Semantic search
Entered date | Site | Region | Reactor type | Event description | |
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ENS 57444 | 26 November 2024 14:14:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via phone and email: At 1158 EST on 11/26/24, the Division 3 diesel generator was declared inoperable due to failure of the right bank air start motor during a planned monthly surveillance run. Troubleshooting of the issue is in progress. This condition could prevent the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). All other emergency core cooling systems were operable during this time. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The Division 3 diesel generator supports high pressure core spray, a single train system. |
ENS 57418 | 10 November 2024 07:59:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via phone and email: On November 10, 2024, at 0337 CST, Grand Gulf Nuclear Station (GGNS) was operating in mode 1 at 100 percent power when a manual scram was initiated due to degrading main condenser vacuum. The cause of the degrading main condenser vacuum is not known at this time and is being investigated. All control rods fully inserted and there were no complications. Reactor pressure was initially maintained with main turbine bypass valves. Reactor water level was initially maintained with main feedwater and condensate. At 0457, operators transitioned pressure control to safety relief valves and began using reactor core isolation cooling (RCIC) to maintain reactor water level. This was performed using plant procedures due to degrading vacuum. GGNS is currently in mode 3. Reactor level is being maintained with RCIC and pressure is being maintained using the safety relief valves. The manual reactor protection system (RPS) actuation is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B) and the RCIC actuation is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A). The NRC Senior Resident Inspector was notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: At the time of the notification, main steam isolation valves had shut on low vacuum.
The following update was provided by the licensee via phone and email: This update is being made to report the following occurrences which took place after the scram reported in event number 57418. On November 10, 2024, at 0545 CST, a group 1 containment isolation signal resulted in the closure of all MSIVs. The signal was due to continued degradation of condenser vacuum post-trip. At 0620, an automatic RPS actuation occurred when reactor water level lowered to level 3. This RPS actuation occurred with all control rods fully inserted. Reactor water level lowered following closure of an open safety relief valve and was recovered to within the established band. The events are being reported as specified system actuations in accordance with 10 CFR 50.72(b)(3)(iv)(A). The NRC Senior Resident Inspector has been informed of the update. Notified R4DO (Dixon) |
ENS 57407 | 29 October 2024 18:07:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via phone and email: At 1730 (EDT), on 10/29/2024, Vistra authorized a report to the State of Ohio in accordance with NEI 07-07, 'Industry Groundwater Protection Initiative,' of a liquid spill to the plant's outdoor ground from an outdoor cask holding radioactive waste. This spill contained radionuclides cobalt-60 and manganese-54 with activities greater than the site procedural limits for state reporting. The outdoor cask has been removed from the onsite storage area; remediation and causal investigation activities are being performed. This exceedance did not exceed any NRC regulations or reporting criteria. There was no impact on the health and safety of the public or plant personnel. This notification is being made solely as a four-hour, non-emergency notification for a Notification of Other Government Agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: No EPA limits were exceeded |
ENS 57406 | 29 October 2024 17:32:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via phone and email: At 1152 EDT, on 10/29/2024, the division 3 diesel generator was declared inoperable due to variations in steady state voltage during a planned monthly surveillance run. Troubleshooting of the issue is in progress. This condition could prevent the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). All other emergency core cooling systems were operable during this time. There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Limiting condition for operations (LCO) 3.8.1.b was entered as a result of this event. |
ENS 57397 | 23 October 2024 16:24:00 | River Bend | NRC Region 4 | GE-6 | The following information was provided by the licensee via phone and email: A non-licensed contract supervisor violated the station's fitness-for-duty program. The employee's access to the plant has been terminated. |
ENS 57349 | 28 September 2024 00:35:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via phone and email: At 1822 CST on September 27, 2024, Grand Gulf Nuclear Station (GGNS) was conducting surveillance testing on the high pressure core spray (HPCS) division Ill diesel generator. Following initiation of the test signal, the HPCS pump room cooler start time exceeded the surveillance procedure allowance of less than or equal to 20 seconds. The HPCS pump room cooler started in 26.2 seconds. HPCS was already inoperable for performance of the surveillance testing. The event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition which could have prevented the fulfillment of a safety function. Troubleshooting is in progress. HPCS, a single-train system, will remain inoperable until the condition is corrected. All sources of offsite power are available. No other safety systems are inoperable. Reactor core isolation cooling was verified to be operable per GGNS technical specification 3.5.1.B.1. The NRC Senior Resident Inspector has been notified.
