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| | issue date = 04/01/1987 | | | issue date = 04/01/1987 |
| | title = LER 87-001-00:on 870303,spurious Signal from Source Range Instrument Channel N-31 Resulted in ESF Actuation.Caused by Malfunction of Detector.Source Range Instrument Detector Removed,Replaced & Declared Operable on 870314 | | | title = LER 87-001-00:on 870303,spurious Signal from Source Range Instrument Channel N-31 Resulted in ESF Actuation.Caused by Malfunction of Detector.Source Range Instrument Detector Removed,Replaced & Declared Operable on 870314 |
| | author name = BLIND A A | | | author name = Blind A |
| | author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG | | | author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG |
| | addressee name = | | | addressee name = |
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{{#Wiki_filter:NRCForm368(84)3)LICENSEEEVENTREPORTHLER)U.S.NUCLEARREOULATORYCOMMISSIONAPPAOVEDOMBNO.31500104EXPIAES:8/31/88FACILITYNAME(I)DC.CookNuclearPlntUnit2DOCKETNUMBER(21050003PAE3I1OFpESFActuation(InadvertentOpeningofReactorTripBreakers)DuetotheFailureofaSourceRaneNuclearInstrumentationDEVENTDATEI5)LERNUMBER(6)REPORTDATE(7)OTHERFACILITIESINVOLVED(8)MONTHDAYYEARYEARSEQUENTIALNUMBERREVISION8'NNUMBERMONTHDAYYEARFACILITYNAMESDOCKETNUMBER(SI050000303878700100040105000OPERATINOMODE(0)POWERLEVELppp20.402(B)20.405(~)(1)D)20A05(s)(1)(E)20,405(s)(1)(ill)20.405(s)(1)(Iv)20,405(~)(1)(v)20.405(c)60.35(c1(I)50.38(cl(2)50.73(~l(2)li)5073(~)(2)lii)50.73(~l(2)(iiBLICENSEECONTACTFORTHISLEA(12)60,73(s)(2)liv)50,73(s)(2l(v)50.73(s)I2)(vii)50.73(sl(2)(vill)(A)60,73(v)(2)(vlii)IS)50.73(~)(2)(x)0THEREOUIREMENTSOF10CFR():(Chockoniormoriofthtfollovflnpl(11)THISREPORTISSUBMITTEDPUASUANTT73.71(b)73.71(c)oTHERIsptcifyInAbstractbtlovvtnd/nTits,IVIICForm3BEAJNAMEA.A.Blind-AssistantPlantManagerTELEPHONENUMBERAREACODE616465-901COMPLETEONELINEFOREACHCOMPONENTFAILUREDESCRIBEDINTHISREPORT(13)CAUSESYSTEMCOMPONENTIGDETMANUFAC.TURERW1,20EPOATABLE'ymTONPRDS?.2A..QgSYSTEMCOMPONENTMANUFAC.TUREREPORTABLE"TONPROS:i'~in~$nQgg'&MÃSUPPLEMENTALREPORTEXPECTED(14(YESflfyts,complitiEXPECTEDSUShllSSIOIVDATE)NOABSTRACTfLImltto/400sptcts,lt.,tpprorrlmtttlyflfttinslntlisptctryptvvrlttinllnisl(18)EXPECTEDSUBMISSIONDATE(16)MONTHDAYYEAROnMarch3,1987,at1511hours,aspurioussignalfromasourcerangeinstrumentchannel(N-31)resultedinanEngineeredSafetyFeatures(ESF)actuation(inadvertentopeningofthereactortripbreakers).Thereactorwassubcriticalatthetime.TheautomaticESFresponseswereverified,allequipmentfunctionedasdesigned.IFollowinginvestigation,andreviewofpostactuationdata,itwasconcludedthatthesignalfromN-31wasspuriousandduetoamalfunctionofthedetector,andnotanincreaseinthecoreneutronlevel.Thesourcerangeinstrumentdetectorwasremoved,replacedanddeclaredoperableonMarch14,1987at2223hours.8704070471870401PDRADOCK0500031(LSPDRNRCForm385 NRCForm356A(983)LICENSEEEVENTREPORTHLER)TEXTCONTINUATIONU.S.NUCLEARREGULATORYCOMMISSIONAPPROVEOOMBNO.3150&l04EXPIRES:8/31/88FACILITYNAME(1)~OOCKETNUMBER(2)LERNUMBER(6)PAGE(3)YEAR4)5SEQUENTIALNUMBERREVISIONNUMBERD.C.CookNuclearPlant,Unit2TEXT//F/rroroSFoco/4r/O/ror/Iroo/I/OI/4////IC%%dnrr35//AB/(IT)p5ppp316870010002OF04ConditionsPriortoEventUnit2inMode3(HotStandby),at1.0E4cpswithaunitshutdowninprogress.DescritionofEventOnMarch3,1987,at1511hours,aspurioussignalfromasourcerangeinstrumentchannel(N-31)(EIIS/CHA)resultedinanEngineeredSafetyFeatures(ESF)actuation[inadvertentopeningofthereactortripbreakers(EIIS/BKR)].Thereactorwassubcriticalatthetimewithallcontrolrodbanks(EIIS/ROD),andoneshutdownrodbank(D),fullyinserted.Anothershutdownrodbank(C)wasbeinginsertedwhentheeventoccurred.OperationspersonnelimmediatelyimplementedEmergencyOperatingProcedure1OHP4023.E-Otoverifyproperresponseoftheautomaticprotectionsystem(EIIS:JC)andtoassessplantconditionsforinitiatingappropriaterecoveryactions.TheN-31sourcerangeinstrumentchannelwasreturnedtoserviceonMarch14,1987at2223hoursfollowingdetectorreplacement.TheautomaticESFresponseswereverified,allequipmentfunctionedasdesigned.However,sincetheunitwasinHotStandbyandshutdown;themainfeedwaterpumps(EIIS/P)werepreviouslyremovedfromservice',theturbine/generator(EIIS/TRB-GEN)wasinatrippedcondition,nosteamdump/pressurereliefwasnecessary,andtheauxiliaryfeedwaterpumpswereinservice.System/Equipmentresponsesthatdidoccurincluded;theopeningofthereactortripbreakersandtheinsertionoftheshutdownrodsremainingtobeinserted.Reactorcoolantpump(EIIS/P)operationwasmaintainedthroughouttheeventandnoabnormaloccurrenceswerenoted.Therewerenostructures,components,orsystemsinoperableatthestartofthiseventwhichcouldhavecontributedtothisESFactuation,withtheexceptionofthesubjectsourcerangemalfunction.CauseofEventFollowinginvestigation,andreviewofpostactuationdata,itwasconcludedthatthesignalfromN-31wasspuriousandduetoamalfunctionofthedetector(EIIS/DET)andnotanincreaseinthecoreneutronlevel.Currentcharacteristicscurveswereobtainedforthedetectorand,basedontheWestinghouseManual,itwasdeterminedthatthedetectorfailedduetoairin-leakage.NRCFORM3SSA(94)3I*U.S.GPO:19880824538/455 NRCForm388A(983ILICENSEEEVENTREPORTHLER)TEXTCONTINUATIONU.S.NUCLEARREGULATORYCOMMISSIONAPPROVEDOMBNO,3')50-0104EXPIRES:8/31/BBFACILITYNAME(I)DOCKETNUMBER(2)YEARLERNUMBERl6)SECVENTIALNUMBERREYIEloNNVMERPAGE(3)D.C.CookNuclearPlant,Unit2T)D(T///moro4/rooo/4Eo//rrr/Irwa//rr/one/HRCForm358AB/(IT)050003167001003oF04AnalsisofEventThiseventisbeingreportedpertherequirementsof10CFR50.73(a)(2)(IV),asaneventthatresultedinautomaticactuationofanyEngineeredSafetyFeatureincludingtheReactorProtectionSystem.Thesourcerangeinstrumentationmonitorsthecoreneutronfluxlevelduringreactorshutdownandtheinitialstagesofreactorstartup.Thesourcerangechannelsprovidereactorprotectionbyinitiatingareactortripatarelativelylowneutroncountratetoterminatealowpower/highstartuprateaccident.Theactuationcoincidenceis1of2channels>1.0E5cps.DuringreactorstartupthesourcerangetripsareblockedabovepermissiveP-6(approximately6.0E-llampsontheintermediaterangenuclearinstrumentation).ThesourcerangechannelprotectionisautomaticallyreinstatedwhenreactorpowerdecreasesbelowP-6duringshutdowns.Priortothisevent,bothsourcerangechannelshadre-energizedwhenreactorpowerhaddecreasedbelowP-6.Sincealowpower/highstartuprateconditiondidnotexistduringthisevent,andallreactorProtectionsystemsfunctionedasdesigneduponthereceiptoftheactuationsig'nal,ithasbeenconcludedthatthehealthandsafetyofthepublicwerenotjeopardized.NRCPOllM388A194)3)-oU.S.CPO;19880824538/455 NRCFI>>)II3MA(94)3)LICENSEEEVENTREPORT(LER)TEXTCONTINUATIONU.S.NUCLEARAEGULATOAYCOMMISSIONAPPROVEOOMBNO.3(50&104EXPIRES:8/31/SBFACILITYNAME(11OOCKETNUMBER(2)YEARLERNUMBER(6)SEGVENTIALNVMSSRREVISIONNVMSSRPAGE(3)D.C.CookNuclearPlant,Unit2TEXT/Fmo>>4P>>c>>/4/sq>>kaf,uds//I/d>>4/NRCFamI36843/(IT)osooo31687001004QF04CorrectiveActionsThesourcerangeinstrumentdetectorwasremoved,replacedanddeclaredoperableonMarch14,1987at2223hours.FailedComonentIdentificationSourceRangeNuclearInstrumentationDetector(plantdesignationN-31).Manufacturer:WestinghouseModelNumber:WL23706EIIS:DETPreviousSimilarEventsNopreviouseventshaveoccurred.NRCFOAMSSSA983)*U.S.GPO:1986.0-824538/455}} | | {{#Wiki_filter:NRC Form 368 U.S. NUCLEAR REOULATORY COMMISSION (84)3) |
| | APPAOVED OMB NO. 31500104 EXPIAES: 8/31/88 LICENSEE EVENT REPORT HLER) |
| | FACILITY NAME (I) DOCKET NUMBER (21 PA E 3I D C. Cook Nuclear Pl nt Unit 2 0 5 0 0 0 3 1 OFp ESF Actuation (Inadvertent Opening of Reactor Trip Breakers) Due to the Failure of a Source Ran e Nuclear Instrumentation D EVENT DATE I5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8) |
| | MONTH DAY YEAR YEAR SEQUENTIAL REVISION MONTH DAY YEAR FACILITYNAMES DOCKET NUMBER(SI NUMBER 8'N NUMBER 0 5 0 0 0 030 3 8 7 8 7 0 0 1 0 0 04 01 0 5 0 0 0 OP E RAT I NO THIS REPORT IS SUBMITTED PUASUANT T 0 THE REOUIREMENTS OF 10 CFR (): (Chock oni or mori of tht follovflnpl (11) |
| | MODE (0) 20.402(B) 73.71(b) 20.405(c) 60,73(s)(2)liv) |
| | POWE R 20.405( ~ )(1)D) 60.35(c 1 (I) 50,73(s) ( 2 l(v) 73.71(c) |
