR-92-004:on 921222,PASS Declared Inoperable for Greater than Seven Days Due to Failure of Containment Air Flow Indicator & Indication of Water Leakage at PASS RCS Sample Septum.Pass Declared Operable on 930105 ML17310A8951994-01-0303 January 1994 Special rept:1-SR-93-008:on 940103,fuel Bldg Ventilation Sys High Range Radiation Monitor Inoperable for Period Greater than 72 Hours.Caused by Difficulties in Installing Mod 1-FJ-SQ-060 ML17310A8701993-12-25025 December 1993 Special Rept 1-SR-93-006:on 931224,30 Day Period for Returning loose-part Detection Sys (Lpds) to Operable Status Exceeded.Inoperable Lpds Channel Scheduled to Be Reworked & Returned to Svc During Next Outage of Sufficient Duration ML17310A8671993-12-15015 December 1993 Special Rept 1-SR-93-007:on 931215,30 Day Period for Returning Accelerometer to Operable Condition Exceeded. Accelerometer Will Be Replaced During Next Outage of Sufficient Duration ML17310A7581993-10-30030 October 1993 Special Rept 1-SR-93-004:on 931008,high Range RM RU-146 Made Inoperable for Period of Greater than 72 H as Result of Scheduled Electrical Bus Outage.Maint on Associated Bus Completed on 931015 & RU-146 Returned to Service ML17310A7001993-10-0909 October 1993 Special Rept 2-SR-93-003:on 931002,thirty Day Period for Returning loose-part Detection Sys Channel 8 to Operable Status Exceeded.Subj Channel Scheduled to Be Reworked & Returned to Svc During Next Outage ML17310A6301993-09-13013 September 1993 Special Rept 3-SR-93-003:on 930806,loose-part Detection Sys (Lpds) Declared Inoperable & Exceeded 30 Day Period for Being Returned to Svc on 930905.LPDS Channel 5 Scheduled to Be Reworked & Returned to Svc During Next Outage ML17310A5401993-08-11011 August 1993 Special Rept 1-SR-93-003:on 930806,NOUE Declared When Unit 1 CR Received Verification That Meteorological Instrumentation Unavailable Due to Loss of Power to Meteorological Tower. Caused by Severe Weather.Instrumentation Repaired ML17310A4961993-08-0202 August 1993 Special Rept 2-SR-93-002:on 930722,Unit 2 in Mode 5,Cold Shutdown During Refueling Outage When ISI of Both SGs Completed.Insp Resulted in Plugging of 74 Tubes in SG 1 & 175 Tubes in SG 2 ML17310A4401993-07-12012 July 1993 Special Rept 1-SR-93-002:on 930526,period for Returning Min Number of Explosive Gas Monitoring Channels to Operable Condition Exceeded.After All Four Cells Rebuilt,Calibr Completed on 930602 & Subj Analyzer Returned to Svc ML17306B4231993-04-24024 April 1993 Suppl 1 to Special Repts 2-SR-92-004 & 3-SR-92-006:on 921222 Unit 2 PASS Declared Inoperable Due to Failure of Containment Air Flow Indicator.On 921217,Unit 3 PASS Declared Inoperable.Equipment Replaced & Sample Obtained ML17306B3371993-03-15015 March 1993 Special Rept 2-SR-93-001:on 930314,control Room Personnel Manually Tripped Reactor Due to Rapid Decrease in Pressurizer Heaters.Personnel Commenced Controlled Plant Cooldown.Unit Remains Shut Down for Further Investigation ML17306B2901993-02-22022 February 1993 Special Rept 1-SR-92-005,suppl 1,provided Per Emergency Plan Implementing Procedure EPIP-03, Notification of Unusual Event Implementing Actions, Occurring on 920822 Re Loss of Power at Meteorological Tower ML17306B2781993-02-0909 February 1993 Special Rept 3-SR-93-001:on 930204,reactor Trip Occurred & Main Feedwater Pump a Experienced Rapidly Decreasing Pump Speed.Valid Actuation of SI Actuation Sys & Containment Isolation Actuation Sys Also Occurred.Evaluation Underway ML17306B2721993-01-27027 January 1993 Special Rept 3-SR-004-03:on 920817,PASS Inoperable for More than 7 Days.On 920902,discovered That PASS Unable to Draw Vacuum on Gaseous Sample Bomb.Vent Line Reworked & Procedure Revised ML17306B2551993-01-24024 January 1993 Special Rept 2-SR-92-004:on 921222,PASS Declared Inoperable for Period Greater than 7 Days Due to Failure of Containment Air Flow Indicator & Indication of Water Leakage at PASS Rcs.Pass Returned to Operable Status on 930105 ML17306B2561993-01-24024 