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 Event dateRegionStateSiteReactor typeEvent description
ENS 5819010 March 2026 18:34:00NRC Region 4ArizonaPalo VerdeCEThe following information was provided by the licensee via phone and email: On March 10, 2026, at 1134 MST, a reactor operator's test results were confirmed positive for alcohol following a for-cause, fitness for duty screening test. The individual's unescorted access has been immediately placed on administrative hold until the denial process has been completed per station procedures. The NRC Resident Inspector has been notified.
ENS 5816312 February 2026 10:49:00NRC Region 4WashingtonColumbiaGE-5The following information was provided by the licensee via phone and email: At 0249 PST, on February 12, 2026, with the unit in Mode 1 at 100 percent power, the reactor was manually tripped due to a loss of both reactor recirculation pumps because of abnormal pump drive parameters. Following reset of the reactor trip signal, operators observed erratic automatic operation of the reactor feed pumps with an associated reactor water level transient to less than plus 13 inches resulting in an additional reactor trip signal. Operators took manual control of the reactor feed pumps and recovered reactor water level, stabilizing water level at above plus 13 inches. The reactor trip signal was reset, and reactor water level was raised to support natural circulation flow of the reactor. Decay heat is being removed via natural circulation in the reactor with steam to the main condenser. Due to the valid reactor protection system actuations, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i), four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B), and eight-hour, non-emergency notification, per 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 581484 February 2026 05:38:00NRC Region 4LouisianaRiver BendGE-6

The following information was provided by the licensee via phone and email: On February 3, 2026, at 2338 CST, River Bend Station (RBS) was operating at 100 percent reactor power when the standby service water pump `C' (SWP-P2C) faulted, tripped, and locked out during the performance of a routine surveillance. The pump fault caused E22-ACB04, the normal division III 4.16 KV bus supply breaker, to trip and lock out. The division Ill emergency diesel generator (EDG) started as designed and powered the division III 4.16 KV bus. There are no signs of fire. The cause of the SWP-P2C fault is still under investigation. The trip of E22-ACB04 resulted in the inability to meet (surveillance requirement) SR 3.8.9.1 forcing entry into (limiting condition for operation) LCO 3.8.9 required action 'E.1' and declaring the (high pressure core spray) HPCS system inoperable. This event is being reported under 10 CFR 50.72(b)(3)(iv)(A) as an event or condition that results in valid actuation of emergency AC electrical power systems and 10 CFR 50.72(b)(3)(v)(D) as an event or condition that at the time of discovery could have prevented the fulfillment of a safety function. The NRC Resident Inspector has been notified.

  • * * PARTIAL RETRACTION ON 02/12/2026 AT 1946 EST FROM TERRY BLANCHARD TO ADAM KOZIOL * * *

This event was initially reported under 10 CFR 50.72(b)(3)(iv)(A) as an event or condition that results in a valid actuation of emergency AC electrical power systems and 10 CFR 50.72(b)(3)(v) as an event or condition that at the time of discovery could have prevented the fulfillment of a safety function. During subsequent investigation, it was determined that the trip of E22-ACB04 did not result in the inability to meet SR 3.8.9.1 which forced entry into LCO 3.8.9 required action 'E.1'. As a result, it has been determined that the HPCS system remained operable. Therefore, this condition is not reportable as an event or condition that at the time of discovery could have prevented the fulfillment of a safety function. However, this event remains reportable as an event or condition that results in a valid actuation of emergency AC electrical power systems. The NRC Resident Inspector has been notified. Notified R4DO (Dodson)

ENS 581422 February 2026 02:09:00NRC Region 4MississippiGrand GulfGE-6The following information was provided by the licensee via phone and email: At 2009 CST on February 1, 2026, Grand Gulf Nuclear Sation (GGNS) was conducting surveillance testing on the high-pressure core spray (HPCS) division III diesel generator. Following the start of the HPCS division III diesel generator, the HPCS standby service water (SSW) pump immediately tripped. As a result, HPCS SSW and HPCS were declared inoperable. The cause of the HPCS SSW pump trip is being investigated. The event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition which could have prevented the fulfillment of a safety function. HPCS, a single-train safety system, will remain inoperable until the condition is corrected. All sources of offsite power are available. No other safety systems are inoperable. Reactor core isolation cooling (RCIC) was verified to be operable per GGNS technical specification 3.5.1.B.1. The NRC Resident has been notified.
ENS 5812927 January 2026 00:23:00NRC Region 4TexasComanche PeakWestinghouse PWR 4-Loop

The following information was provided by the licensee via phone: On January 26, 2026, at 1823 CST, a Notice of Unusual Event was declared on emergency action level HU1.1 due to a security event. The NRC Resident Inspector, the State of Texas, and local authorities have been notified. Notified DHS SWO, FEMA Operations Center, FEMA NWC, CISA Central Watch Officer, CWMD Watch Desk, DHS Nuclear SSA (email), DHS NRCC THD Desk (email).

  • * * UPDATE ON 01/26/2026 AT 2058 EST FROM MATT MAGER TO KERBY SCALES * * *

The following information provided by the licensee via phone: On January 26, 2026, at 1940 CST, the Unusual Event was terminated. The NRC Resident Inspector was notified. Notified R4RA (Monninger), NRR (Groom), NSIR (Williams), R4DO (Dixon), NRR EO (Mckenna), IR MOC (Grant), R4PAO (Smith). Notified DHS SWO, FEMA Operations Center, FEMA NWC, CISA Central Watch Officer, CWMD Watch Desk, DHS Nuclear SSA (email), DHS NRCC THD Desk (email).

