Search by property
Jump to navigation
Jump to search
This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML20080U471 + (13:29:16, 14 December 2024)
- ML20080U465 + (13:29:19, 14 December 2024)
- ML20080U459 + (13:29:20, 14 December 2024)
- ML20080U461 + (13:29:20, 14 December 2024)
- ML20080U454 + (13:29:21, 14 December 2024)
- ML20080U453 + (13:29:22, 14 December 2024)
- ML20080U435 + (13:29:25, 14 December 2024)
- ML20080U444 + (13:29:25, 14 December 2024)
- ML20080U432 + (13:29:26, 14 December 2024)
- ML20080U416 + (13:29:27, 14 December 2024)
- ML20080U407 + (13:29:28, 14 December 2024)
- ML20080U406 + (13:29:29, 14 December 2024)
- ML20080U402 + (13:29:29, 14 December 2024)
- RBG-17132, Provides Info Re Status of Generic & plant-specific Work Concerning Containment Issues Raised by Humphreys,Per Util 830815 Commitment.Status Rept Will Be Provided by 840731 + (13:29:30, 14 December 2024)
- ML20080U397 + (13:29:31, 14 December 2024)
- ML20080U391 + (13:29:31, 14 December 2024)
- SNRC-1007, Forwards Rept on Special Lifting Devices, Per 831111 Response to SER Open Item 59.Rept Covers Design,Fabrication & Initial Acceptance Testing of Six Special Lifting Devices Listed in Table 3 of + (13:29:32, 14 December 2024)
- ML20080U371 + (13:29:34, 14 December 2024)
- ML20080U358 + (13:29:34, 14 December 2024)
- ML20080U343 + (13:29:35, 14 December 2024)
- 05000389/LER-1984-003-01, :on 840129,hi-hi Steam Generator Level Turbine Trip Occurred,Resulting in Reactor Trip.Caused by Leakage Through Main Feed Regulating Valve A.Reactor Started & Plant Returned to Svc + (13:29:37, 14 December 2024)
- ML20080U321 + (13:29:37, 14 December 2024)
- ML20080U307 + (13:29:40, 14 December 2024)
- 05000327/LER-1984-013, :on 840130,turbine Trip Followed by Reactor Trip Occurred.Caused by high-high Level in Steam Generator 4.Unit Stabilized at 547 F + (13:29:41, 14 December 2024)
- ML20080U280 + (13:29:42, 14 December 2024)
- ML20080U246 + (13:29:43, 14 December 2024)
- 3F0395-04, Forwards Nonproprietary Calculation 32-1236435-00, CR-3, Pressurizer Surge Nozzle Stresses + (13:29:44, 14 December 2024)
- W3P84-0498, Forwards Info Re Corrective Actions Identified During Control Room Design Review.Lighting Survey Results,Color Code Convention & Results of Control Room Liveability Review Encl.Lighting Mods Complete + (13:29:44, 14 December 2024)
- ML20080U219 + (13:29:45, 14 December 2024)
- ML20080U196 + (13:29:46, 14 December 2024)
- ML20080U190 + (13:29:46, 14 December 2024)
- ML20080U179 + (13:29:47, 14 December 2024)
- NRC-95-4412, Provides Analyses of Multiple Steam Generator Tube Rupture Events for AP600 Design.Analyses Performed Using MAAP4 Computer Code & Provided in Support of Westinghouse Response to NRC RAIs 440.27 & 440.170 + (13:29:47, 14 December 2024)
- U-602427, Monthly Operating Rept for Feb 1995 for Clinton Power Station Unit 1 + (13:29:48, 14 December 2024)
- ML20080U176 + (13:29:49, 14 December 2024)
- ML20080U174 + (13:29:50, 14 December 2024)
- 3F0395-05, Provides Rept Containing Results of OTSG Tube Pull Performed During Spring 1994 Refueling Outage (9R).Rept Required to Satisfy Item 8 of 940426 CAL Associated W/Util OTSG Tube Insp Program + (13:29:51, 14 December 2024)
- ML20080U168 + (13:29:51, 14 December 2024)
- ML20080U165 + (13:29:52, 14 December 2024)
- ML20080U164 + (13:29:52, 14 December 2024)
- ML20080U159 + (13:29:53, 14 December 2024)
- ML20080U147 + (13:29:53, 14 December 2024)
- ML20080U144 + (13:29:54, 14 December 2024)
- ML20080U143 + (13:29:55, 14 December 2024)
- 05000387/LER-1983-078-03, /03L-0:on 830829,excess Flow Check Valve XV-B21-F009 Could Not Be Tested to Verify Operability.Caused by Present Configuration of Instrument Line Not Allowing Access to Valve W/O Removing Vessel Head + (13:29:56, 14 December 2024)
- 05000289/LER-1983-025-01, /01T-0:on 830915,during once-through Steam Generator testing,3/4-inch Vent Valve Which Serves as Containment Isolation Valve Found Open.Caused by Personnel Error.Operators Counseled + (13:29:58, 14 December 2024)
- ML20080U138 + (13:29:59, 14 December 2024)
- ML20080U132 + (13:30:01, 14 December 2024)
- ML20080U128 + (13:30:01, 14 December 2024)
- ML20080U126 + (13:30:02, 14 December 2024)
- ML20080U127 + (13:30:02, 14 December 2024)
- ML20080U121 + (13:30:03, 14 December 2024)