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| {{#Wiki_filter:, " NRCForm388 U.S. NUCLEAR REGULATORY COMMISSION (9-83) APPROVED OMS NO. 3150-0104 EXPIRES: 8131185 LICENSEE EVENT REPORT (LER) FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3) Consumers Power Company Palisades Plant a I s I a I a I c I 2 I s I s 1 I OF a 1 s TITLE (4) LICENSEE EVENT REPORT 96-004 -SAFETY INJECTION SYSTEM DISABLED WITH PRIMARY COOLANT SYSTEM GREATER THAN 300°F EVENT DATE CSl LER NUMBER I, n REPORT DATE 161 OTHER FACILITTES INVOLVED (8) SEQUENTIAL . REVISION FACILITY NAMES MONTH DAY YEAR YEAR NUMBER NUMBER MONTH DAY YEAR NIA olslololol I 0 I 1 1 I 6 916 -o Io I 4 -olo 012 1 I 9 916 olslololol I 9 6 NIA THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or mONJ of the following) | | {{#Wiki_filter:, " NRCForm388 U.S. NUCLEAR REGULATORY COMMISSION (9-83) APPROVED OMS NO. 3150-0104 EXPIRES: 8131185 LICENSEE EVENT REPORT (LER) FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3) Consumers Power Company Palisades Plant a I s I a I a I c I 2 I s I s 1 I OF a 1 s TITLE (4) LICENSEE EVENT REPORT 96-004 -SAFETY INJECTION SYSTEM DISABLED WITH PRIMARY COOLANT SYSTEM GREATER THAN 300°F EVENT DATE CSl LER NUMBER I, n REPORT DATE 161 OTHER FACILITTES INVOLVED (8) SEQUENTIAL . REVISION FACILITY NAMES MONTH DAY YEAR YEAR NUMBER NUMBER MONTH DAY YEAR NIA olslololol I 0 I 1 1 I 6 916 -o Io I 4 -olo 012 1 I 9 916 olslololol I 9 6 NIA THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or mONJ of the following) |
| (11) OPERATING N MODEC9l 20.402(b) 20.405(c) | | (11) OPERATING N MODEC9l 20.402(b) 20.405(c) |
| : 50. 73(a)(2)(iv) 73.71(b) ---POWER 20.405(a)(1)(1) 50.38(c)(1) | | : 50. 73(a)(2)(iv) 73.71(b) ---POWER 20.405(a)(1)(1) 50.38(c)(1) |
| : 50. 73(a)(2)(v) 73.71(c) LEVEL -....._ --(10) o I o 0 20.405(a)(1)(1i) 50.38(c)(2) | | : 50. 73(a)(2)(v) 73.71(c) LEVEL -....._ --(10) o I o 0 20.405(a)(1)(1i) 50.38(c)(2) |
| : 50. 73(a)(2)(vii) | | : 50. 73(a)(2)(vii) |
| OTHER (Specify in Abstract ---'t : -20.405(a)(1 | | OTHER (Specify in Abstract ---'t : -20.405(a)(1 |
| )(Iii) L 50. 73(a)(2)(ij | | )(Iii) L 50. 73(a)(2)(ij |
| : 50. 73(a)(2)(viii)(A) below and in Telrt, -/:. -20.405(a)(1)[iv) | | : 50. 73(a)(2)(viii)(A) below and in Telrt, -/:. -20.405(a)(1)[iv) |
| -50. 73(a)(2)(1ij | | -50. 73(a)(2)(1ij |
| -50. 73(a)(2)(viiij(B) | | -50. 73(a)(2)(viiij(B) |
| NRC Form 388A) .. *. 20.405CaH1lM | | NRC Form 388A) .. *. 20.405CaH1lM |
| : 50. 73CaH2Hiiil 50.73CaH?Hx) | | : 50. 73CaH2Hiiil 50.73CaH?Hx) |
| LICENSEE CONTACT FOR THIS LER {121 NAME TELEPHONE NUMBER Clayton M Mathews, Licensing Engineer AREACODE I 61116 11614 I -lsl91113 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 1131 MANUFAC-REPORTABL | | LICENSEE CONTACT FOR THIS LER {121 NAME TELEPHONE NUMBER Clayton M Mathews, Licensing Engineer AREACODE I 61116 11614 I -lsl91113 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 1131 MANUFAC-REPORTABL |
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| Various program and process barriers to prevent this occurrence were broken. They were: 1. The Work Order "Technical Specification Involvement" block referenced Technical Specification 3.17. However, this section was not referred to and Technical Section 3.16 was thought to be the applicable requirement. | | Various program and process barriers to prevent this occurrence were broken. They were: 1. The Work Order "Technical Specification Involvement" block referenced Technical Specification 3.17. However, this section was not referred to and Technical Section 3.16 was thought to be the applicable requirement. |
| NRC Form 386A (9-83) FACILITY NAME (1) Palisades Plant LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) YEAR LER NUMBER (3) SEQUENTIAL NUMBER U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 EXPIRES: 8131185 REVISION NUMBER PAGE (4) 0500025596-004 | | NRC Form 386A (9-83) FACILITY NAME (1) Palisades Plant LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) YEAR LER NUMBER (3) SEQUENTIAL NUMBER U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 EXPIRES: 8131185 REVISION NUMBER PAGE (4) 0500025596-004 |
| -0 0 OJ0F05 2. General Operating Procedure (GOP) 9, Attachment 1 "Plant Cooldown (Hot Standby/Shutdown Checklist)" section 4.4 states "When PCS is less than 210°F (ie, Cold Shutdown), then initiate work order to disable Safety Injection actuation circuits [refer to System Operating Procedure (SOP) 3, step 7. 7.1 ]." This step went unheeded in the decision making process to disable SIS since it appears on page 4 of the checklist and the plant conditions at the time had only proceeded the operating crew through page 2 of the checklist. | | -0 0 OJ0F05 2. General Operating Procedure (GOP) 9, Attachment 1 "Plant Cooldown (Hot Standby/Shutdown Checklist)" section 4.4 states "When PCS is less than 210°F (ie, Cold Shutdown), then initiate work order to disable Safety Injection actuation circuits [refer to System Operating Procedure (SOP) 3, step 7. 7.1 ]." This step went unheeded in the decision making process to disable SIS since it appears on page 4 of the checklist and the plant conditions at the time had only proceeded the operating crew through page 2 of the checklist. |
| : 3. SOP 3, "Safety Injection And Shutdown Cooling System," section 7.7.1 notes "This procedure shall only be performed when the Reactor is in Cold or Refueling Shutdown ... " This procedure was not referenced for guidance. | | : 3. SOP 3, "Safety Injection And Shutdown Cooling System," section 7.7.1 notes "This procedure shall only be performed when the Reactor is in Cold or Refueling Shutdown ... " This procedure was not referenced for guidance. |
| : 4. Electrical Maintenance Procedure, ESS-M-24 "Disable/Enable the Safety Injection System Actuation on Low Pressurizer Pressure," prerequisite section 3.3, specifies plant condition to be "cold shutdown." Procedure step 5.1 requires the assigned supervisor ensure all prerequisites are completed. | | : 4. Electrical Maintenance Procedure, ESS-M-24 "Disable/Enable the Safety Injection System Actuation on Low Pressurizer Pressure," prerequisite section 3.3, specifies plant condition to be "cold shutdown." Procedure step 5.1 requires the assigned supervisor ensure all prerequisites are completed. |
| The plant condition of cold shutdown was not verified. | | The plant condition of cold shutdown was not verified. |
| : 5. Technical Specification 3.16 "Engineered Safety Features System Instrumentation Settings" was referenced as the controlling requirement. | | : 5. Technical Specification 3.16 "Engineered Safety Features System Instrumentation Settings" was referenced as the controlling requirement. |
