ML19329F922

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RO 50-366/1980-100:on 800702,while Performing Surveillance Procedures HNP-2-3002 & HNP-2-3172M,high Drywell Pressure Switches 2C71-N002A Through D & 2E11-N011A Through D Found Out of Tolerance.Caused by Setpoint Drift.Switches Recalibr
ML19329F922
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 07/02/1980
From: Manry M
GEORGIA POWER CO.
To:
References
NUDOCS 8007110366
Download: ML19329F922 (2)


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SUBJECT:

llatch Unit II, Dnchet No. 50-366, Notification of Repor t.a b3 e occurrence No. 50-30G/1980-100.

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NOTIFIED: Mr. Pctc Taylor o'

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DATE:

July 2, 3980 DATE: July 2, 1980 TIIC: 0845 EDT

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DESCRIPT2 O'; OF ICPORTABLE O 'CURRC:s CE j

3rtitial Condition k

l At the time of the occurrer: es (July 1, 19 80 at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> CST and y

July 2, 1980 at 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> CST), Unit.Il was operating at 981 power.

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nt.ure,of Occurrence i

1;hile perf ortning survei13ance pr.ocedures HNP-2-3002, High Drywel3

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Preunure (RPS) Functional Test and Calibration, and HNP-2-3172M, 3:.,

High Drywell Pressure (HPCI, RCIC, Core Spray) Functional Test and Ca3ibratio:, Jt was found that switches 2C71-N002A thru D and if 2E11-:;011A thru D were out of acceptable tolerance allowed by r,

Technical Specificatiotis.

Acceptance criteria is less than oc equal 3,

to 2 psig increasing..

All switches actuated above this point.

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  • S. E 1mmediat,e Corrective Action Y

y, All high drywell,pressur.c switches on'HNP-2-3002M and NNP-2-3172M were recalibra'..cd per NNP-2-5279, Darksda3c Pressure Swit.ch Calibration y,

Procedure, and are now within acceptable tolerances as allowed per

'ischnical Syccifications.

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F Setpoint. drift can be attributed as the cause of this occurrence.

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i, S,upplemental Corrective Action investigation is underway to t.ry and determine if any other conditions t-An these instruments to drift out of tolerance.

are caucing Statur. oi )tedundant or Bnchup Systen.s systems are available and capable of performing their

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All redundant intende.d f unc t. ion s.

3mpact on Other Units because Unit I uses the same The occurrence is applicable to Unit 1, ICIP-1-3002 was switches for !!igh Drywell Pressure.

type of. prennurc with satisf actory resul t.s and 11SP-1-3172 perf orced on June 30, 1980, was perior:ned on.3uly 2, l 'J B O, also with satisfactory results.

gusti_fication fo,r Cont.inued Operation Ccnt.inued cperation is justified due to 1.hc recalibrat.fon of the liigh Drywell Pressure Switches.

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