Investigation of the delayed start time of the HPCS pump room cooler indicated that the condition would not have challenged the ability of the room cooler to maintain temperatures less than the temperature limit of 150 degrees Fahrenheit. As a result, HPCS remained capable of fulfilling its safety function. Therefore, EN 57349 is being retracted. The NRC senior resident inspector has been notified of this retraction. Notified R4DO (O'Keefe) |
ENS 57338 | 25 September 2024 02:06:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via phone or email: On September 24, 2024, at 2204 CDT, Grand Gulf Nuclear Station (GGNS) was conducting surveillance testing on the high pressure core spray (HPCS) division III diesel generator. During testing, the HPCS pump breaker unexpectedly tripped after the HPCS diesel generator started and powered the safety bus. The breaker performed its motor protection function and tripped due to an over-frequency indication. The event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition which could have prevented the fulfillment of a safety function. Troubleshooting is in progress. HPCS, a single-train system, will remain inoperable until the condition is corrected. All sources of offsite power are available. No other safety systems are inoperable. Reactor core isolation cooling was verified to be operable per GGNS Technical Specification 3.5.1.B.1. The NRC Senior Resident has been notified. |
ENS 57252 | 30 July 2024 15:10:00 | River Bend | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: At 0146 CDT on June 7, 2024, River Bend Station (RBS) was operating at 100 percent power when a loss of control room envelope (CRE) was declared due to failing to meet Technical Specification (TS) 3.7.2, Surveillance Requirement (SR) 3.7.2.4, during surveillance testing. Mitigating actions were established which included the ability to issue potassium iodide to control room staff. With mitigating actions in place, the dose consequence to control room staff continued to be less than the regulatory limit of 5 rem total effective dose equivalent for the duration of a design basis event. The CRE is considered a single train system at RBS, therefore, this event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfillment of a safety function. The NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The failed surveillance (SR 3.7.2.4) was for unfiltered air in-leakage greater than 300 cubic feet per minute.
This event was initially reported under 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfillment of a safety function. The licensee determined in a subsequent engineering evaluation of the conditions that existed at the time, that there was no adverse impact on the control room emergency ventilation system or the control room envelope (CRE) boundary's ability to perform its safety function. The CRE would not have been challenged to meet the regulatory limit of 5 rem total effective dose equivalent for the duration of a design basis event. Consequently, this condition is not reportable as an event or condition that could have prevented the fulfillment of a safety function. The NRC resident inspector has been notified. Notified R4DO (Vossmar). |
ENS 57238 | 24 July 2024 13:22:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via phone and email: At 1046 EDT on 7/24/2024, fourteen Ashtabula County emergency response sirens were inadvertently activated during system maintenance. Ashtabula County Emergency Management Agency was contacted and made aware of the situation. This notification is being made solely as a four-hour, non-emergency notification for a notification of other government agencies in accordance with 10 CFR 50.72(b)(2)(xi). There was no impact to the health and safety of the public or plant personnel. The NRC resident inspector has been notified of the issue. |
ENS 57206 | 2 July 2024 10:08:00 | River Bend | NRC Region 4 | GE-6 | The following information was provided by the licensee via phone and email: At 1928 CDT on May 13, 2024, River Bend Station (RBS) was operating in Mode 1 at 100 percent power when an invalid isolation signal actuated multiple containment isolation valves in more than one system. The invalid isolation signal was caused by voltage perturbations on the offsite power distribution system due to multiple lightning strikes in the vicinity of RBS. The event caused one containment isolation valve to isolate in the floor and equipment drains system, and two containment isolation dampers to isolate in the auxiliary building ventilation system. This event was a partial system isolation for the affected systems and did not result in a full train actuation. This event meets the reportable criteria for 10 CFR 50.73(a)(2)(iv)(A) and is being reported as any event or condition that resulted in manual or automatic actuation of any systems listed in paragraph (a)(2)(iv)(B). This notification is being provided in lieu of a Licensee Event Report as indicated in 10 CFR 50.73(a)(1). The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The valve and dampers were immediately re-opened. The standby gas treatment system automatically initiated due to the closure of the containment isolation dampers in the auxiliary building ventilation system. |
ENS 57181 | 19 June 2024 15:07:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via phone and email: At 1640 EDT on 06/18/2024, the division 3 diesel generator was declared inoperable. This condition could prevent the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). All other emergency core cooling systems were operable during this time. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The division 3 diesel generator was declared inoperable due to potential water intrusion into the electrical generator. Inspection of the generator is in progress. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: This event resulted in Perry Unit 1 entering a 72 hour limiting condition for operation (LCO) in accordance with Technical Specification 3.8.1. condition 'B'.
