ML19253C332

From kanterella
Jump to navigation Jump to search
LER 79-089/03L-0:on 791104,during drywell-to-torus Vacuum Breaker Test,Close Indication Could Not Be Obtained on Valve 2-CAC-X18D.Caused by Defective Switch.Lead Replaced & Switch to Be Repaired in 1980 Refueling Outage
ML19253C332
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 11/27/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19253C331 List:
References
LER-79-089-03L, LER-79-89-3L, NUDOCS 7911300538
Download: ML19253C332 (1)


Text

.g..g ....... .

LICENSEE EVENT REPORT CONTROL BLOCK:

1 l l l l l 6

lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI

[O IT] l Nl C l B E l P l 2 l@l 0 0l-l 0l 0l 0l 0l 0 l- 0l0l@l4l1l1 1l1l@l l l@

7 8 0 LICENSEE CODE 14 16 LICENSE NUMutR 25 26 LICENSE TYPg 40 57 CAT 58 CD's'T 1

O i 4 *

,g a

gl 0l 5 l 0 l - l 0 l 3 l 2 l 4 @l 1 l 1 l 0 l 4 7l9)@l 68 69 14 75 l l l l REPORT O/.TE l

80 l@

60 61 DOCK ET NUMBER EVFNT D ATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 l While performing PT. 2.3.1, Drywell ~ to Torus Vacuum Breaker Operability Test, a "close"l 0 3 indication could not be obtained on valve 2-CAC-X18D. l o .i l l o s I l 0 6 l . l 0 7 l l

. .n 0 a l Technical Specification 3.6.4.1, 6.9.1.9b '

7 8 9  ; 80 OE CODE SL SC E COMPONENT CODE 58 DE S E 7

O 9 8

lS Dlh 9 10 11 h (,,3,,,,j h 12 13 I l N l S l T l R l U l h d h (__Z_j h 18 19 20 SEQUENTIAL OCCURRENCE REPORT R EVISION

,,,, EVENT YE AR REPORT NO. CODE TYPE N O.

h LER NugRO l- ..l 018 l 9 l l/l l0 l 3l lL [ l-l U '.

,,,, l217 22l9 l 23 24 26 27 ,28 29 30 31 32 1K N AC 0 O4PL NT ME HOURS 22 S8 IT FOR 8. SUPPL E MANLFAC RER lXlglXlg 33 34 3 Z

,,,,,Jg

(,5 M

[Zl@ l0 l0 l0 l0 31 4 Wg 41 42 Y [g yg 43 lL l2 0 6l@

4 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h /

i O l The problem was determined to be a defective position limit switch. As the switch cant-g ]not be~ replaced at this time due to its being in the drvwell, its lead was fifted in I

, 7 l panel JX0, located 'in the Control Room and the lead from an installed spare switch wasl

, , 3 connected. The defective switch will be repaired / replaced during the 1980 refueling l

, ,, j optage. This is considered an isolated event and no further action is required.

7 8 9 80 STA $  % POWE R OTHER STATUS IS O RY DISCOVERY DESCRIPTION i s_ l Elg l 0 l 9 l 0 [gl N/A l l B [gl Periodic Test [

ACTIVITY CO TENT RELE ASED OF RELE ASE AMOUNT OF ACTIVITY LOCA' TION OF RELEASE 1 6 lZ -l @ l10Z l@l N/A l l N/A l 7 8 9 ft 44 45 80 PERSONNEL EXPOSURES NUUSE R TYPE DESCRIPTION i 7 1 01 01 Ol@l' Z l@l N/A l

,E Rr.~E < ,N,U4 E S

.-R oESCR.PT,0~h frTTl8 9' 01 0 Ol@l N/A 144lV 06 7 11 12 .

80 qglis 00 $3{l

'?$5E "x s^C"^ VON '' " @

y y @l N/A 7 8 9 10 80 ISSUE E CHiPTION

  • y lN l@l N/A l llllll))l lll2 i se J 10 68 69 80 .

NAME OF PREPAREH A. C. Tollison, Jr.

PHONE.

919 - 457-9521