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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML18096A273 + (ML18096A273)
- ML18096A274 + (ML18096A274)
- ML18096A275 + (ML18096A275)
- ML18096A276 + (ML18096A276)
- IR 05000272/1991022 + (ML18096A278)
- ND-18-0393, Submittal of 10 CFR 50.46 Annual Report + (ML18096A283)
- ML18096A284 + (ML18096A284)
- ML18096A285 + (ML18096A285)
- 05000311/LER-1991-012-02, :on on 910826,4 Kv Vital Bus 2A Tripped While Starting & Loading Diesel Generator 2A.Caused by Technician Connecting Jumper to Wrong relay.Color-coded Banana Jackets Installed on Relay Terminal Lugs + (ML18096A287)
- 05000272/LER-1991-028, :on 910823,steam Generator Blowdown Outlet Isolation Valve 12GB4 Failed Closed.Caused by Failure of Valve Actuator Diaphragm.Investigation Underway.Valve Repair Completed on 910824 + (ML18096A288)
- 05000311/LER-1991-013-02, :on 910828,0901 & 10,CP/pressure-vacuum Relief Sys Isolation Signal Received.Caused by Problems W/Equipment Design.Scalar Module Replaced,Channel Backplane Cleaned & Inspected.Channel Drawer & Circuits Vacuumed + (ML18096A291)
- ML18096A293 + (ML18096A293)
- 05000311/LER-1990-028-01, :on 900623,data Indicated That 25% Rated Thermal Power Trip Setpoint Would Not Actuate Until 44% for Channel N35 & Until 38.6% for N36.Caused by Procedure Inadequacy.Channel Trip Setpoints Reset + (ML18096A294)
- ML18096A296 + (ML18096A296)
- ML18096A298 + (ML18096A298)
- ML18096A299 + (ML18096A299)
- IR 05000272/1991023 + (ML18096A300)
- ML18096A301 + (ML18096A301)
- ML18096A303 + (ML18096A303)
- ML18096A305 + (ML18096A305)
- IR 05000272/1991025 + (ML18096A307)
- ML18096A308 + (ML18096A308)
- ML18096A309 + (ML18096A309)
- IR 05000272/1991024 + (ML18096A311)
- ML18096A313 + (ML18096A313)
- 05000272/LER-1991-029, :on 910907,control Room Low Flow Trouble Alarm for Containment Radiation Monitoring Sys Pump Received Indicating Pump Seizure.Caused by Inadequate Sys Design. Pump Replaced & Event Reviewed + (ML18096A314)
- ML18096A315 + (ML18096A315)
- ML18096A319 + (ML18096A319)
- ML18096A320 + (ML18096A320)
- ML18096A321 + (ML18096A321)
- 05000272/LER-1991-031, :on 910923,main Steam Line Isolation Actuation Signal Occurred Upon Receipt of High Steam Line Flow Signal, Coincident W/Low Steam Line Pressure Signal.Caused by Design Inadequacy.Flow Measuring Sys Modified + (ML18096A325)
- ML18096A328 + (ML18096A328)
- ML18096A329 + (ML18096A329)
- ML18096A330 + (ML18096A330)
- 05000272/LER-1991-003-01, :on 910209,steam Generator 14 Steamline Flow Channel I Transmitter Sensing Line Isolated During Investigation of Erroneous Reading.Caused by Personnel Error.Disciplinary Action Taken + (ML18096A331)
- ML18096A332 + (ML18096A332)
- ML18096A333 + (ML18096A333)
- ML18096A335 + (ML18096A335)
- ML18096A338 + (ML18096A338)
- ML18096A339 + (ML18096A339)
- ML18096A340 + (ML18096A340)
- ML18096A341 + (ML18096A341)
- ML18096A342 + (ML18096A342)
- ML18096A343 + (ML18096A343)
- ML18096A344 + (ML18096A344)
- ML18096A345 + (ML18096A345)
- ML18096A346 + (ML18096A346)
- ML18096A347 + (ML18096A347)
- ML18096A348 + (ML18096A348)
- 05000311/LER-1991-014-02, :on 911010,monitor 2R12B RMS Channel Failed Low Resulting in ESF Signal for CP/pressure-vacuum Relief Sys Isolation.Caused by Component Failure.Channel Returned to Svc.Mods Planned to Eliminate Spurious RMS + (ML18096A349)
- ML18096A350 + (ML18096A350)