Investigation and assessment of the division 3 diesel generator exciter and generator as-found condition revealed that no water intrusion occurred and, therefore, would not have impacted the diesel generator's ability to start, run, and produce the required electrical power to perform its required safety function. Therefore, EN 57181 is being retracted. The NRC resident inspector has been notified of the Event Notification retraction. Notified R3DO (Feliz-Adorno) |
ENS 57139 | 23 May 2024 11:24:00 | River Bend | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: During a security inspection, it was determined that some past events at Entergy sites that were not reported may have met the reporting criterion of 10 CFR 26.719(b)(4). As a result, the following events at River Bend Station, Unit 1 are now being conservatively reported: On March 21, 2023, a condition report was written to document that an individual who should have been placed in a follow-up fitness for duty (FFD) program was not tested according to this program. On May 11, 2023, a subsequent condition report was written to document that a different individual who should have been placed in a follow-up FFD program was not tested according to this program. The resident inspector has been notified. |
ENS 57138 | 23 May 2024 11:24:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: During a security inspection, it was determined that some past events at Entergy sites that were not reported may have met the reporting criterion of 10 CFR 26.719(b)(4). As a result, the following event at Grand Gulf, Unit 1 is now being conservatively reported: On May 11, 2023, a condition report was written to document that an individual who should have been placed in a follow-up fitness for duty program was not tested according to this program. The resident inspector has been notified. |
ENS 57136 | 23 May 2024 04:25:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via email: At 0400 EDT on May 23, 2024, a technical specification required shutdown was initiated at Perry. Technical specification action 3.4.5 condition B (unidentified reactor coolant system leakage exceeds 5 gallons per minute) was entered on May 23, 2024 at 0000 with a required action to reduce leakage to within limits within 4 hours, due by 0400 on May 23, 2024. This required action was not completed within the completion time, therefore, a technical specification required shutdown was initiated, and this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The reactor coolant leakage was stable at approximately 6 gallons per minute. |
ENS 57130 | 16 May 2024 20:53:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via email: On May 16, 2024 at 0840 EDT, operations declared the reactor water cleanup (RWCU) leak detection instruments related to the high differential flow signal inoperable. Technical specification (TS) 3.3.6.1, primary containment and drywell isolation instrumentation, conditions `A and `B were entered as one required channel of instrumentation was inoperable, and an automatic function with isolation capability was not maintained. Therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72(b)(3)(v)(D). All other RWCU primary containment isolation instrumentation functions remained operable. At 1210 EDT, the affected leak detection instruments were declared operable, and the TS limiting condition for operation 3.3.6.1 was declared met. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 57092 | 25 April 2024 20:24:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via phone and email: On April 25, 2024, it was determined that between March 25, 2024, 2015 (EDT) and March 30, 2024, 2024 (EDT), the condensate transfer and storage system was employed as a method of alternate keepfill in place of the installed residual heat removal (RHR) systems waterleg pump for RHR system loops `B and `C. This condition is not bounded by existing design and licensing documents. Therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 57050 | 25 March 2024 17:38:00 | Clinton | NRC Region 3 | GE-6 | The following information was provided by the licensee via email and phone call: At 1027 CDT on 3/25/24, it was determined that a contract supervisor tested positive in accordance with the fitness for duty testing program. The individuals authorization for site access has been terminated. The NRC Resident Inspector has been notified. |
ENS 56938 | 29 January 2024 16:56:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: At 1005 CST on January 29, 2024, Grand Gulf Nuclear Station was conducting surveillance testing on the high pressure core spray system. During testing, the 1E22F012 minimum flow valve failed to return to the full closed position. The valve went from full open indication to dual indication. The event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition which could have prevented the fulfillment of a safety function. Troubleshooting is in progress. The NRC Senior Resident has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: All off-site power is available. No other systems are out of service and there are no compensatory measures taken. There is no increase to plant risk. |