| | LEVEL p p p 20A05(s)(1)(E) 50.38(cl(2) 50.73(s) I 2) (vii) oTHER Isptcify In Abstract btlovvtnd /n Tits, IVIICForm 20,405(s)(1)(ill) 50.73( ~ l(2)li) 50.73(sl(2)(vill)(A) 3BEAJ 20.405(s)(1) (Iv) 5073( ~ )(2)lii) 60,73(v)(2)(vlii) IS) 20,405( ~ )(1)(v) 50.73( ~ l(2)(iiB 50.73( ~ )(2)(x) |
| | LICENSEE CONTACT FOR THIS LEA (12) |
| | NAME TELEPHONE NUMBER AREA CODE A. A. Blind Assistant Plant Manager 61 646 5- 901 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) |
| | CAUSE SYSTEM COMPONENT MANUFAC. EPOATABLE 'ym SYSTEM COMPONENT MANUFAC. EPORTABLE " |
| | TO NPRDS TO NPROS:i TURER |
| | ?. 2 A.. Qg TURER '~in~ $ |
| | nQgg'&MÃ IG DET W1,2 0 SUPPLEMENTAL REPORT EXPECTED (14( MONTH DAY YEAR EXPECTED SUBMISSION DATE (16) |
| | YES flfyts, compliti EXPECTED SUShllSSIOIV DATE) NO ABSTRACT fLImlt to /400 sptcts, lt., tpprorrlmtttly flfttinslntli sptct ryptvvrlttin llnisl (18) |
| | On March 3, 1987, at 1511 hours, a spurious signal from a source range instrument channel (N-31) resulted in an Engineered Safety Features (ESF) actuation (inadvertent opening of the reactor trip breakers). The reactor was subcritical at the time. The automatic ESF responses were verified, all equipment I functioned as designed. |
| | Following investigation, and review of post actuation data, concluded that the signal from N-31 was spurious and due to a malfunction it was of the detector, and not an increase in the core neutron level. |
| | The source range instrument detector was removed, replaced and declared operable on March 14, 1987 at 2223 hours. |
| | 870407047 1 870401 PDR ADOCK 0500031(L S PDR NRC Form 385 |
| | |
| | NRC Form 356A U.S. NUCLEAR REGULATORY COMMISSION (983) |
| | LICENSEE EVENT REPORT HLER) TEXT CONTINUATION APPROVEO OMB NO. 3150&l04 EXPIRES: 8/31/88 FACILITYNAME (1) ~ OOCKET NUMBER (2) LER NUMBER (6) PAGE (3) |
| | REVISION YEAR 4)5 SEQUENTIAL NUMBER NUMBER D. C. Cook Nuclear Plant, Unit 2 p 5 p p p 3 1 6 8 7 0 0 1 00 02 OF 04 TEXT //F/rroro SFoco /4 r/O/ror/ Iroo /I/OI/4/ ///IC %%dnrr 35//AB/ (IT) |
| | Conditions Prior to Event Unit 2 in Mode 3 (Hot Standby), at 1.0 E4 cps with a unit shutdown in progress. |
| | Descri tion of Event On March 3, 1987, at 1511 hours, a spurious signal from a source range instrument channel (N-31) (EIIS/CHA) resulted in an Engineered Safety Features (ESF) actuation [inadvertent opening of the reactor trip breakers (EIIS/BKR)]. The reactor was subcritical at the time with all control rod banks (EIIS/ROD), and one shutdown rod bank (D), |
| | fully inserted. Another shutdown rod bank (C) was being inserted when the event occurred. Operations personnel immediately implemented Emergency Operating Procedure 1 OHP 4023.E-O to verify proper response of the automatic protection system (EIIS:JC) and to assess plant conditions for initiating appropriate recovery actions. The N-31 source range instrument channel was returned to service on March 14, 1987 at 2223 hours following detector replacement. |
| | The automatic ESF responses were verified, all equipment functioned as designed. However, since the unit was in Hot Standby and shutdown; the main feedwater pumps (EIIS/P) were previously removed from service', |
| | the turbine/generator (EIIS/TRB-GEN) was in a tripped condition, no steam dump/pressure relief was necessary, and the auxiliary feedwater pumps were in service. |
| | System/Equipment responses that did occur included; the opening of the reactor trip breakers and the insertion of the shutdown rods remaining to be inserted. Reactor coolant pump (EIIS/P) operation was maintained throughout the event and no abnormal occurrences were noted. |
| | There were no structures, components, or systems inoperable at the start of this event which could have contributed to this ESF actuation, with the exception of the subject source range malfunction. |
| | Cause of Event Following investigation, and review of post actuation data, it was concluded that the signal from N-31 was spurious and due to a malfunction of the detector (EIIS/DET) and not an increase in the core neutron level. |