| Technical Specification 3.16 applicability statement indicates that "Technical Specification 3.16 is applicable when associated ESF or Isolation Function Instrumentation is req'.;.;:;*ad to be operable by Technical Specification 3.17.2 or 3.17.3. Technical Specification 3.17.2 requires SIS to be operable when the PCS is greater than or equal to 300°F. This information was not recognized and verified. | | Technical Specification 3.16 applicability statement indicates that "Technical Specification 3.16 is applicable when associated ESF or Isolation Function Instrumentation is req'.;.;:;*ad to be operable by Technical Specification 3.17.2 or 3.17.3. Technical Specification 3.17.2 requires SIS to be operable when the PCS is greater than or equal to 300°F. This information was not recognized and verified. |
| : 6. The Equipment Safe Shutdown Operations General Outage Information list contained an entry indicating Safety Injection Actuation Signal (SIAS) will be disabled at less than 210° F for low pressure only. Containment High Pressure will still result in a SIAS. This information was available but was not referred to as a reference source. CAUSE OF EVENT All relevant information was not used in the decision making process and pertinent procedures were violated. | | : 6. The Equipment Safe Shutdown Operations General Outage Information list contained an entry indicating Safety Injection Actuation Signal (SIAS) will be disabled at less than 210° F for low pressure only. Containment High Pressure will still result in a SIAS. This information was available but was not referred to as a reference source. CAUSE OF EVENT All relevant information was not used in the decision making process and pertinent procedures were violated. |
| Therefore, the root cause of the event was personnel error. SAFETY SIGNIFICANCE There was no safety significant condition which resulted from disabling of the SIS on low pressure during plant cooldown on January 18, 1996. The low pressure signal was blocked by design during plant cooldown before PCS pressure decreased below 1593 psia. The plant average temperature and pressure were 364°F. and less than 600 psia when the maintenance was performed disabling SIS on low PCS pressure. | | Therefore, the root cause of the event was personnel error. SAFETY SIGNIFICANCE There was no safety significant condition which resulted from disabling of the SIS on low pressure during plant cooldown on January 18, 1996. The low pressure signal was blocked by design during plant cooldown before PCS pressure decreased below 1593 psia. The plant average temperature and pressure were 364°F. and less than 600 psia when the maintenance was performed disabling SIS on low PCS pressure. |
| The Low Temperature Overpressurization Protection (LTOP) -j | | The Low Temperature Overpressurization Protection (LTOP) -j |
| . NRC Form 368A (9-83) FACILITY NAME (1) * | | . NRC Form 368A (9-83) FACILITY NAME (1) * |
| * LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) YEAR LER NUMBER (3) SEQUENTIAL NUMBER U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 EXPIRES: 8/31/85 REVISION NUMBER PAGE (4) Palisades Plant olslololol2lsls gjs -o lo 14 -o lo ol4 oF o Is setpoint of about 1000 psia would have prevented an auto-reset on increasing pressure above 1593 psia. Whether the SIS on low pressure is available or disabled is not significant to the.plant condition because the plant would have been relying on a Containment High Pressure (CHP) signal or operator action to start High Pressure Safety Injection (HPSI) to maintain or recover PCS inventory for a large break Loss of Coolant Accident (LOCA). The SIS on containment high pressure was still available to start all available safety injection pumps. With the saturation pressure of about 160 psia, the PCS inventory could be quickly recovered with one HPSI pump for both large break and small break LOCAs. At this pressure, Low Pressure Safety Injection (LPSI) pumps would also be able to supply PCS makeup since they remain aligned to the Safety Injection and Refueling Water (SIRW) tank when the PCS temperature is greater than 300°F. The plant response to small break LOCAs with the SIS low pressure signal blocked or disabled requires operator action to start available HPSI and Charging pumps. Throttling of the safety injection pumps would be required to maintain the PCS pressure within the acceptable range below the L TOP set point curve. Also, the probability of a large or small break LOCA occurring after full power operations when the PCS pressure has been reduced to less than 600 psia is very small. The consequences of an accident were not changed by this event. CORRECTIVE ACTIONS The following corrective actions will be taken: 1. Communicate to Shift Supervisors, Control Room Supervisors and Shift Engineers the expectation to validate and verify information using available references (e.g. Work Order information blocks, procedure prerequisite sections) and sources (Technical Specifications, procedures, Daily Orders, schedules, equipment safe shutdown lists, LCO status boards, etc) to assist in achieving informed and accurate decision making. 2. Reinforce the Maintenance Supervisor's responsibility to assure procedure prerequisites are met prior to authorizing a work activity. | | * LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) YEAR LER NUMBER (3) SEQUENTIAL NUMBER U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 EXPIRES: 8/31/85 REVISION NUMBER PAGE (4) Palisades Plant olslololol2lsls gjs -o lo 14 -o lo ol4 oF o Is setpoint of about 1000 psia would have prevented an auto-reset on increasing pressure above 1593 psia. Whether the SIS on low pressure is available or disabled is not significant to the.plant condition because the plant would have been relying on a Containment High Pressure (CHP) signal or operator action to start High Pressure Safety Injection (HPSI) to maintain or recover PCS inventory for a large break Loss of Coolant Accident (LOCA). The SIS on containment high pressure was still available to start all available safety injection pumps. With the saturation pressure of about 160 psia, the PCS inventory could be quickly recovered with one HPSI pump for both large break and small break LOCAs. At this pressure, Low Pressure Safety Injection (LPSI) pumps would also be able to supply PCS makeup since they remain aligned to the Safety Injection and Refueling Water (SIRW) tank when the PCS temperature is greater than 300°F. The plant response to small break LOCAs with the SIS low pressure signal blocked or disabled requires operator action to start available HPSI and Charging pumps. Throttling of the safety injection pumps would be required to maintain the PCS pressure within the acceptable range below the L TOP set point curve. Also, the probability of a large or small break LOCA occurring after full power operations when the PCS pressure has been reduced to less than 600 psia is very small. The consequences of an accident were not changed by this event. CORRECTIVE ACTIONS The following corrective actions will be taken: 1. Communicate to Shift Supervisors, Control Room Supervisors and Shift Engineers the expectation to validate and verify information using available references (e.g. Work Order information blocks, procedure prerequisite sections) and sources (Technical Specifications, procedures, Daily Orders, schedules, equipment safe shutdown lists, LCO status boards, etc) to assist in achieving informed and accurate decision making. 