ML18065A143: Difference between revisions

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__ No. Date Type 1 2 8/30/95 F 3 9/11/95 F l. F: Forced S: Scheduled Duration (Hours) 2. Reason: 12.8 32.5 Reason 2 A A A-Equipment Failure (Explain) 8-Maintenance or Test C-Refue ling D-Regulatory E-Operator Training & License Examination F-Administrative G-Operational Error (Explain)
__ No. Date Type 1 2 8/30/95 F 3 9/11/95 F l. F: Forced S: Scheduled Duration (Hours) 2. Reason: 12.8 32.5 Reason 2 A A A-Equipment Failure (Explain) 8-Maintenance or Test C-Refue ling D-Regulatory E-Operator Training & License Examination F-Administrative G-Operational Error (Explain)
H-Other (Explain)
H-Other (Explain)
UNIT SHUTDOWNS AND POWER REDUCTIONS Method of Licensee Shutting Event Down Reactor 3 Report # 4 4 3. Method: 1-Manual 2-Manual Scram 3-Automatic Scram 4-0ther (Explain)  
UNIT SHUTDOWNS AND POWER REDUCTIONS Method of Licensee Shutting Event Down Reactor 3 Report # 4 4 3. Method: 1-Manual 2-Manual Scram 3-Automatic Scram 4-0ther (Explain)
: 4. System Code 4 Component Code 5 Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG-0161)
: 4. System Code 4 Component Code 5 Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG-0161)
DOCKET NO 50-255 UN IT Pali sades DATE _____lg/04/95 COMPLETED BY BWBerles TELEPHONE (616)764-8913 Cause & Corrective Action to Prevent Recurrence Power was reduced from 99.6% due to a Motor Operated Disconnect in the switchyard overheating.
DOCKET NO 50-255 UN IT Pali sades DATE _____lg/04/95 COMPLETED BY BWBerles TELEPHONE (616)764-8913 Cause & Corrective Action to Prevent Recurrence Power was reduced from 99.6% due to a Motor Operated Disconnect in the switchyard overheating.
The unit was taken off-line at 0208 on 9/2/95 and placed back on-line at 1458 on 9/2. Power was reduced from 100% on 9/11 at 1800 and the unit was off-line at 2106 to repair a conductor between an isophase bus and the main generator.
The unit was taken off-line at 0208 on 9/2/95 and placed back on-line at 1458 on 9/2. Power was reduced from 100% on 9/11 at 1800 and the unit was off-line at 2106 to repair a conductor between an isophase bus and the main generator.
The unit was on-line on 9/13 at 0538. 5. Exhibit I -Same Source !, I 1i .. . .}}
The unit was on-line on 9/13 at 0538. 5. Exhibit I -Same Source !, I 1i .. . .}}

Revision as of 19:44, 25 April 2019

Monthly Operating Rept for Sept 1995 for Palisades Nuclear Plant.W/951004 Ltr
ML18065A143
Person / Time
Site: Palisades Entergy icon.png
Issue date: 09/30/1995
From: BERLES B W, WILLIAMS A L
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9510110092
Download: ML18065A143 (5)


Text

.* ( I consumers Power POWERING lllllCHIGAN"S PROGRESS Palisades Nuclear Plant: 27780 Blue Star Memorial Highway, Coven. Ml 49043 October 4, 1995 US Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 LICENSEE REPORT OF MONTHLY OPERATING DATA DPR-20, DOCKET NO 50-255 Enclosed is a copy of the Monthly Operating Data and Summary of Operating Experience for the Palisades Nuclear Plant for the month of September, 1995. If you have any questions or concerns, please feel free to contact me at (616) 764-8913, extension 0113. Sincerely, A L Wi 11 i ams Reactor Engineer CC: RAVincent, Palisades Senior Resident Inspector, Palisades DRHahn, Div of Rad Health Services, Lansing, MI BWJorgensen, Michigan Dept of Labor, Lansing, MI JPadgett, Michigan Public Service Commission Records Center, INPO, Atlanta, GA CWMain, Palisades SMMclntyre, Pl3-121 Region III Administrator, USNRC

  • Document Control, 950*22*35*10/L Cycle 12 Reports 9510110092 950930 PDR . 'AD.OCK 05000255 R -" ... : . --. ----. . ( . I;' l I A CMS' ENERGY COMPANY
._. OPERAT1NG STATUS
1. UNIT NAME 2. 3. . . . REPORTING PERIOD
* LICENSED THERMAL .POWER (MWt) _4. NAMEPLATE RATING (GROSS MWei 5 *. 6ESIGN ELECTRICAL RATING (NET MWe) 6. MAXIMUM DEPENDABLE-CAPACITY* (GROSS MWe) OPERATING DATA REPORT Pal is"ades 2530.0. 811.7 805.0 . . **no 7. MAXIMUM DEPENDABLE CAPACITY CNET MWe) **730 DOCKET NO. 50-255* DATE COMPLETED BY BWBerles TELEPHONE (616)764-8913 NOTES: 8. IF. CHANGES OCCUR IN CAPCITY RATINGS (ITEM NUMBERS 3 THROUGH ?AND 7) SIN.CE LAST REPORT, GIVE REASONS: 9 .. POWER LEVEL TO WHICH RESTRICTED, _IF ANY (NET MWe): 10. REASONS FOR IF ANY: -l1. HOURS lN REPORTING PERIOD 12. NUMBER OF HOURS REACTOR WAS CRITICAL 13.
  • REACTOR RESERVE SHUTDOWN HOURS 14. HOURS GENERATOR ON-LINE* . . 15: UNIT RESERVE SHUTDOWN HOURS 16. GROSS THERMAL ENERGY GENERATED CMWH) 17. GROS_S EL_ECTRICAL ENERGY GENERATED.

