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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML20082P228 + (11:37:51, 14 December 2024)
- ML20082P220 + (11:37:53, 14 December 2024)
- NRC-95-4427, Forwards Proprietary Rept RCS-GSR-003, AP600 Notrump ADS Preliminary Validation Rept. Rept Withheld Per 10CFR2.790 + (11:37:53, 14 December 2024)
- 05000416/LER-1983-170-03, /03L-0:on 831026,RCIC Sys Declared Inoperable When Attempts to Secure RCIC Turbine Via Trip Pushbutton Failed.Caused by Trip Valve Sticking Due to Oxidation. Mechanical Stop Installed + (11:37:55, 14 December 2024)
- 05000348/LER-1983-057-03, /03L-0:on 831102,entry Into Mode 3 Made While Solid State Protection Sys Train a Removed for Performance of FNP-2-STP-33.0.Caused by Personnel Error.Train a Returned to Svc & Heatup Resumed + (11:37:59, 14 December 2024)
- 05000328/LER-1983-153-03, /03L-0:on 831031,during Attempt to Perform Air Leakage Test on Upper Containment Air Lock While in Mode 1, Outer Door Discovered Not Fully Closed.Probably Caused by Personnel Failure to Fully Seat Door + (11:38:06, 14 December 2024)
- ML20082P196 + (11:38:07, 14 December 2024)
- ML20082P189 + (11:38:12, 14 December 2024)
- ML20082P187 + (11:38:12, 14 December 2024)
- ELV-03078, Responds to NRC Ltr Re Violations Noted in Insp Repts 50-424/91-15 & 50-425/91-15 on 910623-0720.Corrective Actions:Mgt Attention Continue to Focused on Improving Procedural Compliance + (11:38:18, 14 December 2024)
- 3F0495-15, Requests NRC to Update Svc List to Reflect Plant Recent Internal Mail Code Changes.Changes Listed + (11:38:21, 14 December 2024)
- ML20082P176 + (11:38:22, 14 December 2024)
- 05000260/LER-1983-066-31, /03L-0:on 831031,operator Observed Low Flow Alarm in Hydrogen Monitor B (H2AN-76-104).Caused by Moisture Collecting in Sample Lines.Lines Blown Down + (11:38:26, 14 December 2024)
- ML20082P172 + (11:38:27, 14 December 2024)
- ML20082P168 + (11:38:28, 14 December 2024)
- 05000260/LER-1983-067-03, /03L-0:on 831029,operator Observed RHR Loop II Flow Instrumentation Reading Upscale.Caused by Short in GE Type 531 Recorder FR-74-64.Recorder Repaired + (11:38:29, 14 December 2024)
- 05000260/LER-1983-074-01, /01T-0:on 831110,HPCI Sys Initiated,But Immediately Became Inoperable.Caused by Blown Turbine Exhaust Rupture Disc,Fike Model 16-CPV-CBT.Disc Replaced + (11:38:31, 14 December 2024)
- ML20082P163 + (11:38:32, 14 December 2024)
- ML20082P161 + (11:38:33, 14 December 2024)
- ML20082P158 + (11:38:36, 14 December 2024)
- AECM-83-0767, RO 83-105/0:on 831031-1106,fluctuating Temps in Auxiliary Bldg Steam Tunnel Exceeded Tech Spec Limit of 125 F for More than 8 H.Steam Tunnel Cooler Coils Replaced to Resolve Temp Problems + (11:38:37, 14 December 2024)
- ML20082P153 + (11:38:37, 14 December 2024)
- BSEP-83-3720, Ro:On 831020,while Performing Visual Insp of Fire Barrier Penetration Seals on Diesel Generator Bldg,Discovered Several Fire Barrier Penetrations Did Not Meet Test Acceptance Criteria.Caused by Cracked Insulating Cement + (11:38:41, 14 December 2024)
- ML20082P146 + (11:38:41, 14 December 2024)
- 05000338/LER-1983-074-03, /03L-0:on 831106,steam Generator C Channel I Level Indication Drifted High Out of Specified Tolerance.Caused by body-to-bonnet Leakage of Ref Leg Root Valve.Valve Leak Stopped + (11:38:43, 14 December 2024)
- ST-HL-AE-3848, Responds to NRC Inspector Follow-up Item 498/9104-01 Re Inservice Insp Program for Steam Generator Tubes + (11:38:44, 14 December 2024)
- ML20082P133 + (11:38:46, 14 December 2024)
- 05000339/LER-1983-075-03, /03L-0:on 831112,solid State Protection Sys Train a Stop Valve Generator Trip Logic Failed to Meet Acceptance Criteria.Caused by Faulty Universal Card.Card Replaced & Logic Channel Returned to Svc After Calibr + (11:38:48, 14 December 2024)
- 05000259/LER-1983-063-03, /03L-0:on 831102,flow Distribution Through Standby Gas Treatment Train B Failed Acceptance Criteria.Caused by Accumulation of Sand in Moisture Separator.Moisture Separator Repaired + (11:38:49, 14 December 2024)