2. Reinforce the Maintenance Supervisor's responsibility to assure procedure prerequisites are met prior to authorizing a work activity. |
| : 3. Conduct training for licensed operators on the purpose of maintaining operability of equipment listed in Technical Specification Table 3.17.2 when the PCS temperature is greater than or equal to 300°F. 4. Revise the Permanent Maintenance Procedure to disable/enable the Safety Injection System actuation on low pressurizer pressure to align with Technical Specifications. | | : 3. Conduct training for licensed operators on the purpose of maintaining operability of equipment listed in Technical Specification Table 3.17.2 when the PCS temperature is greater than or equal to 300°F. 4. Revise the Permanent Maintenance Procedure to disable/enable the Safety Injection System actuation on low pressurizer pressure to align with Technical Specifications. |
| ;,; NRC Form 366A (9-83) FACILllY NAME (1) Palisades Plant LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) YEAR LER NUMBER (3) SEQUENTIAL NUMBER U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 EXPIRES: 8/31185 REVISION NUMBER PAGE(4) 0500025596-004 | | ;,; NRC Form 366A (9-83) FACILllY NAME (1) Palisades Plant LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) YEAR LER NUMBER (3) SEQUENTIAL NUMBER U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 EXPIRES: 8/31185 REVISION NUMBER PAGE(4) 0500025596-004 |
| -0 0 050F05 5. Align the following procedures to accurately reflect which procedure controls the activity for disabling SIS. A. General Operating Procedure 9, Attachment 1 "Plant Cooldown (Hot Standby/Shutdown Checklist), step 4.4 which refers to System Operating Procedure 3, step 7.7.1 8. System Operating Procedure 3 "Safety Injection And Shutdown Cooling System" section 7. 7. C. Permanent Maintenance Procedure ESS-E-24, "Disable/Enable the Safety Injection System Actuation On Low Pressurizer Pressure." .}} | | -0 0 050F05 5. Align the following procedures to accurately reflect which procedure controls the activity for disabling SIS. A. General Operating Procedure 9, Attachment 1 "Plant Cooldown (Hot Standby/Shutdown Checklist), step 4.4 which refers to System Operating Procedure 3, step 7.7.1 8. System Operating Procedure 3 "Safety Injection And Shutdown Cooling System" section 7. 7. C. Permanent Maintenance Procedure ESS-E-24, "Disable/Enable the Safety Injection System Actuation On Low Pressurizer Pressure." .}} |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18065B1151997-12-0909 December 1997 LER 97-013-00:on 971110,failure to Closure Test Two Check Valves Resulted in Violation of TS 6.5.7 Occurred.Caused by Close Function for Check Valves.Check Valves Tested to Confirm Proper Closure Capability ML18067A7751997-11-11011 November 1997 LER 97-011-00:on 971012,primary Coolant Pump Was Started W/Sg Temperatures Greater than Cold Leg Temperature.Caused by Inadequate Procedures & Operator Decision Making.Critique of Event Conducted W/Operators Involved ML18067A7581997-10-30030 October 1997 LER 97-010-00:on 970930,determined That Inadequacy in App R Analysis Resulted in Condition Outside Design Basis of Plant.Caused by Missing Cable in Circuit & Raceway Schedule. Developed New Evaluation Re ASD Valves Validation ML18067A7461997-10-23023 October 1997 LER 97-009-00:on 970923,discovered Procedure Weakness Re Implementation of App R Shutdown Methodology.Caused by Human Error.Revised Off-Normal Procedure ONP-25.2, Alternate Safe Shutdown Procedure. ML18067A7191997-10-10010 October 1997 LER 97-008-00:on 970912,spurious Valve Operation Could Result in Loss of Shutdown Capabilities Per 10CFR50,App R, Section Iii.L,Was Discovered.Caused by Failure to Validate Info from App R.Design Bases for SW Backup Reviewed ML18067A6951997-09-24024 September 1997 LER 97-007-00:on 970826,discovered Inadequate Testing of DG Sequencer Control Relay Contacts.Caused by Oversight on Part of Personnel Involved in Installation of Facility Change FC-800.Tested 106D-1/XL & 106D-2/XL Relay Contacts ML18067A5651997-06-0303 June 1997 LER 96-013-01:on 961115,DC Breaker Failed During Testing for as-found Trip Setting.Failure Caused by Oversight within Preventive Maint Program.Breaker Was Replaced & Tested ML18067A5461997-05-12012 May 1997 LER 97-006-00:on 970412,overtime Limits Were Exceeded for Radiation Protection Technicians.Caused by Inadequate Design,Review & Proper Verifications of Overtime Work Schedule.Communicate Overtime Limitation Responsibilities ML18067A4431997-03-24024 March 1997 LER 97-004-00:on 970221,trip of High Pressure Safety Injection Pump Occurred While Filling Safety Injection Tank Resulting in TS Violation.Caused by Particle Lodged Between Surface of Indication disk.Y-phase Relay Was OOS ML18067A4391997-03-21021 March 1997 LER 97-005-00:on 961220,operation of Plant Outside Design Basis Occurred Due to an Unacceptable Repair on Main Steam Isolation Valves.Pipe Plugs Permanently Repaired ML18067A4401997-03-21021 March 1997 LER 97-003-00:on 961101,four Piping Lines Were Determined to Be Potentially Susceptible to Pressurization Due to Containment Temperature Increase During an Accident.Cac Discharge Piping Will Be verified.W/970321 Ltr ML18066A8931997-02-21021 February 1997 LER 97-002-00:on 970123,failure to Meet TSs 4.5.2d(1)(b) for Testing of Emergency Escape Airlock Occurred.Caused by Missed Surveillance.Emergency Escape Air Lock Testing Was Completed & Declared operable.W/970221 Ltr ML18066A8751997-02-0505 February 1997 LER 97-001-00:on 970106,TAVE Temp Dropped Below Minimum Temp for Criticality.Caused by Control Rod Withdrawal Rate to Increase Power Not Sufficient to Match Increase in Steam. Turbine Bypass Valve Actuator repaired.W/970205 