ML19332E987

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Monthly Operating Repts for Nov 1989 for Point Beach Nuclear Plant Units 1 & 2.W/891208 Ltr
ML19332E987
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 11/30/1989
From: Fay C, Krause C
WISCONSIN ELECTRIC POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
CON-NRC-89-154 VPNPD-89-640, NUDOCS 8912130236
Download: ML19332E987 (9)


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1Electnc PCNER COMPANY:

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30 231 W Michigan Po. Box 2046. MMaukee. WI 53204 (414)221 2345 p b. , <

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4 .jL December 8, 1989 NUCLEAR: REGULATORY COMMISSION -

iDocument Control Desk Mail; Station'P1-137-

. Washington, D.;C..'20555 Gentlemen: . .<

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QQCKETS'50-266"AND 50-301' I MONTHLY OPERATING' REPORTS ,l POINT BEACH NUCLEAR PLANT, UNITS 1 AND-2

-Aktached are: monthly / operating reports for Units 1 and 2, o<

Point Beach Nuclear Plant, for the calendar month of November 1989; i

'f l Very.truly.yours, j

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j#7 C. W Fay.

Vi President

.N clear Power Attachments  ;

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-Copies to'R. S. Cullen, PSCW NRC Regional Administrator, Region III m

NRC Resident Inspector 8912130236 891130 PDR= ADOCK 05000266 .

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s OPERATING DATA REPORY s DOCKET NO. 50-266 .

DATE December 7, 1989 COMPLETED BY C. W. KRAUSE TELEPHOPE 414 221 2001 OPERATING STATUS

1. UNIT NAME! POINT BEACH NUCLEAR PIANT UNIT 1 . NOTES .
2. FMPORTING PERIOD: NOVEMBER 1989 . .
3. LICENSED THERMAL POWER (MWT): 1518 . .
4. NAMEPLATP: .lATING (GROSS MWE): 523.8 . .
5. DESIGN ELECTRI"AL RATING (NET MWE): 497. . .

G. MAXIMUM DEPENDABLE CAPACITY (GROSS MWE): 509. . .

7. MAXIMUM DEPL*NDABLE CAPACITY (NET MWE): 485. . . . . . . . . . . . . . . . . . . . . . . .
8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:

NOT APPLICABLE

9. POWER LEVEL TO WHICH RESTRICTED, 1F ANY (NET MWE}: NOT APPLICABLE
10. FEASONS FOP RESTRICTIONS, (IF ANY): NOT APPLICABLE THIS MONTH TR TO DATE CUMULATIVE
11. HOURS IN REPORTING PERIOD 720 8,016 167,160
12. NUMBER OF HOURS REACIOR WPLS CRITICAL 720.0 6,984.3 137,599.8
13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 652.7
14. HOURS GENERATOR ON LINE 720.0 6,962.8- 134,795.3
15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 837.9
16. GROSS THERMAL ENERGY GENERATED (MWH) 1,081,457 10,001,058 187,343,882
17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 358,2PO 3,394,010 63,223,060
18. NET ELECTRICAL ENERGY GENERATED (MWH) 352,341 3,240,328 60,224,796
19. UNIT SERVICE FACTOR 100.0 86.9 80.6
20. UNIT AVAILABILITY FACTOR 100.0 86.9 81.1
21. UNIT CAPACITY FACTCR (USING MDC NET) 100.9 83.3 73.9
22. UNIT CAPACITY FACTOR (USING DER NET) 98.5 81.3 72.5
23. UNIT FORCED OUTAGE RATE 0.0 0.0 1.8
24. SHUTDOWNS SCHEDULED OVER NEIT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH):

Forty-two day refueling and maintenance outage scheduled to comance March 30, 1990.

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25. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: NOT SHUTDOWN DATA REPORTED AND FACTORS CAICULATED AS REQUESTED IN NRC LETTER DATED SEPTEMBER 22, 1977 4 g- p g g. W y*m ,. ,,, .1e .:. p w g ya. p & 9 y m <vw.- -+-ee--a..+ -4ar+--va..

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. DOCKET NO.- 50-266 ..~ .

UNIT NAME- Point Beach, Unit 1 . *-

DATE December 7, 1989 COMPLETED BY C. W. Krause TELEPHONE -414/221-2001 AVERAGE DAILY UNIT POWER LEVEL MONTH NOVEMBER 1989 AVERAGE AVERAGE AVERAGE DAILY DAILY DAILY POWER LEVEL POWER LEVEL FOWER LEVEL DAY MWe NET DAY MWe NET DAY MWe NET 1 494 11 486 21 495 2 493 12 474 22 494 3 494 13 495 23 494 4 495 14 495 24 494 5 491 15 496 25 495 6 495 16 495 26 495 7 486 17 495 27 495 8 455 18 495 28 496 9 454 19 494 29 495 10 456 20 496 30 495 EQR-28a (04-86)

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. .. UNIT STCTDOWNS AND POWER REDUCTIONS DOCKET NO.- 50-266 _.

