PNO-III-10-014, Shutdown of Braidwood Reactors Unit 1 & 2

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PNO-III-10-014 - Shutdown of Braidwood Reactors Unit 1 & 2
ML102290293
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 08/17/2010
From: Moore C, Richard Skokowski
NRC/RGN-III
To:
References
PNO-III-10-014
Download: ML102290293 (1)


August 17, 2010 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE - PNO-III-10-014 This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verification or evaluation, and is basically all that is known by the Region III staff on this date.

Facility Braidwood Units 1 and 2 Exelon Generation Co.

Braceville, IL Docket: 50-456 and 50-457 License: NPF-72; NPF-77 Licensee Emergency Classification Notification of Unusual Event Alert Site Area Emergency General Emergency X Not Applicable

SUBJECT:

SHUTDOWN OF BRAIDWOOD REACTORS UNIT 1 & 2 DESCRIPTION:

On August 16, 2010, Exelons Braidwood Station informed the NRC headquarters operation center, the resident inspectors, and Region III (Chicago) that Unit 2 automatically tripped as the result of a main generator fault that occurred at approximately 2:00 a.m. CDT. Following the Unit 2 reactor trip, the reactor shut down as designed. All safety systems functioned normally except for a failed open auxiliary feedwater flow control valve. Operators quickly detected this problem and manually utilized a redundant valve in the flow path to control auxiliary feedwater flow to the Steam Generator.

Thirteen minutes later, Unit 1 automatically tripped on a turbine trip due to a loss of main condenser vacuum. The loss of main condenser vacuum was caused by the tripping of two of the three main condenser circulating water pumps. The main condenser removes turbine heat via lake water. During the summer, three circulating water pumps are used to cool the main condensers at the Braidwood Station. The degraded main condenser vacuum on Unit 1 caused plant operators to utilize the Unit 1 Steam Generator Atmospheric Power Operated Relief Valves to maintain reactor coolant temperature. The steam release created a loud noise, which could be heard by plant neighbors. The steam contained tritium at concentrations lower than the regulatory limit for the public.

The NRC resident inspectors and specialists in the NRCs Region III office in Lisle, Ill., are closely evaluating the situation. Agency resident inspectors, who are stationed at the plant, are verifying that the utility is addressing the causes of both reactors being shut down; and the utilitys repair plans. They will continue to monitor the plants activities.

The licensee notified the State of Illinois on August 16, 2010. The information in this preliminary notification has been reviewed with licensee management and is current as of 10:00 a.m. on August 17, 2010.

CONTACTS:

Richard Skokowski Carl Moore 630/829-9620 630/829-9732 ML102290293