January 1993 Special Rept 1-SR-92-007:on 921227,CB Atmosphere RM Inoperable for Period Greater than 72 H Due to High Flow Conditions.Temporary Mod Installed on Subj RM to Remove Monitor from Dedicated Rms Grounding Sys ML17306B2541993-01-22022 January 1993 Special Rept 3-SR-92-006:on 921217,PASS Declared Inoperable Following Failure to Meet Pressurized Sample Portion of Acceptance Criteria for Monthly Functional Sr.Pass Returned to Operable Status Following Satisfactory Repairs & Testing ML17306B1911992-12-21021 December 1992 Special Rept 3-SR-92-004-01:on 920201 PASS Declared Inoperable for Period Greater than Seven Days.Caused by Tubing Being Rerouted.Pass Reworked & Operability Restored on 920905 ML17306B1841992-12-14014 December 1992 Special Rept:On 920810,PASS Declared Inoperable Due to Tubing Being Rerouted.Chemistry Sys Status Procedure 74DP-9ZZ04 Revised to Direct Chemistry Personnel to Ensure That Functional Test Is performed.W/921214 Ltr ML17306B1291992-11-17017 November 1992 Special Rept 2-SR-92-003:on 921113,reactor Trip Occurred While Motor Generator Set a Out of Svc for Scheduled Maint & Set B Inadvertently Deenergized,Resulting in Loss of Power. State & Local Agencies Notified & Sys Reset ML17306B0931992-10-30030 October 1992 Suppl 1 to Special Rept 3-SR-92-004:on 920817,seven-day Period for Returning PASS to Service exceeded.30DP-9WP04 Revised to Retest for PASS & Gaseous Radwaste to Be Completed by 921120 ML17306A9951992-09-18018 September 1992 Special Rept 3-SR-92-004:seven-day Period for Returning PASS to Svc Exceeded on 920817.On 920902,discovered That PASS Unable to Draw Vacuum on Gaseous Sample Bomb.Possibly Caused by Maint on 920810.PASS Reworked & Operability Restored ML17306A9651992-09-16016 September 1992 Special Rept 3-SR-92-003:on 920903,discovered That PASS Unable to Draw Vacuum on Gaseous Sample Bomb & Declared Inoperable for More than 7 Days.Cause Under Investigation. Sys Returned to Operable Status on 920905 ML17306A9401992-08-28028 August 1992 Special Rept 1-SR-92-005:on 920822,discovered That Info Could Not Be Dispatched from Meterological Tower During Routine Surveillance of Daily Midnight Logs.Tower Declared Operable on 920823 Following Power Restoration ML17306A8101992-06-27027 June 1992 Special Rept 1-SR-92-004:on 920620,loose Part Detection Sys Inoperable for More than 30 Days.Caused by Hardware Problems Associated W/Installation of Loose Part Detection Sys Mods.New Computer Processor Board Installed ML17306A7971992-06-18018 June 1992 Special Rept 3-SR-92-003:on 920520,RMs RU-145 & 146 Declared Inoperable & Removed from Svc.Caused by Personnel Errors in Documenting Clearance for Retest of RU-146.Shift Supervisor Disciplined & Technician Verified That Pumps Were Energized ML17306A7961992-06-18018 June 1992 Special Rept 1-SR-92-003:on 920514,unit 1 Entered Mode 3 & PASS Declare Inoperable & Failed Surveillance Test.Caused by Leaking Relief Valve & Malfunctioning Pressure Transducer. Relief Valve & Pressure Transducer Replaced ML17306A7101992-05-0606 May 1992 Special Rept:On 920504,Control Room Received Alarms on All Seven Control Boards.Plan Computer Returned to Svc & Was Declared operable.W/920506 Ltr ML17306A6811992-04-18018 April 1992 Special Rept SR-92-002:on 920411,insp of SGs Resulted in Plugging of 23 Tubes in SG 1 & 18 Tubes in SG 2.Complete Results of SG Tube ISI Will Be Submitted by 930411 ML17306A4521992-02-0707 February 1992 Special Rept:On 920101,PASS Declared Inoperable When Chemistry Personnel Could Not Obtain a Containment Air Sample.Caused by Malfunctioning Flow Sensor.Pass Expected to Be Returned to an Operable status.W/920207 Ltr ML17306A3901992-01-0707 January 1992 Special Rept 1-SR-92-001:on 920102,determined That Leak Existed in Pressurizer Steam Space Instrument Nozzle Mfg from Inconnel 600.Caused by Nonvisible Intergranular Crack.Addl Investigation Underway ML17306A2981991-12-0505 December 1991 Special Rept 2-SR-91-002:on 911107,fuel Bldg Ventilation