UNIT NAME Point Beach Unit 1 DATE December 7, 1989 - '

REPORT MONTH NOVEMBER 1989 COMPLETED BY C. W. Krause.~

TELEPHONE 414/221-2001 c

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O 4 d^ N 4-4 Q n C O to c O 1-4 o

.* -e-4 14 O tP O IEe dn e 90 vs 'o c o vo Oc g g Licensee Event gy No. Date g o g] 'Cause & Corrective Action a s- m $gOvo Report No. >,o Ou To Prevent Recurrence o ose m u 2:.c v2 1F: Forced 2 Reason: 3 Method:

  • Exhibit F-Instructions S: Scheduled A - Equipment Failure (explain) 1 - Manual for preparation of B - Maintenance or Test 2 - Manual Scram data entry sheets C - Refueling 3 - Automatic Scram LER file (NUREG-0161)

D - Regulatory Restriction 4 - Continuation of E - Operator Training & Previous Shutdown Licensing Exam 5 - Reduced Load 5 Exhibit H-Same Source F - Administrative 6 - Other (explain)

G - Operational Error (explain)

H - Other (explain)

EQR-28B (00.-87) -

+.

NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE Docket No. 50-266 Unit Name Point Beach Unit 1 Date December 7, 1989 Completed By C. W. Krause

, Telephone 414/221-2001 Unit 1 operated at approximately 494 MWe net throughout the

! period with no major load reductions.

On November 7, 1989, it was discovered that the Point Beach Nuclear Plant was in a condition which was outside.of the requirements of TS 15. 3. 7.B.1. f and 15. 3. 7.B.1.g . These TS state:

L "15.3.7 B.1.f: One of the batteries, DOS or D06, may be inoperable for a period not exceeding 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> provided the other three batteries and four battery chargers remain operable with one charger carrying the DC loads of each DC main distribution bus."

"15.3.7.B.1.g: One of the batteries, D105 or D106, may be inoperable for a period not exceeding 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> provided the other three batteries and four battery chargers remain operable with one charger carrying the DC loads of each DC main distribution bus."

On November 9, 1989, at 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br />, the PBNP Manager's Supervisory Staff determined that the DOS and D06 station batteries were technically inoperable as a result of the discovery of an original plant design deficiency which could render one or both of the two plant main DC systems inoperable as a result of a single bus fault. The potential problem had been reported to the manager - PBNP at 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br /> by our corporate l headquarters Nuclear Engineering group. Upon arrival at the plant site approximately two hours, the issue was presented to the Manager's Supervisory Staff. LER 89-009 was written to document this incident.

1 During the steam generator crevice flush, the steam generator i specific auxiliary flow indicators from the aux feed line into the steam generator were supposed to be isolated. The flow indicators from Unit 1 were isolated rather than Unit 2. They were left in i this condition for more than 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />. This is a condition L prohibited by Technical Specifications. LER 89-010 is being l drafted to document this incident.

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'O OPERATING DATA REPORT .

DOCKET NO. 50-3~J1 -

DATE December 7, 1989 COMPLETED BY C. W. KRAUSE TELEPHONE 414 221 2001 OPERATING STATUS

1. UNIT NAME: POINT BEACH NUCLEAR PLANT UNIT 2 . NOTES .
2. REPORTING PERIOD: NOVEMBER 1989 . .
3. LICENSED THERMAL POWER (MWT): 1518 . .
4. NAMEPLATE RATING (GROSS MWE): 523.8 . .
5. DESIGN ELECTRICAL RATING (NET MWE): 497. . .
6. MAXIMUM DEPENDABLE CAPACITY (GROSS MWE): 509. . .
7. MAXIMUM DEPENDABLE CAPACITY (NET MWE): 485. . . . . . . . . . . . . . . . . . . . . . . ..