ENS 5805421 November 2025 18:08:00NRC Region 4TexasSouth TexasWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: At 1208 CST on 11/21/2025, with Unit 2 in Mode 1 at 100 percent power, (the) Unit 2 reactor automatically tripped due to a main transformer lockout. The trip was not complex, with all systems responding normally post-trip. One of three essential chillers (chiller 22C) was inoperable at the time of (the) trip due to planned maintenance activities. All other engineered safety feature (ESF) equipment was operable at the time of the event. Operations responded and stabilized the plant. Decay heat is being removed by steam generator pressure operated relief valves (PORV). There was no impact to Unit 1. All control rods fully inserted. Primary pressurizer PORV '655A' opened twice to relieve pressure in response to (the) pressure transient. (South Texas Project Unit 2) entered Technical Specification 3.8.1.1.e due to a loss of two off-site power sources, `A' and `C' ESF busses. Upon main turbine trip, throttle valves closed as expected. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) due to valid actuation of two of the three emergency diesel generators. There was no impact on the health and safety of the public or plant personnel, and Unit 2 remains at normal operating temperature and normal operating pressure. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Emergency diesel generators '21' and '23' automatically started upon loss of power as expected. Auxiliary feedwater actuated post-trip as expected. Offsite power to ESF busses has been restored.
ENS 5805521 November 2025 14:35:00NRC Region 4LouisianaRiver BendGE-6The following information was provided by the licensee via phone and email: On November 21, 2025, at 0835 CST, River Bend Station (RBS) was operating at 78 percent reactor power when the (radioactive waste) shipping department received a cask from the Waste Control Specialists disposal facility in Andrews County, TX via (a common carrier). A smear sample was collected and exhibited surface contamination above the Department of Transportation (DOT) limits, specified in 49 CFR 173. The carrier was notified at 1713 CST. The surface contamination exceeded 24,000 (disintegrations per minute per centimeter squared) for beta gamma (activity). Supervision was immediately contacted and placed the shipment into a radiological controlled area. An investigation was performed to the extent of the condition of the loose surface contamination of the cask to determine if it was isolated to the immediately accessible areas of the cask due to an installed rain cover. The investigation concluded that the condition was extended to the surface of the cask where the average surface area exceeded DOT limits. This condition is immediately reportable to the NRC headquarters operations center per 10 CFR 20.1906(d)(1).
ENS 5810912 November 2025 13:48:00NRC Region 4MissouriCallawayWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: This report is being made in accordance with 10 CFR 50.73(a)(2)(iv)(A), using the telephone option in 10 CFR 50.73(a)(1) in lieu of a written licensee event report, concerning an event in which Callaway experienced an automatic actuation of the auxiliary feedwater (AFW) system in response to invalid AFW actuation signals. The reactor protection system was not involved. A low suction pressure signal was also received which aligned the AFW pumps to essential service water. An unknown amount of water from the ultimate heat sink entered the steam generators, necessitating a plant shutdown after secondary water chemistry program action levels were exceeded. This AFW actuation was complete and the AFW system started and functioned successfully in accordance with the initiating actuation signals. This actuation occurred at 0748 CST on November 12, 2025, and was reported (and later retracted) as event notification 58035. The most probable cause of the actuations was the intermittent failure of a 15V DC logic power supply within engineered safety features actuation system logic cabinet SA036D. The power supply was replaced.
ENS 5803512 November 2025 13:48:00NRC Region 4MissouriCallawayWestinghouse PWR 4-Loop

The following information was provided by the licensee via phone and email: At 0748 CST, on November 12, 2025, Callaway Plant experienced an automatic actuation of the auxiliary feedwater (AFW) system in response to auxiliary feedwater actuation signals (AFAS). A low suction pressure signal was also received which aligned the AFW pumps to essential service water (ESW). An unknown amount of water from the ultimate heat sink (UHS) entered the steam generators, necessitating a plant shutdown due to exceeding secondary water chemistry program action levels. During the shutdown, with the plant at approximately 28 percent power, high vibration was received on the main turbine, requiring a manual turbine trip. The cause of the AFAS is not yet known. The plant is currently stable in mode 3. This condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Decay heat is being removed via steam dump valves to the main condenser.

  • * * RETRACTION ON NOVEMBER 20, 2025, AT 1409 EST FROM ZACH MILLIGAN TO JORDAN WINGATE * * *

The following is a summary of the retraction provided by the licensee via phone and email. Event Notification 58035, made on November 12, 2025, pursuant to 10 CFR 50.72(b)(3)(iv)(A), is being retracted following a review of the cause of the auxiliary feedwater system's automatic actuation. The AFW system actuation was traced to a power supply malfunction, which also caused the auxiliary feedwater pumps to align with essential service water. Because the actuation resulted from a spurious power supply failure, rather than signals triggered by plant conditions or parameters meeting system initiation criteria, it is considered invalid and not reportable under 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident Inspector has been informed. Notified R4DO (Drake)

ENS 580265 November 2025 16:03:00NRC Region 4KansasWolf CreekWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: At 1003 Central Standard Time (CST), with (Unit 1) in mode 5 at 0 percent power, an actuation of the 'A' emergency diesel generator (EDG) occurred when energizing main transformers from the switchyard for post-installation soak. The energization was coordinated with transmission system operators using approved procedures, however, grid conditions external to the substation allowed the voltage to drop below the NB01 undervoltage relay setpoint. The EDG automatically started as designed and picked up the loads on the NB01 bus. All safety systems responded as designed. Substation parameters immediately recovered to normal values, and all systems were restored to (normal) standby conditions. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the 'A' EDG. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5800726 October 2025 05:40:00NRC Region 4LouisianaWaterfordCEThe following information was provided by the licensee via phone and email: On October 26, 2025, at 0040 CDT, the Waterford 3 Steam Electric Unit 3 operating crew declared the control room envelope inoperable in accordance with technical specification (TS) 3.7.6.1 due to the discovery of a hairline crack in the station air supply header in the passageway outside the control room. Operations entered TS 3.7.6.1 action b. TS 3.7.6.1 action b was complied with by closing manual valves SA-502 and SA-514, thus isolating the section of piping that developed the crack. The station air leak was isolated at time 0120. There was no impact on the health and safety of the plant or plant personnel. This event is reportable pursuant to 10 CFR 50.72(b)(3)(v)(D), event or condition that could have prevented fulfillment of a safety function of structures or systems that are needed to `(D) mitigate the consequences of an accident,' due to the control room envelope being inoperable. The licensee notified the NRC Resident Inspector.
ENS 5799421 October 2025 11:10:00NRC Region 4KansasWolf CreekWestinghouse PWR 4-LoopThe following is a summary of information provided by the licensee via phone and email: On October 21, 2025, at 0610 CDT, while reloading fuel to the reactor vessel, an electrical perturbation initiated a control room ventilation isolation signal (CRVIS). The control room air conditioning system (CRACS) 'A' train A/C unit did not start upon the CRVIS due to a blown fuse. The 'B' CRACS A/C unit was out of service for planned maintenance at the time. At 1020 CDT, the 'A' train CRACS A/C unit was returned to service. Both trains of the control room emergency ventilation system (CREVS) were inoperable for 10 minutes. Due to both trains of CRACS and CREVS being inoperable, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). This condition caused entry into technical specification (TS) limiting condition for operation (LCO) 3.7.10 condition `E' and 3.7.11 condition `D'. Upon discovery of the condition, fuel movement and core alterations were suspended in accordance with the TS LCO required actions. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector was notified.
ENS 5798615 October 2025 04:05:00NRC Region 4TexasSouth TexasWestinghouse PWR 4-LoopThe following is a summary of information that was provided by the licensee via phone and email: On October 13, 2025, at 2305 CDT, South Texas Project issued a press release on the threat of a potential security concern directed against the licensee's facility and the resultant declaration of an Unusual Event. This media release was reported to the NRC in accordance with 10 CFR 50.72(b)(2)(xi): Any event or situation, related to the health and safety of the public or onsite personnel, or protection of the environment, for which a news release is planned or notification to other government agencies has been or will be made.
ENS 5798414 October 2025 00:00:00NRC Region 4TexasSouth TexasWestinghouse PWR 4-Loop

The following information was provided by the licensee via phone: An Unusual Event was declared on October 13, 2025, at 1914 CDT under EAL HU1.1 due to notification of a credible security threat. State and local agencies were notified. The NRC Resident Inspector was notified. Notified DHS SWO, FEMA Operations Center, CISA Central Watch Officer, FEMA NWC, DHS Nuclear (email), CWMD Watch Desk (email)