| | Current characteristics curves were obtained for the detector and, based on the Westinghouse Manual, it was determined that the detector failed due to air in-leakage. |
| | NRC FORM 3SSA *U.S.GPO:1988 0 824 538/455 (94)3 I |
| | |
| | NRC Form 388A U.S. NUCLEAR REGULATORY COMMISSION (983 I LICENSEE EVENT REPORT HLER) TEXT CONTINUATION APPROVED OMB NO, 3')50-0104 EXPIRES: 8/31/BB FACILITY NAME (I) DOCKET NUMBER (2) LER NUMBER l6) PAGE (3) |
| | YEAR SECVENTIAL REYIEloN NUMBER NVM ER D. C. Cook Nuclear Plant, Unit 2 0 5 0 0 0 3 1 6 7 001 0 0 3 oF 0 4 T)D(T ///moro 4/rooo /4 Eo//rrr/ Irw a//rr/one/HRC Form 358AB/ (IT) |
| | Anal sis of Event This event is being reported per the requirements of 10CFR50.73 (a)(2)(IV), as an event that resulted in automatic actuation of any Engineered Safety Feature including the Reactor Protection System. |
| | The source range instrumentation monitors the core neutron flux level during reactor shutdown and the initial stages of reactor startup. The source range channels provide reactor protection by initiating a reactor trip at a relatively low neutron count rate to terminate a low power/high startup rate accident. The actuation coincidence is 1 of 2 channels > 1.0 E5 cps. During reactor startup the source range trips are blocked above permissive P-6 (approximately 6.0 E-ll amps on the intermediate range nuclear instrumentation). |
| | The source range channel protection is automatically reinstated when reactor power decreases below P-6 during shutdowns. Prior to this event, both source range channels had re-energized when reactor power had decreased below P-6. |
| | Since a low power/high startup rate condition did not exist during this event, and all reactor Protection systems functioned as designed upon the receipt of the actuation sig'nal, concluded that the health and safety of the public were not it has been jeopardized. |
| | NRC POllM 388A -oU.S.CPO;1988 0 824 538/455 194)3) |
| | |
| | NRC FI>>)II 3MA U.S. NUCLEAR AEGULATOAYCOMMISSION (94)3) |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO OMB NO. 3(50&104 EXPIRES: 8/31/SB FACILITY NAME (11 OOCKET NUMBER (2) LER NUMBER (6) PAGE (3) |
| | YEAR SEGVENTIAL REVISION NVMSSR NVMSSR D. C. Cook Nuclear Plant, Unit 2 o s o o o 3 1687 001 0 0 4 QF 0 4 TEXT /Fmo>> 4P>>c>> /4/sq>>kaf, uds //I/d>>4/NRC FamI 36843/(IT) |
| | Corrective Actions The source range instrument detector was removed, replaced and declared operable on March 14, 1987 at 2223 hours. |
| | Failed Com onent Identification Source Range Nuclear Instrumentation Detector (plant designation N-31). |
| | Manufacturer: Westinghouse Model Number: WL23706 EIIS:DET Previous Similar Events No previous events have occurred. |
| | NRC FOAM SSSA *U.S.GPO:1986.0-824 538/455 983)}} |
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Updated LER Will Be Submitted by 990405 ML17335A5011999-02-0101 February 1999 LER 98-060-00:on 981231,identified That Rt Sys Response Time Testing Did Not Comply with TS Definition.Caused by Inadequate Procedures.Corrective Actions Will Be Developed & Update to LER Will Be Submitted by 990415.With 990201 Ltr ML17335A4951999-01-29029 January 1999 LER 98-059-00:on 981230,interim LER -single Failure in Containment Spray Sys Could Result in Containment Spray Ph Outside Design Occurred.Investigation Into Condition Continuing.Update Will Be Submitted by 990514 Ltr ML17335A4961999-01-27027 January 1999 LER 98-057-00:on 981228,discovered That AFW Valves Were Not Tested IAW Inservice Testing Program.Caused by Failure to Recognize Design Bases Features Re Afws by Personnel. Updated LER Will Be Submittted by 990415.With 990127 Ltr ML17335A4921999-01-19019 January 1999 LER 98-052-01:on 981128,no Analysis for NSR Sc Manual Loader for Tdafwp Could Be Found in Original Design.Cause Due to All Failure Modes Not Considered When Compressed Air Sys Originally Designed.Performed Review of Components ML17335A4721999-01-0606 January 1999 LER 98-055-00:on 