O. IF CHANGES OCCUR IN CAPACITT RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:

NOT APPLICABLE

9. POWER LEVEL TO WHICH RESTRICTED, IF ANT (URT MhT,): NOT APPLICABLE
10. REASONS FOR RESTRICTIONS, (IF ANY): NOT APPLICABLE THIS MONTH YR TO DATE CUMULATIVE
11. HOURS IN REPORTING PERIOD 720 6.016 151,945
12. NUMBER OF HOURS REACIOR WAS CRITICAL 168.0 6,499.6 132,601.8
13. REACTOR RESERVE SHUTDOWN HOUES 0.0 0.6 216.7
14. HOURS GENERATOR ON LINE 132.0 6,364.7 130,461.3
15. UNIT RESERVE SHUTDOWN HOURS 0.0 4.8 302.2
16. GROSS THERMAL ENERGY GENERATED (MWH) 141,690 9,514,380 185,460,214
17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 47,730 3,263,740 62,937,440
18. NET ELECTRICAL ENERGY GENERATED (HWH) 42,431 3,112,332 59,966,754
19. UNIT SERVICE FACTOR 18.3 19.4 85.9
20. UNIT AVAILABILITY FACTOR 18.3 79.5 86.1
21. UNIT CAPACITY FACTOR (USING MDC NET) 12.2 80.1 80.6
22. UNIT CAPACITY FACTOR (USING DER NET) 11.9 78.1 79.4
23. UNIT FORCED OUTAGE RATE O.0 2.0 1.2
24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (T!PE, DATE, AND DURATION OF EACH):

NONE

25. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: NOT SHisTDOWN DATA REPORTED AND FACTORS CALCULATED AS REQUEtTTED IN NRC LETTER DATED SEPTEMBER 22, 1977

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DOCKET NOo. 50-301 . c. ...

UNIT ~NAME Point Beach, Unit'2' .

DATE December 7, 1989 COMPLETED BY C. W. Krause TELEPHONE 414/221-2001 AVERI.GE DAILY UNIT POWER LEVEL MONTH ' NOVEMBER 1989

. AVERAGE AVERAGE AVERAGE DAILY DAILY DAILY POWER LEVEL POWER' LEVEL POWER LEVEL DAY MWe NET DAY MWe NET DAY MWe NET 1 -2 11 -2 21 -12 2 -2 12 -2 22 -14

-3 -2 13 -2 23 -13 4 -2 14 -2 24 -14 5 -2 15 -2 25 35 6 -1 16 -2 26 116 7 -2 17 -5 27 262 8 -2 18 -11 28 460 9 -2 19 -3 29 501 10 -2 20 -3 30 500 EQR-28a (04-86)

- l, UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-301 6 -

UNIT NAME Point Beach Unit 2 DATE December 7, 1989 REPORT MONTH NOVEMBER 1989 COMPLETED BY C. W. Krause ~

TELEPHONE 414/221-2001 5

o 9 C^ es M D es C o U2 c o La e

- H ks o tP o Ev ce e 43 OC4 ee oe No. Date g yy t/J y "y y Licensee Event #y g] Cause & Corrective Action E-4 c- cr; ooe Report No. No oo To Prevent Recurrence o e c cr: m o

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4 ;390923 S 588 C 4 Not Applicable ZZ ZZZZZZ Continue the annual refueling and maintenance outage.

5 .391125 S 1 B 6 Not Applicable ZZ ZZZZZZ Overspeed testing.

"F: Forced 2 Reason: 3 Method:

  • Exhibit F-Instructions S: Scheduled A - Equipment Failure (explain) 1 - Manual for preparation of B - Maintenance or Test 2 - Manual Scram data entry sheets C - Refueling 3 - Automatic Scram LER file (NUREG-Ol61)

D - Regulatory Restriction 4 - Continuation of E - Operator Training & Previous Shutdown Licensing Exam 5 - Reduced Load sExhibit H-Same Source F - Administrative 6 --Other (explain)

G - Operational Error (explain)

H - Other (explain)

EQR-28B (04-87)

t - .

,, eo NARRATIVE

SUMMARY

OF OPERATING EXPEPIENCE i-Docket No. 50-301 Unit Name Point Beach Unit 2 Date December 7, 1989 Completed By C. W. Krause Telephone 414/221-2001 The Unit 2 refueling and maintenance outage was completed November 25, 1989, when the unit was phased back on line. The '

unit'was taken off line for about one hour during the turbine overspeed testing and was phased back on at 9:32 p.m. on November 25, 1989.

Major work completed includes replacement of D06 station battery, replacement of the B main feedwater pump, performance testing of the D105 and D106 station batteries, and repair and replacement of damaged low pressure turbine blades.

On November 3, 1989, during refueling operations, contractor personnel generated a false trip signal while investigating a wiring discrepancy in the reactor protection system instrument >

racks. The reactor was defueled and the reactor trip breakers were open. Therefore, no safety-related equipment started.

An original wire labeling error was considered the root cause of '

the event.- LER 89-008 was written to document this event.

During the test of the emergency lighting, a lighting breaker was opened as a part of the test. At the same time the steam generator level indication was being tested and an " artificial" steam generator level generator was plugged into a lighting receptacle. The breaker opened for the emergency lighting also supplying power for the steam generator level generator. When the breaker was opened, the steam generator level lost power and indicated a "no level" in the steam generator. This caused a trip signal to be generated. LER 89-009 is being drafted to document this event.

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