  • * * UPDATE ON 10/13/2025 AT 2315 EDT FROM VERONICA ROHAN TO ADAM KOZIOL * * *

The Unusual Event was terminated on October 13, 2025, at 2148 CDT. Notified R4RA (Monninger), NRR (Bowman), NSIR (Williams), R4DO (Miller), NRR EO (Mckenna), IR MOC (Grant), PAO (Gasperson). Notified DHS SWO, FEMA Operations Center, CISA Central Watch Officer, FEMA NWC, DHS Nuclear (email), CWMD Watch Desk (email)

ENS 5798213 October 2025 00:05:00NRC Region 4WashingtonColumbiaGE-5

The following information was provided by the licensee via phone and email: On October 12, 2025, Columbia Generating Station (CGS) was performing a reactor building emergency cooling test. At 1428 (PDT), an air damper associated with the division 1 motor control center (MCC) room cooling failed to perform its intended function to close. This MCC supports the operation of one subsystem of the standby gas treatment system (SGT). At 1440, a second air damper, associated with the division 2 MCC room cooling, also failed. This MCC supports the operation of the other SGT subsystem. Field operators were dispatched to investigate the potential cause. At 1627, the first air damper that had failed was observed to have closed on its own without further operator action. Operators subsequently determined that failure of the air damper to close rendered the associated emergency room coolers inoperable. At 1705, (the division 2 MCC) was declared inoperable and technical specification action statement 3.8.7.A was entered. From 1440 to 1627, CGS was in a condition that required both SGT subsystems to be declared inoperable due to the loss of emergency room cooling to their associated MCCs. This condition constitutes a loss of safety function of SGT and secondary containment. It could have challenged the station's ability to control a radioactive release had one occurred during that time. This notification is being made pursuant to 10 CFR 50.72(b)(3)(v)(C) and (D) due to the loss of safety function of both trains of SGT and secondary containment for approximately 2 hours. The Resident Inspector was notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: At the time of notification, the licensee had exited all technical specification action statements.

  • * * RETRACTION ON 11/5/2025 AT 1925 EST FROM JERRY AINSWORTH TO ERNEST WEST * * *

On October 12, 2025, at 2152 PDT, Columbia Generating Station notified the NRC pursuant to 10 CFR 50. 72(b)(3)(v)(C) and (D) due to the loss of safety function of both trains of standby gas treatment (SGT) and secondary containment for approximately 2 hours under Event Notification 57982. The notification was made due to the failure of two dampers to close during testing of the Reactor Building Emergency Cooling System. The dampers that failed to close were cross-divisional and affected rooms with equipment necessary for both trains of the SGT system which supports the safety function of secondary containment. Following the event, engineering conducted an evaluation to determine if both air dampers remaining open during a loss of cooling accident would have put any safety-related equipment at risk due to potential changes in radiological and environmental conditions within the associated motor control center (MCC) rooms. The engineering evaluation determined temperatures and humidities would not have exceeded limits in the MCC rooms due to the dampers being left open. Additionally, any increase in radiation would be considered negligible and would not affect the ability of the equipment to perform their design functions. Therefore, the safety-related equipment within the MCC rooms would have been available and operable to perform their design function were an accident to occur. Consequently, the failure of two dampers to close during testing is not considered to be an event or condition that could have prevented fulfillment of the safety function of SGT and secondary containment and did not impact the ability to mitigate the consequences of an accident or control the release of radioactive material, therefore, event notification 57982 is retracted. The Resident Inspector has been notified. Notified R4DO (Vossmar)

ENS 579759 October 2025 17:07:00NRC Region 4LouisianaRiver BendGE-6The following information was provided by the licensee via phone and email: On October 9, 2025, at 1207 CDT, River Bend Station (RBS) was operating at 100 percent reactor power when a manual reactor protection system (RPS) actuation was inserted as a result of a division-I balance of plant (BOP) isolation. The BOP isolation was a result of a blown fuse during surveillance activity. The BOP isolation resulted in the loss of instrument air system (IAS) and component cooling primary system (CCP) to containment. Following the isolation, control room operators entered the applicable abnormal operating procedures (AOP). In accordance with AOP guidance, control room operators inserted a manual reactor scram. All plant systems responded as designed. Immediately after the scram, a reactor water level 3 isolation signal was received as expected. Due to the swell from the main turbine trip, a reactor water high level 8 actuation signal was received at 1208 CDT. The level 8 actuation signal was reset at 1211 CDT. At 1237 CDT, control room operators entered the emergency operating procedure (EOP) for high containment pressure. The increase in containment pressure was due to the isolation of the containment vent flow path. The isolation signal for IAS and CCP was reset at 1255 CDT. Following the restoration of the isolation signal, control room operators lowered containment pressure and exited the EOP at 1305 CDT. Reactor pressure is being maintained by the main turbine bypass valves. Reactor level is being maintained by condensate and main feedwater. RBS is currently in mode 3. No radiological releases have occurred due to this event. The event is being reported under 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A) as an event or condition that results in actuation of the RPS when the reactor is critical and as a specified system actuation due to the expected reactor water level 3 isolation signal immediately following the reactor scram, and a subsequent level 8 signal. The NRC Resident Inspector has been notified.
ENS 580686 October 2025 15:13:00NRC Region 4NebraskaCooperGE-4The following information was provided by the licensee via phone and email: At 0913 CDT, on October 6, 2025, a partial actuation of the division 1 emergency diesel generator (DG1) occurred during the performance of the 4160-volt bus 1F undervoltage relay channel functional test. The DG1 automatic start in the emergency mode was the result of the inadvertent contact between a jumper and another component. However, due to the test configuration, the output breaker for DG 1 did not close and pick up the load of the 4160-volt bus 1F since no actual undervoltage condition was present. DG1 components functioned as expected in response. Following the actuation, DG1 was restored to a standby lineup in accordance with plant procedures. This event is considered an invalid system actuation reportable under 10 CFR 50.73(a)(2)(iv)(A). The actuation was not initiated in response to actual plant conditions or parameters and was not a manual initiation. Therefore, in accordance with 10 CFR 50.73(a)(1), this telephone notification is provided within 60 days after discovery of the event instead of submitting a written licensee event report. The NRC Resident lnspector has been notified.
ENS 579632 October 2025 21:52:00NRC Region 4TexasSouth TexasWestinghouse PWR 4-Loop

The following information was provided by the licensee via phone and email: On October 2, 2025, at 1651 CDT, essential cooling water pump '1C' tripped. Essential chiller '1C' and cascading equipment, including emergency core cooling system (ECCS) train '1C,' was declared inoperable. Essential chiller '12A' and cascading equipment, including ECCS train '1A,' was concurrently inoperable for ongoing maintenance. This condition resulted in an inoperable condition on 2 out of 3 safety trains for the accident mitigating functions, including the train 'A' and train 'C' high head safety injection (SI), low head SI, containment spray, electrical auxiliary building heating ventilation and air conditioning (HVAC), and essential chilled water. All 'B' train safety related equipment remains operable. There was no impact on the health and safety of the public or plant personnel. The repair timeline is unknown. We have already entered the configuration risk management program to mitigate additional maintenance induced risk with a risk informed completion time of October 19, 2025, at 1140 CDT. We are limited by TS 3.7.7.C to restore 1 train of control room HVAC by October 5, 2025, at 1651 CDT. This condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The 'C' emergency diesel generator is unavailable due to the loss of cooling water. Maintenance on the ECCS train '1A' is partially complete and operators are working to restore the train to an operable status prior to the technical specification deadline. The essential cooling water pump trip was due to a hot spot causing the pump to overheat. The cause of the hot spot is still under investigation.