981207,potential for Condition Outside of Design Bases for Rod Control Sys Was Noted.Caused by Calibration Error Coupled with Single Rod Failure.Condition Rept Investigation Is Ongoing ML17335A4691999-01-0606 January 1999 LER 98-056-00:on 981211,hot Leg Nozzle Gaps Resulted in Plant Being in Unanalyzed Condition.Analyses Are Being Performed by W to Resolve Problem.Updated LER Will Be Submitted by 990211.With 990106 Ltr ML17335A4661999-01-0505 January 1999 LER 98-049-00:on 981020,emergency Boron Injection Flow Path Was Inoperable.Caused by Original Design Deficiency. Engineering Evaluation of Event Is Continuing ML17335A4631999-01-0404 January 1999 LER 98-054-00:on 981202,discovered That at Least One MSSV Had Not Been Reset as Required by Ts.Engineering Is Continuing Review of Extent of Condition for Event.Updated LER Will Be Submitted by 990129.With 990104 Ltr ML17335A4481998-12-30030 December 1998 LER 98-053-00:on 981130,discovered Use of Inoperable Substitute Subcooling Margin Monitor.Caused by Condition Existing Since Installation of Plant Process Computer in 1992.Updated LER Will Be Submitted.With 981230 Ltr ML17335A4581998-12-28028 December 1998 LER 98-052-00:on 981128,turbine Driven AFW Pump Speed Controller Failure Mode Occurred.Caused Because Not All Failure Modes Were Considered When Compressed Air Sys Was Originally Designed.Verified Current Design Change Process ML17335A4281998-12-22022 December 1998 LER 98-051-00:on 981122,reactor Trip Signal from Manual Safety Injection Not Verified as Required by TS Surveillance,Was Discovered.Maintenance Currently Evaluating Significance & Cause of Event ML17335A4111998-12-17017 December 1998 LER 98-047-00:on 981117,potential for Increase Leakage from Reactor Coolant Pump Seals Was Identified.Util Is Working with W to Resolve Issue.Current Expectations Are to Submit Update to LER by 990215.With 981217 Ltr ML17335A4141998-12-16016 December 1998 LER 98-058-00:on 981216,postulated High Line Break Could Result in Condition Outside Design Bases for AF Occurred. Caused by Deficiencies Associated with Administration of HELB Program.Analysis of AF Will Be Completed by 990122 ML17335A4181998-12-16016 December 1998 LER 98-050-00:on 980814,ancillary Equipment Installed in Ice Condenser Was Not Designed to Withstand Design Basis Accident/Earthquake Loads.Caused by Lack of Established Design Criteria.Developed Design Criteria ML17335A3871998-12-11011 December 1998 LER 98-031-01:on 980610,potential Common Mode Failure of RHR Pumps Were Noted.Caused by Inaccurate Values.Accurate Miniflow Numbers Have Been Determined by Flow Testing ML17335A3821998-12-0808 December 1998 LER 98-039-01 Re EOP Step Conflicts with Small Break LOCA Analysis.Ler 98-039-00 Has Been Canceled.With 981208 Ltr ML17335A3781998-12-0707 December 1998 LER 98-007-00:on 981106,high Energy Line Break Effects in Auxiliary FW Sys Was Noted.Cause of Event Is Under Investigation & Will Be Completed by 990220.Updated LER Will Be Submitted by 990310.With 981207 Ltr ML17335A3771998-12-0303 December 1998 LER 98-046-00:on 981103,determined That Afs Was Unable to Meet Design Flow Requirements During Special Test.Caused by Failure to Consider All Aspects of Sys Operation in Design of Suction Basket Strainers.Sys Will Be Redesigned ML17335A3741998-12-0202 December 1998 LER 97-011-02:on 970822,operation Was Noted Outside Design Bases for ECCS & CSP for Switchover to Recirculation Sump Suction.Caused by Ineffective Change Mgt.Revised Procedure for Switchover 01(02) Ohp 4023.ES-1.3 1999-09-17
[Table view] Category:RO)
