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 Event dateRegionStateSiteReactor typeEvent description
ENS 582281 April 2026 13:24:00NRC Region 1PennsylvaniaPeach BottomGE-4The following information was provided by the licensee via phone and email: At 0924 EDT on April 1, 2026, it was determined that Unit 3 was in an unanalyzed condition because two emergency diesel generators (EDGs) were inoperable. One EDG was inoperable due to scheduled maintenance, and the second EDG was inoperable due to blocking for an emergent plant issue. This condition is not bounded by existing design and licensing documents; however, it poses no impact to the health and safety of the public or plant personnel. The second EDG was returned to service, and the condition was exited. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Unit 2 was unaffected by this condition. No other limiting conditions exist. The second EDG was blocked due to a failed transformer, but the transformer has been repaired.
ENS 5820217 March 2026 12:54:00NRC Region 1ConnecticutMillstoneWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: At 0854 (EDT) on March 17, 2026, it was determined that a licensed operator failed a test specified by the fitness for duty (FFD) testing program. The employee's unescorted access has been placed on hold in accordance with the licensee's FFD policy. The event was determined to be reportable under 10 CFR 26.719(b)(2)(ii). The NRC Resident Inspector has been notified.
ENS 5820014 March 2026 11:00:00NRC Region 1PennsylvaniaBeaver ValleyWestinghouse PWR 3-LoopThe following information was provided by the licensee via phone and email: At 0700 EDT on March 14, 2026, the emergency operations facility (EOF) lost normal and alternate electrical power. At the time of the event, the normal power source to the EOF (offsite power) was lost due to the effects of weather in the wider area and attempts to establish the alternate power generator were unsuccessful. At the time of this notification, power is not yet restored to the facility but is anticipated to be restored within the next few hours. The cause of the backup generator failure to run is unknown at this time. If an emergency is declared requiring EOF activation while there is no available power, compensatory measures have been established to ensure that all assessment and communications functions will be available, which include staffing the EOF at a location within the on-site emergency response facility and activating using existing emergency planning procedures. This is an eight-hour, non-emergency notification for a loss of emergency assessment capability. This event is reportable in accordance with 10 CFR 50.72(b)(3)(xiii) because the loss of normal and alternate electrical power affects the functionality of an emergency response facility. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5816823 February 2026 07:09:00NRC Region 1New JerseyHope CreekGE-4

The following information was provided by the licensee via phone and email: At 0209 EST on 02/23/2026, with Hope Creek in Mode 1 at 100 percent power, the reactor automatically tripped due to a loss of offsite power. All emergency diesel generators (EDGs) started and loaded as expected to power vital buses. Operations responded and stabilized the plant in Mode 3. Reactor water level is being maintained via high pressure coolant injection (HPCI) and reactor core isolation cooling (RCIC). Reactor pressure is being maintained using safety relief valves (SRVs). Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). An Unusual Event (SU1.1) was declared at 0229 on 02/23/2026, due to a loss of offsite power to all vital buses for greater than 15 minutes. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified, and all offsite notifications have been made. Notified DHS SWO, FEMA Operations Center, FEMA NWC, CISA Central Watch Officer, CWMD Watch Desk, DHS Nuclear SSA (email), DHS NRCC THD Desk (email).

  • * * UPDATE ON 02/23/2026 AT 1352 EST FROM HOPE CREEK TO NESTOR MAKRIS * * *

On 02/23/2026, at 1340 EST, Hope Creek terminated their Unusual Event (SU1.1), which was declared due to a loss of offsite power.

ENS 5809116 December 2025 05:00:00NRC Region 1PennsylvaniaPeach BottomGE-4The following information was provided by the licensee via email: This is a non-emergency notification required by 10 CFR 21.21(d)(3)(i). A written report in accordance with 10 CFR 21.21(d)(3)(ii) will be provided within 30 days. On December 16, 2025, Peach Bottom engineering staff determined that a defect identified during a causal evaluation could constitute a substantial safety hazard. Failure analysis testing of a Fairbanks Morse Defense, emergency diesel generator (EDG) engine cylinder liner documented gross delamination between layers of the cylinder liner chrome plating. The delamination and subsequent loss of chrome plating contributed to piston ring damage that enabled combustion gas leakage into the engine crankcase, tripping the EDG on high crankcase pressure. The Fairbanks Morse Defense part number: LINER, CYLINDER, KIT, F/DIESEL GEN, MOD-38TD8-1/8, is purchased as a safety related part. Peach Bottom's procurement specification requires one single layer of chrome plating which is inconsistent with the defect exhibited, 'at least two passes of chrome plating' during failure analysis. The EDG piston ring failure and ensuing inoperability resulted in the loss of a sub-component function, which could constitute a substantial safety hazard. The defect extent of condition potentially includes 5-cylinder liners with serial numbers: H837-1, H837-2, H832-2, H838-1, and H9311-2. On December 17, 2025, the Peach Bottom site Vice President was notified of the requirement to report this event under 10 CFR 21.21. The NRC Senior Resident Inspector at Peach Bottom has been notified The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: This condition effects safety related diesel generators "E-1" and "E-3". After repair of "E-1" and an operability determination on "E-3", no limiting conditions of operability were entered as a result of the defect. Limerick Generating Station is potentially affected by this defect. Fairbanks Morse Defense has also been notified.
ENS 5808815 December 2025 16:31:00NRC Region 1PennsylvaniaLimerickGE-4The following information was provided by the licensee via phone and email: On December 15, 2025, at approximately 1131 EST, a manager violated the FFD policy, which is reportable under 10 CFR 26.719(b)(2)(ii). Site access personnel detected the odor of alcohol during in-processing activities. For-cause testing was performed, and the test confirmed the individual was positive for alcohol. The individual was denied access. The NRC Resident Inspector has been notified.
ENS 5804919 November 2025 08:28:00NRC Region 1PennsylvaniaLimerickGE-4

The following is a summary of information provided by the licensee via phone and email: On November 18, 2025, at 0328 CST, as the licensee was initiating the standby gas treatment system in support of planned maintenance on normal reactor building ventilation, the '2A' reactor enclosure recirculation system (RERS) fan failed to establish flow upon the system initiation signal. The '2B' RERS fan was previously inoperable due to a planned maintenance window. Technical specification action statement 3.6.5.4.B was entered with both Unit 2 RERS fans inoperable. The '2B' RERS fan was restored to operable at 0523 EST. The licensee returned normal reactor building ventilation to service to restore secondary containment differential pressure. Due to inoperability of both RERS trains, the system was in a condition that could have prevented the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72.(b)(3)(v)(C). The licensee reported there was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector was notified.