Sys high-range Radioactive Gaseous Effluent Monitor Inoperable for More than 72 H.Caused by Power Supply Deenergized for Scheduled Maint.Monitor Returned to Svc on 911114 ML17306A2791991-11-20020 November 1991 Special Rept 3-SR-91-007:on 911115,mobile Crane Came in Contact W/Energized 13.8 Kv Power Line Resulting in Arcing of Crane Outrigger Pads to Ground & Burning of Asphalt Area in Contact W/Pads.Investigation Re Event Being Performed ML17306A2221991-10-10010 October 1991 Special Rept 1-SR-91-001-01:on 910111,fuel Bldg Ventilation Sys High Range Radioactive Gaseous Effluent Monitor Declared Inoperable for Period Greater than 72 H in Order to Perform Scheduled 18-month Surveillance Testing & Maint ML17306A2211991-10-10010 October 1991 Special Rept 2-SR-89-007-03:on 891002,fuel Bldg Ventilation Sys High Range Gaseous Effluent Monitor Declared Inoperable for More than 72 H.Caused by Low Flow Limit Switch Being Out of Adjustment.Microprocessor Operated Manual Mode ML17306A2201991-10-10010 October 1991 Special Rept 2-SR-90-005-01:on 900716,plant Vent Sys High Range Effluent Monitor Inoperable for More than 72 H.Caused by Requirement to Perform Scheduled 18-month Surveillance Testing.Monitor Returned to Svc on 900729 ML17306A2181991-10-10010 October 1991 Special Rept 2-SR-90-004-01:on 910613,fuel Bldg Ventilation Sys high-range Radioactive Gaseous Effluent Monitor Inoperable for More than 72 H.Caused by Need to Perform 18 Month Surveillance Testing.Monitor Returned to Svc ML17305B7441991-09-18018 September 1991 Special Rept 1-SR-91-002,on 910914:steam Generator Econimizer Valve SGN-FV-1112 Fully Opened Causing Level in Steam Generator 1 to Rapidly Increase.Caused by Malfunction of Lower Gripper High Voltage on Slipped Part Length CEA 1999-06-21
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17300B3811999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pvngs,Units 1,2 & 3.With 991007 Ltr ML17300B3271999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pvngs,Units 1,2 & 3 ML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0611999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pvngs,Units 1,2 & 3.With 990810 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17300B3151999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pvngs,Units 1,2 & 3.With 990714 Ltr ML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A9731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pvngs,Units 1,2 & 3.With 990608 Ltr ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A9201999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pvngs,Units 1,2 & 3.With 990512 Ltr ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17300B3071999-03-31031 March 1999 Seismic Portion of Submittal-Only Screening Review of Palo Verde Nuclear Generating Station Units Ipeee. ML17313A8801999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pvngs,Units 1,2 & 3.With 990412 Ltr ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207H7471999-03-10010 March 1999 1999 Emergency Preparedness Exercise 99-E-AEV-03003 ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A8501999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Palo Verde Nuclear Generating Station.With 990311 Ltr ML17313A7791999-02-0505 February 1999 Safety Evaluation Accepting Licensee Rev to Emergency Plan That Would Result in Two Less Radiation Protection Positions Immediatelu Available During Emergencies ML17313A8061999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Pvngs,Units 1,2 & 3.With 990218 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A7381998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.With 990113 Ltr ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML17313A7031998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pvngs,Unit 1,2 & 3. with 981209 Ltr ML17313A6701998-11-0404 November 1998 Rev 2 to PVNGS Unit 2 Colr. ML17313A6741998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pvngs,Units 1,2 & 3.With 981109 Ltr ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A6561998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for PVNGS Units 1,2 & 3.With 981007 Ltr ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML20151S0941998-08-21021 August 1998 Rev 6 to COLR for PVNGS Unit 3 ML20151S0861998-08-21021 August 1998 Rev 4 to COLR for PVNGS Unit 1 ML20151S0901998-08-21021 August 1998 Rev 1 to COLR for PVNGS Unit 2 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A5301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pvgns,Units 1,2 & 3.W/980812 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A5791998-07-0707 July 1998 to PVNGS SG Tube ISI Results for Seventh Refueling Outage Mar & Apr 1998. ML17313A5001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.W/980710 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4521998-06-19019 June 1998 Rev 5 to COLR for Pvngs,Unit 3. ML17313A4501998-06-19019 June 1998 Rev 4 to COLR for Pvngs,Unit 3. ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A4211998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pvngs,Units 1,2 & 3.W/980609 Ltr ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3691998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for PVNGS.W/980412 Ltr ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 1999-09-30
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Text
ACCELERATED DISTRIBUTION DEMONSTRATION SYSTEM i1 I
/"p REGULATORY IN FORMATION DISTRX BUTION SYSTEM (RI DS )
ACCESSXON NBR:9008300181 DOC.DATE: 90/08/21 NOTARIZED: NO DOCKET FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH. NAME AUTHOR AFFILIATION LEVINE,J.M. Arizona Public Service Co. (formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SUBJECT:
Special Rept 1-SR-90-005:on 900725,performance of loose parts detection sys might result in alarm condition.
DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR ENCL L SIZE:
Uincident TITLE: 50.73/50.9 Licensee Event Report (LER), Rpt, etc.
NOTES 'TANDARDIZED PLANT 05000528 /
RECXPIENT COPIES RECIPIENT COPIES A ID CODE/NAME LTTR ENCL XD CODE/NAME LTTR ENCL D
PD5 LA 1 1 PD5 PD 1 1 PETERSON,S. 1 1 TRAMMELL,C. 1 1 INTERNAL: ACNW 2 .2 ACRS 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DS P 2 2 NRR/DET/ECMB 9H 1 1 NRR/DET/EMEB9H3 1 1 NRR/DLPQ/LHFB1 1 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB11 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1 EXTERNAL NRR/DST/SICB 7E NRR/DST/SRXB 8E RES/DSIR/EIB EG&G BRYCE i J H 1
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Arizona Public Service Company PALO VERDE NUCLEAR GENERATING STATION P.O, BOX 52034 ~ PHOENIX, ARIZONA 85072-2034 JAMES M, LEVINE 192-00686-JML/TRB/SBJ VICE PAESIDEN7 August 21, 1990 NDCt.EAR PRDDUC7ION U. S. Nuclear Regulatory Commission NRC Document Control Desk
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Pl-37 Washington, D.C. ,20555
Dear Sirs:
Subj ect: Palo Verde Nuclear Generating Station (PVNGS)
Unit 1 Docket No. STN 50-528 (License. No. NPF-41)
Special Report 1-SR-90-005 File: 90-020-404 Attached please find Special Report 1-SR-90-005 which is being voluntarily submitted to describe the performance of the Unit 1 Loose Parts Detection System.
If you have any questions on this matter, please contact T. R. Bradish, Compliance Manager, at (602) 393-2521.
Very truly yours, JML/TRB/SBJ/dmn Attachment cc: W. F. Conway (all w/attachment)
J. B. Martin C. M. Tramell D. H. Coe A. C. Gehr A. H. Gutterman INPO Records Center
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PALO VERDE NUCLEAR GENERATING STATION UNIT 1 License No. NPF-41 Docket No. 50-528 Special Report 1-SR-90-005 Initial Conditions:
On July 25, 1990 Palo Verde Unit 1 was in Mode 1 (POWER OPERATION) at one hundred percent power with the Reactor Coolant System (RCS) at normal operating temperature and pressure.
Descri tion of Event:
This Special Report is being voluntarily submitted to provide information on the performance of the Unit 1 Loose Part Detection System (LPDS).