  • * * RETRACTION ON 10/20/2025 AT 1636 EDT FROM MARC HILL TO JOSUE RAMIREZ * * *

The following information was provided by the licensee via phone and email: The purpose of this notification is to retract EN 57963, which was made on October 2, 2025, at 2055 EDT. (The) notification was initially made due to two of three trains of emergency core cooling system (ECCS) being declared inoperable. After the notification was made, South Texas Project determined, using an engineering evaluation, that one of the two inoperable ECCS trains was operable because the elevated chilled water outlet temperature of the associated essential chiller (Train A) did not impact the technical specification specified function. Therefore, this event was not a condition that could have prevented fulfillment of a safety function. The NRC Resident Inspector has been notified. Notified R4DO (Vossmar)

ENS 5795225 September 2025 17:29:00NRC Region 4TexasSouth TexasWestinghouse PWR 4-Loop

The following information was provided by the licensee via phone and email: On 9/23/2025 at 2214 CDT, the South Texas Project Unit 1 (STP-1) train 'B' reactor containment fan cooler (RCFC) chilled water supply outside containment isolation valve, 1-CC-MOV-0137, was declared inoperable due to a material condition. This rendered train 'B' component cooling water inoperable which cascaded to train 'B' emergency core cooling system (ECCS) subsystem to render it inoperable. STP-1 entered technical specification (TS) 3.5.2 action 'A' for train 'B' ECCS, requiring restoration within 7 days or apply the requirements of the Configuration Risk Management Program (CRMP). On 09/25/2025 at 1229 CDT, train 'A' essential chiller 12A was declared inoperable due to inability to maintain chiller water outlet temperature less than 52 degrees Fahrenheit. This cascaded down to the train 'A' ECCS subsystem to render it inoperable. STP-1 entered TS 3.5.2 action 'B' due to less than two of the required subsystems operable, to within 1 hour restore at least two subsystems to operable status or apply the requirements of the CRMP, or be in at least hot standby within the next 6 hours and in hot shutdown within the following 6 hours. On 09/25/2025 at 1329 CDT, STP-1 entered the CRMP based on two ECCS subsystems remaining inoperable longer than 1 hour. These subsystems are used for accident mitigation. Unit 1 remains in mode 1.

  • * * RETRACTION ON 10/20/2025 AT 1636 EDT FROM MARC HILL TO JOSUE RAMIREZ * * *

The following information was provided by the licensee via phone and email: The purpose of this notification is to retract EN 57952, which was made on September 25, 2025, at 1736 EDT. (The) notification was initially made due to two of three trains of emergency core cooling system (ECCS) being declared inoperable. After the notification was made, South Texas Project determined using an engineering evaluation, that one of the two inoperable ECCS trains was operable because the elevated chilled water outlet temperature of the associated essential chiller (Train A) did not impact the technical specification specified function. Therefore, this event was not a condition that could have prevented fulfillment of a safety function. The NRC Resident Inspector has been notified. Notified R4DO (Vossmar)

ENS 5795024 September 2025 23:29:00NRC Region 4TexasComanche PeakWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: "On September 24, 2025, at 1829 CDT, Comanche Peak, Unit 1, was manually tripped due to a trip of both main feed water (MFW) pumps. All auxiliary feedwater pumps started due to the trip of both MFW pumps. This event is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B) for a reactor trip and 10 CFR 50.72(b)(3)(iv)(A) for an actuation of auxiliary feedwater. Unit 1 is being maintained in mode 3 in accordance with integrated plant operating procedures. Decay heat is being rejected to the main condenser via the steam dump valves. The cause of both MFW pumps tripping is unknown and under investigation. "The NRC Resident Inspector was notified." The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: No evolutions were ongoing at the time of the event.
ENS 5794924 September 2025 18:47:00NRC Region 4ArkansasArkansas NuclearB&W-L-LPThe following information was provided by the licensee via phone and email: "On September 24, 2025, at 1347 CDT, Arkansas Nuclear One, Unit 1, (ANO-1) experienced an issue with the X-01B main phase transformer which led to an automatic trip on reactor protection system (RPS). "ANO-1 is currently stable in mode 3, maintaining pressure and temperature with the P-1A and P-1B main feedwater pumps and steaming to the main condenser. All rods inserted and systems functioned as expected. "There is no radiological release on either unit as a result of this event. "This report satisfies the reporting criteria of 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A) for the reactor protection system actuation. "The NRC Senior Resident Inspector has been notified. "Unit 2 was not affected." The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: ANO-1 retains access to all normal sources of offsite power.
ENS 5794415 September 2025 18:00:00NRC Region 4TexasSouth TexasWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: "At 1300 CDT on September 15, 2025, it was determined that a non-licensed supervisor had tested positive for a controlled substance, in violation of South Texas Project's fitness for duty policy. Prior to this, the individual's unescorted access had been administratively withdrawn pending retesting. This is reportable under 10 CFR 26.719 and is a late 24-hour notification. "The NRC Resident Inspector has been notified.
ENS 5792915 September 2025 01:20:00NRC Region 4TexasComanche PeakWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: At 2020 CDT (on 9/14/2025), (Comanche Peak) Unit 2 reactor was manually tripped due to a malfunction of the electro-hydraulic control (EHC) system on the main turbine. All auxiliary feedwater pumps started due to steam generator `Lo-Lo' levels post trip. This event is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B) for a reactor trip and 10 CFR 50.72(b)(3)(iv)(A) for an actuation of auxiliary feedwater. Unit 2 is being maintained in hot standby (mode 3) in accordance with integrated plant operating procedures. Decay heat is being rejected to the main condenser via the steam dump valves." The NRC Resident Inspector was notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Unit 1 was not affected. The cause of the malfunction of EHC is unknown and under investigation. All rods fully inserted upon the reactor being tripped.
ENS 5791911 September 2025 07:55:00NRC Region 4MissouriCallawayWestinghouse PWR 4-Loop

The following information was provided by the licensee via phone and email: On September 11, 2025, Callaway was performing a planned maintenance window causing the 'B' train emergency diesel generator and the 'B' train essential service water system to be inoperable. At 0255 CDT the 'A' train centrifugal charging pump was declared inoperable due to an unexpected loss of control room indication for the 'A' train centrifugal charging pump miniflow valve. Therefore, both trains of the centrifugal charging (high head injection) system were simultaneously inoperable. This condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). A fuse was replaced on the 'A' train centrifugal charging pump miniflow valve breaker, restoring operability of that system at 0500. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 9/17/2025 AT 1747 EDT FROM ZACHARY MILLIGAN TO KAREN COTTON * * *