CMWH). 18: NET GENERATED CMWH). 19. UNIT SERVICE. FACTOR 20. UNIT AVAILABILITY .FACTOR 21. "UNIT CAPACITY FACTOR (USIN°G MDC NET) . 22. UNIT. CAPACITY FACTOR (USING DE_R NET) 23. UNIT-. FORCED *OUTAGE *RATE* ----* This Month 720.0 720.0 674.7. 154.4662.3 502789.0.

476223.0 93.7% 93.7%. .90.6% .

24:

.6.: MONTHS (TYPE,* DATE AND DURATION OF EACH): _,:r:f

]'. " . . 25_. IF SHUTDOWN AT.END;,OF_REl?ORT-PERIOO, ESTI.MATED DATE OF STARTUP: 26. UNITS JN TEST *S-TATIJS'°CPRIOR TO COMMERCIAL OPERATION):

INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

    • Based on*condenser backpressure
  • Weighted Av.er age (635 MWe used as MDC Net pr for to October 1985) * ,._. Yr-to-Date Cumulative 6551.0 208478.0 4430.3 4315.6 113977. 7 ----

248639441.0 3350229.0 . 787'15020.

0 . 3181433. 0 . 742n994.o 65;9% 54. ?"!. 65.9%: 54. ?"!. 66.5% 52.6%* ..

44.3% -* .. .. 4.5% 29.1% Forecast Achieved AVERAGE DAILY UNIT POWER LEVEL MONTH DAY AVERAGE DAILY POWER LEVEL DAY (MWe Net) 1. 267 17. 2. 159 18. 3. 453 19. 4. 728 20. 5. 758 21. 6. 756 22. 7. 763 23. 8. 777 24. 9. 776 25. 10. 778 26. 11. 726 27. 12. 0 28. 13. 172 29. 14. 592 30. 15. 770 31. 16. 766 INSTRUCTIONS:

DOCKET NO 50-255 UNIT Palisades DATE 10/04/95 COMPLETED BY BWBerles TELEPHONE (616)764-8913 AVERAGE DAILY POWER LEVEL (MWe Net) 769 775 771 768 775 777 778 778 776 772 772 771 769 764 On this format, list the average daily unit power level in MWe-NET for each day in the reporting month. Compute to the nearest whole megawatt.

.. J '

SUMMARY

OF OPERATING EXPERIENCE FOR SEPTEMBER 1995 The unit began the month at 49% power. Power was reduced on 9/01/95 and the unit was taken off-line at 0208 on 9/02/95 (the reactor remained critical) for a forced outage to repair a Motor Operated Disconnect in the switchyard.

The unit was back on-1 ine at 1458 on 9/02/95. The unit was re.turned to 100% by 0900 on 9/04/95. On 9/11/95, a broken conductor was discovered between an i sophase bus and the main generator.

A power reduction was initiated from 100% at 1800 and the unit was off-line at 2106 ( the reactor remained cal) for a forced outage to repair the isophase bus. The unit was placed line on 9/13/95 at 0538, and 100% power was reached by 0600 on 9/15/95. The unit operated at 100% for the remainder of the month.

RE PORT MONTH -----'S"""E'--P T'-=E""'"MB=E=R-'1=9-=-9"'-5

__ No. Date Type 1 2 8/30/95 F 3 9/11/95 F l. F: Forced S: Scheduled Duration (Hours) 2. Reason: 12.8 32.5 Reason 2 A A A-Equipment Failure (Explain) 8-Maintenance or Test C-Refue ling D-Regulatory E-Operator Training & License Examination F-Administrative G-Operational Error (Explain)

H-Other (Explain)

UNIT SHUTDOWNS AND POWER REDUCTIONS Method of Licensee Shutting Event Down Reactor 3 Report # 4 4 3. Method: 1-Manual 2-Manual Scram 3-Automatic Scram 4-0ther (Explain)

4. System Code 4 Component Code 5 Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG-0161)

DOCKET NO 50-255 UN IT Pali sades DATE _____lg/04/95 COMPLETED BY BWBerles TELEPHONE (616)764-8913 Cause & Corrective Action to Prevent Recurrence Power was reduced from 99.6% due to a Motor Operated Disconnect in the switchyard overheating.

The unit was taken off-line at 0208 on 9/2/95 and placed back on-line at 1458 on 9/2. Power was reduced from 100% on 9/11 at 1800 and the unit was off-line at 2106 to repair a conductor between an isophase bus and the main generator.

The unit was on-line on 9/13 at 0538. 5. Exhibit I -Same Source !, I 1i .. . .