The Palo Verde Unit 1 Loose Parts Detection System, (LPDS) consists of eight (8) channels. Each channel consists of a piezoelectric crystal motion sensor and associated amplification, indication, and recording circuitry. The sensors are positioned in the following locations: two (2) mounted on the Reactor Vessel upper head (channels 1 and 2), two (2) mounted on the Reactor Vessel lower incore nozzle (channels 3 and 4),
and one (1) on each of the two (2) Steam Generators'nlet and outlet nozzles (channels 5, 6, 7 and 8). The piezoelectric sensors detect the loose parts using acoustic signals which are generated when loose parts impact a Reactor Coolant System component or structure. Signals in excess of the alarm setpoint will result in an alarm condition. The alarms are the "latch-on" type, i.e., the alarms will remain on'when the system returns to normal and will not clear until the alarm is manually reset. There is one alarm indicator in the Control Room for the eight channels such that a "latch on" alarm effectively renders the Control Room alarm indication inoperable for the remaining channels upon receipt of an alarm condition. In addition to the alarm in the Control Room, tape recorders will start when the system is in 'Auto'. There are two tape recorders; each tape recorder can record four system channels at a time.
Technical Specification 3.3.3.7 requires all eight channels of LPDS to be OPERABLE in Modes 1 and 2 (POWER OPERATIONS and STARTUP). Tech'nical Specification 4.3.3.7 requires each channel to be demonstrated OPERABLE by a) a channel check at least once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, b) a Channel Functional Test at least once per 31 days, and c) a Channel Calibration at least once per 18 months'
NRC Document Control Desk Special Report 1-SR-90-005 Page 2 During the previous fuel cycle (March 1988 to March 1989) channel 5, located on Hot Leg 1A, experienced numerous spurious alarms. An engineering evaluation completed in October 1988 determined the system was functioning properly. The channel 5 alarm setpoint was temporarily raised and additional manual monitoring of the LPDS was initiated during the remainder of the fuel cycle (Reference 'Special Report 1-SR-88-008).
During the subsequent refueling outage, the channel 5 alarm setpoint was re'set, the required surveillance tests were performed, and the system placed in service The LPDS was not declared operable because of documentation that could not be closed until after full power was achieved. With the reactor at full power, the LPDS was monitored and Channel 5 was found to be spuriously activating. Therefore, the LPDS was not declared operable pending an evaluation of the actuations. The surveillance tests required by the Technical Specification 4.3.3.7 were performed and kept current during the time the evaluation was being performed. On June 25, 1990 at approximately 1951 MST Unit 1 entered Mode 2 (STARTUP). Technical Specifications permit entry into Mode 1 or Mode 2 with the LPDS inoperable. Unit 1 subsequently entered Mode 1 on June 30, 1990 at approximately 0226 MST.
An engineering evaluation determined that LPDS was operating properly.
The spurious alarms were caused by the system sensitivity required to meet the requirements of Regulatory Guide 1.133, the same cause established in 1988.
Following the engineering evaluation, an action plan for responding to and monitoring the LPDS after spurious alarms was developed. On July 25, 1990 at approximately 1910 MST, LPDS was declared operable.
Cause of Event'he cause of the LPDS Spurious alarms is the sensitivity of the system, as discussed above. The LPDS Channel response is reflective of the excitative energy from the Reactor Coolant System (RCS). APS has observed that, at different power levels and during different plant transients, RCS excitative energies vary which affect the response of the LPDS. Also, other sources (e.g., flow vortexing, core barrel bypass flow, etc.) can produce energy waves which excite the accelerometers.
In many cases, it takes a significant length of time after a plant transient for the RCS to "stabilize" to the point where spurious LPVMS alarms do not occur. This sensitivity is required to meet the requirements of Regulatory Guide 1.133.
Corrective Actions:
An engineer'ing evaluation was performed and determined LPDS was operating properly. The LPDS was declared operable on July 25, 1990 prior to the 30 day Technical Specification Action expiring.
NRC Document Control Desk Special Report 1-SR-90-005 Page 3 The operating procedure for the LPDS has been revised to include a 'high alarm rate condition'lassification for LPDS channels that alarm four or more times in one shift without any 'correlation to plant events or conditions. If a channel is determined to be in the 'high alarm rate condition', the audio from the channel will be monitored once per shift instead of on each alarm occurrence, and a work authorization document initiated to have the channel evaluated every 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. The 'high alarm rate condition's cancelled if a channel does not alarm for 24 .hours.
APS is continuing to evaluate the LPDS to identify opportunities for improvements. An Event Analysis Computer modification is under development which is intended to enhance the ability of the system to discriminate false alarms.