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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML20009G008 + (ML20009G008)
- 05000348/LER-1981-040-03, /03L-0:on 810529,diesel Generator 1-2A Could Not auto-start Due to Mode Selector Switch Being Placed in Mode 3.Caused by Generator Being Shut Down for Cleaning. Switch Returned to Mode 1 + (ML20009G009)
- 05000260/LER-1981-027-03, /03L-0:on 810604,during Mod Outage,Switch 2-PdIS-75-56 Was Found Outside Tech Spec Limits.Caused by Setpoint Drift of Barton Model 288 D/P Switch.Switch Recalibr + (ML20009G010)
- 05000369/LER-1981-033-01, /01T-0:on 810403,discovered Ductwork Inside of Inside Isolation Valves for Containment Purge Sys Not Constructed of 10-gauge Stainless Steel Per Fsar.Caused by Design Drawing Details Not Specifying Matl + (ML20009G011)
- 05000261/LER-1981-014, Forwards LER 81-014/03L-0 + (ML20009G013)
- ML20009G014 + (ML20009G014)
- 05000369/LER-1981-092, Forwards LER 81-092/03L-0.Detailed Event Analysis Encl + (ML20009G015)
- ML20009G016 + (ML20009G016)
- 05000369/LER-1981-092-03, /03L-0:on 810530,auxiliary Feedwater Flow Rate Instrumentation Pegged High.Caused by Failed Transmitters. Transmitters Replaced & Calibr.Power Supply Removed & Will Be Replaced + (ML20009G017)
- 05000261/LER-1981-014-03, /03L-0:on 810523,discovered That Hagan Summator PM-446B Had Shifted Nonconservatively Approx 3%.Caused by Failure of Filter Capacitor Due to Normal Wear.Faulty Capacitor Replaced + (ML20009G018)
- 05000369/LER-1981-078, Forwards LER 81-078/03L-0.Detailed Event Analysis Encl + (ML20009G019)
- ML20009G020 + (ML20009G020)
- ML20009G022 + (ML20009G022)
- 05000369/LER-1981-078-03, /03L-0:on 810507,reset Pushbutton on Pressurizer Safety Injection Train B Pressed Instead of Safety Injection Reset Train 1B Button.Caused by Personnel Error.Different Method to Be Used to Reset Valve Timing Computer Program + (ML20009G023)
- 05000327/LER-1981-067, Forwards LER 81-067/01T-0 + (ML20009G025)
- ML20009G026 + (ML20009G026)
- 05000369/LER-1981-096, Forwards LER 81-096/01T-0.Detailed Event Analysis Encl + (ML20009G027)
- ML20009G028 + (ML20009G028)
- 05000369/LER-1981-096-01, /01T-0:on 810624,Type C Leak Test Not Performed as Required for Bypass Leakage Paths on Penetration Used for Ice Loading.Caused by Not Being Listed in FSAR as Requiring Leak Test.Test Performed Satisfactorily + (ML20009G030)
- 05000369/LER-1981-097, Forwards LER 81-097/03L-0.Detailed Event Analysis Encl + (ML20009G031)
- ML20009G032 + (ML20009G032)
- 05000327/LER-1981-067-01, /01T-0:on 810626,while in Mode 4,site Evaluation Identified That Steam Generator Level Transmitters 1-LT-3-148,156,164,172,174 & 175 Would Fail During Loca. Caused by Incorrect Insulating Sleeving + (ML20009G033)
- 05000338/LER-1981-034, Forwards LER 81-034/03L-0 + (ML20009G034)
- ML20009G035 + (ML20009G035)
- 05000369/LER-1981-097-03, /03L-0:on 810612,in Mode 5,routine Surveillance Discovered That Quantity of Fire Detection Equipment Installed in Five Fire Zones Did Not Comply W/Tech Specs. Caused by Typographical Error & Incorrect Blueprints + (ML20009G036)
- ML20009G038 + (ML20009G038)
- 05000338/LER-1981-034-03, /03L-0:on 810627,quadrant Power Tilt Ratio Indicated Tilt in Excess of 1.02 During Power Escalation. Caused by Control Rods Being Inserted Lower in Core than Desired While Increasing Reactor Power to 100% + (ML20009G039)
- ML20009G040 + (ML20009G040)
- L-81-316, Final Deficiency Rept Re Protuberance on Local Control Station Switches Supplied by Gould Rundel,Initially Reported 810625.Purchase Spec Revised to Specify Contact Maint During Position Change + (ML20009G041)
- 05000369/LER-1981-091-03, /03L-0:on 810530,peak Shock Annuciator Amber Light Observed On.Caused by Light Reed Switch from Triaxial response-spectrum Recorder Making Contact.Reed Switch Adjusted,Tested & Delared Operable + (ML20009G042)
- ML20009G043 + (ML20009G043)
- 05000259/LER-1981-031, Forwards LER 81-031/03L-0 + (ML20009G044)
- ML20009G045 + (ML20009G045)
- ML20009G046 + (ML20009G046)
- 05000259/LER-1981-031-03, /03L-0:on 810610,discovered That Eight Level Switches Would Not Operate During Maint on Scram Accumulator.Caused by Excessive Amounts of Substance on Switch Float & Guide Stem,Causing Float to Stick + (ML20009G047)
- ML20009G049 + (ML20009G049)
- ML20009G051 + (ML20009G051)
- ML20009G052 + (ML20009G052)
- ML20009G053 + (ML20009G053)
- ML20009G054 + (ML20009G054)
- ML20009G057 + (ML20009G057)
- ML20009G058 + (ML20009G058)
- ML20009G061 + (ML20009G061)
- BSEP-81-1271, Confirms 810625 Conversation Between CS Bohanan & R Butcher Re United Engineers & Constructors,Inc Notification That 38 Control Rod Driveline Gang Pipe Supports Would Fail in as-built Condition During Design Seismic Event + (ML20009G062)
- BSEP-81-0945, Ro:On 810506,investigation on RHR Heat Exchangers Determined That B Heat Exchanger Baffle Was Deformed at Bottom Allowing Bypass Flow.Cause Being Evaluated.Repairs on 2B RHR Heat Exchanger in Progress + (ML20009G063)
- ML20009G064 + (ML20009G064)
- IR 05000412/1981005 + (ML20009G065)
- ML20009G066 + (ML20009G066)
- 05000369/LER-1981-080, Forwards LER 81-080/03L-0.Detailed Event Analysis Encl + (ML20009G068)
- ML20009G069 + (ML20009G069)