ENS 56914 | 5 January 2024 15:56:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via phone and email: At 1552 (EST) on 01/05/2024, Perry Nuclear Power Plant reported elevated levels of tritium in the underdrain system to the state of Ohio as a non-voluntary reporting of tritium. An investigation is currently ongoing to identify the cause of the elevated tritium levels. The tritium levels in this location do not exceed any NRC regulations or reporting criteria. This notification is being made solely as a four-hour, non-emergency notification for a notification of other government agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56894 | 16 December 2023 08:22:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: On December 16, 2023, at 0350 CST, Grand Gulf Nuclear Station was operating in mode 1 at 81 percent power when an automatic scram occurred due to a turbine trip signal. Before the scram the unit was performing a rod sequence exchange, and no critical work was underway. The cause of the turbine trip signal is not known at this time and is being investigated. All control rods fully inserted, there were no complications, and all plant systems responded as designed. Reactor water level is being maintained by main feedwater and condensate. Reactor pressure is being maintained with main turbine bypass valves. No radiological releases have occurred due to this event. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A), as any event or condition that results in actuation of the reactor protection system when the reactor is critical and specified system actuation due to expected reactor water level 3 isolation signals on a reactor scram. The NRC Senior Resident Inspector has been notified of this event. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Group 2 and Group 3 isolations occurred on the Level 3 isolation signal. |
ENS 56887 | 13 December 2023 05:50:00 | River Bend | NRC Region 4 | GE-6 | The following information was provided by the licensee via phone and email: At 0102 CST, while operating at 100 percent (reactor) power, River Bend Station experienced an automatic reactor scram caused by a turbine trip signal. The cause of the turbine trip signal is not known at this time and is being investigated. At 0108, reactor core isolation cooling (RCIC) was initiated due to a loss of reactor feed pumps following feedwater heater string isolation. At 0114, reactor water level control was transferred back to feedwater and RCIC was secured. Reactor water level is being maintained by feedwater pumps and reactor pressure is being maintained by turbine bypass valves. The scram was uncomplicated and all other plant systems responded as designed. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B), as any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical and 10 CFR 50.72(b)(3)(iv)(A) specified system actuation as result of expected post scram (reactor water) level 3 isolations and manual initiation of RCIC. No radiological releases have occurred due to this event from the unit. The NRC Senior Resident Inspector has been notified of this event. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the turbine trip, while still under investigation, was likely due to an electrical transient involving the main generator. Walkdowns in the switchyard post-scram identified damage to one of the output breaker disconnects. |
ENS 56863 | 18 November 2023 02:51:00 | River Bend | NRC Region 4 | GE-6 | The following information was provided by the licensee via phone and email: On November 17, 2023, at 2215 CST, River Bend Station (RBS) was operating at 30 percent reactor power performing plant startup activities when an isolation of low-pressure feedwater string `A' occurred. The team entered applicable alternate operating procedures and inserted control rods to exit the restricted region of the power to flow map. Feedwater temperature continued to lower until it challenged the prohibited region of the AOP-0007 graph requiring a reactor scram. The team inserted a manual reactor scram at 2355 from 24 percent reactor power. All control rods fully inserted and there were no complications. All systems responded as designed. Currently RBS Unit 1 is stable with reactor level being maintained 10 to 51 inches with feed and condensate, and pressure being maintained 500 to 1090 psig using steam drains. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B), as any event or condition that results in actuation of the Reactor Protection System (RPS) when the reactor is critical and 10 CFR 50.72(b)(3)(iv)(A) Specified System Actuation as result of Group 3 isolations. The NRC Senior Resident inspector has been notified. No radiological releases have occurred due to this event from the unit. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The electric plant is in a normal lineup for current plant conditions with all emergency diesel generators available. The cause of the initial isolation of low-pressure feedwater string "A" is still under investigation. |
ENS 56825 | 31 October 2023 14:20:00 | River Bend | NRC Region 4 | GE-6 | The following information was provided by the licensee via phone call and email: On October 31, 2023, at 0800 CDT, River Bend Station discovered that the results of a blind performance sample provided to an Health and Human Services (HHS)-certified testing facility were inaccurate (false negative). This report is being made in accordance with 10 CFR 26.719(c)(3). The HHS-certified testing facility has been informed of the error. The licensee notified the NRC resident inspector.