Ltr ML18066A8041996-12-23023 December 1996 LER 96-014-00:on 961124,class 1E Raychem Cable Splices Were Installed Incorrectly.Caused by Incorrectly Made Electrical Splices.Total of 270 Splices Have Been Replaced within Containment ML18066A7831996-12-16016 December 1996 LER 96-013-00:on 961115,DC Breaker Failure During Testing for as-found Trip Setting Occurred.Cause Under Investigation.All molded-case Circuit Breakers in DC Distribution Panels Were Replaced ML18065A9951996-10-0404 October 1996 LER 96-002-01:on 960116,initiated TS Required Shutdown Due to Safeguards Cable Fault.Both Sets (Six Cables) of Cables Were Replaced & Installed Through Turbine Generator Bldg ML18065A9171996-09-0909 September 1996 LER 95-012-00:on 960809,TS Violation Occurred,Due to No Senior Reactor Operator in Cr.Caused by Extensive Remodeling.Cr Remodeling completed.W/960909 Ltr ML18065A8961996-08-29029 August 1996 LER 96-011-00:on 960730,CR Continuous Air Monitor Alarm Setpoint Improperly Established.Caused by Failure to Utilize Mod Process in 1988 Leading to Failure to Properly Select & Calibrate Instruments ML18065A8811996-08-20020 August 1996 LER 96-005-01:on 960207,determined Fuse on Main Supply to Two Safety Related DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Lack of Thorough Associated Circuits Analysis.Supply Fuse to Panels Replaced ML18065A8741996-08-16016 August 1996 LER 96-010-00:on 960717,high Pressure Safety Injection Pump Tripped While Filling Safety Injection Tank.Caused by Faulty 150/151Y-207 Time Overcurrent Relay.All Similar Relays in Time Overcurrent Application Have Been Inspected ML18065A8651996-08-12012 August 1996 LER 96-009-00:on 960712,identified Penetration Seal Deficiency on Fire Barriers Caused by Failure to Perform & Document Comprehensive Fire Barrier Evaluation.Developed Basis document.W/960812 Ltr ML18065A8601996-08-0202 August 1996 LER 96-006-01 on 960207,discovered Limits of Design Analysis Could Have Been Violated.Subsequent Tests & Analyses Facility Did Not Exceed Basis.Operating Procedures Have Been Revised to Treat 2530 Megawatts Limit as Absolute Limit ML18065A8321996-08-0101 August 1996 LER 96-003-01:on 960115,alternate Shutdown Panel Inverter Resulted in Unavailability of Panel.Replaced Defective Inverter Alarm Logic Board ML18065A7691996-06-12012 June 1996 LER 96-008-00:on 960513,fire Door Not Maintained Open in Accordance W/Design Basis.Cause Under Investigation. Engineering Evaluation Performed & Revised Documents, Surveillance & Test procedures.W/960612 Ltr ML18065A6901996-05-0101 May 1996 LER 95-001-01:on 950302,malfunction of Left Channel DBA Sequencer Resulted in Inadvertent Actuation of Left Channel Safeguards Equipment.Replaced microprocessor.W/960501 Ltr ML18065A6681996-04-22022 April 1996 LER 96-007-00:on 960321,inadequate Emergency Lighting & Ventilation in post-fire Safe Shutdown Areas.Caused by App R Program Documentation Insufficient to Demonstrate Regulatory Compliance.Lighting modified.W/960422 Ltr ML18065A5721996-03-11011 March 1996 LER 96-006-00:on 960207,average Reactor Power Level Exceeded License Limit Due to Insufficient Procedural Guidance. GOP-12 Revised to Treat 2,530 Mwt Limit as Absolute Limit Requiring Immediate Corrective Action If Exceeded ML18065A5261996-03-0101 March 1996 LER 96-005-00:on 960202,fuse on Main Supply to Two SR DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Inadequate Electrical/App R Design Review.Implemented Hourly Fire tours.W/960301 Ltr ML18065A5111996-02-19019 February 1996 LER 94-012-02:on 940427,determined That Internal Ground in Thermal Margin Monitor Causes Nonconformance W/Rps Design Basis.Incorporated RPS Failure Modes & Effects Analysis in Plant DBD.W/960219 Ltr ML18065A5061996-02-19019 February 1996 LER 96-004-00:on 960118,SIS Disabled W/Primary Coolant Sys Greater than 300 F.Caused by Personnel Error.Permanent Maint Procedure to Disable/Enable SIS Actuation on Low Pressurizer Pressure Will Be Revised to Align W/Ts ML18065A5021996-02-15015 February 1996 LER 96-003-00:on 960115,technicians Found Low Voltage cut- Off for Alternate Shutdown Panel Inverter Set That Resulted in Unavailability of Panel.Caused by Inadequate Post Mod. Readjusted Set Point to Minimum setting.W/960215 Ltr ML18065A4581996-01-31031 January 1996 LER 96-001-00:on 960103,failed to Test Duplicate Equipment. Caused by STS No Longer Containing Requirement for cross- Train Testing of Duplicate Components.Will Submit Request to Delete Subj Requirements from TS.W/960131 Ltr ML18065A4421996-01-19019 January 1996 LER 95-016-00:on 951226,did Not Analyze Primary Coolant Samples within 72 H.Caused by Belief Acceptability to Save Pcs Samples for Choride Analysis Past 72 H.Counseled Chemistry Supervision.W/960119 Ltr ML18065A4041996-01-15015 January 1996 LER 95-014-00:on 950119,PCP Oil Collection Deficiencies Created by FC-860 Piping Mod.Caused by Inadequate DBD for Sys & Lack of Review by Experienced Fire Protection Personnel.Updated Design Basis documentation.W/960115 Ltr ML18065A3291995-12-0404 December 1995 LER 95-013-00:on 951103,circuit Fuse Coordination Deficiency Which Affects App R Safe Shutdown Equipment Noted.Design of Fuse Coordination in Potential Transformer Circuits Will Be Evaluated & Modified as required.W/951204 Ltr ML18065A2361995-11-0202 November 1995 LER 95-012-00:on 950701,discovered Unqualified Electrical Connection in Containment SW Outlet Valve Controller.Caused by Failure of Assigned Engineers to Available Info.Replaced Wire Nuts W/Inline Butt connections.W/951102 Ltr ML18065A2051995-10-20020 October 1995 LER 95-008-01:on 950728,discovered That None of Four Containment High Pressure Channels Would Initiate Reactor Trip Due to Programmatic Deficiencies.Administrative Procedure (AP) 9.44,AP 9.45 & AP 10.44 Will Be Revised ML18065A0841995-09-18018 September 1995 LER 95-011-00:on 950817,CR 40 Withdrawal Occurred When Given Insertion Signal Due to skill-based Error in Crimping & Removing Foreign Matl from CRDM Motor Connection Box.Crd Package replaced.W/950918 Ltr ML18065A0681995-09-14014 September 1995 LER 95-010-00:on 950815,ESFA Resulted in Manual Rt Following Isolation of Pcs.Replaced Failed Instrument Line ML18065A0651995-09-0808 September 1995 LER 95-009-00:on 950728,discovered Lack of Procedural Guidance for Pump Repair Following Fire.Proposed Use of Power Supply Breaker Did Not Adequately Address Effect of Loss of Control Power.Performed Independent Assessment ML18064A8781995-08-28028 August 1995 LER 95-008-00:on 950728,discovered During Design Change Testing That None of Four Containment High Pressure Channels Would Initiate Rt.Caused by Programmatic Deficiencies. Reviewed Selected Tests & Mods from Recent Refueling Outage ML18064A8831995-08-21021 August 1995 LER 95-007-00:on 950720,discovered That 12 Instrument Loops Had V-bolted Type Qualified Cable Splices Connected to Wires W/Exposed Kapton Insulation.Caused by Human Error.All V- Bolted Splices Replaced w/in-line design.W/950821 Ltr 1999-09-02