  • * * RETRACTION ON 01/08/2026 AT 0838 EST FROM BRAD SMITH TO ROBERT THOMPSON * * *

The following information was provided by the licensee via phone and email: Limerick completed a review and confirmed that '2B' RERS fan operability was established following routine maintenance, prior to the '2A' RERS fan being declared inoperable. Consequently, the '2B' RERS fan remained capable of performing its safety-related function during the period when the '2A' RERS fan was unavailable, thereby ensuring the overall RERS safety function was maintained. As such, no condition existed that would have prevented the fulfillment of a safety function. Based on this assessment, event notification 58049 is being retracted. The NRC Senior Resident Inspector has been notified. Notified R1DO (Seeley).

ENS 580296 November 2025 15:14:00NRC Region 1ConnecticutMillstoneWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: On November 6, 2025, at 1014 (EST), it was determined that a licensed supervisory operator was in violation of the licensee's fitness for duty (FFD) policy. The test result was negative but determined to be reportable under 10 CFR 26.719(b)(2)(ii) due to violation of the licensee's FFD policy. The employee's unescorted access has been placed on hold in accordance with the licensee's FFD policy. The NRC Senior Resident Inspector has been notified.
ENS 5801228 October 2025 23:04:00NRC Region 1PennsylvaniaSusquehannaGE-4The following is a summary of information provided by the licensee via phone and email: At 1904 EDT on 10/28/2025, there was a full reactor scram at Susquehanna Unit 2 from 100 percent power. All systems operated as expected, and the plant is stable in mode 3 with decay heat removal via the main condenser. The cause of the scram is under investigation. Unit 1 was not affected. Concurrent with the Unit 2 scram, the control room received a report of a fire outside of the protected area near the Susquehanna Steam Electric Station 500-kilovolt switchyard. The local fire department responded to the site with lights and sirens active which caused heightened public concern on social media. An event of potential public interest notification was made to the Pennsylvania Emergency Management Agency (PEMA). It was determined no fire existed, no actions were taken by the offsite fire company, and no personnel were injured during the event. Whether the reported fire and the reactor scram are related, is being investigated. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(2)(xi) for the unplanned actuation of the reactor protection system while the reactor is critical and for the offsite notification to PEMA. The NRC Resident Inspector has been notified.
ENS 5807511 October 2025 10:09:00NRC Region 1New JerseyHope CreekGE-4The following information was provided by the licensee via phone and email: This sixty-day telephone notification is being made per 10 CFR 50.73(a)(2)(iv)(A) under the provision 10 CFR 50.73(a)(1), as an invalid actuation of containment isolation valves in more than one system. On October 11, 2025, while in mode 5 for a refueling outage, an invalid actuation signal occurred while performing preventative maintenance on a 120V AC inverter. At the time of the event, one channel of the refuel floor exhaust (RFE) high radiation monitor was tripped due to a scheduled electrical bus outage. This electrical bus outage, in combination with the unexpected loss of power from the 120V AC inverter on another channel, caused the actuation of containment isolation valves in more than one system. The actuation was not the result of an actual plant condition and, therefore, is invalid. The containment isolation valves functioned as designed for the actuation signal received. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 579696 October 2025 12:33:00NRC Region 1New JerseySalemWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone: A licensee non-licensed supervisor failed a random fitness-for-duty test. The individual was not on-site at the time of the determination. The individual's access has been revoked. The NRC Resident Inspector has been notified.
ENS 5791210 September 2025 02:50:00NRC Region 1ConnecticutMillstoneCE

The following information was provided by the licensee via phone and fax: Entry into shutdown technical specification action statement due to an identified breach in ventilation ductwork. At 2250 EDT on September 9, 2025, it was discovered that there was degraded manway sealant on the manway to fire damper HV-298A. This degraded sealant results in a direct path from the enclosure building to the atmosphere, challenging the enclosure building boundary. This condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(C). There is no impact on the health and safety of the public or plant personnel. The plant is currently in a 24-hour technical specification action statement (3.6.5.2) for Unit 2. Unit 3 is not impacted and continues to operate at 100 percent power. The Resident Inspector has been notified.

  • * * RETRACTION ON SEPTEMBER 12, 2025, AT 0908 EDT FROM JARED FARLEY TO ERIC SIMPSON * * *

The following information was provided by the licensee via phone and fax: Millstone Unit 2 is retracting NRC Event Notification (EN) 57912, made on September 10, 2025, at 0523 EDT, regarding a condition identified at Millstone Power Station Unit 2. The condition involved degraded sealant on manways to fire dampers HV-298A/B/G, which resulted in a direct path from the enclosure building to the atmosphere, challenging the integrity of the enclosure building boundary. This condition was initially reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(C) for an event or condition that could have prevented the fulfillment of a safety function (control of release of radioactive material). A subsequent review using additional information on hatch design and actual seating surface determined that there is reasonable assurance the enclosure building boundary remained operable and retained its safety function to control the release of radioactive material and mitigate the consequences of an accident. Based on this assessment, Unit 2 exited Technical Specification action statement 3.6.5.2, and the condition is not reportable under 10 CFR 50.72(b)(3)(v)(C). Therefore, NRC EN 57912 is being retracted. The Resident Inspector has been notified. Notified R1DO (Ford).