The following information was provided by the licensee via phone and email: Event Notification (EN) 57919, made on 09/11/25, pursuant to 10 CFR 50.72(b)(3)(v)(D), is being retracted based on further review of the timing of when the 'B' train essential service water (ESW) system was operable and capable of performing its support function for the 'B' train centrifugal charge pump (CCP). Further review of restoration procedures/processes determined that the 'B' train ESW system was operable by 0232 CDT on 9/11/25, which was prior to the loss of the 'A' train CCP mini-flow valve (0255 on 09/11/25). Thus, the 10 CFR 50.72(b)(3)(v)(D) reporting criterion was not met. The NRC Resident Inspector has been notified of this retraction. Notified R4DO (Agrawal)

ENS 579014 September 2025 13:55:00NRC Region 4MississippiGrand GulfGE-6The following information was provided by the licensee via phone and email: On September 4, 2025, at 0855 CDT, Grand Gulf Nuclear Station operators discovered the enclosure building roof hatch was unsecured and open approximately 1 inch. This resulted in inoperability of secondary containment. Following discovery, the hatch was immediately closed and latched. Secondary containment operability was restored at 0940 CDT. This event is being reported under 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented fulfillment of a safety function. The NRC Resident Inspector has been notified.
ENS 5788020 August 2025 15:20:00NRC Region 4LouisianaRiver BendGE-6The following information was provided by the licensee via phone and email: On August 20, 2025, at 1020 CDT, River Bend Station (RBS) was operating at 100 percent reactor power when it was discovered that previously implemented enhancement compensatory measures were determined to have rendered containment unit cooler `A' (HVR-UC1A) and containment unit cooler `B' (HVR-UC1B) inoperable. On August 14, 2025, RBS placed 'HVR-UC1A' and 'HVR-UC1B' in lockout as a compensatory measure to enhance operability following a Part 21 notification from General Electric. On August 20, 2025, it was discovered that the lockout function would delay the start of a time relay needed for load sequencing in the event of an accident. This condition would prevent the unit coolers from starting within their required sequence timing following a loss of offsite power. 'HVR-UC1A' and 'HVR-UC1B' were declared inoperable. By 1219 CDT, these compensatory measures were no longer in place. This event is being reported under 10 CFR 50.72(b)(3)(ii)(B) as any event or condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety, as well as 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented fulfillment of a safety function that is needed to control the release of radioactive material and mitigate the consequences of an accident. The NRC Resident Inspector has been notified.
ENS 5787318 August 2025 14:45:00NRC Region 4NebraskaCooperGE-4The following information was provided by the licensee via phone and email: On August 18, 2025, a licensed supervisor tested positive on a follow-up test. The test was conducted on August 13, 2025, and sent to the Health and Human Services certified laboratory on August 14, 2025. The results were reported out as positive by the medical review officer on August 18, 2025, at 0945 CDT. The individual's access has been terminated and a notification to the NRC Resident inspector was made.
ENS 5787218 August 2025 12:15:00NRC Region 4TexasSouth TexasWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: On August 18, 2025, a licensed operator violated the station's Fitness for Duty policy. The event was determined to be reportable under 10 CFR 26.719(b)(2)(ii)." The NRC Resident Inspector has been notified.
ENS 5787115 August 2025 23:26:00NRC Region 4WashingtonColumbiaGE-5The following information was provided by the licensee via phone and email: On August 15, 2025, Columbia Generating Station received a report of a sheen of oil in the circulating water basin. This basin is connected to the Columbia River via a blowdown line. This blowdown line was secured at 1423 PDT on August 15, 2025. A visual inspection of the Columbia River did not identify any oily sheen or film. It did not appear that the oil posed a threat to human health or the environment, however, because there could have been a discharge of an unknown quantity of oil into the Columbia River, the event became immediately reportable under 40 CFR 302.6a to the National Response Center, Benton County, Washington State Department of Emergency Management (under Revised Code of Washington 90.56.280), Washington Department of Ecology, as well as the Coast Guard National Response Center. This is being reported pursuant to 10 CFR 50. 72(b)(2)(xi) for notification of other government agencies concerning an event related to the health and safety of the public or protection of the environment. Notifications to offsite agencies was performed at 1626 on August 15, 2025. The NRC Resident Inspector has been notified.
ENS 5783129 July 2025 04:29:00NRC Region 4MississippiGrand GulfGE-6

The following information was provided by the licensee via phone and fax: At 2324 CDT, on July 28, 2025, control room air conditioning (CRAC) 'B' tripped at Grand Gulf Nuclear Station (GGNS) approximately 5 minutes after loading the compressor by adjusting the thermostat (down) per standby service water quarterly surveillance instructions. CRAC 'A' was manually started at 2326 CDT and at 2329 CDT it subsequently tripped. After investigating the compressors and breakers per the alarm response instructions with no abnormal indications, CRAC 'B' was restarted and tripped again. Cooling water was rotated from plant service water to standby service water and CRAC 'A' was successfully restarted at 2358 CDT and remains in service. While both control room air conditioning subsystems were inoperable GGNS entered technical specification limiting condition of operation (LCO) 3.7.4 condition 'B', actions requiring verification of control room temperatures less than 90 degrees F and restoring one subsystem to operable status in 7 days. Control room temperatures reached 79 degrees F, maximum, before CRAC 'A' was restarted. GGNS has exited condition 'B' in LCO 3.7.4 and entered condition 'A' to restore CRAC 'B' in 30 days. This event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition which could have prevented the fulfillment of a safety function. The NRC Senior Resident Inspector has been notified.

  • * * RETRACTION FROM JEFFERY HARDY TO SAMUEL COLVARD AT 1648 EDT ON 07/30/2025 * * *

Investigation of the cause of the control room air conditioning (CRAC) `A' and `B' trips identified a plant service water / standby service water (SSW) crosstie valve which failed in its safety-related (closed) position as the cause. In an accident or transient, cooling water to CRAC `A' compressors would have been successfully provided by the safety-related SSW. As a result, CRAC `A' remained capable of fulfilling its safety function to maintain the control room environment less than 90 degrees F. The NRC Senior Resident Inspector has been notified of this retraction. Notified R4DO (Drake).

