ML19270F535

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LER 79-014/03L-0 on 790124:secondary Containment Violation Surveillance Not Performed Immediately After Restoration of Secondary Containment,Due to Misinterpretation of Tech Specs.Memo Subsequently Issued to Clarify Requirements
ML19270F535
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 02/08/1979
From: Thomas Greene
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19270F532 List:
References
LER-79-014-03L-01, LER-79-14-3L-1, NUDOCS 7902150394
Download: ML19270F535 (1)


Text

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l restoration of Secondary Containment was not nau t There are_no_cnnseq"nnce as the 1

0 s I procedure was acceptably performed approximately four hours later. 1 0 6 l 1

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44 CAUSE DESCRIPTION ANO CCRRECTIVE ACTIONS h i o l Cause of event was mis-interpreta tien of Tned,_Sy rn ui rn-nn '- +n n rnva ability nf I i i  ! standby cas treatment system to maintain b inch of water vacuum o ro v uro 'tr a r @ l i

1 (<5 moh) wind conditions.

Since wind sceed was creater than 15 moh. licened nerso __J

' 3 Lnel thoucht test could not be oerformed. Corrective action was to issue a re o int r_]

8 9 1 prettino the recuirement indicatino that the test bn run reoardless of win ! conM tire-j F s. rill TV 83 STATU3 *. FOVER OTHE R STAT US N/

h 8.t E T 6400 O F CISCC% E RY DISCOVERY CE SC5PTiCN Ja i 5 0 8 9 to 0 0 10 _12 @ N/A l l A G LOSserretic, bv nersenoni I 13 44 4 :, 43 ACTIVtTY CONTENT go F E L E A';E D CFF' ELE.WE A7.10UNT CF ACTivlTY > LCCATION CT HE L E ASE

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NAYE Cf PHTPAHEH Tom Greeme, Supt. of Pl t. Eng. ServicesNONE (912) 307-7701 o

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