ENS 578994 September 2025 15:10:00NRC Region 1PennsylvaniaPeach BottomGE-4The following information was provided by the licensee via phone email: On September 4, 2025, at 1110 EDT, it was determined that the units are in an unanalyzed condition. A review of DC control circuit protection schemes identified circuits which are uncoordinated due to inadequate fuse sizing. This results in a concern that postulated fire damage in one area could cause a short circuit without adequate protection, leading to the unavailability of equipment credited for 10 CFR 50 Appendix R safe shutdown. This condition is not bounded by existing design and licensing documents; however, it poses no impact to the health and safety of the public or plant personnel. Therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). Compensatory actions for affected fire areas have been implemented. The NRC Senior Resident Inspector has been notified.
ENS 5787820 August 2025 00:30:00NRC Region 1New JerseyHope CreekGE-4The following information was provided by the licensee via phone and email: At 2030 EDT on 08/19/2025, it was discovered that the main control room master fire control panel '10-C-672' had faulted and could no longer receive information from any remote panel. Due to this condition, the panel, and thereby the main control room, is unable to receive fire alarms. This is an eight-hour, non-emergency notification for a loss of emergency assessment capability. This event is reportable in accordance with 10 CFR 50.72(b)(3)(xiii) because the condition affects the evaluation of all emergency action levels for an emergency initiating condition. There is no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The Lower Alloways Creek Township will be notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Fire watches have been posted at remote panels and other required areas as a compensatory measure until the fire computer is returned to service.
ENS 5784431 July 2025 21:44:00NRC Region 1MarylandCalvert CliffsCEThe following information was provided by the licensee via phone and email: At 1744 EDT, on 7/31/2025, it was discovered both trains of control room emergency ventilation (CREVS) and control room emergency temperature system (CRETS) were simultaneously inoperable due to a damper going shut in the control room ventilation system. The damper went back to its normal open position in less than a minute. Due to this inoperability, the system was in a condition that could have prevented the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified." The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Multiple technical specification limiting conditions for operation (LCOs) such as LCO 3.0.3, 3.7.8, and 3.7.9 were entered as a result of this event.
ENS 5782222 July 2025 19:10:00NRC Region 1PennsylvaniaSusquehannaGE-4The following information was provided by the licensee via phone and email: At 1510 (EDT) with Unit 1 in mode 1 at 96 percent reactor power, the reactor was manually scrammed due to loss of main transformer cooling. The scram was not complex, all systems responded normally post-scram. Main turbine bypass valves opened automatically to maintain reactor pressure. Operations responded to stabilize the plant. High pressure coolant injection momentarily injected into the reactor vessel and was subsequently placed in standby. Reactor water level has stabilized and is being maintained with the '1B' reactor feed pump. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 2 was not impacted. Due to the reactor protection system actuation while critical and the emergency core coolant system discharge to the reactor coolant system, this event is being reported as a four-hour and eight-hour non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B), 10 CFR 50.72(b)(2)(iv)(A), and 10 CFR 50.72(b)(3)(iv)(A). The Unit 1 reactor is currently stable in mode 3. An investigation is in progress into the cause of the loss of main transformer cooling. There was no impact to the health or safety of the public or plant personnel. The NRC Resident Inspector has been informed. The state of Pennsylvania has been informed.
ENS 577942 July 2025 12:42:00NRC Region 1MarylandCalvert CliffsCEThe following information was provided by the licensee via phone and email: At 0842 EDT on 7/2/25 with Unit 2 in mode 1 at 100 percent reactor power, an actuation of the emergency safety features actuation system (ESFAS) undervoltage (UV) occurred on the safety related 4kV bus '21' during steady state conditions. The cause of the UV actuation was the loss of the 13/4 kV transformer 'U-4000-12' due to its feeder breaker tripping open. The '2A' emergency diesel generator automatically started as designed when the UV signal was received and re-powered 4kV bus '21'. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the ESFAS. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5770815 May 2025 12:20:00NRC Region 1New HampshireSeabrookWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: At 0820 EDT on May 15, 2025, it was determined that a NextEra Energy Seabrook non-licensed supervisor failed a test specified by the Fitness For Duty testing program. The individual's unescorted access has been terminated. This event is being reported pursuant to 10 CFR 26.719(b)(2)(ii). The NRC Resident Inspector has been notified.
ENS 5770310 May 2025 15:30:00NRC Region 1ConnecticutMillstoneCE
Westinghouse PWR 4-Loop
The following information was provided by the licensee via phone and fax: On May 10, 2025, at approximately 1130 EDT, security discovered a full, un-opened can of beer in a rental vehicle inside the protected area. Security took possession of the item and removed it from site. The NRC Resident Inspector and Connecticut State Department of Energy and Environmental Protection were notified.
ENS 577937 May 2025 01:08:00NRC Region 1ConnecticutMillstoneWestinghouse PWR 4-LoopThe following is a summary of information that was provided by the licensee via phone and fax: Millstone Power Station Unit 3 is submitting a 60-day telephonic notification in lieu of a licensee event report (LER) submittal as allowed by 10 CFR 50.73 (a)(1) for an invalid system actuation reportable under 10 CFR 50.73(a)(2)(iv)(A). On May 6, 2025, at approximately 2108 EDT, while Millstone Power Station Unit 3 was in mode 5 during a refueling outage, an invalid safety injection (SI) signal was initiated. The actuation was not the result of intentional manual actuation and not in response to actual plant conditions requiring safety system operation. This resulted in the automatic start of both emergency diesel generators (EDGs), and the complete initiation on both trains of the following: main steam line isolation, containment isolation phase 'A', and safety injection signal. No injection into the reactor coolant system occurred, and the EDGs remained unloaded. All equipment not administratively locked out responded as designed, and the plant remained stable throughout the event. Control room operators responded in accordance with appropriate operating procedures and restored the affected systems. This notification is made pursuant to the reporting requirements specified in 10 CFR 50.73(a)(2)(iv)(A) for an invalid actuation of one of the systems listed in 10 CFR 50.73(a)(2)(iv)(B)- including safety injection signal, containment isolation signal, and start of both emergency diesel generators. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector was notified of the event.
ENS 576947 May 2025 01:08:00NRC Region 1ConnecticutMillstoneWestinghouse PWR 4-Loop