- 05000416/LER-1983-174-03, /03L-0:on 831026,during Div II Diesel Generator Monthly Surveillance,Fuel Oil Leak Discovered on Cylinder Injector Return Line 81B.Caused by Unknown Bump by Tool or Personnel.Line Replaced + (11:38:51, 14 December 2024)
- 05000260/LER-1983-071-03, /03L-0:on 831104,while Performing Surveillance Insp 4.2.B-7,2-PS-3-74A Pressure Switch 1 Had as-found Setpoint of 214.43 Psig.Caused by Calibr Drift.Barksdale B 2T-M12SS Switch Recalibr + (11:38:53, 14 December 2024)
- 05000389/LER-1983-069-03, /03L-0:on 831027,while Performing Periodic Control Element Assembly (CEA) Exercise,Cea 86 Dropped to Full Insertion.Caused by Control Element Drive Mechanism Failure to Close Upper Gripper + (11:38:58, 14 December 2024)
- 05000339/LER-1983-073-03, /03L-0:on 831107 & 14,w/unit in Mode 1 at 100% Power,Inner Personnel Hatch Door Found to Have Unacceptable Leak Rate,Contrary to Tech Spec 3.6.1.3.Caused by Dirty Door Seals Due to Multiple Containment Entries + (11:39:00, 14 December 2024)
- 05000302/LER-1995-005, :on 950322,engineering Performed Net Positive Suction Head Evaluation for Unique ECCS Configuration. Condition Caused by Insufficient Review During EOP Change Process.Affected Procedures Annotated + (11:39:02, 14 December 2024)
- 05000333/LER-1995-007, :on 950313,reactor Coolant Temp Raised Above 212 Degrees W/Less than Min Number of Required Operable Crev Air Supply Fans.Caused by Inoperability of Fan Motor.Fan Repaired + (11:39:04, 14 December 2024)
- 05000425/LER-1991-009-02, :on 910813,safety Injection Pump Start Occurred During Surveillance Testing.Caused by Intermittent Failure of Reset.Shift Briefings Held Informing Control Room Personnel of Switch Malfunction + (11:39:06, 14 December 2024)
- 05000338/LER-1983-076-03, /03L-0:on 831101,individual Rod Position Indication for Channel N-09 Deviated from Group Demand Position by Greater than 12 Steps.Caused by Instrument Drift.Channel Recalibr + (11:39:08, 14 December 2024)
- RBG-16-438, Forwards Responses to Draft SER & Changes to FSAR Re Safe Shutdown Sys & Fire Hazards Analysis,Reflecting Resolution of Each Open Item.Changes Will Be Incorporated Into Next FSAR Amend + (11:39:10, 14 December 2024)
- ML20082P088 + (11:39:11, 14 December 2024)
- 05000328/LER-1983-160-03, /03L-0:on 831102,turbine-driven Auxiliary Feedwater Pump Failed Criteria SI-166.32 by Not Obtaining 880 Gpm Min Flow Rate.Caused by High Reading Due to Air in Instrument Sense Line.Lines Vented + (11:39:13, 14 December 2024)
- BSEP-83-3848, Ro:On 831111,conservative Determination Made That Drywell Equipment Drain Line,Floor Drain & Svc Air Header Not Adequately Supported.Investigation Incomplete.Rept Expected by 831209 + (11:39:14, 14 December 2024)
- ML20082P085 + (11:39:14, 14 December 2024)
- ML20082P076 + (11:39:15, 14 December 2024)
- 05000260/LER-1983-065-03, /03L-0:on 831013,reactor Protective Sys Channel a Manually Tripped W/O Performing Functional Test on Scram Discharge Instrument Vol Channel B.Caused by Personnel Oversight.Tech Spec Criteria Stressed + (11:39:19, 14 December 2024)
- 05000328/LER-1983-161-03, /03L-0:on 831102,w/unit in Mode 2 at Zero Power, Rod Bottom Light for Control Rod H-10 Did Not Come on at Shutdown.Light Declared Inoperable.Caused by Failed Resistor in Module.Module Replaced + (11:39:21, 14 December 2024)
- ML20082P067 + (11:39:23, 14 December 2024)
- 05000327/LER-1983-152-03, /03L-0:on 831028,containment Isolation Valve 1-FCV-77-20 in Reactor Coolant Drain Tank Nitrogen Supply Line Found Inoperable.Valve Isolated.Caused by Bad Cable. Cable Will Be Replaced + (11:39:24, 14 December 2024)
- RBG-16-413, Forwards Response to Draft SER Open Item Re Reactor Vessel Matls Surveillance Program.Response Will Be Incorporated Into Future FSAR Amend + (11:39:25, 14 December 2024)
- ML20082P062 + (11:39:26, 14 December 2024)
- ML20082P055 + (11:39:26, 14 December 2024)
- 05000327/LER-1983-155-03, /03L-0:on 831104,loop 4 Feedwater Flow Transmitter 1-FT-103A Became Inoperable When Line Pulled Loose from Connection Upstream of Isolation Valve.Caused by Incorrectly Installed Fitting.Connection Repaired + (11:39:28, 14 December 2024)