On November 1, 2023, River Bend Station personnel were informed by the HHS-certified testing facility that the cut-off levels used for analysis of the performance testing sample in question were the correct (higher) cut-off levels currently being used by the licensee. This resulted in a correct negative test. The performance testing sample sent to the HHS-certified testing facility was purchased for use based on the new lower cut-off levels in accordance with the new fit for duty (FFD) rule being implemented by the licensee on November 6, 2023. Because the higher confirmatory cut-off levels were used at the HHS-certified testing facility, the results provided were correct. The NRC Resident Inspector has been notified." Notified R1DO (Eve) and FFD Group (email) |
ENS 56745 | 18 September 2023 23:26:00 | Clinton | NRC Region 3 | GE-6 | The following information was provided by the licensee via email: On 9/18/2023 at 2007 CDT, Clinton reported to the Illinois Emergency Management Agency, National Response Center and DeWitt County a hazardous substance release of 1300 gallons of Sodium Bisulphite. The release was at the site's flume discharge building due to a crack on a fitting inside the building. This release did not exceed any NRC regulations or reporting criteria. This notification is being made solely as a four-hour, non-emergency notification for a Notification of Other Government Agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56724 | 7 September 2023 10:01:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: On September 6 at 15:00 CDT, Grand Gulf Nuclear Station personnel identified a bottle of vanilla extract in a kitchen area located within the Protected Area. Ingredients were listed as 'pure vanilla extract in water and alcohol. The percentage by volume of alcohol was not specified. It was subsequently determined that the alcohol by volume was likely 35 percent. The NRC Resident Inspector has been notified. |
ENS 56696 | 24 August 2023 21:30:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: On August 23, 2023 at 2100 CDT, Grand Gulf Nuclear Station was notified that a non-licensed supervisor violated the station's Fitness for Duty policy. The employee's unescorted access at Grand Gulf Nuclear Station has been terminated. This event was determined to be reportable under 10 CFR 26.719(b)(2)(ii). The NRC Resident Inspector has been notified. |
ENS 56673 | 10 August 2023 04:03:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via email: At 0039 (EDT) on 8/10/23, with Unit 1 in Mode 1 at 100 percent power, the reactor automatically tripped during a reactor protection system (RPS) bus shift. All systems responding normally post-trip. There was no equipment inoperable at the time of the trip. Operations responded and stabilized the plant. Reactor water level being maintained via feedwater. Decay heat is being removed by cycling safety relief valves. An actuation of high-pressure core spray, division 3 diesel generator, and reactor core isolation cooling occurred during the scram and main steam line isolation closure. The reason for the auto-start was reaching Level 2 (130 inches in the reactor pressure vessel) during the transient. The systems automatically started as designed and injected to the reactor vessel when the Level 2 signal was received. The RPS actuation is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The emergency core cooling system (ECCS) injection is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A). The ECCS actuation is being reported as a eight-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56641 | 26 July 2023 09:10:00 | River Bend | NRC Region 4 | GE-6 | The following information is a synopsis provided by the licensee via email: River Bend Station completed an internal Part 21 evaluation concerning a motor driven relay that failed pre-installation testing due to a buildup of corrosion between the rotor and relay core. The relay was planned for use in the Remote Shutdown System. The NRC Resident has been notified. A written notification will be provided within 30 days. Affected known plants include only River Bend at the time of the notification. |
ENS 56598 | 29 June 2023 15:41:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: A non-licensed supervisor had a confirmed positive for alcohol during a random fitness-for-duty test. The employee's access to the plant has been terminated. The NRC Resident Inspector has been notified. |
ENS 56588 | 23 June 2023 17:04:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via email: At 1521 EDT on 6/23/2023, Perry Nuclear Power Plant reported elevated levels of tritium in the underdrain system to the State of Ohio as a non-voluntary reporting of tritium. An investigation is currently ongoing to identify the cause of the elevated tritium levels. The tritium levels did not exceed any NRC regulations or reporting criteria. Tritium has not been detected in any other locations and is not expected to impact groundwater or exceed any limits in the Off Site Dose Calculation Manual (ODCM). This notification is being made solely as a four-hour, non-emergency notification for a Notification of Other Government Agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The following agencies were notified by licensee: Lake County Emergency Management Agency (EMA) Ashtabula County EMA Geauga County Department of Emergency Services Ohio EMA Radiological Branch |
ENS 56491 | 26 April 2023 16:30:00 | River Bend | NRC Region 4 | GE-6 | A non-licensed supervisor had a confirmed positive for alcohol during a random fitness-for-duty test. The employee's access to the plant has been terminated. The NRC Resident Inspector has been notified. |