The following is a summary of information that was provided by the licensee via phone and fax: At 2108 EDT, on May 6, 2025, with Unit 3 in mode 5 at zero percent power, the plant received main steam line isolation, containment isolation phase 'A', and a safety injection signal which caused the emergency diesel generator to automatically start. The initiation signals were cause by inadvertent clearing of the pressurizer pressure low interlock during maintenance. There was no impact to decay heat removal, no injection into the core, and no loading of the emergency diesel generator. Operations staff responded and returned the plant to normal mode 5 operations. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM TED DI ANGELO TO BRIAN P. SMITH AT 1238 EDT ON 06/19/25 * * *

The following is a summary of information that was provided by the licensee via phone and email: Millstone Unit 3 is retracting NRC event notification (EN) 57694 regarding the inadvertent main steam line isolation, containment isolation phase 'A' and a safety injection (SI) signal which caused the emergency diesel generators to automatically start on May 6, 2025. This was reported as a valid actuation under 10 CFR 50.72(b)(3)(iv)(A). Subsequent evaluation has determined that the actuations were the result of an invalid signal caused by pinching a wire during a maintenance activity, which automatically unblocked the P-11 permissive. P-11 is a reactor protection permissive that automatically enables SI actuation when pressurizer pressure increases above 2000 psia. The permissive was unblocked as the result of the spiked pressurizer pressure indication caused by the pinched wires coincident with bistables associated with a separate pressurizer pressure channel tripped to support rescaling activities. With the plant shutdown, steam line pressures were low which met the condition to require a SI actuation with P-11 unblocked. This unblocking and resultant actuation was not a result of valid signals and was not an intentional manual actuation. The pinching of a wire causing a spike is not a valid signal and was not representative of actual plant conditions. Therefore, this condition is not reportable, and NRC EN 57694 is being retracted. The basis for this conclusion has been provided to the acting NRC Senior Resident Inspector." Notified R1DO (Warnek)

ENS 576528 April 2025 00:00:00NRC Region 1New HampshireSeabrookWestinghouse PWR 4-Loop

The following information was provided by the licensee via phone and email: On April 7, 2025, at 2000 EDT, it was discovered that all pumps in the auxiliary feedwater system were inoperable due to the loss of control power to the `B' train emergency feedwater (EFW) flow control valve which supplies the `D' steam generator. The redundant `A' Train EFW flow control valve for the `D' steam generator remains functional, as well as the capability of the auxiliary feedwater system to supply all steam generators. The `A' and `B' EFW flow control valves are arranged in a series configuration for each steam generator. Failure of any of the 8 EFW flow control valves to meet its surveillance requirements will render all EFW pumps inoperable per technical specifications (TS). This condition is being reported pursuant to 10 CFR 50.72(b)(3)(v)(B). The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Troubleshooting is ongoing for the cause of the loss of control power. The licensee is currently in technical specification limiting condition for operation 3.7.1.2 action statement 'D' to restore at least one auxiliary feedwater pump to operable status as soon possible.

  • * * RETRACTION ON 04/09/2025 AT 1049 EDT FROM BOB MURRELL TO JORDAN WINGATE * * *

The following information was provided by the licensee via phone and email: The purpose of this notification is to retract a previous report made on 04/08/2025 at 1344 EDT, EN 57652. Notification of the event to the Nuclear Regulatory Commision was initially made because of declaring all pumps in the emergency feedwater system inoperable in response to discovering the loss of control power to the `B' train emergency feedwater (EFW) flow control valve, which supplies the `D' steam generator. The redundant `A' train EFW flow control valve for the `D' steam generator remained functional, as well as the capability of the EFW system to supply all steam generators. Subsequent to the initial report, NextEra has concluded that the loss of control power to the `B' train EFW flow control valve did not prevent EFW from fulfilling its safety function. Specifically, the `A' train of EFW was fully capable of fulfilling all EFW safety functions. Therefore, this event is not considered a safety system functional failure and is not reportable pursuant 10 CFR 50.72(b)(3)(v)(B). The NRC Resident Inspector has been notified. Notified R1DO (Schussler)

ENS 5761518 March 2025 14:26:00NRC Region 1ConnecticutMillstoneWestinghouse PWR 4-Loop

The following information was provided by the licensee via phone and fax: At 1026 (EDT) on March 18, 2025, it was discovered that the secondary containment boundary door was found fully open, rendering the secondary containment boundary inoperable, therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72 (b)(3)(v). The door was closed at 1029 on March 18, 2025, and the secondary containment boundary was declared operable. There is no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. There has been no impact to Unit 2 and Unit 3 continues to operate at 100 percent power.

  • * * RETRACTION ON 04/04/25 AT 1049 EDT FROM RYAN ROBILLARD TO JOSUE RAMIREZ * * *

The following information was provided by the licensee via phone and fax: This report retracts the 8-hour notification made on March 18, 2025, for NRC Event Number EN #57615. NRC Event report number 57615 describes a condition at Millstone Power Station Unit 3 (MPS3) where a secondary containment boundary door was found fully open, rendering the secondary containment boundary inoperable. This condition was reported in accordance with 10CFR 50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of a safety function to mitigate the consequences of an accident. Upon further review of the conditions that existed at the time, MPS3 has concluded that the door was not blocked open. The time duration from the activation of the door security alarm to the arrival of security personnel and the subsequent closure of the door was less than four minutes. The door was left unattended for less than 40 seconds, which is less than the five-minute criteria for entry and egress without special provisions. The supplementary leak collection and release system drawdown test has sufficient margin to accommodate this unattended door time. The evaluation concluded that the secondary containment boundary remained operable throughout this event and did not lose the ability to perform its safety function to control the release of radioactive material and mitigate the consequences of an accident. The basis for this conclusion will be provided to the NRC Resident Inspector. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: This event was originally reported in accordance with 10CFR 50.72(b)(3)(v)(D) and 10CFR 50.72(b)(3)(v)(C). The licensee confirmed that the retraction is applicable to both notifications. Notified R1DO (Bickett)