[Table view] Category:RO)
MONTHYEARML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18065B1151997-12-0909 December 1997 LER 97-013-00:on 971110,failure to Closure Test Two Check Valves Resulted in Violation of TS 6.5.7 Occurred.Caused by Close Function for Check Valves.Check Valves Tested to Confirm Proper Closure Capability ML18067A7751997-11-11011 November 1997 LER 97-011-00:on 971012,primary Coolant Pump Was Started W/Sg Temperatures Greater than Cold Leg Temperature.Caused by Inadequate Procedures & Operator Decision Making.Critique of Event Conducted W/Operators Involved ML18067A7581997-10-30030 October 1997 LER 97-010-00:on 970930,determined That Inadequacy in App R Analysis Resulted in Condition Outside Design Basis of Plant.Caused by Missing Cable in Circuit & Raceway Schedule. Developed New Evaluation Re ASD Valves Validation ML18067A7461997-10-23023 October 1997 LER 97-009-00:on 970923,discovered Procedure Weakness Re Implementation of App R Shutdown Methodology.Caused by Human Error.Revised Off-Normal Procedure ONP-25.2, Alternate Safe Shutdown Procedure. ML18067A7191997-10-10010 October 1997 LER 97-008-00:on 970912,spurious Valve Operation Could Result in Loss of Shutdown Capabilities Per 10CFR50,App R, Section Iii.L,Was Discovered.Caused by Failure to Validate Info from App R.Design Bases for SW Backup Reviewed ML18067A6951997-09-24024 September 1997 LER 97-007-00:on 970826,discovered Inadequate Testing of DG Sequencer Control Relay Contacts.Caused by Oversight on Part of Personnel Involved in Installation of Facility Change FC-800.Tested 106D-1/XL & 106D-2/XL Relay Contacts ML18067A5651997-06-0303 June 1997 LER 96-013-01:on 961115,DC Breaker Failed During Testing for as-found Trip Setting.Failure Caused by Oversight within Preventive Maint Program.Breaker Was Replaced & Tested ML18067A5461997-05-12012 May 1997 LER 97-006-00:on 970412,overtime Limits Were Exceeded for Radiation Protection Technicians.Caused by Inadequate Design,Review & Proper Verifications of Overtime Work Schedule.Communicate Overtime Limitation Responsibilities ML18067A4431997-03-24024 March 1997 LER 97-004-00:on 970221,trip of High Pressure Safety Injection Pump Occurred While Filling Safety Injection Tank Resulting in TS Violation.Caused by Particle Lodged Between Surface of Indication disk.Y-phase Relay Was OOS ML18067A4391997-03-21021 March 1997 LER 97-005-00:on 961220,operation of Plant Outside Design Basis Occurred Due to an Unacceptable Repair on Main Steam Isolation Valves.Pipe Plugs Permanently Repaired ML18067A4401997-03-21021 March 1997 LER 97-003-00:on 961101,four Piping Lines Were Determined to Be Potentially Susceptible to Pressurization Due to Containment Temperature Increase During an Accident.Cac Discharge Piping Will Be verified.W/970321 Ltr ML18066A8931997-02-21021 February 1997 LER 97-002-00:on 970123,failure to Meet TSs 4.5.2d(1)(b) for Testing of Emergency Escape Airlock Occurred.Caused by Missed Surveillance.Emergency Escape Air Lock Testing Was Completed & Declared operable.W/970221 Ltr ML18066A8751997-02-0505 February 1997 LER 97-001-00:on 970106,TAVE Temp Dropped Below Minimum Temp for Criticality.Caused by Control Rod Withdrawal Rate to Increase Power Not Sufficient to Match Increase in Steam. Turbine Bypass Valve Actuator repaired.W/970205 Ltr ML18066A8041996-12-23023 December 1996 LER 96-014-00:on 961124,class 1E Raychem Cable Splices Were Installed Incorrectly.Caused by Incorrectly Made Electrical Splices.Total of 270 Splices Have Been Replaced within Containment ML18066A7831996-12-16016 December 1996 LER 96-013-00:on 961115,DC Breaker Failure During Testing for as-found Trip Setting Occurred.Cause Under Investigation.All molded-case Circuit Breakers in DC Distribution Panels Were Replaced ML18065A9951996-10-0404 October 1996 LER 96-002-01:on 960116,initiated TS Required Shutdown Due to Safeguards Cable Fault.Both Sets (Six Cables) of Cables Were Replaced & Installed Through Turbine Generator Bldg ML18065A9171996-09-0909 September 1996 LER 95-012-00:on 960809,TS Violation Occurred,Due to No Senior Reactor Operator in Cr.Caused by Extensive Remodeling.Cr Remodeling completed.W/960909 Ltr ML18065A8961996-08-29029 August 1996 LER 96-011-00:on 960730,CR Continuous Air Monitor Alarm Setpoint Improperly Established.Caused by Failure to Utilize Mod Process in 1988 Leading to Failure to Properly Select & Calibrate Instruments ML18065A8811996-08-20020 August 1996 LER 96-005-01:on 960207,determined Fuse on Main Supply to Two Safety Related DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Lack of Thorough Associated Circuits Analysis.Supply Fuse to Panels Replaced ML18065A8741996-08-16016 August 1996 LER 96-010-00:on 960717,high Pressure Safety Injection Pump Tripped While Filling Safety Injection Tank.Caused by Faulty 150/151Y-207 Time Overcurrent Relay.All Similar Relays in Time Overcurrent Application Have Been Inspected ML18065A8651996-08-12012 August 1996 LER 96-009-00:on 960712,identified Penetration Seal Deficiency on Fire Barriers Caused by Failure to Perform & Document Comprehensive Fire Barrier Evaluation.Developed Basis document.W/960812 Ltr ML18065A8601996-08-0202 August 1996 LER 96-006-01 on 960207,discovered Limits of Design Analysis Could Have Been Violated.Subsequent Tests & Analyses Facility Did Not Exceed Basis.Operating Procedures Have Been Revised to Treat 2530 Megawatts Limit as Absolute Limit ML18065A8321996-08-0101 August 1996 LER 96-003-01:on 960115,alternate Shutdown Panel Inverter Resulted in Unavailability of Panel.Replaced Defective Inverter Alarm Logic Board ML18065A7691996-06-12012 June 1996 LER 96-008-00:on 960513,fire Door Not Maintained Open in Accordance W/Design Basis.Cause Under Investigation. Engineering Evaluation Performed & Revised Documents, Surveillance & Test procedures.W/960612 Ltr ML18065A6901996-05-0101 May 1996 LER 95-001-01:on 950302,malfunction of Left Channel DBA Sequencer Resulted in Inadvertent Actuation of Left Channel Safeguards Equipment.Replaced microprocessor.W/960501 Ltr ML18065A6681996-04-22022 April 1996 LER 96-007-00:on 960321,inadequate Emergency Lighting & Ventilation in post-fire Safe Shutdown Areas.Caused by App R Program Documentation Insufficient to Demonstrate Regulatory Compliance.Lighting modified.W/960422 Ltr ML18065A5721996-03-11011 