ENS 5782021 July 2025 20:48:00NRC Region 4LouisianaRiver BendGE-6The following information was provided by the licensee via phone and email: On July 21, 2025, at 1548 CDT, River Bend Station (RBS) was operating at 100 percent reactor power when the central alarm station received a door alarm indicating that PW123-01 was not fully secured. A security officer was dispatched and found the door closed with the dogs (latches) not engaged. The security officer fully engaged the dogs at 1551 CDT. PW123-01 is a secondary containment door. With the dogs not being engaged, secondary containment was inoperable for 3 minutes. This event is being reported under 10 CFR 50.72(b)(3)(v) as an event or condition that could have prevented fulfillment of a safety function due to the inoperability of secondary containment. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The licensee entered technical specification LCO 3.6.4.1 while the door was unsecured.
ENS 5779030 June 2025 21:41:00NRC Region 4NebraskaCooperGE-4

The following information was provided by the licensee via phone and fax: On 6/29/2025, at 1641 CDT, the National Weather Service reported to Cooper Nuclear Station that the National Warning System (NAWAS) radio tower near Shubert, Nebraska was non-functional. The Shubert Tower transmitter activates the Emergency Alert System (EAS)/tone alert radios used for public prompt notification which is part of Cooper's primary alert and notification system (ANS). On 6/30/2025, at 1641 CDT, the Shubert Tower transmitter remained non-functional for 24 hours. This primary ANS equipment was not restored to service within 24 hours, and therefore this condition is reportable under 10 CFR 50.72(b)(3)(xiii), since the backup alerting methods do not meet the primary system design objective. The backup notification system is available to use for notifications if needed. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 07/09/2025 AT 1453 EDT FROM BAILEY GILES TO ERIC SIMPSON * * *

At 1045 CDT, on 7/09/2025, Cooper Nuclear Station was informed that the NAWAS radio tower near Shubert, Nebraska has been restored to service. The NRC Resident Inspector was notified. Notified R4DO (Dodson).

ENS 5778523 June 2025 15:27:00NRC Region 4WashingtonColumbiaGE-5The following information was provided by the licensee via phone and email: Valcor supplied replacement V70900-45 solenoid valves with substitute EM163-80 EPDM O-ring material (due to the obsolescence of the original E0515-80 material) and certified to the original qualification test report based on Delta Qualification report QRSKC26022-1. These replacement solenoid valves were installed at Columbia Generating Station (CGS) in July 2024 as control rod drive scram discharge volume solenoid drain valves. On September 26, 2024, CGS identified this change in material and the issue was entered into the corrective action program. Columbia's review of the Delta Qualification report identified the justification of the thermal life of the new O-ring compound when used in normally energized valves such as those supplied to CGS was not adequate. This issue was communicated to the NRC with an interim Part 21 notification on November 21, 2024 (ML24326A362). Valcor's report of additional testing to attempt to justify the new O-ring material as equal to or better than the original material was submitted to CGS on February 24, 2025. Columbia concluded the justification was inadequate and submitted to a third party for evaluation. The Senior Resident Inspector has been notified.
ENS 5776317 June 2025 09:26:00NRC Region 4MississippiGrand GulfGE-6The following information was provided by the licensee via phone and email: On June 17, 2025, at 0426 CDT, Grand Gulf Nuclear Station (GGNS) was operating at 70 percent power when a manual scram was initiated due to degraded main condenser vacuum caused by the loss of the 'A' circulating water pump. All control rods fully inserted, there were no complications, and all plant systems responded as designed. Immediately after the scram, an expected reactor water Level 3 isolation signal was received. Reactor pressure is being maintained via the turbine bypass valves. Reactor level is being maintained via main feedwater. GGNS is currently in Mode 3. No radiological releases have occurred due to the event. The cause of the circulating water pump trip is under investigation. The manual reactor protection system actuation is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B). The expected reactor water Level 3 isolation signal is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident Inspector was notified.
ENS 5773123 May 2025 04:58:00NRC Region 4LouisianaRiver BendGE-6The following information was provided by the licensee via phone and email: On May 22, 2025, at 2358 CDT, River Bend Station determined that a degraded condition existed following the performance of a VT-3 examination of E12-AOVF041A, Residual Heat Removal (RHR) 'A' injection line testable check valve. The cause of this event is currently being investigated. This examination was conducted following the plant shutdown, which was reported in Event Notification (EN) 57725. This event is being reported as an 8-hour reportable condition in accordance with 10 CFR 50.72(b)(3)(ii)(A) for the degraded condition of the pressure boundary. The NRC Resident Inspector has been notified." The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: This degraded condition resulted in a leakage rate of approximately 3.6 gallons per minute when at pressure. The plant is shutdown and depressurized which has caused the leakage to stop. No release is occurring or expected and possible corrective actions are being evaluated.
ENS 5777022 May 2025 05:00:00NRC Region 4NebraskaCooperGE-4The following information was provided by the licensee via phone and email: On April 8, 2025, while in Mode 1 and at 100 percent power, during performance of a scheduled monthly surveillance test, Nebraska Public Power District (NPPD) Cooper Nuclear Station (CNS) identified Diesel Generator (DG) 1 jacket water (DGJW) pump may not be providing sufficient cooling water to the DG. The DGJW pump impeller was found to have slipped on the shaft as a result of a failure to achieve the required interference fit during preventive maintenance replacing the pump seal. On May 22, 2025, subsequent investigation identified a deviation in that the originally supplied Cooper-Bessemer DGJW impeller bore was not provided in accordance with the design drawing. Due to the bore dimensional deviation, the required interference fit was not achieved, resulting in shaft rotational and torsional forces challenging the compromised fit until the impeller was able to spin freely on the shaft. On June 19, 2025, NPPD completed an evaluation and determined that the deviation represents a defect that could create a substantial safety hazard as defined in 10 CFR 21, as this pump was approved for use in a safety application. NPPD is not aware of any other plants being impacted by this issue. The NRC Resident Inspector has been notified. A written notification will be provided within 30 days. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Maintenance performed on the DGJW pump was completed on April 9, 2025.
ENS 5772521 May 2025 11:26:00NRC Region 4LouisianaRiver BendGE-6The following information was provided by the licensee via phone and email: On May 21, 2025, at 0656 CDT, River Bend Station (RBS) was operating at 100 percent reactor power when a plant shut down was initiated due to technical specification (TS) requirements. At 0324 on May 21, 2025, unidentified drywell leakage exceeded a 2 gallon per minute change over a 24-hour period. TS limiting condition of operation 3.4.5 condition 'C' was entered with a required action to verify the source of the unidentified leakage increase is not from service sensitive type 304, type 316 austenitic stainless steel, or other inter-granular stress corrosion cracking susceptible material within 4 hours. This required action could not be completed within the completion time. This event is being reported under 10 CFR 50.72(b)(2)(i) as an event or condition that results in a TS required plant shut down. The NRC Resident has been notified.
ENS 5770210 May 2025 15:30:00NRC Region 4TexasSouth TexasWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: At 1030 CDT on 5/10/2025, it was determined that a non-licensed supervisor has tested positive for a controlled substance, in violation of South Texas Project's fitness for duty policy. The individual's unescorted access has been revoked. The NRC Resident Inspector has been notified.
ENS 576957 May 2025 03:20:00NRC Region 4MissouriCallawayWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: On May 6, 2025, with Callaway Plant in mode 3 ascending from refueling outage 27, plant personnel identified a dry white residue resembling boric acid at the interface between the reactor vessel and bottom-mounted instrument nozzle No.48. At 2220 CDT, the shift manager determined that a reactor coolant pressure boundary leak had been identified. The determination was based on the residue appearing to be in the annulus of the nozzle where it penetrates the bottom head and the residue did not previously exist during earlier inspections of the area during refueling outage 27. Detailed examination of the apparent leak has not yet been performed due to radiological conditions, but the condition is being treated as a reactor coolant pressure leak. As such, the condition is being reported pursuant to 10 CFR 50.72 (b)(3)(ii)(A) as an eight-hour, non-emergency notification. The NRC Resident Inspector has been notified." The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The apparent leak placed the plant in LCO 3.4.13.B. The plant is evaluating the leak repair corrective actions and preparing for cooldown.
ENS 576894 May 2025 17:30:00NRC Region 4MissouriCallawayWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: On May 4, 2025, with the plant in mode 4 during restart from a refueling outage, operators were flushing the chemical volume and control system (CVCS) `B' train mixed bed demineralizers, with makeup (water) from the refueling water storage tank (RWST). During the evolution at 1230 CDT, it was discovered that the borated water level in the RWST had been inadvertently lowered to less than the technical specification (TS) limit of 394,000 gallons. Under TS 3.5.4, `Refueling Water Storage Tank (RWST),' surveillance requirement (SR) 3.5.4.2 requires verifying that the RWST borated water volume is (greater than or equal to) 394,000 gallons (93.7 percent level). The minimum level (volume) reached in the tank during the flushing operation was 93 percent. Upon discovery of the lowered level in the RWST, the flushing activity was terminated, and water level in the RWST was restored to above the TS limit by 1427. The RWST supplies borated water to the CVCS during abnormal operating conditions, and to the emergency core cooling system (ECCS) and the containment spray system during accident conditions. The RWST supplies both trains of the ECCS and the containment spray system through a common suction supply header during the injection phase of a loss of coolant accident recovery. During mode 4, in accordance with TS 3.5.3, `ECCS - Shutdown,' only one ECCS train is required to be operable. With the RWST declared inoperable, the one required ECCS train in mode 4 was not supported. Therefore, the identified condition is being reported pursuant to 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. The NRC Resident Inspector was notified.
ENS 5768328 April 2025 15:26:00NRC Region 4NebraskaCooperGE-4The following information was provided by the licensee via phone and email: On 4/28/2025, at 1026 CDT, the National Weather Service notified Cooper Nuclear Station that the Shubert tower is disabled due to planned maintenance. The planned maintenance will continue from Monday, 4/28/2025 to Wednesday, 4/30/2025. This constitutes a loss of the primary public prompt notification system for greater than 24 hours. The Shubert tower transmitter activates the emergency alert system/tone alert radios used for public notification. The backup notification system has been verified to be available for use, if needed, throughout this period. This condition is reportable under 10 CFR 50.72(b)(3)(xiii) as a major loss of the public prompt notification system capability since the backup alert methods do not meet the primary systems design objective. The NRC Resident Inspector has been notified." The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The National Weather Service notified the local authorities that the Shubert tower is disabled due to planned maintenance.
ENS 5767622 April 2025 15:00:00NRC Region 4WashingtonColumbiaGE-5