ENS 575823 March 2025 15:44:00NRC Region 1PennsylvaniaLimerickGE-4The following information was provided by the licensee via phone and email: At 1044 EST, Unit 2 high pressure coolant injection (HPCI) system was declared inoperable per technical specification 3.5.1.C.1 during planned surveillance testing due to test equipment failure and subsequent inadvertent isolation of the outboard HPCI turbine exhaust line vacuum breaker primary containment isolation valve. The test equipment was removed, and the vacuum breaker isolation valve was re-opened. HPCI was restored to operable status at 1351. Due to inoperability, the system was in a condition that could have prevented the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72.(b)(3)(v)(D). There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5757527 February 2025 13:00:00NRC Region 1PennsylvaniaSusquehannaGE-4The following information was provided by the licensee via phone and email: A non-licensed supervisor had a confirmed positive for alcohol during a random fitness-for-duty test. The employee's access to the plant has been terminated. The NRC Resident Inspector has been notified.
ENS 5755518 February 2025 07:30:00NRC Region 1ConnecticutMillstoneCE
Westinghouse PWR 4-Loop

The following information was provided by the licensee via phone and email: At approximately 0230 EST on 2/18/2025, it was determined that the primary and backup methods of activating the site Emergency Response Organization (ERO) were not available. External network access was unavailable, to include access to the Dominion Energy Emergency Notification System (DEENS) rendering the system non-functional. Subsequently, the backup method for activating the station ERO was attempted and was unable to be verified. On 2/18/2025, at approximately 0400, an additional backup ERO activation phone number was provided and verified to be functional. At approximately 0740 on 2/18/2025, external network access was restored and DEENS was restored to functional. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(xiii). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 2/19/25 AT 1030 EST FROM JOSHUA LINDSEY TO JORDAN WINGATE * * *

The following information was provided by the licensee via phone and email: It has since been determined that the (backup) phone number provided at 0400 would not have worked to activate the ERO. The NRC Resident Inspector has been notified. Notified R1DO (Deboer)

ENS 575365 February 2025 19:00:00NRC Region 1New JerseyHope CreekGE-4The following information was provided by the licensee via phone and email: A non-licensed employee supervisor had a confirmed positive during a random fitness for duty test. The employee's unescorted access to the plant has been revoked. The NRC Senior Resident Inspector has been notified.
ENS 575355 February 2025 15:02:00NRC Region 1PennsylvaniaBeaver ValleyWestinghouse PWR 3-LoopThe following information was provided by the licensee via phone and email: At 1002 EST, on February 5, 2025, with Unit 2 in mode 1 at 100 percent power, the reactor automatically tripped due to lowering 'B' steam generator level. All control rods fully inserted into the core and the auxiliary feedwater system automatically started as designed in response to the full power reactor trip. The trip was not complex, with all systems responding normally post-trip. There was no equipment inoperable prior to the event that contributed to the reactor trip or adversely impacted plant response. Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the main condenser using the condenser steam dump valves. Unit 1 is not affected and remains at 100 percent power and stable. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, this event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of the auxiliary feedwater system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 575301 February 2025 01:15:00NRC Region 1New JerseyHope CreekGE-4The following information was provided by the licensee via phone and email: On 1/31/2025, at 2015 EST, a technical specification required shutdown was initiated at Hope Creek Unit 1. Technical Specification 3.8.1.1.e. 'AC sources - operating' was entered on 1/31/2025, at 0735 EST, with a required action to restore at least one of the inoperable diesel generators to operable status within 2 hours. This required action was not completed within the allowed outage time; therefore a technical specification required shutdown was initiated, and this event is being reported as a four-hour, non-emergency notification per 10CFR50.72(b)(2)(i). On 1/31/2025, at 2121 EST, one of the inoperable diesel generators was restored to operable prior to the Technical Specification 3.8.1.1.e required time to be in hot shutdown. The Unit 1 shutdown was suspended at that time. Technical Specification 3.8.1.1.b remains active for one diesel inoperable. There was never an impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5743119 November 2024 18:50:00NRC Region 1New HampshireSeabrookWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: At 1350 (EST) on 11/19/2024, with Unit 1 in mode 1 at 100% power, the reactor was manually tripped due to an automatic trip of the `B' main feedwater pump turbine. The reactor trip was uncomplicated with all systems responding normally post trip. Operations stabilized the plant in mode 3. Decay heat removal is being accomplished by the steam dumps to the condenser. Emergency feedwater actuated due to low-low steam generator (water) level, as expected. This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the 'B' main feedwater pump trip is under investigation. There was maintenance involving the 'B' main feedwater pump at the time of the scram.
ENS 5743219 November 2024 18:50:00NRC Region 1New HampshireSeabrookWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: At 1350 (EST) on 11/19/2024, with Unit 1 in mode 1 at 100 percent power, the reactor was manually tripped due to an automatic trip of the `B' main feedwater pump turbine. The reactor trip was uncomplicated with all systems responding normally post trip. Operations stabilized the plant in mode 3. Decay heat removal is being accomplished by the steam dumps to the condenser. Emergency feedwater actuated due to low-low steam generator level, as expected. This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the 'B' main feedwater pump turbine trip is under investigation.
ENS 5742011 November 2024 22:31:00NRC Region 1PennsylvaniaEaver ValleyWestinghouse PWR 3-Loop

The following information was provided by the licensee via phone and email: At 2250 EST on November 11, 2024, a technical specification required shutdown was initiated at Beaver Valley Power Station Unit 2. The following technical specification limiting conditions of operation (LCOs) were entered at 1939 EST on November 11, 2024: LCO 3.6.3, containment isolation valves, condition C, one or more penetration flow paths with one containment isolation valve inoperable; required action C.1, isolate the affected penetration flow path by use of at least one closed and de-activated automatic valve, closed manual valve, or blind flange. LCO 3.7.2, main steam isolation valves (MSIVs), condition C, one or more MSIVs inoperable in mode 2 or 3; required action C.1, close MSIV within 8 hours. These technical specification required actions will not be completed within the completion time; therefore, a technical specification required shutdown was initiated, and this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i). With one main steam isolation valve inoperable, this condition is also being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The failure occurred during planned surveillance testing in preparation for reactor startup.