ENS 56455 | 6 April 2023 16:46:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via phone and email: On March 4, 2023, it was determined that the main steam line (MSL) local leak rate test results for MSL 'B' were in exceedance of technical specification (TS) surveillance requirement (SR) 3.6.1.3.10 limits. Additionally, the leakage at the outboard main steam isolation valve (MSIV) 'B', was indeterminate due to a gross packing gland leak. An engineering calculation dated April 6, 2023, showed that this leakage, in conjunction with a design basis loss of coolant accident, would result in the radiological dose exceeding Updated Safety Analysis Report limits to the exclusion area boundary, the low population zone, and the control room. Therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B) as a condition that results in the power plant being in an unanalyzed condition that degrades plant safety. Both inboard and outboard 'B' MSIVs have been reworked and are within the TS SR limits. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56428 | 23 March 2023 16:46:00 | River Bend | NRC Region 4 | GE-6 | A non-licensed contract supervisor was confirmed to have violated the FFD policy by attempting to subvert the testing process. The individual's authorization for site access was immediately terminated. The licensee notified the R4 Branch Chief (Josey)
The following information was provided by the licensee via email: The Medical Review Officer (MRO) was provided with additional information on the collection process in question. Based on this additional information, the MRO was unable to conclude with a high degree of certainty that an attempt to subvert the FFD collection process had occurred." Notified R4DO (Gaddy) and via email the FFD Group. |
ENS 56417 | 17 March 2023 10:15:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via email: On March 16, 2023, at 2226 EDT, a site supervisor had a confirmed positive for alcohol during a random fitness-for-duty test. The employee's authorization for access to the plant has been terminated. The Resident Inspector has been notified. |
ENS 56390 | 5 March 2023 03:02:00 | River Bend | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: At 2300 CST on March 4, 2023, River Bend Station (RBS) was shut down in Mode 5 when an individual was transported offsite for treatment at an offsite medical facility. Due to the nature of the medical condition, the individual was not thoroughly surveyed prior to being transported offsite. Follow-up surveys performed by radiation protection technicians identified no contamination of the worker or of the ambulance and response personnel. This is an eight-hour notification, non-emergency for the transportation of a contaminated person offsite. This event is reportable in accordance with 10 CFR 50.72(b)(3)(xii). The NRC Resident Inspector has been notified. |
ENS 56356 | 6 February 2023 13:26:00 | Clinton | NRC Region 3 | GE-6 | The following information was provided by Constellation via email: On 02/06/2023 at 0416 EST, the Constellation Emergency Response Organization (ERO) Notification Database System uploaded data files into the Mass Notification System (Everbridge) which is used to notify ERO personnel when activated. At 0630, the individual reviewing the uploaded files discovered that the data files did not upload properly and that Everbridge may not notify all ERO individuals within the required 10 minutes of system initiation. Constellation resolved the issue by 0752. During the time period of 0416 to 0752, control room operators would have been unaware that the ERO notification was not successful. Therefore, this issue constitutes a loss of offsite communications capability and is reportable under 10 CFR 50.72(b)(3)(xiii), 'The licensee shall notify the NRC as soon as practical and in all cases within eight hours of the occurrence of any event that results in a major loss of emergency assessment capability, offsite response capability, or offsite communications capability (e.g., significant portion of control room indication, Emergency Notification System, or offsite notification system).' This loss of offsite communications capability affected all Constellation nuclear stations. There was no impact on the health and safety of the public or plant personnel. Each affected station NRC Resident Inspectors have been or will be notified. |
ENS 56328 | 1 February 2023 01:40:00 | Clinton | NRC Region 3 | GE-6 | The following information was provided by the licensee via fax and telephone: Generator trip due to power load unbalance which caused a turbine trip and subsequent reactor scram. Experienced a trip on circulating water pump A. NRC Resident Inspector notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Off-site power available and unaffected. Decay heat removal via main steam line and drains to condenser. Plant is stable in mode 3. |