The following information was provided by the licensee via phone and email: A non-licensed supervisor had a confirmed positive fitness-for-duty follow-up test. The employee's unescorted access has been terminated. This report is being made pursuant to 10 CFR 26.719(b)(2)(ii). The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 04/24/25 AT 1742 EDT FROM BRIAN STANISZEWSKI TO JOSUE RAMIREZ * * *

The following information was provided by the licensee via phone and email: This is to retract event notification 57676. On April 22, 2025, Columbia Generating Station notified the NRC (event notification 57676) under 26.219(b)(2)(ii) of a non-licensed supervisor with a confirmed positive fitness-for-duty follow-up test. Subsequent to the notification the medical review officer (MRO) has reversed their decision of a positive test result based on additional research and information provided by the certifying scientist of the laboratory. Due to this, the original notification (57676) is being retracted. The NRC Resident Inspector has been notified. Notified R4DO (Rollins) and FFD Group (email).

ENS 5766312 April 2025 09:23:00NRC Region 4WashingtonColumbiaGE-5The following information was provided by the licensee via phone and email: During a planned shutdown at Columbia Generating Station for a refueling outage, pressure boundary leakage was identified from the bonnet vent line of loop `B' discharge motor operated isolation valve during a drywell inspection. Leakage was initially identified during a drywell entry at 15 percent (reactor) power and identified as pressure boundary leakage during a subsequent entry in mode 3. The leak exceeds technical specification (TS) 3.4.5 'RCS Operational Leakage' of no pressure boundary leakage. TS action `C' was entered, requiring (the plant to be in) mode 3 in 12 hours and mode 4 in 36 hours. Columbia Generating Station was in mode 3 at time of determination for (entering TS) 3.4.5. Therefore, the event is reportable within 4 hours per 10 CFR 50.72(b)(2)(i) due to the initiation of a plant shutdown required by the plant's TS. The event is also reportable within 8 hours per 10 CFR 50.72(b)(3)(ii)(A) due to an event that resulted in the condition of the nuclear power plant, including principal safety barriers, being seriously degraded. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The NRC Resident Inspector has been informed. Columbia Generating Station estimates the leak rate to be less than 0.2 gallons per minute. Columbia Generating Station expects to enter mode 4 within the required 36 hours.
ENS 5766110 April 2025 16:24:00NRC Region 4ArkansasArkansas NuclearB&W-L-LPThe following information was provided by the licensee via phone and email: On April 10, 2025, at 1124 CDT, a licensed operator at Arkansas Nuclear One, Unit 1, had a confirmed positive result for alcohol during random testing per the Entergy fitness for duty (FFD) program. The individual's unescorted access has been terminated. This event is being reported under 10 CFR 26.719(b)(2)(ii). The NRC Resident Inspector has been informed.
ENS 5765910 April 2025 14:11:00NRC Region 4ArizonaPalo VerdeCE

The following information was provided by the licensee via phone and email: On 4/10/2025, Unit 1 was defueled at 0 percent power. The `A' train class bus was being powered by the `A' diesel generator (DG) and the `B' train bus was out of service for maintenance. Additionally, the `A' train offsite power transformer is currently out of service for maintenance. Abnormal indication was observed on the `A' DG with lowering voltage and the decision was made to manually trip the `A' DG. Power was restored to the `A' class bus by crosstieing `B' train offsite power via engineering safety feature transformer NBN-X04. This resulted in a loss of all but one AC power source to emergency buses for 15 minutes or longer which is an Unusual Event (UE) CU2.1. It is currently not known at this time what caused the abnormal voltage indications on the `A' DG. State and local agencies were notified. The NRC Resident Inspector has been notified. Notified DHS SWO, FEMA Operations Center, CISA Central Watch Officer, FEMA NWC, DHS Nuclear SSA (email), CWMD Watch Desk (email). The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Palo Verde Units 2 and 3 were not affected by this event. The licensee restored spent fuel pool cooling.