  • * * RETRACTION ON 12/30/2024 AT 1025 EST FROM JAMIE SMITH TO JORDAN WINGATE * * *

The following information was provided by the licensee via phone and email: On 11/12/2024 an 8-hour notification was made describing the failure of one main steam isolation valve (MSIV) to close during testing while the plant was in MODE 3. This notification was made pursuant to 10 CFR 50.72(b)(3)(v) as a condition that could have prevented the fulfillment of a safety function. Further engineering evaluation has determined that this condition was not reasonably expected to prevent the fulfillment of a safety function based on a review of the accident analyses and the redundant equipment which is known to have been capable of performing the safety functions. Therefore, this does not result in a reportable condition under this criterion. At the same time, a 4-hour notification was made pursuant to 10 CFR 50.72(b)(2)(i) as an initiation of a shutdown required by plant technical specification due to initiating a transition to MODE 4 to exit TS applicability. The plant was in hot standby (MODE 3) at the time of the event and negative reactivity was not added in order to move to MODE 4, therefore, this event is not reportable under this criterion. The NRC Resident Inspector has been notified. Notified R1DO (Lilliendahl)

ENS 5741911 November 2024 20:10:00NRC Region 1MassachusettsPilgrimGE-3The following is summary of information provided by the licensee via phone and email: On November 11, 2024, at 1510 EST, site personnel identified what appeared to be water bubbling up from the pavement adjacent to the sanitary lift station 'C' outside of the facility industrial area. Less than 100 gallons of non-radiological sanitary water ran to a catch basin connected to permitted outfall number 007. Visual inspection did not identify any odor or indication of flow at outfall number 007 discharge. By 1530, the lift station pumps had been secured, sources of influent to the lift station were removed from service, and efforts were underway to pump the tank. At 1611, an offsite notification was made to the Environmental Protection Agency's Enforcement and Compliance Assurance Division in accordance with Section B of the station's National Pollutant Discharge Elimination System (NPDES) Permit No. 0003557. The event was associated with leakage from underground sewage system piping from a non-radiological underground tank and lift station. The NRC Resident Inspector will be notified.
ENS 574889 November 2024 13:41:00NRC Region 1PennsylvaniaEaver ValleyWestinghouse PWR 3-LoopThe following information was provided by the licensee via phone and email: This 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(l) to describe an invalid specific system actuation. At 0841 EST on November 9, 2024, with Unit 2 in mode 5, at 0 percent power, an actuation of the 2-1 emergency diesel generator (EDG) occurred when an invalid start signal was generated during troubleshooting activities associated with the 2AE diesel start relay. The 2-1 EDG automatically started as designed when the start signal was received. The output breaker did not close and the 2AE emergency bus remained energized from offsite power consistent with plant design. This was a complete actuation of an EDG to start and come to rated speed, and all affected systems functioned as expected in response to the actuation. Following the actuation, the 2-1 EDG was shut down in accordance with plant procedures. Unit 1 was in mode 1 at 100 percent power and was not affected by this event. This event is considered an invalid system actuation reportable under 10 CFR 50.73(a)(2)(iv)(A). The actuation was not initiated in response to actual plant conditions or parameters and was not a manual initiation. Therefore, in accordance with 10 CFR 50.73(a)(l), this telephone notification is provided within 60 days after discovery of the event instead of submitting a written licensee event report. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5742210 October 2024 14:02:00NRC Region 1ConnecticutMillstoneWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: At 0902 EST, on 10/10/2024, with Millstone Unit 3 in mode 1 at 100 percent power, it was discovered that the secondary containment boundary was inoperable when the latch that secured a hatch that was part of the secondary containment boundary was not functional. The latch was repaired by 1115, on 10/10/2024, and the secondary containment boundary was declared operable at 1200, on 10/10/2024. The initial assessment of reportability concluded that an immediate report was not required. However, upon additional review, it has been determined that because the secondary containment boundary is a single-train system that performs a safety function, an 8-hour report was required in accordance with 10 CFR 50. 72 (b)(3)(v)(C) and (D). This report should have been made on 10/10/2024 and is late. There has been no impact to Unit 2, and Unit 3 continues to operate in mode 1 at 100 percent power. There is no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5737210 October 2024 09:57:00NRC Region 1MarylandCalvert CliffsCEThe following information was provided by the licensee via phone and email: At 0557 EDT on 10/10/2024, with Unit 2 in mode 1 at 100 percent power, the reactor automatically tripped due to turbine generator loss of field. The trip was not complex with all systems responding normally post-trip. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Operations responded using EOP-0, post trip immediate actions, and stabilized the plant in mode 3. Decay heat is removed by discharging steam to the main condenser using the turbine bypass valves. Unit 1 is not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The exciter is suspected to being the cause and is under investigation. All control rods fully inserted.
ENS 574241 October 2024 12:38:00NRC Region 1New HampshireSeabrookWestinghouse PWR 4-LoopThe following information was provided by the licensee via phone and email: NextEra Energy Seabrook LLC. makes the following notification under 10 CFR 21.21(d)(3)(i) of a defect found in a GE - Hitachi Relay, CR120B (Model #DD945E118P0060) during pre-installation bench testing. During bench testing, the relay failed to energize and transfer all associated contacts. The relay was purchased from GE - Hitachi (GEH) as safety-related, GE CR-120B relays. All GE CR-120B relays that were purchased in the same batch as the failed relay were located and quarantined in order to be returned to GEH for forensic testing. NextEra Energy Seabrook, LLC has concluded that this defect constitutes a substantial safety hazard (SSH). A SSH exists because the nature of the defect was such that, if installed in certain safety-related applications and failed, it would have prevented the fulfillment of a safety function. On November 12, 2024, the Seabrook site Vice President was notified of the requirement to report this event under 10 CFR 21.21. This is a non-emergency notification required by 10 CFR 21.21(d)(3)(i). A written notification will be provided in accordance with 10 CFR 21.21(d)(3)(ii). Because the defect was discovered prior to installation, there was no impact to safety-related equipment. The NRC Senior Resident Inspector has been informed.
ENS 5743726 September 2024 22:01:00NRC Region 1New YorkFitzPatrickGE-4The following information was provided by the licensee via phone and email: This notification is a 10 CFR 21.21(a)(2) interim report for General Electric thermal overload relay, model CF124G011, part number DD317A7861P003. A sample of overload relays were sent to PowerLabs for parts quality initiative testing. The results were reviewed by James A. FitzPatrick Nuclear Power Plant (JAF) and a deviation in one relay component was discovered. Testing identified a failure to latch on trip, which is a deviation from the performance characteristics of the relay. Under normal operation, the relay would latch in the tripped state requiring a manual reset of the relay. If the relay with the deviation were installed, the relay would trip when required; however, it would automatically reset. The unexpected reset could result in unintended cycling of associated equipment including repeated exposure to inrush current and potential damage. Bench testing would be expected to identify this condition prior to installation. Based on a review, this potential condition does not affect installed equipment. The affected relay was stored at JAF since July 1998. The cause of the deviation cannot be investigated because the part is not available; however, the evaluation of the potential effect of the condition on equipment where the relay could have been used at JAF is ongoing, and it is expected to be completed by February 28, 2025. This notification is being submitted as an interim report per 10CFR21.21(a)(2). The NRC resident inspector has been notified.
ENS 5733323 September 2024 11:20:00NRC Region 1New YorkFitzPatrickGE-4