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors ML17335A5171999-02-11011 February 1999 LER 99-002-00:on 990112,determined That RCS Pressurizer PORVs Had Not Been Tested,Per Ts.Caused by Inadequate Scheduling Controls Allowing Personnel Error.Surveillance Procedure Was Completed & Updated LER Will Be Submitted ML17335A5141999-02-10010 February 1999 LER 99-001-00:on 990106,noted That GE Hfa Relays Installed in EDGs May Not Meet Seismic Qualification.Caused by Operating Experience Info Incorrectly Dispositioned in 1985. Updated LER Will Be Submitted by 990405 ML17335A5011999-02-0101 February 1999 LER 98-060-00:on 981231,identified That Rt Sys Response Time Testing Did Not Comply with TS Definition.Caused by Inadequate Procedures.Corrective Actions Will Be Developed & Update to LER Will Be Submitted by 990415.With 990201 Ltr ML17335A4951999-01-29029 January 1999 LER 98-059-00:on 981230,interim LER -single Failure in Containment Spray Sys Could Result in Containment Spray Ph Outside Design Occurred.Investigation Into Condition Continuing.Update Will Be Submitted by 990514 Ltr ML17335A4961999-01-27027 January 1999 LER 98-057-00:on 981228,discovered That AFW Valves Were Not Tested IAW Inservice Testing Program.Caused by Failure to Recognize Design Bases Features Re Afws by Personnel. Updated LER Will Be Submittted by 990415.With 990127 Ltr ML17335A4921999-01-19019 January 1999 LER 98-052-01:on 981128,no Analysis for NSR Sc Manual Loader for Tdafwp Could Be Found in Original Design.Cause Due to All Failure Modes Not Considered When Compressed Air Sys Originally Designed.Performed Review of Components ML17335A4721999-01-0606 January 1999 LER 98-055-00:on 981207,potential for Condition Outside of Design Bases for Rod Control Sys Was Noted.Caused by Calibration Error Coupled with Single Rod Failure.Condition Rept Investigation Is Ongoing ML17335A4691999-01-0606 January 1999 LER 98-056-00:on 981211,hot Leg Nozzle Gaps Resulted in Plant Being in Unanalyzed Condition.Analyses Are Being Performed by W to Resolve Problem.Updated LER Will Be Submitted by 990211.With 990106 Ltr ML17335A4661999-01-0505 January 1999 LER 98-049-00:on 981020,emergency Boron Injection Flow Path Was Inoperable.Caused by Original Design Deficiency. Engineering Evaluation of Event Is Continuing ML17335A4631999-01-0404 January 1999 LER 98-054-00:on 981202,discovered That at Least One MSSV Had Not Been Reset as Required by Ts.Engineering Is Continuing Review of Extent of Condition for Event.Updated LER Will Be Submitted by 990129.With 990104 Ltr ML17335A4481998-12-30030 December 1998 LER 98-053-00:on 981130,discovered Use of Inoperable Substitute Subcooling Margin Monitor.Caused by Condition Existing Since Installation of Plant Process Computer in 1992.Updated LER Will Be Submitted.With 981230 Ltr ML17335A4581998-12-28028 December 1998 LER 98-052-00:on 981128,turbine Driven AFW Pump Speed Controller Failure Mode Occurred.Caused Because Not All Failure Modes Were Considered When Compressed Air Sys Was Originally Designed.Verified Current Design Change Process ML17335A4281998-12-22022 December 1998 LER 98-051-00:on 981122,reactor Trip Signal from Manual Safety Injection Not Verified as Required by TS Surveillance,Was Discovered.Maintenance Currently Evaluating Significance & Cause of Event ML17335A4111998-12-17017 December 1998 LER 98-047-00:on 981117,potential for Increase Leakage from Reactor Coolant Pump Seals Was Identified.Util Is Working with W to Resolve Issue.Current Expectations Are to Submit Update to LER by 990215.With 981217 Ltr ML17335A4141998-12-16016 December 1998 LER 98-058-00:on 981216,postulated High Line Break Could Result in Condition Outside Design Bases for AF Occurred. Caused by Deficiencies Associated with Administration of HELB Program.Analysis of AF Will Be Completed by 990122 ML17335A4181998-12-16016 December 1998 LER 98-050-00:on 980814,ancillary Equipment Installed in Ice Condenser Was Not Designed to Withstand Design Basis Accident/Earthquake Loads.Caused by Lack of Established Design Criteria.Developed Design Criteria ML17335A3871998-12-11011 December 1998 LER 98-031-01:on 980610,potential Common Mode Failure of RHR Pumps Were Noted.Caused by Inaccurate Values.Accurate Miniflow Numbers Have Been Determined by Flow Testing ML17335A3821998-12-0808 December 1998 LER 98-039-01 Re EOP Step Conflicts with Small Break LOCA Analysis.Ler 98-039-00 Has Been Canceled.With 981208 Ltr ML17335A3781998-12-0707 