ENS 56298 | 5 January 2023 15:39:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via phone and email: At 1242 (EST) on 05 January 2023, with the Unit in Mode 1 at 99 percent power, the reactor automatically tripped on low Reactor Pressure Vessel level while restoring power to Digital Feedwater Control Stations when there was a perturbation to the level controls. The reason for perturbation is unknown at this time. The trip was not complex, with all systems responding normally post trip. Operations responded and stabilized the plant. High pressure core spray was manually initiated in accordance with site procedures. Reactor water level is being maintained via the Feedwater System. Decay heat is being removed by the Main Condenser. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(A) and 10 CFR 50.72(b)(2)(iv)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56282 | 20 December 2022 00:24:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: At 2101 (CST) on December 19, 2022, a manual reactor scram was initiated at Grand Gulf Nuclear Station (GGNS). Following the reactor scram, the high pressure core spray (HPCS) system was used to maintain reactor water level. The manual (reactor protection system) RPS actuation is being reported in accordance with 10 CFR 50.72(b)(2) and the HPCS actuation is being reported in accordance with 10 CFR 50.72(b)(3). At 2058, GGNS experienced a loss of a condensate booster pump. At 2101, the `A' reactor feedwater pump tripped and the reactor was manually scrammed. All control rods were fully inserted into the core. At 2104, the `B' reactor feedwater pump tripped and HPCS was manually started. HPCS was manually injected to maintain reactor water level at 2121. The `A' reactor feedwater pump was successfully restarted at 2126. GGNS is currently in Mode 3. Reactor level is being maintained with the `A' reactor feedwater pump and pressure is being maintained with the turbine bypass valves. The NRC Resident Inspector was notified. |
ENS 56185 | 27 October 2022 19:49:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: At 1228 CDT on October 27, 2022, Grand Gulf Nuclear Station (GGNS) was in Mode 1 at 88 percent power when a failure of a draw down surveillance resulted in the loss of secondary containment. During the performance of the surveillance GGNS was unable to maintain secondary containment pressure, as required by Technical Specification Surveillance Requirement 3.6.4.1.4, greater than or equal to 0.266 inches of water vacuum for 1 hour at a flow rate of less than or equal to 4000 cfm. The test was secured. Secondary containment was declared inoperable and Technical Specification 3.6.4.1 A.1 was entered at 1228 CDT. Secondary containment was restored to operable status at 1240 CDT by restoring the configuration to a previously known operable condition. This event is being reported as an event or condition that could have prevented the fulfillment of a safety function. The NRC Resident Inspector was notified. |
ENS 56171 | 20 October 2022 11:31:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: At 0427 CDT on October 20, 2022, Grand Gulf Nuclear Station (GGNS) was in Mode 1 at 100 percent power when a failure of a draw down surveillance resulted in the loss of secondary containment. During the performance of the surveillance GGNS was unable to maintain secondary containment pressure, as required by Technical Specification Surveillance Requirement 3.6.4.1.4, greater than or equal to 0.266 inches of water vacuum for 1 hour at a flow rate of less than or equal to 4000cfm. The test was secured. Secondary containment was declared inoperable and Technical Specification 3.6.4.1 A.1 was entered at 0427 CDT. Secondary containment was restored to operable status at 0520 CDT by restoring the configuration to a previously known operable condition. This event is being reported as an event or condition that could have prevented the fulfillment of a safety function. The NRC Resident Inspector was notified. |
ENS 56118 | 19 September 2022 19:29:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: At approximately 1520 CDT on September 19, 2022, Grand Gulf Nuclear Station (GGNS) requested transport for treatment of a non-responsive individual, a contract employee, to an offsite medical facility. The offsite medical facility notified GGNS at approximately 1630 CDT that the individual had been declared deceased. The fatality was not work-related, and the individual was outside of the Radiological Control Area. This is a four-hour non-emergency notification in accordance with 10 CFR 50.72(b)(2)(xi) related to the notification of a government agency. The contractor's employee will be notifying the Occupational Safety and Health Administration. The NRC Senior Resident Inspector has been notified. |
ENS 56116 | 19 September 2022 08:37:00 | River Bend | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: At 0132 CDT on September 19, 2022, River Bend Station (RBS) was operating at 100% power when the high pressure core spray (HPCS) system was declared inoperable in accordance with technical specification 3.8.9, condition E (declare HPCS and standby service water system pump 2C inoperable immediately) due to a E22-S003, HPCS transformer feeder malfunction. The HPCS is a single train system at RBS, therefore this event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfilment of a safety function. The reactor core isolation cooling system has been verified to be operable. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: RBS has entered a 14-day limiting condition for operation due to the loss of HPCS and they have upgraded their on-line plant risk model to "yellow". |
ENS 56059 | 20 August 2022 02:11:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via fax or email: At 2342 CDT on August 19, 2022, with Grand Gulf Nuclear Station in Mode 1 and at 40 percent power, the station initiated a normal shutdown to comply with its Technical Specifications (TS). The station entered Mode 3 at 0000 CDT August 20, 2022 to comply with (LCO) 3.5.1 Condition G Action G.1 due to the condition reported to NRC previously (EN 56058). This event is being reported under 10 CFR 50.72(b)(2)(i) as a shutdown required by the plant's technical specifications. The NRC Senior Resident Inspector was notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The plant is now in a 36-hour LCO to be in Mode 4 due to Low Low Set Valves inoperability per TS 3.6.1.6.