The following information was provided by the licensee via phone and email: At 0720 EDT on September 23, 2024, James A. FitzPatrick was at 100 percent power when an automatic scram occurred as a result of a main turbine trip due to an automatic trip of the generator output breakers; the cause is still under investigation. The scram was not complex. The automatic scram inserted all control rods. A subsequent reactor pressure vessel (RPV) low water level resulted in a group 2 isolation and initiation of high pressure coolant injection (HPCI) and reactor core isolation cooling (RCIC) systems. RCIC did inject, but HPCI did not inject, as expected, based on RPV water level recovery with the feedwater system. Reactor pressure is being maintained by main steam line bypass valves. The plant is stable in Mode 3 with the 'A' reactor feed pump maintaining RPV water level. The initiation of the reactor protection system (RPS) due to the automatic scram signal while critical is reportable per 10 CFR 50.72(b)(2)(iv)(B). The general containment Group 2 isolations and HPCI and RCIC system actuations are reportable per 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The group 2 containment isolation affects multiple systems.

  • * * UPDATE ON 9/23/2024 AT 1540 EDT FROM RYAN PERRY TO SAMUEL COLVARD * * *

On 9/23/2024 at 1156 EDT Constellation communications provided a media statement to Oswego area news media contacts summarizing the events that had occurred at Nine Mile Point Unit 2 and FitzPatrick Unit 1. This is a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(xi). The NRC Senior Resident Inspector has been notified. Notified R1DO (Dimitriadis)

ENS 5733423 September 2024 11:20:00NRC Region 1New YorkNine Mile PointGE-5

The following information was provided by the licensee via phone and email: On 9/23/2024 at 0720 EDT, with Unit 2 in mode 1 at 100 percent power, the reactor automatically scrammed due to turbine stop valve closure on a turbine trip. The scram was not complex. Due to the reactor protection system (RPS) actuation while critical, this event is being reported as a four hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Following the scram, reactor water level dropped below level 2 (108.8 inches), starting high pressure core spray (HPCS) and reactor core isolation cooling (RCIC); both injected into the reactor. RCIC is being used with turbine bypass valves to remove decay heat. Due to the emergency core cooling systems HPCS and RCIC discharging into the reactor coolant system, this event is being reported a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(A), and an eight hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A). In addition, with reactor water level below level 2 (108.8 inches), primary containment isolation signals actuated resulting in group 2 recirculation sample system isolation, group 3 traveling in-core probe (TIP) isolation valve isolation, group 6 and 7 reactor water cleanup isolation, group 8 containment isolations, and group 9 containment purge isolations. This event is being reported as an eight hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A). Operations responded using procedure N2-EOP-RPV (1-3) and stabilized the plant in mode 3. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector was informed. There was no impact on Unit 1.

  • * * UPDATE ON 9/23/2024 AT 1550 EDT FROM RYAN LOOMIS TO IAN HOWARD * * *

On 9/23/2024 at 1156 EDT Constellation communications provided a media statement to Oswego area news media contacts summarizing the events that had occurred at Nine Mile Point Unit 2 and FitzPatrick Unit 1. This is a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(xi). The NRC Senior Resident Inspector has been notified. Notified R1DO (Dimitriadis), NRR EO (Felts), and IR MOC (Grant).