December 1998 LER 98-007-00:on 981106,high Energy Line Break Effects in Auxiliary FW Sys Was Noted.Cause of Event Is Under Investigation & Will Be Completed by 990220.Updated LER Will Be Submitted by 990310.With 981207 Ltr ML17335A3771998-12-0303 December 1998 LER 98-046-00:on 981103,determined That Afs Was Unable to Meet Design Flow Requirements During Special Test.Caused by Failure to Consider All Aspects of Sys Operation in Design of Suction Basket Strainers.Sys Will Be Redesigned ML17335A3741998-12-0202 December 1998 LER 97-011-02:on 970822,operation Was Noted Outside Design Bases for ECCS & CSP for Switchover to Recirculation Sump Suction.Caused by Ineffective Change Mgt.Revised Procedure for Switchover 01(02) Ohp 4023.ES-1.3 1999-09-17
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5481999-09-30030 September 1999 Non-proprietary DC Cook Nuclear Plant Units 1 & 2 Mods to Containment Sys W SE (Secl 99-076,Rev 3). ML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors 1999-09-30
[Table view] |
Text
NRC Form 368 U.S. NUCLEAR REOULATORY COMMISSION (84)3)
APPAOVED OMB NO. 31500104 EXPIAES: 8/31/88 LICENSEE EVENT REPORT HLER)
FACILITY NAME (I) DOCKET NUMBER (21 PA E 3I D C. Cook Nuclear Pl nt Unit 2 0 5 0 0 0 3 1 OFp ESF Actuation (Inadvertent Opening of Reactor Trip Breakers) Due to the Failure of a Source Ran e Nuclear Instrumentation D EVENT DATE I5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR SEQUENTIAL REVISION MONTH DAY YEAR FACILITYNAMES DOCKET NUMBER(SI NUMBER 8'N NUMBER 0 5 0 0 0 030 3 8 7 8 7 0 0 1 0 0 04 01 0 5 0 0 0 OP E RAT I NO THIS REPORT IS SUBMITTED PUASUANT T 0 THE REOUIREMENTS OF 10 CFR (): (Chock oni or mori of tht follovflnpl (11)
MODE (0) 20.402(B) 73.71(b) 20.405(c) 60,73(s)(2)liv)
POWE R 20.405( ~ )(1)D) 60.35(c 1 (I) 50,73(s) ( 2 l(v) 73.71(c)
LEVEL p p p 20A05(s)(1)(E) 50.38(cl(2) 50.73(s) I 2) (vii) oTHER Isptcify In Abstract btlovvtnd /n Tits, IVIICForm 20,405(s)(1)(ill) 50.73( ~ l(2)li) 50.73(sl(2)(vill)(A) 3BEAJ 20.405(s)(1) (Iv) 5073( ~ )(2)lii) 60,73(v)(2)(vlii) IS) 20,405( ~ )(1)(v) 50.73( ~ l(2)(iiB 50.73( ~ )(2)(x)
LICENSEE CONTACT FOR THIS LEA (12)
NAME TELEPHONE NUMBER AREA CODE A. A. Blind Assistant Plant Manager 61 646 5- 901 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFAC. EPOATABLE 'ym SYSTEM COMPONENT MANUFAC. EPORTABLE "
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nQgg'&MÃ IG DET W1,2 0 SUPPLEMENTAL REPORT EXPECTED (14( MONTH DAY YEAR EXPECTED SUBMISSION DATE (16)
YES flfyts, compliti EXPECTED SUShllSSIOIV DATE) NO ABSTRACT fLImlt to /400 sptcts, lt., tpprorrlmtttly flfttinslntli sptct ryptvvrlttin llnisl (18)
On March 3, 1987, at 1511 hours0.0175 days <br />0.42 hours <br />0.0025 weeks <br />5.749355e-4 months <br />, a spurious signal from a source range instrument channel (N-31) resulted in an Engineered Safety Features (ESF) actuation (inadvertent opening of the reactor trip breakers). The reactor was subcritical at the time. The automatic ESF responses were verified, all equipment I functioned as designed.
Following investigation, and review of post actuation data, concluded that the signal from N-31 was spurious and due to a malfunction it was of the detector, and not an increase in the core neutron level.
The source range instrument detector was removed, replaced and declared operable on March 14, 1987 at 2223 hours0.0257 days <br />0.618 hours <br />0.00368 weeks <br />8.458515e-4 months <br />.
870407047 1 870401 PDR ADOCK 0500031(L S PDR NRC Form 385
NRC Form 356A U.S. NUCLEAR REGULATORY COMMISSION (983)
LICENSEE EVENT REPORT HLER) TEXT CONTINUATION APPROVEO OMB NO. 3150&l04 EXPIRES: 8/31/88 FACILITYNAME (1) ~ OOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
REVISION YEAR 4)5 SEQUENTIAL NUMBER NUMBER D. C. Cook Nuclear Plant, Unit 2 p 5 p p p 3 1 6 8 7 0 0 1 00 02 OF 04 TEXT //F/rroro SFoco /4 r/O/ror/ Iroo /I/OI/4/ ///IC %%dnrr 35//AB/ (IT)
Conditions Prior to Event Unit 2 in Mode 3 (Hot Standby), at 1.0 E4 cps with a unit shutdown in progress.