March 1996 LER 96-006-00:on 960207,average Reactor Power Level Exceeded License Limit Due to Insufficient Procedural Guidance. GOP-12 Revised to Treat 2,530 Mwt Limit as Absolute Limit Requiring Immediate Corrective Action If Exceeded ML18065A5261996-03-0101 March 1996 LER 96-005-00:on 960202,fuse on Main Supply to Two SR DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Inadequate Electrical/App R Design Review.Implemented Hourly Fire tours.W/960301 Ltr ML18065A5111996-02-19019 February 1996 LER 94-012-02:on 940427,determined That Internal Ground in Thermal Margin Monitor Causes Nonconformance W/Rps Design Basis.Incorporated RPS Failure Modes & Effects Analysis in Plant DBD.W/960219 Ltr ML18065A5061996-02-19019 February 1996 LER 96-004-00:on 960118,SIS Disabled W/Primary Coolant Sys Greater than 300 F.Caused by Personnel Error.Permanent Maint Procedure to Disable/Enable SIS Actuation on Low Pressurizer Pressure Will Be Revised to Align W/Ts ML18065A5021996-02-15015 February 1996 LER 96-003-00:on 960115,technicians Found Low Voltage cut- Off for Alternate Shutdown Panel Inverter Set That Resulted in Unavailability of Panel.Caused by Inadequate Post Mod. Readjusted Set Point to Minimum setting.W/960215 Ltr ML18065A4581996-01-31031 January 1996 LER 96-001-00:on 960103,failed to Test Duplicate Equipment. Caused by STS No Longer Containing Requirement for cross- Train Testing of Duplicate Components.Will Submit Request to Delete Subj Requirements from TS.W/960131 Ltr ML18065A4421996-01-19019 January 1996 LER 95-016-00:on 951226,did Not Analyze Primary Coolant Samples within 72 H.Caused by Belief Acceptability to Save Pcs Samples for Choride Analysis Past 72 H.Counseled Chemistry Supervision.W/960119 Ltr ML18065A4041996-01-15015 January 1996 LER 95-014-00:on 950119,PCP Oil Collection Deficiencies Created by FC-860 Piping Mod.Caused by Inadequate DBD for Sys & Lack of Review by Experienced Fire Protection Personnel.Updated Design Basis documentation.W/960115 Ltr ML18065A3291995-12-0404 December 1995 LER 95-013-00:on 951103,circuit Fuse Coordination Deficiency Which Affects App R Safe Shutdown Equipment Noted.Design of Fuse Coordination in Potential Transformer Circuits Will Be Evaluated & Modified as required.W/951204 Ltr ML18065A2361995-11-0202 November 1995 LER 95-012-00:on 950701,discovered Unqualified Electrical Connection in Containment SW Outlet Valve Controller.Caused by Failure of Assigned Engineers to Available Info.Replaced Wire Nuts W/Inline Butt connections.W/951102 Ltr ML18065A2051995-10-20020 October 1995 LER 95-008-01:on 950728,discovered That None of Four Containment High Pressure Channels Would Initiate Reactor Trip Due to Programmatic Deficiencies.Administrative Procedure (AP) 9.44,AP 9.45 & AP 10.44 Will Be Revised ML18065A0841995-09-18018 September 1995 LER 95-011-00:on 950817,CR 40 Withdrawal Occurred When Given Insertion Signal Due to skill-based Error in Crimping & Removing Foreign Matl from CRDM Motor Connection Box.Crd Package replaced.W/950918 Ltr ML18065A0681995-09-14014 September 1995 LER 95-010-00:on 950815,ESFA Resulted in Manual Rt Following Isolation of Pcs.Replaced Failed Instrument Line ML18065A0651995-09-0808 September 1995 LER 95-009-00:on 950728,discovered Lack of Procedural Guidance for Pump Repair Following Fire.Proposed Use of Power Supply Breaker Did Not Adequately Address Effect of Loss of Control Power.Performed Independent Assessment ML18064A8781995-08-28028 August 1995 LER 95-008-00:on 950728,discovered During Design Change Testing That None of Four Containment High Pressure Channels Would Initiate Rt.Caused by Programmatic Deficiencies. Reviewed Selected Tests & Mods from Recent Refueling Outage ML18064A8831995-08-21021 August 1995 LER 95-007-00:on 950720,discovered That 12 Instrument Loops Had V-bolted Type Qualified Cable Splices Connected to Wires W/Exposed Kapton Insulation.Caused by Human Error.All V- Bolted Splices Replaced w/in-line design.W/950821 Ltr 1999-09-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18066A6901999-11-0101 November 1999 Rev 5 to Palisades Nuclear Plant Colr. ML18066A6761999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Palisades Nuclear Plant ML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6351999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Palisades Nuclear Plant ML18066A6771999-08-31031 August 1999 Operating Data Rept Page of MOR for Aug 1999 for Palisades Nuclear Plant ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A6061999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Palisades Nuclear Plant.With 990803 Ltr ML18066A5201999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Palisades Nuclear Plant.With 990702 Ltr ML18066A4841999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Palisades Nuclear Plant.With 990603 Ltr ML18066A6371999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Palisades Nuclear Plant ML18068A5941999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Palisades Nuclear Plant.With 990503 Ltr ML18066A4161999-04-0101 April 1999 Rev 4 to COLR, for Palisades Nuclear Plant ML18066A4501999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Palisades Nuclear Plant.With 990402 Ltr ML18066A4671999-03-31031 March 1999 Rev 0 to SIR-99-032, Flaw Tolerance & Leakage Evaluation Spent Fuel Pool Heat Exchanger E-53B Nozzle Palisades Nuclear Plant. ML18068A5351999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Palisades Nuclear Plant.With 990302 Ltr ML18066A3931999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Palisades Nuclear Plant.With 990202 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML20206F6131998-12-31031 December 1998 1998 Consumers Energy Co Annual Rept. with ML18066A3651998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Palisades Nuclear Plant.With 990105 Ltr ML18066A3421998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Palisades Nuclear Plant.With 981202 Ltr ML18066A3301998-11-11011 November 1998 Part 21 Rept Re Potential Safety Hazard Associated with Wrist Pin Assemblies for FM-Alco 251 Engines at Palisades Nuclear Power Plant.Caused by Insufficient Friction Fit Between Pin & Sleeve.Supplier of Pin Will No Longer Be Used ML18068A4921998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Palisades Nuclear Plant.With 981103 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A3181998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Palisades Nuclear Plant ML18066A2901998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Palisades Nuclear Power Plant.With 980903 Ltr ML18066A3191998-08-31031 August 1998 Revised Monthly Operating Rept Data for Aug 1998 for Palisades