Grand Gulf Nuclear Station (GGNS) is performing this notification to retract event EN 56059 that was reported on August 20, 2022. Previously, GGNS notified the NRC that it had initiated a shutdown required by Technical Specifications to comply with Limiting Condition of Operation (LCO) 3.5.1 Condition G.1 due to the inoperability of four Automatic Depressurization System (ADS) valves. Following the shutdown, GGNS completed walkdowns and determined that the condition affected only one ADS valve. As a result, the shutdown to satisfy the required actions of TS LCO 3.5.1 Condition G.1 was not required. The NRC Resident Inspector has been notified of the retraction. R4DO (Kellar) was notified. |
ENS 56058 | 19 August 2022 20:46:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via email: At 1215 CDT on 8/19/2022, with Grand Gulf Nuclear Station in Mode 1 and at 100 percent power, four Automatic Depressurization System (ADS) valves were rendered inoperable due to a loss of system pressure. The station entered Technical Specification 3.5.1 Condition G. This event is being reported under 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfillment of a safety function. There were no other systems affected as a result of this condition. The NRC Senior Resident Inspector was notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Plans are to remain in Mode 1 until corrected or until driven by the Technical Specifications to shut down (12-hour LCO from 1215 CDT on 8/19/2022).
Grand Gulf Nuclear Station (GGNS) is performing this notification to retract event EN 56058 that was reported on August 19, 2022. Previously, GGNS notified the NRC that four Automatic Depressurization System (ADS) valves were inoperable due to a loss of system pressure. Based upon further investigation, the condition reported in EN 56058 was found to affect only a single ADS valve. As a result, it was determined that an event or condition that could have prevented the fulfillment of a safety function did not exist at GGNS. Sufficient redundancy existed to perform the safety function. The NRC Resident Inspector has been notified of the retraction. R4DO (Kellar) was notified. |
ENS 55973 | 30 June 2022 18:07:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via phone and email: At 1445 (CDT) on June 30, 2022, with Grand Gulf Nuclear Station in Mode 1 and at 100 percent power, the reactor was manually scrammed due to the loss of balance of plant (BOP) transformer 23. All control rods fully inserted into the core and all systems responded appropriately. Reactor level is being maintained with condensate and feedwater. Reactor pressure is being maintained with turbine bypass valves. The cause of the loss of BOP transformer 23 is under investigation at this time. Standby Service Water 'A' and 'B' were manually initiated to supply cooling to Control Room A/C, ESF switchgear room coolers, and plant auxiliary loads. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B) as an event or condition that resulted in actuation of the Reactor Protection System and 10 CFR 50.72(b)(3)(iv)(A) due to the actuation of Standby Service Water. The NRC Senior Resident Inspector was notified. |
ENS 55962 | 24 June 2022 16:28:00 | Perry | NRC Region 3 | GE-6 | The following information was provided by the licensee via telephone: At 1257 EDT on June 24, 2022, it was discovered the Low Pressure Core Spray System (LPCS) was INOPERABLE. At Perry, the Low Pressure Core Spray System is considered a single train system in Modes 1, 2, and 3; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). Inoperability of the Low Pressure Core Spray system was caused by a loss of power to the LPCS Minimum Flow Valve during surveillance activities. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 55915 | 26 May 2022 10:34:00 | Grand Gulf | NRC Region 4 | GE-6 | The following information was provided by the licensee via phone and email: On May 26, 2022, at 0753 CDT, the Grand Gulf Nuclear Station was notified of a spurious actuation of a single Alert Notification System siren in Tensas Parish, Louisiana. The actuation occurred during siren testing conducted at approximately 0630 CDT - no emergency conditions are present at Grand Gulf Nuclear Station. A press release from Entergy is not planned at this time. This condition is reportable under 10 CFR 50.72(b)(2)(xi) as a notification of an offsite government agency. The NRC Senior Resident Inspector has been notified. |
ENS 55561 | 4 November 2021 09:12:00 | Grand Gulf | NRC Region 4 | GE-6 | A non-licensed employee had a confirmed positive for alcohol during a random fitness-for-duty test. The employee's access to the plant has been terminated. The NRC Resident Inspector has been notified. |
ENS 55451 | 9 September 2021 04:19:00 | Grand Gulf | NRC Region 4 | GE-6 | At 0033 CDT on September 9, 2021, Grand Gulf Nuclear Station (GGNS) was operating at 70 percent power when the High Pressure Core Spray (HPCS) was declared inoperable. The inoperability determination was made due to control room annunciations. In accordance with GGNS Technical Specification 3.5.1.B.1, the Reactor Core Isolation Cooling system was verified to be operable. Troubleshooting is in progress. This event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition which could have prevented the fulfillment of a safety function. The NRC Resident Inspector has been notified. |