Descri tion of Event On March 3, 1987, at 1511 hours0.0175 days <br />0.42 hours <br />0.0025 weeks <br />5.749355e-4 months <br />, a spurious signal from a source range instrument channel (N-31) (EIIS/CHA) resulted in an Engineered Safety Features (ESF) actuation [inadvertent opening of the reactor trip breakers (EIIS/BKR)]. The reactor was subcritical at the time with all control rod banks (EIIS/ROD), and one shutdown rod bank (D),
fully inserted. Another shutdown rod bank (C) was being inserted when the event occurred. Operations personnel immediately implemented Emergency Operating Procedure 1 OHP 4023.E-O to verify proper response of the automatic protection system (EIIS:JC) and to assess plant conditions for initiating appropriate recovery actions. The N-31 source range instrument channel was returned to service on March 14, 1987 at 2223 hours0.0257 days <br />0.618 hours <br />0.00368 weeks <br />8.458515e-4 months <br /> following detector replacement.
The automatic ESF responses were verified, all equipment functioned as designed. However, since the unit was in Hot Standby and shutdown; the main feedwater pumps (EIIS/P) were previously removed from service',
the turbine/generator (EIIS/TRB-GEN) was in a tripped condition, no steam dump/pressure relief was necessary, and the auxiliary feedwater pumps were in service.
System/Equipment responses that did occur included; the opening of the reactor trip breakers and the insertion of the shutdown rods remaining to be inserted. Reactor coolant pump (EIIS/P) operation was maintained throughout the event and no abnormal occurrences were noted.
There were no structures, components, or systems inoperable at the start of this event which could have contributed to this ESF actuation, with the exception of the subject source range malfunction.
Cause of Event Following investigation, and review of post actuation data, it was concluded that the signal from N-31 was spurious and due to a malfunction of the detector (EIIS/DET) and not an increase in the core neutron level.
Current characteristics curves were obtained for the detector and, based on the Westinghouse Manual, it was determined that the detector failed due to air in-leakage.
NRC FORM 3SSA *U.S.GPO:1988 0 824 538/455 (94)3 I
NRC Form 388A U.S. NUCLEAR REGULATORY COMMISSION (983 I LICENSEE EVENT REPORT HLER) TEXT CONTINUATION APPROVED OMB NO, 3')50-0104 EXPIRES: 8/31/BB FACILITY NAME (I) DOCKET NUMBER (2) LER NUMBER l6) PAGE (3)
YEAR SECVENTIAL REYIEloN NUMBER NVM ER D. C. Cook Nuclear Plant, Unit 2 0 5 0 0 0 3 1 6 7 001 0 0 3 oF 0 4 T)D(T ///moro 4/rooo /4 Eo//rrr/ Irw a//rr/one/HRC Form 358AB/ (IT)
Anal sis of Event This event is being reported per the requirements of 10CFR50.73 (a)(2)(IV), as an event that resulted in automatic actuation of any Engineered Safety Feature including the Reactor Protection System.
The source range instrumentation monitors the core neutron flux level during reactor shutdown and the initial stages of reactor startup. The source range channels provide reactor protection by initiating a reactor trip at a relatively low neutron count rate to terminate a low power/high startup rate accident. The actuation coincidence is 1 of 2 channels > 1.0 E5 cps. During reactor startup the source range trips are blocked above permissive P-6 (approximately 6.0 E-ll amps on the intermediate range nuclear instrumentation).
The source range channel protection is automatically reinstated when reactor power decreases below P-6 during shutdowns. Prior to this event, both source range channels had re-energized when reactor power had decreased below P-6.
Since a low power/high startup rate condition did not exist during this event, and all reactor Protection systems functioned as designed upon the receipt of the actuation sig'nal, concluded that the health and safety of the public were not it has been jeopardized.
NRC POllM 388A -oU.S.CPO;1988 0 824 538/455 194)3)
NRC FI>>)II 3MA U.S. NUCLEAR AEGULATOAYCOMMISSION (94)3)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO OMB NO. 3(50&104 EXPIRES: 8/31/SB FACILITY NAME (11 OOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR SEGVENTIAL REVISION NVMSSR NVMSSR D. C. Cook Nuclear Plant, Unit 2 o s o o o 3 1687 001 0 0 4 QF 0 4 TEXT /Fmo>> 4P>>c>> /4/sq>>kaf, uds //I/d>>4/NRC FamI 36843/(IT)
Corrective Actions The source range instrument detector was removed, replaced and declared operable on March 14, 1987 at 2223 hours0.0257 days <br />0.618 hours <br />0.00368 weeks <br />8.458515e-4 months <br />.
Failed Com onent Identification Source Range Nuclear Instrumentation Detector (plant designation N-31).
Manufacturer: Westinghouse Model Number: WL23706 EIIS:DET Previous Similar Events No previous events have occurred.
NRC FOAM SSSA *U.S.GPO:1986.0-824 538/455 983)