  • * * UPDATE ON 4/10/2025 AT 1701 EDT FROM TANNER GOODMAN TO SAMUEL COLVARD * * *

The following information was provided by the licensee via phone and email: The following event description is based on information currently available. If through subsequent reviews of this event additional information is identified that is pertinent to the event or alters the information being provided at this time, a follow up notification will be made via the ENS or under the reporting requirements of 10 CFR 50.73. Train `A' emergency diesel generator (DG) was supplying power to PBA-S03 bus. At 0658 MST on April 10th, 2025, train `A' DG was exhibiting erratic and degraded voltage and was placed in emergency stop, which caused a loss of power to PBA-S03. When the `A' DG was stopped, train `A' balance of plant engineered safety features actuation system (BOP ESFAS) detected the loss of power condition on PBA-S03, and sent an emergency start signal to the train `A' DG. Train `A' DG did not respond as it was placed in emergency stop. Operators restored power to PBA-S03 at 0703 MST. At the time of the (loss of power), the reactor was defueled with the core offloaded to the spent fuel pool. Unit 2 and Unit 3 are not impacted by this event and remain in Mode 1, 100 percent power. Unit 1 is still currently in Unusual Event, CU2.1 This (update) is in addition to the event reported at 1029 EDT EN 57659. The original EN reported an Emergency Classification definition as a loss of all but 1 AC power source to emergency buses for 45 minutes. The correct time is 15 minutes. The NRC Senior Resident Inspector has been notified of the update. (This update is an 8-hour, non-emergency, 10 CFR 50.72(b)(3)(iv)(A) report of a valid specified system actuation due to the BOP ESFAS attempting to start 'A' DG upon loss of the PBA-SO3 bus during the initial event.) Notified R4DO (Vossmar).

  • * * UPDATE ON 4/10/2025 AT 2245 EDT FROM NGOC NGUYEN TO SAMUEL COLVARD * * *

The following information was provided by the licensee via phone: On 4/10/2025, at 2224 EDT, Palo Verde Unit 1 terminated the Unusual Event. Restoration of 'A' DG was made by swapping to its redundant automatic voltage regulator and performance of a functional startup. This restores two sources of power to the class 1E bus: offsite power and 'A' DG in a standby configuration. The redundant automatic voltage regulator was tested in surveillance in the previous cycle and remains operable. The issues that led to the declaration of Unusual Event with 'A' DG have been entered into the corrective action program. State and local authorities have been notified. The NRC Resident Inspector has been notified. Internal notifications: R4DO (Vossmar), NRR EO (Felts), IR MOC (Crouch), R4 RA (Monninger), NRR (King), R4 PAO (Dricks), and NSIR (Erlanger) External notifications: DHS SWO, FEMA Operations Center, CISA Central Watch Officer, FEMA NWC, DHS Nuclear SSA (email), CWMD Watch Desk (email)

ENS 576569 April 2025 02:24:00NRC Region 4ArizonaPalo VerdeCEThe following information was provided by the licensee via phone and email: At 1924 MST on April 8, 2025, a loss of power (LOP) occurred to 'Train-A' 4.16 kV class 1E electrical bus while re-energizing 'Train-A' balance of plant (BOP) engineered safety features actuation system (ESFAS) from pre-planned maintenance. The LOP occurred when the circuit breaker supplying off-site power to the 'Train-A' 4.16 kV class 1E bus tripped when 'Train-A' BOP ESFAS system was re-energized. Operators restored power to 'Train-A' 4.16 kV class 1E bus with 'EDG-A' (emergency diesel generator for 'Train-A') at 1934 MST. Operators restored all necessary plant loads which had lost power. Per the Palo Verde emergency plan, no emergency classification was required. At the time of the LOP, the reactor was defueled with the core offloaded to the spent fuel pool. Unit 2 and Unit 3 are not impacted by this event and remain in mode 1, 100 percent power. The cause of the circuit breaker supplying off-site power to the 'Train-A' 4.16 kV class 1E bus tripping is under investigation. NRC Resident Inspector has been notified. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of emergency AC electrical power systems.
ENS 576558 April 2025 21:07:00NRC Region 4LouisianaRiver BendGE-6The following information was provided by the licensee via phone and email: On April 08, 2025, at 1607 CDT, River Bend Station (RBS) was operating at 81 percent reactor power when a manual reactor protection system (RPS) actuation was inserted due to the loss of all normal service water pumps. Standby service water initiated and operated as expected. The scram was uncomplicated and all other plant systems responded as designed. Immediately after the scram, a reactor water level 3 isolation signal was received as expected. Reactor pressure is being maintained by the main turbine bypass valves. Reactor water level is being maintained by condensate and main feed water. RBS is currently in mode 3. No radiological releases have occurred due to this event. The loss of all normal service water is currently under investigation. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A), as an event or condition that results in actuation of the RPS while the reactor is critical and as a specified system actuation due to the expected reactor water level 3 isolation signal immediately following the reactor scram. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: RBS intends to maintain temperature and pressure and remain in mode 3 while the event is under investigation.
ENS 576588 April 2025 18:33:00NRC Region 4LouisianaRiver BendGE-6The following information was provided by the licensee via phone and email: On April 8, 2025, at 1333 CDT, it was determined that a licensed operator violated the station's fitness-for-duty program. The employee's access to the plant has been terminated. This event is being reported under 10 CFR 26.719(b)(2)(ii). The NRC Resident has been notified.
ENS 5763328 March 2025 08:06:00NRC Region 4ArizonaPalo VerdeCEThe following information was provided by the licensee via phone or email: On 3/28/2025 at 0106 MST, Palo Verde Generating Station Unit 1 entered Technical Specification Limiting Condition for Operation (LCO) 3.0.3 due to discovering `A' essential chiller (EC) oil temperature at 80 degrees Fahrenheit, which is below the operability limit of 120 degrees Fahrenheit. `A' EC inoperable rendered the `A' high pressure safety injection (HPSI) pump inoperable. At the time of discovery, `B' HPSI was inoperable due to recirculating the refueling water tank for chemistry purposes (LCO 3.5.3 condition B entered on 3/27/2025 at 2127 MST). This resulted in inoperability for both trains of HPSI, leading to a loss of the HPSI safety function. On 3/28/2025 at 0115 MST, `B' HPSI was restored to operable condition, LCO 3.0.3 was exited, and the loss of safety function was restored. There were no power reductions (control rod insertions or boron concentration changes). The event did not result in any challenges to the fission product barrier or result in any release of radioactive materials. Unit 2 and 3 remained at 100%. NRC resident has been notified of the event.
ENS 5760915 March 2025 18:48:00NRC Region 4MississippiGrand GulfGE-6The following information was provided by the licensee via phone and email: On March 15, 2025, at 1248 CDT, Grand Gulf Nuclear Station (GGNS) was operating in mode 1 at 100 percent reactor power when a grid disturbance (degraded voltage) resulted in a valid specified system actuation (automatic start) of the division Ill emergency diesel generator (EDG). The division Ill EDG started and repowered the '17' AC safety-related electrical bus as designed. GGNS is currently in mode 1 at 100 percent reactor power. No radiological releases have occurred due to this event and no other safety system actuations occurred. This event is being reported under 10 CFR 50.72(b)(3)(iv)(A), as an event or condition that results in a valid specified system actuation due to the automatic start of the division Ill EDG on bus undervoltage due to a grid disturbance. The NRC Senior Resident Inspector has been notified.