Nuclear Plant ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237E0301998-07-31031 July 1998 ISI Rept 3-3 ML18066A2701998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Palisades Nuclear Plant.W/980803 Ltr ML18066A2311998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Palisades Nuclear Plant ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A3061998-06-18018 June 1998 SG Tube Inservice Insp. ML20249C4951998-06-17017 June 1998 Rev 1 to EA-GEJ-98-01, Palisades Cycle 14 Disposition of Events Review ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18066A1711998-06-0101 June 1998 Part 21 Rept Re Impact of RELAP4 Excessive Variability on Palisades Large Break LOCA ECCS Results.Change in PCT Between Cycle 13 & Cycle 14 Does Not Constitute Significant Change Per 10CFR50.46 ML18066A1741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Palisades Nuclear Plant.W/980601 Ltr ML18066A2321998-05-31031 May 1998 Revised MOR for May 1998 for Palisades Nuclear Plant ML18068A4701998-05-31031 May 1998 Annual Rept of Changes in ECCS Models Per 10CFR50.46. ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18066A2331998-04-30030 April 1998 Revised MOR for Apr 1998 for Palisades Nuclear Plant ML18068A3461998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Palisades Nuclear Plant.W/980501 Ltr ML18066A3411998-04-22022 April 1998 Rev 0 to EMF-98-013, Palisades Cycle 14:Disposition & Analysis of SRP Chapter 15 Events. ML18065B2071998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Palisades Nuclear Plant.W/980403 Ltr ML20217C2741998-03-31031 March 1998 Independent Review - Is Consumers Energy Method (W Method) of Determining Palisades Nuclear Plant Best Estimate Fluence by Combining Transport Calculation & Dosimetry Measurements Technically Sound & Does It Meet Intent of Pts ML18066A2341998-03-31031 March 1998 Revised MOR for Mar 1998 for Palisades Nuclear Plant ML18068A3041998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Palisades Nuclear Plant.W/980302 Ltr ML18066A2351998-02-28028 February 1998 Revised MOR for Feb 1998 for Palisades Nuclear Plant ML18065B1641998-02-0505 February 1998 Rev 0 to Regression Analysis for Containment Prestressing Sys at 25th Year Surveillance. ML18067A8211998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Palisades Nuclear Plant.W/980203 Ltr 1999-09-30
[Table view] |
Text
, " NRCForm388 U.S. NUCLEAR REGULATORY COMMISSION (9-83) APPROVED OMS NO. 3150-0104 EXPIRES: 8131185 LICENSEE EVENT REPORT (LER) FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3) Consumers Power Company Palisades Plant a I s I a I a I c I 2 I s I s 1 I OF a 1 s TITLE (4) LICENSEE EVENT REPORT 96-004 -SAFETY INJECTION SYSTEM DISABLED WITH PRIMARY COOLANT SYSTEM GREATER THAN 300°F EVENT DATE CSl LER NUMBER I, n REPORT DATE 161 OTHER FACILITTES INVOLVED (8) SEQUENTIAL . REVISION FACILITY NAMES MONTH DAY YEAR YEAR NUMBER NUMBER MONTH DAY YEAR NIA olslololol I 0 I 1 1 I 6 916 -o Io I 4 -olo 012 1 I 9 916 olslololol I 9 6 NIA THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or mONJ of the following)
(11) OPERATING N MODEC9l 20.402(b) 20.405(c)
- 50. 73(a)(2)(iv) 73.71(b) ---POWER 20.405(a)(1)(1) 50.38(c)(1)
- 50. 73(a)(2)(v) 73.71(c) LEVEL -....._ --(10) o I o 0 20.405(a)(1)(1i) 50.38(c)(2)
- 50. 73(a)(2)(vii)
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- 50. 73(a)(2)(viii)(A) below and in Telrt, -/:. -20.405(a)(1)[iv)
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NRC Form 388A) .. *. 20.405CaH1lM
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LICENSEE CONTACT FOR THIS LER {121 NAME TELEPHONE NUMBER Clayton M Mathews, Licensing Engineer AREACODE I 61116 11614 I -lsl91113 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 1131 MANUFAC-REPORTABL
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I I I I I I I I I I I I I I I I I I I I I SUPPLEMENT AL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED ---, YES (If ve.s. comolete EXPECTED SUBMISSION DA TEI SUBMISSION I I I 0ATE(15) ABSTRACT (Limit to 1400 *pace3, i.e .. approximately fift""n *ing/.,.,,pace typewritten
/in.,.) (18) On January 18, 1996, the reactor was being placed in cold shutdown conditions due to faulted 2400 VAC cables that supply 1 D Bus. The Safety Injection System actuation on low pressurizer pressure was disabled when the Primary Coola.nt System (PCS) temperature was approximately 364°F. This was a violation of Technical Specification section 3.17.2 which requires these Engineered Safety Feature logic channels and associated instrumentation to be operable whenever PCS temperature is greater than or equal to 300°F. 9602260303 960219 POR ADOCK 05000255 S PDR NRC Form 366A (9-83) FACILITY NAME (1) Palisades Plant EVENT DESCRIPTION
- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) YEAR LER NUMBER (3) SEQUENTIAL NUMBER U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO.
EXPIRES: 8131/85 REVISION NUMBER PAGE(4) 0 I 5 I 0 I 0 I 0 I 2 I 5 I 5 9 I 6 -*) I 0 I 4 -0 I 0 0 I 2 OF 0 I 5 On January 18, 1996, the reactor was being placed in cold shutdown conditions due to faulted 2400 VAC cables that supply 1 D Bus. During the "C" shift (1600-2400 hrs) a work order for disabling the Safety Injection System (SIS) was noted by the Electrical Maintenance Supervisor during his review of upcoming work. A review of the Electrical Maintenance Daily Schedule and the forced outage schedule did not indicate that this work order was to be performed on that shift: After a discussion with the Shift Supervisor, a review of plant conditions, and a review of what were thought to be the applicable requirements, the work order was released at 2046 hours0.0237 days <br />0.568 hours <br />0.00338 weeks <br />7.78503e-4 months <br />. Primary coolant temperature at that time was approximately 364 ° F. The work order activity was completed at 2130 hours0.0247 days <br />0.592 hours <br />0.00352 weeks <br />8.10465e-4 months <br />. Therefore, this work disabled the Safety Injection System actuation on low pressurizer pressure when the Primary Coolant System (PCS) temperature was approximately 364°F. This was a violation of Technical Specification section 3.17.2 which requires these Engineered Safety Feature logic channels and associated instrumentation to be operable whenever PCS temperature is greater than or equal to 300°F. Disabling the low pressurizer pressure safety injection actuation signal at a PCS temperature greater than 300° F went unnoticed until 0615 hours0.00712 days <br />0.171 hours <br />0.00102 weeks <br />2.340075e-4 months <br /> on January 19 when the Planning and Scheduling Manager questioned the completion of the activity.