ENS 5728221 August 2024 16:00:00NRC Region 1ConnecticutMillstoneWestinghouse PWR 4-LoopThe following information was provided by the licensee via fax and phone: At 1200 EDT on 8/21/2024, with Millstone unit 3 in mode 1 at 100 percent power, it was discovered that the secondary containment boundary was inoperable while maintenance activities on the system were in progress. Therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(C) and (D). There is no impact on the health and safety of the public and plant personnel. The NRC Resident Inspector has been notified. Unit 3 continues to operate in mode 1 at 100 percent power with actions in progress to restore the system to operable within the technical specification allowed outage time. There has been no impact to unit 2, which remains at 100 percent power. The state of Connecticut and local towns were notified.
ENS 5723318 July 2024 19:24:00NRC Region 1MarylandCalvert CliffsCEThe following information was provided by the licensee via phone and email: At 1524 (EDT) on 07/18/2024, with Unit 2 in Mode 1 at 100 percent power, the reactor automatically tripped due to a turbine trip. The trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 1 implemented AOP-7K (abnormal operating procedure), overcooling event, due to a grid transient. Operations responded and stabilized Unit 1 in Mode 1 at 100 percent power. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: All rods fully inserted. There were no other specified system actuations.
ENS 5730210 July 2024 13:02:00NRC Region 1New JerseyHope CreekGE-4The following information was provided by the licensee via phone and email: A 10 CFR 50.73(a)(1) invalid specified system actuation reported under 10 CFR 50.73(a)(2)(iv)(a) invalid actuation of residual heat removal (RHR). This 60-day telephone notification is being made per 10 CFR 50.73 (a)(2)(iv)(a) under the provision of 10 CFR 50.73 (a)(1) as an invalid actuation of the RHR. On July 10, 2024, while at 100 percent power, a partial train actuation of RHR was initiated by an invalid actuation signal while performing RHR valve logic testing. The cause for the RHR system logic actuation was due to improper configuration of an emergency core cooling system (ECCS) logic tester. The RHR system started and functioned as designed for the actuation signals it received from the ECCS logic tester. There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector was notified.
ENS 5722110 July 2024 11:28:00NRC Region 1PennsylvaniaPeach BottomGE-4The following information was provided by the licensee via phone and email: At 0728 EDT on July 10, 2024, with Unit 2 in Mode 1 at 24 percent power, the reactor automatically scrammed due to a manual turbine trip. The (reactor) scram was not complex with all systems responding normally. Reactor vessel level reached the low-level set-point following the scram, resulting in valid Group 2 and Group 3 containment isolation signals. Due to the reactor protection system actuation while critical, this event is being reported as a four hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for the Group 2 and Group 3 isolations. Operations responded using emergency operating procedures and stabilized the plant in Mode 3. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 3 was not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5717213 June 2024 17:31:00NRC Region 1New YorkFitzPatrickGE-4At 1331 EDT on 6/13/2024, it was determined that a non-active licensed operator supervisor tested positive in accordance with the fitness for duty testing program. The individual's authorization for site access has been denied. The NRC Resident Inspector has been notified.
ENS 5714525 May 2024 08:00:00NRC Region 1ConnecticutMillstoneCE
Westinghouse PWR 4-Loop
The following information was provided by the licensee by phone and email: A 50 ml bottle of vodka was found in the Unit 3 debris basket on the exterior of the intake structure. The bottle likely came from the ultimate heat sink (Niantic Bay) during normal backwash operations by the system that collects debris. Security has discarded the contraband. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers report guidance: The bottle was found unsealed.
ENS 5713219 May 2024 04:30:00NRC Region 1PennsylvaniaBeaver ValleyWestinghouse PWR 3-LoopThe following information was provided by the licensee via email: At 0030 (EDT) on 5/19/24, with Beaver Valley Unit 1 in mode 1 at 14 percent power, the reactor was manually tripped due to inability to control the A steam generator water level. The trip was not complex, with all systems responding normally post-trip. The turbine driven auxiliary feedwater pump automatically started on a valid actuation signal. All control rods inserted into the core. Operations responded and stabilized the plant. Decay heat is being removed by the feedwater system and the main condenser. Beaver Valley Unit 2 is unaffected. Due to the reactor protection system system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Due to the emergency safety feature system actuation (automatic start of the turbine driven auxiliary feedwater pump) while critical, this event is being reported as an eight-hour, non-emergency notification per 10CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been verbally notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Unit 1 is stable on off-site power, normal configuration. All emergency systems are available.
ENS 571209 May 2024 20:29:00NRC Region 1New YorkFitzPatrickGE-4

The following information was provided by the licensee via phone and email: At 1629 EDT on 05/09/2024, the high pressure coolant injection (HPCI) system was declared inoperable due to a pinhole through-wall leak identified on the seal drain line for 23HOV-1 (HPCI trip throttle valve) downstream of the restricting orifice 23RO-137A. The location of the defect is in the class 2 safety related piping. HPCI is a single train safety system and this notification is being made in accordance with 10 CFR 50.72(b)(3)(v)(D). The NRC Senior Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: This pinhole leak was discovered during normal operator rounds. Although HPCI is declared inoperable and in a 14-day limited condition of operation, the system function remains available. In addition, all other ECCS systems are currently operable. Compensatory measures (walkdowns) have been implemented to ensure the leak rate does not significantly increase.

  • * * RETRACTION ON 06/20/2024 AT 1423 EDT FROM CAMERON KELLER TO ROBERT THOMPSON * * *

FitzPatrick performed an additional technical evaluation of the steam leak identified on May 9, 2024. The evaluation concluded that the HPCI system would have remained operable and performed its specified safety function with a postulated complete failure of this pipe, considering its size, location, and impact of the leak. Additionally, all components in the vicinity would have retained their required safety functions. Based on this conclusion, EN 57120 is being retracted. The NRC Senior Resident Inspector has been notified. Notified R1DO (Elkhiamy).

ENS 571159 May 2024 12:00:00NRC Region 1PennsylvaniaBeaver ValleyWestinghouse PWR 3-LoopThe following information was provided by the licensee via phone and email: At 0800 EDT on May 9, 2024, it was identified during leak rate testing that through-wall flaws existed on reactor plant river water piping inside the containment building. This determination resulted in a containment bypass condition such that a gaseous release could have occurred at a location not analyzed for a release in the loss of coolant accident dose consequence analysis. This condition is not bounded by existing design and licensing documents. Evaluation of the condition of the piping is ongoing to support repair prior to startup. With the plant currently in cold shutdown, the containment, as specified in Technical Specification 3.6.1, is not required to be operable. There was no impact on the health and safety of the public or plant personnel. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(A), 10 CFR 50.72(b)(3)(ii)(B), and 10 CFR 50.72(b)(3)(v)(C). The NRC Resident Inspector has been notified.
ENS 571033 May 2024 08:11:00NRC Region 1New JerseyHope CreekGE-4The following information was provided by the licensee via email: At 0411 EDT on 5/03/2024, it was determined that primary containment did not meet TS (Technical Specification) 4.6.1.2 (surveillance) requirement due to a primary containment leak rate test exceeding `La (allowable leakage rate). This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The final observed leak rate is still being calculated as the test is still within the stabilization period. Testing is allowed within the stabilization period for an unspecified amount of time. Short term corrective actions are to identify and repair any leak paths. No mode changes are required due to this event.