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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML20043G014 + (ML20043G014)
- ML20043G016 + (ML20043G016)
- ML20043G019 + (ML20043G019)
- ML20043G021 + (ML20043G021)
- ML20043G023 + (ML20043G023)
- ML20043G024 + (ML20043G024)
- ML20043G027 + (ML20043G027)
- ML20043G028 + (ML20043G028)
- ML20043G044 + (ML20043G044)
- PMNS20200113, Notice of Public Meeting with the Nuclear Energy Institute Regulatory Issues Task Force + (ML20043G046)
- ML20043G050 + (ML20043G050)
- ML20043G056 + (ML20043G056)
- ML20043G057 + (ML20043G057)
- ML20043G060 + (ML20043G060)
- PNO-III-90-038, on 900612,controlled Shutdown Initiated After Small Leak Identified in Inlet Flange Joint on Pressurizer Safety Valve.In Nov 1989,leak Also Identified in Unit 2. Possible Generic Implications of Leak Being Reviewed + (ML20043G061)
- PNO-II-90-032, on 900610,hydrogen Burn in Charcoal Absorbers in Gas Treatment Bldg Occurred.Fire Lasted for More than 10 Minutes Based on Levels of Carbon Dioxide/Carbon Monoxide. Gas Treatment Bldg Purged W/Nitrogen + (ML20043G062)
- ML20043G065 + (ML20043G065)
- 0CAN069011, Responds to Deviations Noted in Insp Repts 50-313/90-11 & 50-368/90-11.Corrective Actions:Further Evaluations Conducted to Develop Optimum List of post-accident Instruments Requiring Identification on Control Panels + (ML20043G066)
- ML20043G070 + (ML20043G070)
- 05000324/LER-1990-005-03, :on 900514,unplanned Closure of HPCI Isolation Valve Occurred During Maint Surveillance Test.Caused by Technician Placing RCIC Instead of HPCI Test Switch to Test Position.Personnel Counseled & Trained + (ML20043G071)
- ML20043G072 + (ML20043G072)
- PNO-I-90-046, on 900607,control Element Assemblies (Ceas) Fully Withdrawn from Fully Inserted Position During Tests. Attempts to Insert CEAs Further Were Unsuccessful.Fuel Assembly Visually Inspected.State of Me Notified + (ML20043G073)
- 05000482/LER-1990-011, :on 900514,feedwater Isolation Signal & Main Turbine Trip Signal Occurred When Steam Generator B Reached hi-hi Level Setpoint & Generator C Reached lo-lo Setpoint. Caused by Power Oscillations.Procedure Revised + (ML20043G074)
- ML20043G075 + (ML20043G075)
- ML20043G077 + (ML20043G077)
- 05000259/LER-1990-008-02, :on 900512,actuations/isolations of Various ESF Sys Occurred Due to Blown Fuse in Primary Containment Isolation Sys Logic Panel.Caused by Jumpering Wrong Relay Contact.Fuse Replaced & Logic Reset + (ML20043G079)
- ML20043G080 + (ML20043G080)
- 05000278/LER-1990-006-03, :on 900511,blown Fuse from Battery Charger 3B Resulted in Declaring HPCI Sys,Core Spray B Logic,Rhr B Logic,Core Spray Subsystem B,Rhr Subsystem B & E2 & E4 Emergency Diesel Generators Inoperable + (ML20043G082)
- IR 05000320/1990003 + (ML20043G083)
- ML20043G084 + (ML20043G084)
- ML20043G088 + (ML20043G088)
- ML20043G091 + (ML20043G091)
- IR 05000271/1990004 + (ML20043G092)
- 05000219/LER-1990-006, :on 900511,average Power Level Exceeded Licensed Limit by Approx 1.64 MW When Cleanup Sys Placed in Svc W/O 7.84 MW Loss Added Into Heat Balance Calculation. Caused by Personnel Error.Procedures Changed + (ML20043G093)
- ML20043G095 + (ML20043G095)
- 05000311/LER-1990-023, :on 900516,4 Kv Vital Bus Deenergized During 2A Safeguard Equipment Control 18-month Surveillance.Caused by Personnel Error.Personnel Reprimanded & Procedure M3U Revised + (ML20043G097)
- 05000311/LER-1990-022, :on 900522,radiation Monitoring Sys Channel 2R12A Failed Low.Probably Caused by Equipment/Design Concerns.Anticipates That Several Sys Design Mods Will Eliminate Spurious ESF Actuation Signals + (ML20043G099)
- ELV-01738, Requests Temporary Waiver of Compliance from Requirements of Action Statement 27 of Tech Spec 3.3.2 for Period of 6 H When Two Operating Control Room Emergency Filtration Sys Trains Shut Down for Required Testing + (ML20043G102)
- 05000423/LER-1990-016, :on 900513,steam Generator B lo-lo Signal Generated Reactor Trip Signal,Causing Automatic Start of motor-driven Auxiliary Feedwater Pumps a & B.Caused by Inadequate Guidance.Procedure Revised + (ML20043G103)
- 05000245/LER-1990-007-01, :on 900512,determined That One Emergency Power Source Did Not Have Sufficient Capacity for Accident Loading Conditions.Gas Turbine Generator Declared Inoperable & Orderly Reactor Shutdown Initiated + (ML20043G105)
- ML20043G110 + (ML20043G110)
- 05000445/LER-1990-014, :on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order Issued + (ML20043G112)
- ML20043G114 + (ML20043G114)
- 05000461/LER-1990-011, :on 900514,during Routine Testing,Diesel Generators 1A Tripped on High Coolant Temp.Caused by Lack of Procedures for Correctly Positioning Diesel Generator SX Throttle Valves.Caution Tags Replaced + (ML20043G115)
- ML20043G116 + (ML20043G116)
- ML20043G117 + (ML20043G117)
- ML20043G118 + (ML20043G118)
- PY-CEI-NRR-1185, Monthly Operating Rept for May 1990 for Perry Unit 1 + (ML20043G119)
- ML20043G120 + (ML20043G120)
- ML20043G121 + (ML20043G121)
- 3F0690-09, Monthly Operating Rept for May 1990 for Crystal River Unit 3 + (ML20043G122)