ANALYSIS OF EVENT Various references provide the necessary information to identify the applicable requirements for disabling SIS. However, all relevant references were not utilized to validate the decision to allow the disabling of the low pressurizer pressure safety injection actuation signal. The applicable Technical Specification requirement was not utilized and the maintenance procedure prerequisites were not met. When the Electrical Maintenance Supervisor noted the work order to disable SIS and went to seek more information as to when it was required, a series of miscommunications, improper verification of plant requirements, and lack of attention to detail resulted in a decision to perform the work order activity prematurely.
The required pre-established plant conditions and sequence were unknowingly altered for this activity.
Various program and process barriers to prevent this occurrence were broken. They were: 1. The Work Order "Technical Specification Involvement" block referenced Technical Specification 3.17. However, this section was not referred to and Technical Section 3.16 was thought to be the applicable requirement.
NRC Form 386A (9-83) FACILITY NAME (1) Palisades Plant LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) YEAR LER NUMBER (3) SEQUENTIAL NUMBER U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 EXPIRES: 8131185 REVISION NUMBER PAGE (4) 0500025596-004
-0 0 OJ0F05 2. General Operating Procedure (GOP) 9, Attachment 1 "Plant Cooldown (Hot Standby/Shutdown Checklist)" section 4.4 states "When PCS is less than 210°F (ie, Cold Shutdown), then initiate work order to disable Safety Injection actuation circuits [refer to System Operating Procedure (SOP) 3, step 7. 7.1 ]." This step went unheeded in the decision making process to disable SIS since it appears on page 4 of the checklist and the plant conditions at the time had only proceeded the operating crew through page 2 of the checklist.
- 3. SOP 3, "Safety Injection And Shutdown Cooling System," section 7.7.1 notes "This procedure shall only be performed when the Reactor is in Cold or Refueling Shutdown ... " This procedure was not referenced for guidance.
- 4. Electrical Maintenance Procedure, ESS-M-24 "Disable/Enable the Safety Injection System Actuation on Low Pressurizer Pressure," prerequisite section 3.3, specifies plant condition to be "cold shutdown." Procedure step 5.1 requires the assigned supervisor ensure all prerequisites are completed.
The plant condition of cold shutdown was not verified.
- 5. Technical Specification 3.16 "Engineered Safety Features System Instrumentation Settings" was referenced as the controlling requirement.
Technical Specification 3.16 applicability statement indicates that "Technical Specification 3.16 is applicable when associated ESF or Isolation Function Instrumentation is req'.;.;:;*ad to be operable by Technical Specification 3.17.2 or 3.17.3. Technical Specification 3.17.2 requires SIS to be operable when the PCS is greater than or equal to 300°F. This information was not recognized and verified.
- 6. The Equipment Safe Shutdown Operations General Outage Information list contained an entry indicating Safety Injection Actuation Signal (SIAS) will be disabled at less than 210° F for low pressure only. Containment High Pressure will still result in a SIAS. This information was available but was not referred to as a reference source. CAUSE OF EVENT All relevant information was not used in the decision making process and pertinent procedures were violated.
Therefore, the root cause of the event was personnel error. SAFETY SIGNIFICANCE There was no safety significant condition which resulted from disabling of the SIS on low pressure during plant cooldown on January 18, 1996. The low pressure signal was blocked by design during plant cooldown before PCS pressure decreased below 1593 psia. The plant average temperature and pressure were 364°F. and less than 600 psia when the maintenance was performed disabling SIS on low PCS pressure.
The Low Temperature Overpressurization Protection (LTOP) -j
. NRC Form 368A (9-83) FACILITY NAME (1) *
- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) YEAR LER NUMBER (3) SEQUENTIAL NUMBER U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 EXPIRES: 8/31/85 REVISION NUMBER PAGE (4) Palisades Plant olslololol2lsls gjs -o lo 14 -o lo ol4 oF o Is setpoint of about 1000 psia would have prevented an auto-reset on increasing pressure above 1593 psia. Whether the SIS on low pressure is available or disabled is not significant to the.plant condition because the plant would have been relying on a Containment High Pressure (CHP) signal or operator action to start High Pressure Safety Injection (HPSI) to maintain or recover PCS inventory for a large break Loss of Coolant Accident (LOCA). The SIS on containment high pressure was still available to start all available safety injection pumps. With the saturation pressure of about 160 psia, the PCS inventory could be quickly recovered with one HPSI pump for both large break and small break LOCAs. At this pressure, Low Pressure Safety Injection (LPSI) pumps would also be able to supply PCS makeup since they remain aligned to the Safety Injection and Refueling Water (SIRW) tank when the PCS temperature is greater than 300°F. The plant response to small break LOCAs with the SIS low pressure signal blocked or disabled requires operator action to start available HPSI and Charging pumps. Throttling of the safety injection pumps would be required to maintain the PCS pressure within the acceptable range below the L TOP set point curve. Also, the probability of a large or small break LOCA occurring after full power operations when the PCS pressure has been reduced to less than 600 psia is very small. The consequences of an accident were not changed by this event. CORRECTIVE ACTIONS The following corrective actions will be taken: 1. Communicate to Shift Supervisors, Control Room Supervisors and Shift Engineers the expectation to validate and verify information using available references (e.g. Work Order information blocks, procedure prerequisite sections) and sources (Technical Specifications, procedures, Daily Orders, schedules, equipment safe shutdown lists, LCO status boards, etc) to assist in achieving informed and accurate decision making. 2. Reinforce the Maintenance Supervisor's responsibility to assure procedure prerequisites are met prior to authorizing a work activity.
- 3. Conduct training for licensed operators on the purpose of maintaining operability of equipment listed in Technical Specification Table 3.17.2 when the PCS temperature is greater than or equal to 300°F. 4. Revise the Permanent Maintenance Procedure to disable/enable the Safety Injection System actuation on low pressurizer pressure to align with Technical Specifications.
- ,; NRC Form 366A (9-83) FACILllY NAME (1) Palisades Plant LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) YEAR LER NUMBER (3) SEQUENTIAL NUMBER U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 EXPIRES
- 8/31185 REVISION NUMBER PAGE(4) 0500025596-004
-0 0 050F05 5. Align the following procedures to accurately reflect which procedure controls the activity for disabling SIS. A. General Operating Procedure 9, Attachment 1 "Plant Cooldown (Hot Standby/Shutdown Checklist), step 4.4 which refers to System Operating Procedure 3, step 7.7.1 8. System Operating Procedure 3 "Safety Injection And Shutdown Cooling System" section 7. 7. C. Permanent Maintenance Procedure ESS-E-24, "Disable/Enable the Safety Injection System Actuation On Low Pressurizer Pressure." .